Similar Documents at Perry |
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Category:OPERATING LICENSES & AMENDMENTS
MONTHYEARML20212A6731999-08-31031 August 1999 Amend 106 to License NPF-58,approving Proposed Mod Incorporating leak-off Line in RHR Sys Which Will Eliminate Operator Work Around & Significantly Reduce Collective Dose to Operations Personnel ML20206G8221999-05-0404 May 1999 Errata to Amend 105 Issued to License NPF-58,correcting Page 5.0-15a to Included Word Continued ML20205D6861999-03-26026 March 1999 Amend 104 to License NPF-58,revises Minimum Critical Power Ratio Safety Limit Contained in TS 2.1.1.2.In Addition,Amend Removes Note to TS 2.1.1.2 & Footnote to TS 5.6.5.b That References MCPR Safety Limit Valves as Cycle Specific ML20204C0521999-03-11011 March 1999 Amend 102 to License NPF-58,revising TS Requirements for Handling Irradiated Fuel in Primary Containment & Fuel Handling Bldg & Selected Specifications Associated with Performing Core Alterations ML20207F4271999-03-0303 March 1999 Amend 101 to License NPF-58,revising TS 3.4.4, Safety/Relief Valves (Srvs), by Increasing Present 1% Tolerance on Safety Mode Lift Setpoint for Safety Relief Valves to 3% ML20207L4791999-02-24024 February 1999 Amend 100 to License NPF-58,revising TS Surveillance Requirement 3.6.1.3.4 to Permit Removal of Inclined Fuel Transfer Sys Primary Containment Blind Flange While Primary Containment Integrity Required ML20203F8241999-02-0808 February 1999 Amend 97 to License NPF-58,revises TS 3.1.7, Standby Liquid Control Sys, by Increasing Boron Concentration in Standby Liquid Control Sys for Cycle 18 Fuel Design ML20196D2591998-11-23023 November 1998 Amend 94 to License NPF-58,revising TS 3.8.3 by Increasing Div 3 Diesel Generator Fuel Oil Level Requirements to Account for Rounding Error in Calculation & Unusable Vol Due to Vortex Formation at Educator Suction Nozzle ML20153D0251998-09-15015 September 1998 Amend 93 to License NPF-58,revising TS Tables 3.3.5.1-1, Emergency Core Cooling Sys Instrumentation & 3.3.6.1-1, Primary Containment & Drywell Isolation Instrumentation, by Revising Allowable Values for Selected Plant Process ML20216G4571998-03-12012 March 1998 Amend 92 to License NPF-58,revising TS 3.8.1 to Be Consistent W/Recommendations in NRC GL 94-01 ML20217E1981997-09-24024 September 1997 Amend 89 to License NPF-58,revising Existing Exception to LCO 3.0.4 as It Applies to LCO 3.6.1.9 for MSIV LCS by Making Exception Permanent ML20217D9861997-09-24024 September 1997 Amend 88 to License NPF-58,revising Test Interval for Drywell Bypass Leakage Rate Test from 18 Months to 10 Years ML20198H5471997-09-0909 September 1997 Amend 86 to License NPF-58 Approving Use of Option B, Performance Based Requirements, to 10CFR50,App J, Primary Reactor Containment Leakage Testing for Water Cooled Power Reactors ML20101G8241996-03-22022 March 1996 Amend 84 to License NPF-58,to Allow Drywell Personnel Air Lock Shield Doors to Be Opened During Operations 1,2 & 3 ML20106H6721996-03-18018 March 1996 Amend 83 to License NPF-58,allowing One Main Steam Line Leakage Rate to Be as High as 30 Scfh as Long as Total Leakage Through All Four Main Steam Lines Does Not Exceed 100 Scfh Until End of Operating Cycle 6 ML20106H6051996-03-15015 March 1996 Corrected Amend 81 to License NPF-58,correcting Error ML20101B2931996-03-0808 March 1996 Correction to Amend 79 to License NPF-58.Correction Due to Page Being Inadvertently Deleted During Reproduction of Document ML20101B1811996-03-0808 March 1996 Amend 82 to License NPF-58,revising TS in Response to Application & Approving Part of Request That Defers Drywell Bypass Leakage Rate Test During Current Refueling Outage ML20100R0881996-02-27027 February 1996 Amend 81 to License NPF-58,revising TS to Add OES Nuclear Inc,As Owner ML20097D5221996-01-29029 January 1996 Amend 79 to License NPF-58,revising TS Re Replacement of Analog Temp Instrumentation Associated W/Leak Detection W/Digital Equipment ML20100C7991996-01-19019 January 1996 Amend 78 to License NPF-58,changing TS to Grant one-time Extension of Performance Intervals for Certain TS Surveillance Requirements ML20095G0081995-12-0808 December 1995 Amend 76 to License NPF-58,revising Spec 3/4.6.1.2, Primary Containment Leakage & Associated Bases to Reflect Partial Exemptions to Requirements of 10CFR50,App J ML20094M8911995-11-16016 November 1995 Amend 74 to License NPF-58,removing License Conditions for Transamerica Delaval,Inc EDGs Specified by Paragraph 2.C.(9) & Defined in Attachment 2 of Operating License ML20092N0561995-09-26026 September 1995 Amend 73 to License NPF-58,revising TS to Make Them More Restrictive Re CRD Scram Time Testing ML20092J1331995-09-15015 September 1995 Amend 72 to License NPF-58,revising TS Consistent W/Gl 89-01, Implementation of Programmatic Controls for Radiological Effluent TS in Administrative Controls Section of TS & Relocation of Procedural Details of RETS to .. ML20086C1491995-06-27027 June 1995 Amend 70 to License NPF-58,revising TS 6.3.1 to Make Consistent W/Current Requirements of 10CFR55,deletes TS 6.4.1 & Allows an Operations Middle Manager to Hold Plant Senior Reactor Operator License in Lieu of OM ML20078D1171995-01-20020 January 1995 Amend 68 to License NPF-58,revising TS Snubber Visual Insp Schedule ML20078L9161994-11-22022 November 1994 Amend 67 to License NPF-58,revising TS Sections 3/4.3, Intrumentation, 3/4.4.2, Safety/Relief Valves, & Associated Bases to Increase STI & Allowable out-of-svc Times ML20149G4481994-10-12012 October 1994 Corrected Pages 3/4 8-21 & 3/4 6-12 to Amends 42 & 66 to License NPF-58 Due to Error in Section Number on Page ML20073G1851994-09-21021 September 1994 Amend 66 to License NPF-58,incorporating Listed Clarifications or Administrative Changes ML20072F1701994-08-17017 August 1994 Amend 65 to License NPF-58,revising PORC Composition & Quorum Description & Presenting Membership Composition Through Set of Requirements Defining Necessary Mgt Titles to Functional Titles ML20070H3951994-07-18018 July 1994 Amend 64 to License NPF-58,revising TS Re Actions to Take If Control Room Ventilation Radiation Monitor Becomes Inoperable ML20070H3731994-07-15015 July 1994 Emergency Amend 63 to License NPF-58 Changing TS in Response to Application ML20069K1751994-06-0202 June 1994 Amend 61 to License NPF-58,revising TS to Permit Operation of Perry Npgs,Unit 1 W/One Recirculation Pump Only in Operation ML20069G8911994-05-26026 May 1994 Amend 60 to License NPF-58 Providing Specific Actions to Take If Primary Containment Leakage Limits Exceeded & Cannot Be Restored ML20070N1701994-04-28028 April 1994 Amend 59 to License NPF-58,revising TS 3.3.2,Tables 3.3.2-1, 3.3.2-2,3.3.2-3 & 4.3.2.1-1 to Delete RCIC Sys Isolation on High RCIC Room Differential Temp to Improve Reliability of RCIC Sys ML20070M9721994-04-22022 April 1994 Amend 58 to License NPF-58.Amend Removing Functions Associated W/Msl RM from TSs 2.2,3.3.1 & 3.3.2 ML20065D0181994-03-30030 March 1994 Reissued Cover Sheet & TS for Amend 56 to License NPF-58 ML20065C8451994-03-23023 March 1994 Amend 57 to License NPF-58,revising TS Re Primary Containment Pressure,Temp & Suppression Pool Water Levels ML20067D1261994-02-23023 February 1994 Amend 56 to License NPF-58,revising TS 3.6.1.3 to Add Action Statement Re Condition of Inoperable Interlock Mechanism in One or Both Primary Containment Air Locks ML20067A4811994-02-14014 February 1994 Amend 55 to License NPF-58,allowing Alternate Method for Verifying Whether Control Rod Drive Pump Operating ML20059J7161994-01-19019 January 1994 Amend 54 to License NPF-58,revising TS 3.1.3.2, Control Rod Max Scram Insertion Times ML20062K9681993-12-17017 December 1993 Amend 53 to License NPF-58,revising TS Table 3.3.3-1, ECCS Actuation Instrumentation ML20058L7501993-12-13013 December 1993 Amend 52 to License NPF-58,revising TS 3.5.1,emergency Core Cooling Sys ML20057F8621993-10-15015 October 1993 Amend 51 to License NPF-58,revising TS Table 3.3.7.4-1, Remote Shutdown Sys Controls, by Removing Line Item for Controls to RCIC Pump Discharge Valve for Lube Oil Cooler ML20056F3501993-08-11011 August 1993 Amend 50 to License NPF-58,clarifying Logic for Instrumentation Used to Isolate HPCS Test Return Valve ML20035F9421993-04-16016 April 1993 Amend 47 to License NPF-58,permitting Person to Assume Manager Duties W/O Holding SRO License ML20126F8401992-12-18018 December 1992 Amend 45 to License NPF-58,revising TS to Reflect Changes in Reactor Vessel Pressure/Temp Limits ML20116H2401992-10-28028 October 1992 Amend 44 to License NPF-58,revising TSs by Removing Component List from Sections 3.6.4 & 3.8.4.1,per Guidelines in GL-91-08, Removal of Component Lists from Tss ML20101U3001992-07-0707 July 1992 Corrected Tech Spec Page 3/4 3-82 W/Correct Backup Page to Amend 42 to License NPF-58,reflecting Recent Organizational Changes 1999-08-31
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARPY-CEI-NRR-2427, Application for Amend to License NPF-58,deleting License Condition 2.C.10 Re Controls Over Containment Air Locks During Plant Outages & Clarifying License Condition 2.F Re Reporting Requirements of TS & EPP Violations1999-09-14014 September 1999 Application for Amend to License NPF-58,deleting License Condition 2.C.10 Re Controls Over Containment Air Locks During Plant Outages & Clarifying License Condition 2.F Re Reporting Requirements of TS & EPP Violations PY-CEI-NRR-2430, Application for Amend to License NPF-58,revising Allowables Values for CST Low Water Level Limits from Greater than or Equal to 59,700 Gallons to Greater than or Equal to 90,300 Gallons1999-09-0909 September 1999 Application for Amend to License NPF-58,revising Allowables Values for CST Low Water Level Limits from Greater than or Equal to 59,700 Gallons to Greater than or Equal to 90,300 Gallons PY-CEI-NRR-2406, Application for Amend to License NPF-58,eliminating Requirement in EPP to Sample Lake Erie Sediment in Perry & Eastlake Plant Area for Corbicula.Summary & Description of Change Is Encl1999-09-0909 September 1999 Application for Amend to License NPF-58,eliminating Requirement in EPP to Sample Lake Erie Sediment in Perry & Eastlake Plant Area for Corbicula.Summary & Description of Change Is Encl PY-CEI-NRR-2420, Application for Amend to License NPF-58,increasing Present 100% Authorized Rated Thermal Power Level of 3579 Megawatts Thermal to 3758 Megawatts Thermal.Proprietary SAR Encl. Proprietary SAR Withheld,Per 10CFR2.790(a)(4)1999-09-0909 September 1999 Application for Amend to License NPF-58,increasing Present 100% Authorized Rated Thermal Power Level of 3579 Megawatts Thermal to 3758 Megawatts Thermal.Proprietary SAR Encl. Proprietary SAR Withheld,Per 10CFR2.790(a)(4) ML20212A6731999-08-31031 August 1999 Amend 106 to License NPF-58,approving Proposed Mod Incorporating leak-off Line in RHR Sys Which Will Eliminate Operator Work Around & Significantly Reduce Collective Dose to Operations Personnel PY-CEI-NRR-2418, Application for Amend to License NPF-58,incorporating Addl Option Into TS 3.9.1 Required Actions When Refueling Interlocks Are Inoperable1999-08-0404 August 1999 Application for Amend to License NPF-58,incorporating Addl Option Into TS 3.9.1 Required Actions When Refueling Interlocks Are Inoperable PY-CEI-NRR-2398, Application for Amend to License NPF-58,changing SRs as Identified to Support Implementation of 24-month Operating Cycle at PNPP1999-06-17017 June 1999 Application for Amend to License NPF-58,changing SRs as Identified to Support Implementation of 24-month Operating Cycle at PNPP ML20206F5971999-05-0505 May 1999 Application for Amend to License NPF-58,authorizing CEI to Possess Dl 13.74% Undivided Ownership Interest in PNPP ML20206G8221999-05-0404 May 1999 Errata to Amend 105 Issued to License NPF-58,correcting Page 5.0-15a to Included Word Continued ML20205D6861999-03-26026 March 1999 Amend 104 to License NPF-58,revises Minimum Critical Power Ratio Safety Limit Contained in TS 2.1.1.2.In Addition,Amend Removes Note to TS 2.1.1.2 & Footnote to TS 5.6.5.b That References MCPR Safety Limit Valves as Cycle Specific PY-CEI-NRR-2362, Application for Amend to License NPF-58,proposing Change in Plant USAR by Incorporating leak-off Line in RHR Sys, Which Will Significantly Reduce Collective Dose to Plant Operations Personnel.Annotated USAR Pages,Encl1999-03-17017 March 1999 Application for Amend to License NPF-58,proposing Change in Plant USAR by Incorporating leak-off Line in RHR Sys, Which Will Significantly Reduce Collective Dose to Plant Operations Personnel.Annotated USAR Pages,Encl PY-CEI-NRR-2373, Application for Amend to License NPF-58,correcting Typos Found in TS Table 3.3.6.1-11999-03-15015 March 1999 Application for Amend to License NPF-58,correcting Typos Found in TS Table 3.3.6.1-1 ML20204C0521999-03-11011 March 1999 Amend 102 to License NPF-58,revising TS Requirements for Handling Irradiated Fuel in Primary Containment & Fuel Handling Bldg & Selected Specifications Associated with Performing Core Alterations ML20207F4271999-03-0303 March 1999 Amend 101 to License NPF-58,revising TS 3.4.4, Safety/Relief Valves (Srvs), by Increasing Present 1% Tolerance on Safety Mode Lift Setpoint for Safety Relief Valves to 3% ML20207L4791999-02-24024 February 1999 Amend 100 to License NPF-58,revising TS Surveillance Requirement 3.6.1.3.4 to Permit Removal of Inclined Fuel Transfer Sys Primary Containment Blind Flange While Primary Containment Integrity Required ML20203F8241999-02-0808 February 1999 Amend 97 to License NPF-58,revises TS 3.1.7, Standby Liquid Control Sys, by Increasing Boron Concentration in Standby Liquid Control Sys for Cycle 18 Fuel Design PY-CEI-NRR-2359, Suppl Application for Amend to License NPF-58,involving Rev of Main Steam Line Leakage Requirements & Elimination of Main Steam Isolation Valve Leakage Control Sys.Proprietary Calculations Encl.Proprietary Encls Withheld1999-01-18018 January 1999 Suppl Application for Amend to License NPF-58,involving Rev of Main Steam Line Leakage Requirements & Elimination of Main Steam Isolation Valve Leakage Control Sys.Proprietary Calculations Encl.Proprietary Encls Withheld PY-CEI-NRR-2352, Suppl to 980909 LAR to License NPF-58,improving Licensing & Design Basis for Isolation of Feedwater Penetrations, Including Sensitivity Study Performed to Examine Radiological Significance of Leakage Through FW Sys Cvs1999-01-0606 January 1999 Suppl to 980909 LAR to License NPF-58,improving Licensing & Design Basis for Isolation of Feedwater Penetrations, Including Sensitivity Study Performed to Examine Radiological Significance of Leakage Through FW Sys Cvs ML20196D2591998-11-23023 November 1998 Amend 94 to License NPF-58,revising TS 3.8.3 by Increasing Div 3 Diesel Generator Fuel Oil Level Requirements to Account for Rounding Error in Calculation & Unusable Vol Due to Vortex Formation at Educator Suction Nozzle PY-CEI-NRR-2325, Application for Amend to License NPF-58,applying Addl Conservatism by Modifying MCPR Safety Limit Values,As Calculated by Ge.Proprietary Addl Info Re 1.09 Cycle Specific Slmcpr,Encl.Proprietary Info Withheld1998-10-27027 October 1998 Application for Amend to License NPF-58,applying Addl Conservatism by Modifying MCPR Safety Limit Values,As Calculated by Ge.Proprietary Addl Info Re 1.09 Cycle Specific Slmcpr,Encl.Proprietary Info Withheld ML20153D0251998-09-15015 September 1998 Amend 93 to License NPF-58,revising TS Tables 3.3.5.1-1, Emergency Core Cooling Sys Instrumentation & 3.3.6.1-1, Primary Containment & Drywell Isolation Instrumentation, by Revising Allowable Values for Selected Plant Process PY-CEI-NRR-2322, Application for Amend to License NPF-58,stipulating That Water Leakage from Feedwater motor-operated CIVs Will Be Added Into Primary Coolant Sources Outside of Containment Program & Valves Need Not Be Included in Test Program1998-09-0909 September 1998 Application for Amend to License NPF-58,stipulating That Water Leakage from Feedwater motor-operated CIVs Will Be Added Into Primary Coolant Sources Outside of Containment Program & Valves Need Not Be Included in Test Program PY-CEI-NRR-2298, Application for Amend to License NPF-58,increasing Present Div 3 DG Fuel Oil Level Requirements to Account for Rounding Error in Calculation & Unusable Vol Due to Vortex Formation at Eductor Suction Nozzles Located in Fuel Oil Storag1998-09-0303 September 1998 Application for Amend to License NPF-58,increasing Present Div 3 DG Fuel Oil Level Requirements to Account for Rounding Error in Calculation & Unusable Vol Due to Vortex Formation at Eductor Suction Nozzles Located in Fuel Oil Storage Tank PY-CEI-NRR-2319, Application for Amend to License NPF-58,permitting EDG TS Action Completion Time of Up to 14 Days for Div 1 or 2 EDG & Allow Performance of EDG 24-hour TS SR Test in Modes 1 & 21998-09-0303 September 1998 Application for Amend to License NPF-58,permitting EDG TS Action Completion Time of Up to 14 Days for Div 1 or 2 EDG & Allow Performance of EDG 24-hour TS SR Test in Modes 1 & 2 PY-CEI-NRR-2300, Application for Amend to License NPF-58,allowing Blind Flange in Inclined Fuel Transfer Sys (Ifts) Containment Penetration to Be Removed While Primary Containment Is Required to Be Operable1998-08-31031 August 1998 Application for Amend to License NPF-58,allowing Blind Flange in Inclined Fuel Transfer Sys (Ifts) Containment Penetration to Be Removed While Primary Containment Is Required to Be Operable PY-CEI-NRR-2299, Supplemental Application for Amend to License NPF-58, Revising MSL Leakage Requirements & Eliminating Msli Valve Leakage Control Sys.Proprietary & non-proprietary Rev 1 to Calculation Psat 08401T.03,encl.Proprietary Info Withheld1998-07-22022 July 1998 Supplemental Application for Amend to License NPF-58, Revising MSL Leakage Requirements & Eliminating Msli Valve Leakage Control Sys.Proprietary & non-proprietary Rev 1 to Calculation Psat 08401T.03,encl.Proprietary Info Withheld ML20151P1891998-07-13013 July 1998 Application for Amend to License NPF-58,revising Safety Setpoint Requirements for Srv.Proprietary Info & Affidavit Are Contained in Attachment 5.Proprietary Info Withheld ML20236H6931998-06-30030 June 1998 Application for Amend to License NPF-58,transferring Operating Authority for PNPP from Ceic & Centerior Svc Co to New Operating Company Named Firstenergy Nuclear Operating Co.Marked Up License,Safety & Environ Assessments,Included PY-CEI-NRR-2295, Application for Amend to License NPF-58,revising TS 3.1.7, Standby Liquid Control Sys to Increase Boron Concentration in Standby Liquid Control Sys for Cycle 8 Fuel Design & to Provide Margin for Future Cycles as Required1998-06-30030 June 1998 Application for Amend to License NPF-58,revising TS 3.1.7, Standby Liquid Control Sys to Increase Boron Concentration in Standby Liquid Control Sys for Cycle 8 Fuel Design & to Provide Margin for Future Cycles as Required ML20216G4571998-03-12012 March 1998 Amend 92 to License NPF-58,revising TS 3.8.1 to Be Consistent W/Recommendations in NRC GL 94-01 PY-CEI-NRR-2245, Application for Amend to License NPF-58,revising TS 3.8.1, AC Sources - Operating, to Be Consistent W/Recommendations in GL 94-01, Removal of Accelerated Testing & Special Reporting Requirements for Edgs1997-12-23023 December 1997 Application for Amend to License NPF-58,revising TS 3.8.1, AC Sources - Operating, to Be Consistent W/Recommendations in GL 94-01, Removal of Accelerated Testing & Special Reporting Requirements for Edgs PY-CEI-NRR-2230, Application for Amend to License NPF-58,incorporating Temp Control Valves & Associated Bypass Lines Around Emergency Closed Cooling Sys Heat Exchangers1997-10-22022 October 1997 Application for Amend to License NPF-58,incorporating Temp Control Valves & Associated Bypass Lines Around Emergency Closed Cooling Sys Heat Exchangers ML20217D9861997-09-24024 September 1997 Amend 88 to License NPF-58,revising Test Interval for Drywell Bypass Leakage Rate Test from 18 Months to 10 Years ML20217E1981997-09-24024 September 1997 Amend 89 to License NPF-58,revising Existing Exception to LCO 3.0.4 as It Applies to LCO 3.6.1.9 for MSIV LCS by Making Exception Permanent ML20198H5471997-09-0909 September 1997 Amend 86 to License NPF-58 Approving Use of Option B, Performance Based Requirements, to 10CFR50,App J, Primary Reactor Containment Leakage Testing for Water Cooled Power Reactors PY-CEI-NRR-2207, Application for Amend to License NPF-58,revising TS 5.2.2.e, Organization-Unit Staff, by Removing Ref to NRC Policy Statement on Working Hours1997-09-0808 September 1997 Application for Amend to License NPF-58,revising TS 5.2.2.e, Organization-Unit Staff, by Removing Ref to NRC Policy Statement on Working Hours PY-CEI-NRR-2206, Application for Amend to License NPF-58,revising Pressure- Temp Limits,Per Reactor Vessel Matl Surveillance Program Requirements Contained in App H of 10CFR50.901997-08-28028 August 1997 Application for Amend to License NPF-58,revising Pressure- Temp Limits,Per Reactor Vessel Matl Surveillance Program Requirements Contained in App H of 10CFR50.90 ML20217F5751997-07-28028 July 1997 Application for Amends to Licenses DPR-66,NPF-73 & NPF-58, Authorizing Holders to Possess Beaver Valley Power Station, Unit 1 & Authorizes Duquesne Light to Use & Operate Beaver Valley Unit 1 in Accordance W/Procedures PY-CEI-NRR-2164, Application for Amend to License NPF-58,revising Existing Exception to LCO 3.0.4 as Applies to LCO 3.6.1.9 for MSIV Leakage Control Sys1997-05-0202 May 1997 Application for Amend to License NPF-58,revising Existing Exception to LCO 3.0.4 as Applies to LCO 3.6.1.9 for MSIV Leakage Control Sys PY-CEI-NRR-2165, Application for Amend to License NPF-58,revising Tech Specs Surveillance Requirement for MSIV Leakage Rate Acceptance Criteria1997-05-0202 May 1997 Application for Amend to License NPF-58,revising Tech Specs Surveillance Requirement for MSIV Leakage Rate Acceptance Criteria PY-CEI-NRR-2155, Application for Amend to License NPF-58,revising TS Surveillance Requirements 3.9.1.1 & 3.9.2.2,extending SR Frequency on Refueling Equipment & one-rod-out Interlocks1997-04-0909 April 1997 Application for Amend to License NPF-58,revising TS Surveillance Requirements 3.9.1.1 & 3.9.2.2,extending SR Frequency on Refueling Equipment & one-rod-out Interlocks PY-CEI-NRR-2133, Application for Amend to License NPF-58,requesting Implementation of App J,Option B,Performance-based Primary Containment Leakage Rate Testing Program for Type A,B & C Leak Rate Tests1997-01-31031 January 1997 Application for Amend to License NPF-58,requesting Implementation of App J,Option B,Performance-based Primary Containment Leakage Rate Testing Program for Type A,B & C Leak Rate Tests ML20132C7601996-12-13013 December 1996 Application for Amend to License NPF-58,authorizing Transfers of Control PY-CEI-NRR-2104, Application for Amend to License NPF-58,modifying MCPR Reactor Core Safety Limit Contained in TS 2.1.1.21996-10-24024 October 1996 Application for Amend to License NPF-58,modifying MCPR Reactor Core Safety Limit Contained in TS 2.1.1.2 ML20117E7821996-08-27027 August 1996 Application for Amend to License NPF-58,revising MSL Leakage Requirements & Eliminating MSIV Leakage Control Sys. Attachment 7 Provides Proprietary Dose Calculations. Attachment 7 Withheld PY-CEI-NRR-1999, Application for Amend to License NPF-58,revising Improved Tech Specs.Changes Either Administrative in Nature or Reflect Minor Technical Errors Discovered During Implementation Process1996-04-26026 April 1996 Application for Amend to License NPF-58,revising Improved Tech Specs.Changes Either Administrative in Nature or Reflect Minor Technical Errors Discovered During Implementation Process ML20101G8241996-03-22022 March 1996 Amend 84 to License NPF-58,to Allow Drywell Personnel Air Lock Shield Doors to Be Opened During Operations 1,2 & 3 ML20106H6721996-03-18018 March 1996 Amend 83 to License NPF-58,allowing One Main Steam Line Leakage Rate to Be as High as 30 Scfh as Long as Total Leakage Through All Four Main Steam Lines Does Not Exceed 100 Scfh Until End of Operating Cycle 6 ML20106H6051996-03-15015 March 1996 Corrected Amend 81 to License NPF-58,correcting Error ML20101B2931996-03-0808 March 1996 Correction to Amend 79 to License NPF-58.Correction Due to Page Being Inadvertently Deleted During Reproduction of Document 1999-09-09
[Table view] |
Text
.. _. _ _.... _. _ ~ _
I UNITED STATES p
s P;
NUCLEAR REGULATORY COMMIS810N WASNINGTON, D.C. 300084eM THE CLEVELAfE ELECTRIC ILLtBIINATING COMPANY. ET AL.
DOCKET NO. 50-440 PERRY NUCLEAR POWER PLANT. UNIT N0. 1-AMENDNENT TO FACILITY OPERATING LICENSE Amendment No. 76 License No. NPF-58 1.
The Nuclear Regulatory Commission (the Commission) has found that:
A.
The application for amendment by The Cleveland Electric Illuminating Company, Centerior Service Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania Power Company, and Toledo Edison Company (the licensees) dated October 21, 1994, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act), and the Commission's rules'and regulations set forth in 10 CFR Chapter I; B.
The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Commission; C.
There is reasonable assurance (1) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commission's regulations; D.
The issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public; and E.
The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commission's regulations and all applicable requirements have been satisfied.
2.
Accordingly, the license is amended by changes to the Technical Specifi-cations as indicated in the attachment to this license amendment, and paragraph 2.C.(2) of Facility Operating License No. NPF-58 is hereby amended to read as follows:
i 9512190450 951208 PDR ADOCK 05000440 P
PDR
. =. _......
i.
4 (2)
Technical Specifications l
The Technical Specifications contained in Appendix A and the Environmental Protection Plan contained in Appendix B, as revised through Amendment No. 76 are hereby incorporated-i into this license. The Cleveland Electric Illuminating Company shall operate the facility in accordance with the 1
Technical Specifications and the Environmental Protection Plan.
1 3.
This license amendment is effective as of its date of issuance and shall be implemented not later than 90 days after issuance.
j 3
FOR THE NUCLEAR REGULATORY C0fMISSION
/
i on B. Hopkins, Senior Project Manager Project Directorate III-3 Division of Reactor Projects III/IV Office of Nuclear Reactor Regulation
Attachment:
Changes to the Technical j
Specifications Date of issuance:
December 8, 1995 i
i a
1 i
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n 1
i
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ATTACHMENT TO LICENSE AMENDMENT NO. 76 FACILITY OPERATING LICENSE NO. NPF-58 1
DOCKET NO. 50-440 i
Replace the following pages of the Appendix "A" Technical Specifications with 1
the attached pages. The revised pages are identified by amendment number and contain vertical lines indicating the area of change.
Remove Iratrl j
1 3/4 6-3 3/4 6-3 I
3/4 6-4 3/4 6-4 i
B 3/4 6-2 B 3/4 6-2 B 3/4 6-2a B 3/4 6-2a
)
l B 3/4 6-2b B 3/4 6-2b l
4 4
1 4
i b'
i M
4 l.
l.-
CONTAINMENT SYSTEMS PRIMARY CONTAINMENT LEAKAGE 4
l LIMITING CONDITION FOR OPERATION j
3.6.1.2 P.rimary containment leakage rates shall be limited to:
a.
An overall integrated leakage rate, except for the main steam line isolation valvest, of less than or equal to 0.75 L, where L is 0.20 percent by weight of the primary containment air p,er 24-hour,s at P,.
i b.
A combined leakage rate of less than or equal to 0.60 L, isolation for all j
penetrations and all valves, except for main steam line valves # and valves which are hydrostatically leak tested, subject to Type B and C tests when pressuriztd to P,.
?
c.
Less than or equal to 25 scf per hour for any one main steam line through the isolation valves when tested at P,.
d.
A combined leakage rate of less than cr equal to 0.0504 L, for all penetrations that are secondary containment bypass leakage paths when j
pressurized to the required test pressure.
e.
A combined leakage rate of less than or equal to 1 gpm times the total number of containment isolation valves in hydrostatically i
tested line:; which penetrate the primary containment, when tested at j
greater than or equal to 1.10 P,.
APPLICABILITY: OPERATIONAL CONDITIONS 1, 2, AND 3, with the reactor coolant i
system temperature greater than 200 'F.
ACTION:
I i
With: a.
The measured overall integrated primary containment leakage rate,
}
except for the main steam line isolation valvest, exceeding 0.75 L,,
l or 4,
b.
The measured combined leakage rate for all penetrations and all j
valves except for main steam line isolation valves # and valves which l
j t
are hydrostatically leak tested, subject to Type B and C tests exceeding 0.60 L., or The measured leakage rate exceeding 25 scf per hour for any one main c.
j steam line through the isolation valves, or d.
The combined leakage rate for all penetrations that are secondary
[;
containment bypass leakage paths exceeding 0.0504 L., or i
i 4
j f
Exemption to Appendix J of 10 CFR 50.
PERRY - UNIT 1 3/4 6-3 Amendment No. (4, H, H, 76 l
l
CONTAINMENT SYSTEMS l
PRIMARY CONTAINMENT LEAKAGE LIMITING CONDITION FOR OPERATION (Continued) e.
The measured combined leakage rate for all containment isolation-valves in hydrostatically tested lines which penetrate the primary containment exceeding I gpa times the total number of such valves:
l Restore t'ae leakage rate to less than or equal to the above limit (s) within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> or be in at least HOT SHUTDOWN within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in COLD i
1
. SHUTDOWN within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
SURVEILLANCE REOUIREMENTS 4.6.1.2 The primary containment leakage rates shall be demonstrated at the following test schedule and shall be determined in conformance with the cri'.eria specified in Appendix J of 10 CFR Part 50, except that the provisions of Becntel Topical Report BN-TOP-1 may be used for Type A tests having a duration less than 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />s:
a.
Three Type A Overall Integrated Containment Leakage Rate tests shall be conducted at 40 i 10 month intervals during shutdown at P, during each 10-year service period.
b.
If any periodic Type A test fails to meet 0.75 L the test schedule for subsequent Type A tests shall be reviewed an8, approved by the Commission.
If two consecutive Type A tests fail to meet 0.75 L Type A test shall be performed at least every 18 months until tw, a o
consecutive Type A tests meet 0.75 L, at which time the above test schedule may be resumed.
c.
The accuracy of each Type A test shall be verified by a supplement al test which:
i i
PERRY - UNIT I 3/4 6-4 Amendment No. ((, Et, (Q, 76
- 4 CONTAINMENT SYSTEMS BASES 3/4.6.1 CONTAINMENT (Continued) 3/4.6.1.2 CONTAINMENT LEAKAGE (Continued)
The surveillance testing for measuring leakage rates is consistent with the requirements of Appendix J to 10 CFR 50 with the exception of the exemptions listed below. Additionally, Bechtel Topical Report BN-TOP-1 may be utilized for ILRTs with a duration of less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in accordance with Section 7.6 of ANSI N45.4-1972 (Reference 1).
.a)
Section III.D.2(b)(ii) - The air lock seal leakage test of Section III.D.2(b)(iii) of Appendix J may be substituted (following normal air lock door opening) for the full-pressure test provided that no maintenance has been performed that would affect the air locks sealing capability (Reference 2).
b)
Sections III.A.l(d), III.A.5(b)(2), and III.B.3 and III.C.3 - The main steam lines between the inboard and outboard MSIVs (including the volume up to the outboard MSIV before seat drain line valves) are not required to be vented and drained for Type A testing, and the main steam line isolation valve leak rates are exempted from inclusion in the overall integrated primary-containment leak rate and the combined local leak rate (Reference 3).
c)Section III.D.1(a) - The third Type A test for each 10-year service period is not required to be conducted when the plant is shutdown for the 10-year plant inservice inspection (Reference 3).
d)
Section III.D.3 - Type C local leak rate testing may be performed at other convenient intervals in addition to shutdown during refueling, but at intervals no greater than 2 years (Reference 3).
References (1) Letter from NRC (B. J. Youngblood) to CEI (M. R. Edelman), " Performance of the Preoperational Containment Integrated Leak Rate Test - Perry Nuclear Power Plant, Unit 1," dated June 10, 1985.
(2) PNPP Safety Evaluation Report Supplement 7, Section 6.2.6 " Containment Leakage Testing," November 1985.
(3) Letter from NRC (J. B. Hopkins) to CEI (D. C. Shelton), " Issuance of
' Exemption from the Requirements of 10 CFR Part 50, Appendix J - Perry Nuclear Power Plant, Unit 1," dated December 4, 1995.
3/4.6.1.3 CONTAINMENT AIR LOCKS The limitations on closure and leak rate for the containment air locks are required to meet the restrictions on PRIMARY CONTAINMENT INTEGRITY and the containment leakage rate given in Specifications 3.6.1.1 and 3.6.1.2.
The specification makes allowances for the fact that there may be long periods of time when the air locks will be in a closed and secured position during reactor operation. Only one closed door in each air lock is required to maintain the integrity of the containment.
PERRY - UNIT I B 3/4 6-2 Amendment No.1),$,76
- - = - _.
CONTAINMENT SYSTEMS BASES 3/4.6.1 CONTAINMENT (Continued) 3/4.6.1.3 CONTAINMENT AIR LOCKS (Continued)
An allowance has been provided within Action a.1 for access into or through the containment air-locks when an interlock mechanism in one or.both air locks is inoperable. ~ Action a.1 requires that at least one of the two 0PERABLE doors for each affected air lock be maintained closed, and if the interlock mechanism has not been restored to OPERABLE status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, one door must be locked closed. The provisions of footnote
- may be utilized for entries and exits. The administrative controls of footnote
- allow the unlocking and use of the air lock provided that an individual is stationed at the air lock, dedicated to assuring that at least one OPERABLE air lock door remains closed at all times. This allowance is provided to address those situations when the use of an air lock with only an-inoperable interlock mechanism may be preferred over the use of the other air lock, such as when the other air lock has an inoperable door.
An allowance has also been provided in Action a.2 for access into or.
through the containment air locks when one air lock door in one or both air locks is inoperable. The first sentence of footnote ** provides that entry and exit through the OPERABLE door on one or both air locks is sermissible under administrative controls for the performece of repairs of tie affected air lock components.
The second sentence of footnote. ** provides for entry into and exit from the containment for activities other then just the repairs of affected air i
lock components under administrative controls, but only permits these entries when both air locks have an inoperable door, and limits such use to 'a 7 day i
period. The administrative controls for the second sentence shall define limits on entry and exit, in order to minimize openings of the OPERABLE door.
The administrative controls for both sentences of footnote ** include provisions that after each entry and exit, the OPERABLE door must be promptly closed. The allowances of footnote ** are acceptable because of the low probability of an event that could pressurize the containment during the short time that the OPERABLE door will be open for entry into and exit from the containment.
The air supply to the containment air lock and seal system is the service and instrument air system.
The system consists of two 100% capacity air compressors per unit and can be cross-connected. This system is redundant and extremely reliable and provides system pressure indication in the control room.
-3/4.6.1.4 MSIV LEAKAGE CONTROL SYSTEM Calculated doses resulting from the maximum leakage allowance for the main steam line isolation valves in the postulated LOCA situations would be a small fraction of the 10 CFR 100 guidelines, provided the main steam line system from the isolation valves up to and including the turbine condenser remains intact.
Operating experience has indicated that degradation has occasionally occurred in the leak tightness of the MSIV's such that the specified leakage requirements have not always been maintained continuously. The requirement for the leakage PERRY - UNIT 1 B 3/4 6-2a Amendment No.%.,'15,,%lfi7,V1,76
1 CONTAINMENT SYSTEMS i
BASES 3 /4.6.1 CONTAINMENT (Continued) 3/4.6.1.4 MSIV LEAKAGE CONTROL SYSTEM (Continued) i i
control system will reduce the untreated leakage from the MSD's when isolation of the primary system and containment is required. An LC0 3.0.4 exception is provided to permit changes in Operational Conditions when the Inboard MSIV-LCS
' subsystem becomes inoperable due to condensate buildup between the MSIVs when the plant is operated below 50% rated thermal power..
3/4.6.1.5 CONTAINMENT STRUCTURAL INTEGRITY This limitation ensures that the structural integrity of the containment t
}
will be maintained comparable to the original design standards for the life of the unit. Structural integrity is required to ensure that the containment will 4
withstand the maximum pressure of 15 psig in the event of a LOCA. A visual i
inspection in conjunction with Type A leakage tests is sufficient to demonstrate i
this capability.
I d
4 3/4.6.1.6 CONTAINMENT INTERNAL PRESSURE 4
i The limitations on primary containment to secondary containment differential pressure ensure that the primary containment peak pressure of 7.80 psig does not exceed the design pressure of 15.0 psig during LOCA conditions or that the external pressure differential does not exceed the design maximum external pressure differential of +0.8 psid. The limit of -0.1 to +1.0 psid for initial positive primary containment to secondary containment pressure will limit the primary containment pressure to 7.80 psig which is less than the design pressure and is consistent with the safety analysis.
3 /4.6.1.7 CONTAINMENT AVERAGE AIR TEMPERATURE The limitation on containment average air temperature ensures that the containment peak air temperature does not exceed the design temperature of 185'F during LOCA conditions and is consistent with the safety analysis.
3/4.6.1.8 DRYWELL AND CONTAINMENT PURGE SYSTEM The use of the drywell and containment purge lines is restricted to the 42-inch outboard and 18-inch purge supply and exhaust isolation valves. These valves will close during a LOCA or steam line break accident and therefore the site boundary dose guidelines of 10 CFR Part 100 would not be exceeded in the event of an accident during purging operations. The term sealed closed as used in this context means that the valve is secured in its closed position by deactivating the valve motor operator, and does not pertain to injecting seal water between the isolation valves by a seal water system.
PERRY - UNIT I B 3/4 6-2b Amendment No. M, M, 5(,76 (Next page is B 3/4 6-3)
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