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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20216H5141999-09-24024 September 1999 Safety Evaluation Supporting Amend 209 to License DPR-16 ML20195C8141999-06-0202 June 1999 Safety Evaluation Supporting Amend 208 to License DPR-16 ML20206U9511999-05-18018 May 1999 Safety Evaluation Supporting Amend 207 to License DPR-16 ML20206P0241999-05-13013 May 1999 Safety Evaluation Supporting Amend 206 to License DPR-16 ML20206P0881999-05-12012 May 1999 Safety Evaluation Supporting Amend 205 to License DPR-16 ML20205A7451999-03-17017 March 1999 Safety Evaluation Supporting Amend 204 to License DPR-16 ML20196E2741998-11-30030 November 1998 Safety Evaluation Supporting Amend 203 to License DPR-16 ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155G9311998-11-0404 November 1998 Safety Evaluation Supporting Amend 201 to License DPR-16 ML20154M6311998-10-15015 October 1998 Safety Evaluation Supporting Amend 200 to License DPR-16 ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20237B7331998-08-13013 August 1998 Safety Evaluation Supporting Amend 196 to License DPR-16 ML20248L1611998-06-0404 June 1998 Safety Evaluation Supporting Amend 195 to License DPR-16 ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20197B4971998-02-11011 February 1998 Corrected Safety Evaluation for Amend 194 to License DPR-16.Page 2 of SE Was Incorrectly Numbered as Page 3 ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20217Q6581997-08-26026 August 1997 Safety Evaluation Supporting Amend 192 to License DPR-16 ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20140H7761997-05-0808 May 1997 Safety Evaluation Supporting Amend 191 to License DPR-16 ML20137X1071997-04-14014 April 1997 Safety Evaluation Supporting Amend 190 to License DPR-16 ML20137D6111997-03-24024 March 1997 Safety Evaluation Supporting Amend 189 to License DPR-16 ML20136D6001997-03-0606 March 1997 Safety Evaluation Supporting Amend 188 to License DPR-16 ML20133E1681997-01-0707 January 1997 Safety Evaluation Re Third 10-yr Interval ISI Plan,Rev 1 to Relief Request R11 for Plant.Proposed Alternative to ASME Requirements Authorized ML20134G2061996-11-0707 November 1996 Safety Evaluation Supporting Amend 187 to License DPR-16 ML20128L1601996-10-0303 October 1996 Safety Evaluation Accepting Third 10-yr Interval Inservice Insp Plan Request for Relief R15 ML20128F4791996-10-0101 October 1996 Safety Evaluation Accepting Rev to Inservice Testing Program Re Leakage Testing of Containment Isolation Valves ML20115F4151996-07-15015 July 1996 Safety Evaluation Supporting Amend 185 to License DPR-16 ML20117K5371996-06-0404 June 1996 Safety Evaluation Supporting Amend 184 to License DPR-16 ML20100Q4231996-03-0404 March 1996 Safety Evaluation Supporting Amend 183 to License DPR-16 ML20092A3011995-09-0606 September 1995 Safety Evaluation Supporting Amend 182 to License DPR-16 ML20087D0531995-08-0707 August 1995 Safety Evaluation Supporting Amend 181 to License DPR-16 ML20087J2831995-05-0101 May 1995 Safety Evaluation Supporting Amend 180 to License DPR-16 ML20081G9711995-03-21021 March 1995 Safety Evaluation Supporting Amend 178 to License DPR-16 ML20080D9851994-12-29029 December 1994 Safety Evaluation Accepting Licensee Requesting to Change TS to Establish Addl Requirements for Availability of LPRM Associated W/Aprm Sys ML20080D9501994-12-29029 December 1994 Safety Evaluation Supporting Amend 176 to License DPR-16 ML20077E7441994-12-0707 December 1994 Revised Page 18 of SE in Accordance W/Actions Described in Section 8.1.3 of OCNGS IPE Submittal Rept ML20077F7081994-11-30030 November 1994 Safety Evaluation Supporting Amend 174 to License DPR-16 ML20076H7361994-10-19019 October 1994 Safety Evaluation Supporting Amend 172 to License DPR-16 ML20076G4911994-10-11011 October 1994 Safety Evaluation Supporting Amend 171 to License DPR-16 ML20071M8121994-07-29029 July 1994 Safety Evaluation Supporting Amend 169 to License DPR-16 ML20029E6021994-05-11011 May 1994 SER Recommends That Licensee Monitor Conditions of Dsw & Bsw at Periodic Intervals to Ensure Continued Functions ML20063M2281994-03-0707 March 1994 Safety Evaluation Supporting Amend 168 to License DPR-16 ML20198Q4311994-01-14014 January 1994 Safety Evaluation Supporting Amend 194 to License DPR-16 ML20062M2811993-12-21021 December 1993 Safety Evaluation Supporting Amend 167 to License DPR-16 ML20057A9221993-09-13013 September 1993 Safety Evaluation Supporting Amend 165 to License DPR-16 ML20056H2651993-08-24024 August 1993 SE Re Inservice Testing Program Requests for Relief ML20056E0911993-08-0404 August 1993 SE Re Util 930614 Response to Bulletin 93-03, Resolution of Issues Related to Reactor Vessel Water Level Instrumentation in Bwrs. Util Justification for Not Implementing Addl Short Term Actions Acceptable ML20046B2301993-07-13013 July 1993 SER Concluding That Licensee pipe-support Anchorages Are in Conformance W/Requirements of NRC Bulletin 79-02 ML20045A4381993-06-0707 June 1993 Safety Evaluation Supporting Amend 164 to License DPR-16 ML20035E4171993-04-0707 April 1993 Safety Evaluation Re Reg Guide 1.97 Involving post-accident Neutron Flux Monitoring Instrumentation for BWRs 1999-09-24
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-011, :on 980914,three Small Bore Pipe Lines Did Not Meet Design Bases for Seismic & Thermal Allowables.Caused by Inadequate Structural Piping Analysis.Two 1/2 Sdcs Lines Were Modified During 17R RFO & 3rd Was Modified During 19991999-09-30030 September 1999
- on 980914,three Small Bore Pipe Lines Did Not Meet Design Bases for Seismic & Thermal Allowables.Caused by Inadequate Structural Piping Analysis.Two 1/2 Sdcs Lines Were Modified During 17R RFO & 3rd Was Modified During 1999
ML20216H5141999-09-24024 September 1999 Safety Evaluation Supporting Amend 209 to License DPR-16 ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With 05000219/LER-1999-001, :on 990208,prolonged Operation of TB with Condenser & Heater Bay Pressure Less than Design Was Noted. Caused by Lack of Clearly Documented Design Description. Placed Alternate Exhaust Fan in Service.With1999-07-29029 July 1999
- on 990208,prolonged Operation of TB with Condenser & Heater Bay Pressure Less than Design Was Noted. Caused by Lack of Clearly Documented Design Description. Placed Alternate Exhaust Fan in Service.With
ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1999-004, :on 990510,determined That Configurations of Two Pipe Supports in Spent Fuel Pool Cooling Sys Do Not Meet Design Requirements for Deadweight Loads.Caused by Inadequate Analysis.Pipes Upgraded.With1999-06-22022 June 1999
- on 990510,determined That Configurations of Two Pipe Supports in Spent Fuel Pool Cooling Sys Do Not Meet Design Requirements for Deadweight Loads.Caused by Inadequate Analysis.Pipes Upgraded.With
ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195C8141999-06-0202 June 1999 Safety Evaluation Supporting Amend 208 to License DPR-16 ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206U9511999-05-18018 May 1999 Safety Evaluation Supporting Amend 207 to License DPR-16 ML20206P0241999-05-13013 May 1999 Safety Evaluation Supporting Amend 206 to License DPR-16 ML20206P0881999-05-12012 May 1999 Safety Evaluation Supporting Amend 205 to License DPR-16 ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1999-003, :on 990402,cable Trays Did Not Meet Separation Criteria.Caused by Inadequate Engineering Review.Fire Watch Was Stationed Immediately Upon Discovery.With1999-04-30030 April 1999
- on 990402,cable Trays Did Not Meet Separation Criteria.Caused by Inadequate Engineering Review.Fire Watch Was Stationed Immediately Upon Discovery.With
05000219/LER-1999-002-01, :on 990330,fire Protection Deluge Sys Isolation Valve Was Found Out of Position.No Root Cause Determined. Technical Assessment Was Performed.With1999-04-29029 April 1999
- on 990330,fire Protection Deluge Sys Isolation Valve Was Found Out of Position.No Root Cause Determined. Technical Assessment Was Performed.With
ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20205A7451999-03-17017 March 1999 Safety Evaluation Supporting Amend 204 to License DPR-16 05000219/LER-1999-001-02, :on 990208,noted Prolonged Operation of TB with Condenser & Heater Bay Pressure.Caused by Loss of Integrity of Ventilation Envelope (Physical Boundaries).Alternate Exhaust Fan Was Placed in Service.With1999-03-0808 March 1999
- on 990208,noted Prolonged Operation of TB with Condenser & Heater Bay Pressure.Caused by Loss of Integrity of Ventilation Envelope (Physical Boundaries).Alternate Exhaust Fan Was Placed in Service.With
ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-016, :on 981028,single DG Start,Occurred.Caused by Loss of One Source of Offsite Power.Generator Relay Surveillance Revised to Eliminate Possibility of Inadvertent Procedural Breaker Trips.With1999-01-0505 January 1999
- on 981028,single DG Start,Occurred.Caused by Loss of One Source of Offsite Power.Generator Relay Surveillance Revised to Eliminate Possibility of Inadvertent Procedural Breaker Trips.With
ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-019, :on 981118,missed TS Required Surveillance Test.Caused by Inadequate Administrative Controls.Revised Related Surveillance Task Descriptions to Provide Improved Ref.With1998-12-18018 December 1998
- on 981118,missed TS Required Surveillance Test.Caused by Inadequate Administrative Controls.Revised Related Surveillance Task Descriptions to Provide Improved Ref.With
ML20196E2741998-11-30030 November 1998 Safety Evaluation Supporting Amend 203 to License DPR-16 ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-017, :on 981027,discovered That Station Battery Racks Did Not Comply with Seismic Design Basis.Caused by Inadequate Engineering Review.Restored Battery Rack Retainer Plates to Appropriate Configuration.With1998-11-25025 November 1998
- on 981027,discovered That Station Battery Racks Did Not Comply with Seismic Design Basis.Caused by Inadequate Engineering Review.Restored Battery Rack Retainer Plates to Appropriate Configuration.With
05000219/LER-1998-018, :on 981023,DG 2 Failed to Start from App R Local Shutdown Panel During Functional Test.Caused by Incorrectly Designed Wiring.Incorrect Wiring Was Modified & Demonstrated by Testing to Be Correct.With1998-11-23023 November 1998
- on 981023,DG 2 Failed to Start from App R Local Shutdown Panel During Functional Test.Caused by Incorrectly Designed Wiring.Incorrect Wiring Was Modified & Demonstrated by Testing to Be Correct.With
ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155G9311998-11-0404 November 1998 Safety Evaluation Supporting Amend 201 to License DPR-16 ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-014, :on 980928,noted Failure of Isolation Condenser Tube Bundles.Caused by Thermal Stresses/Tgscc Due to Leaky Valve.Replaced Failed Tubes Bundles & Repaired Condensate Return Valve.With1998-10-29029 October 1998
- on 980928,noted Failure of Isolation Condenser Tube Bundles.Caused by Thermal Stresses/Tgscc Due to Leaky Valve.Replaced Failed Tubes Bundles & Repaired Condensate Return Valve.With
05000219/LER-1998-015, :on 980929,SDC Isolation Occurred Due to Equipment Failure.Caused by Damaged Conduit That Appeared to Have Been Damaged by Personnel Error.Instrument Was Repaired & Bypass Was Removed.With1998-10-28028 October 1998
- on 980929,SDC Isolation Occurred Due to Equipment Failure.Caused by Damaged Conduit That Appeared to Have Been Damaged by Personnel Error.Instrument Was Repaired & Bypass Was Removed.With
05000219/LER-1998-013-01, :on 980926,LLRT Results Indicated That MSIV NS03B Exceeded TS Leak Rate Limit.Caused by Component Wear. Maint Was Performed on Subject Valve to Restore Seat Integrity & as-left LLRT Was Acceptable.With1998-10-26026 October 1998
- on 980926,LLRT Results Indicated That MSIV NS03B Exceeded TS Leak Rate Limit.Caused by Component Wear. Maint Was Performed on Subject Valve to Restore Seat Integrity & as-left LLRT Was Acceptable.With
ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R 05000219/LER-1998-012-01, :on 980916,unplanned Actuation of Esfs Occurred.Caused by Written Communication.Procedure Revised to Include Signature Verifications to Install & Subsequently Remove Ohmmeter1998-10-16016 October 1998
- on 980916,unplanned Actuation of Esfs Occurred.Caused by Written Communication.Procedure Revised to Include Signature Verifications to Install & Subsequently Remove Ohmmeter
ML20154M6311998-10-15015 October 1998 Safety Evaluation Supporting Amend 200 to License DPR-16 05000219/LER-1998-011-01, :on 980914,discovered That Three Small Bore Piping Lines Did Not Meet Design Basis Seismic &/Or Thermal Allowables.Caused by Design Deficiency.Subject Lines Will Be Modified During Present Refueling Outage.With1998-10-15015 October 1998
- on 980914,discovered That Three Small Bore Piping Lines Did Not Meet Design Basis Seismic &/Or Thermal Allowables.Caused by Design Deficiency.Subject Lines Will Be Modified During Present Refueling Outage.With
ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification 05000219/LER-1998-010, :on 980724,DG Switchgear Was Found Beyond Design Bases.Caused by Inadequate Installation During Original Construction.Evaluated Temporary Mod to Determine If It Should Be Reclassified as Permanent Mod1998-08-24024 August 1998
- on 980724,DG Switchgear Was Found Beyond Design Bases.Caused by Inadequate Installation During Original Construction.Evaluated Temporary Mod to Determine If It Should Be Reclassified as Permanent Mod
ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B7331998-08-13013 August 1998 Safety Evaluation Supporting Amend 196 to License DPR-16 ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station 05000219/LER-1997-013, Has Been Canceled1998-06-30030 June 1998 Has Been Canceled 1999-09-30
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pusco UNITED STATES y-j j
NUCLEAR REGULATORY COMMISSION t
WASHINGTON. D.C. 2055 5 0001
,o SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO. 182 TO FACILITY OPERATING LICENSE NO. DPR-16 GPU NUCLEAR CORPORATION AND JERSEY CENTRAL POWE2 & LIGHT COMPANY OYSTER CREEK NUCLEAR GENERATING STATION DOCKET NO. 50-219
1.0 INTRODUCTION
By letter dated June 26, 1995, GPU Nuclear Corporation (GPUN\\the licensee) proposed changes to the Technical Specifications (TS) for the Oyster Creek Nuclear Generating Station. The amendment proposes removing the snubber visual examination schedule in the existing TS and replacing it with a refueling outage based visual examination schedule as shown in Table 4.7-2,
" Snubber Visual Inspection Interval" of Enclosure B to Generic Letter (GL) 90-09, " Alternate Requirements for Snubber Visual Inspection Interval and Corrective Actions." The proposed change revises the snubber visual inspection intervals to match the schedule developed by the NRC staff for use with a 24-month refueling interval. GPUN also proposed to revise the bases for the snubber visual inspection interval to be consistent with the bases described in Generic Letter 90-09.
2.0 EVALUATION The snubber visual examination schedule in the existing TS is based on the permissible number of inoperable snubbers found during the visual examination.
Because the existing snubber visual examination schedule is based only on the absolute number of inoperable snubbers found during the visual examination irrespective of the total population of snubbers, licensees with a large snubber population find the visual ext,nination schedule excessively restrictive.
The purpose of the alternative visual examination schedule is to allow the licensee to perform visual examinations and corrective actions during plant outages without reduction of the confidence level provided by the existing visual examination schedule.
The new visual examination schedule specifies the permissible number of inoperable snubbers for various snubber populations.
The basic examination interval is the normal fuel cycle up to 24-months.
This interval may be extended to as long as twice the fuel cycle or reduced to as small as two-thirds of the fuel cycle depending on the number of unacceptable snubbers found during the visual examination.
The examination interval may vary by i25 percent to coincide with the actual outage.
9509000315 950906 PDR ADOCK 05000219 P
PDR
e
. During the recent 15R refueling outage, one snubber failed a scheduled visual inspection. This failure was located on the main steamline. An engineering evaluation was performed by GPUN as pr Technical Specifications which determined that no damage had occurred on any snubber.
This snubber was in service since 1977.
There were thirteen additional snubbers on the main steamline.
Eleven of these were replaced and two were tested satisfactorily and reinstalled (one was originally installed in 1988 and the other in 1993).
The sample size for mechanical snubber visual inspections was 100% as required by technical specifications.
The sample size for mechanical snubber functional inspections was increased from 10% to 42% since one functional failure was found on the other main steamline and subsequently was replaced.
This snubber was in service since 1977.
It was determined that the causes of the snubber failures were sustained high temperatures and high frequency vibration for an extended length of service.
l The high temperature caused the snubber grease to degrade, whereupon the extended high frequency vibration caused excessive wear.
The snubbers had been in service since 1977.
Tne existing Technical Specification would require a reactor shutdown and drywell entry one year into the operating cycle solely for the purpose of performing an inspection on the snubbers which were replaced or reinctalled on
'the main steam system in 15R.
The purpose of this change request is to amend the technical specifications to not require the reactor shutdown, and update the Technical Specification requirements to those previously approved in Generic letter 90-09.
The exact wording of GL 90-09 has been utilized by GPUN to the greatest extent practical. However, minor changes have been requested to allow for the design specifics of the Oyster Creek Plant.
Each change from the prescribed wording in GL 90-09 is discussed and evaluated separately.
GPUN proposes the following plant specific wording changes:
Section 4.5.Q.1 GL 90-09 wording:
... performance of the following augmented inservice inspection program in addition to the requirements of 4.0.5."
Technical specification change request (TSCR) wording:
"... performance of the following inspection program."
Reason for the chance: Oyster Creek controls the inspection and testing of the snubbers in the Technical Specifications and not in the Augmented Inservice Testing Program.
Further, Section 4.0.5 referenced in the Generic letter states in Section e "Nothing in the ASME Boiler and Pressure Vessel Code shall be construed to supersede the requirements of any Technical Specification."
1
=_
4
, The staff agrees with GPUN that since Oyster Creek controls the inspection and testing of the snubbers in the TS and not in the Augmented Inservice Testing Program the wording change is appropriate.
Section 4.5.Q.1.a GL 90-09 wording:
" based on the criteria of Table 4.7.2 and the first inspection interval determined using the criteria shall be based upon the previous inspection interval established by the requirements in effect before Amendment (*)"
TSCR wording:
... based on the criteria provided in Table 4.5-1."
Reason for the Chance:
- 1) Table 4.7.2 in the Generic Letter is Table 4.5-1 in the TSCR, 2) Although there was a single visual failure during the last interval, all snubbers in the same temperature and vibration environment were aither replaced or tested satisfactorily and reinstalled. There is no need to perform a plant shutdown for the sole purpose of inspecting snubbers which have seen one year of service when the single failed snubber had been in service for seventeen years.
The replacement /reinsta11ation of all snubbers in a similar application (main steam system) has effectively removed the failure mechanism for the single visual inspection failure that was observed last outage. Additionally, the replacement /reinsta11ation of all the snubbers in similar applications (main steam system) has significantly decreased the probability of occurrence and consequences of any accident previously evaluated as all snubbers in thf s application have been functionally tested during the last surveillance interval. Therefore, the one time increase in interval from the existing 12 months to 24 months is within the inspection interval which would have been in effect for the majority of the snubbers had the single failure not occurred.
The staff agrees with GPUN that since all snubbers were either replaced or tested satisfactorily and reinstalled there is no need to perform a plant shutdown for the reasons stated above.
Section 4.5.Q.l.b GL 90-09 wording:
...A11 snubbers found connected to an inoperable common hydraulic fluid reservoir shall be counted as unacceptable for determining the next inspection interval.
TSCR wording:
--Sentence was deleted--
GPUN has stated that Oyster Creek does not have any snubbers sharing a common reservoir.
The staff finds this change acceptable but notes that if Oyster Creek Nuclear i
Generating Station implements this type of system, GPUN must submit the appropriate changes.
(
I i
i
GPUN has proposed changes to TS 4.5.Q.a and the associated Bases that are consistent with the guidance provided in GL 90-09 for the replacements of the visual examination schedule with Table 4.7-2 (including footnotes 1 through 6) of the Generic Letter 90-09. On the basis of its review of this matter, the staff finds that the proposed changes to the TS for the Oyster Creak Nuclear Generating Station are acceptable.
3.0 STATE CONSULTATION
In accordance with the Commission's regulations, the New Jersey State official was notified of the proposed issuance of the amendment. The State official had no comments.
4.0 ENVIRONMENTAL CONSIDERATION
The amendment changes surveillance requirements. The NRC staff has determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that the amendment involves no significant hazards consideration, and there has been no public comment on such finding (60 FR 39440).
Accordingly, the amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9).
Pursuant to 10 CFR 51.22(b) no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendment.
5.0 CONCLUSION
The Commission has concluded, based on the considerations discussed above, i
that:
(1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, (2) such activities will be conducted in compliance with the Commission's regulations, j
and (3) the issuance of the amendment will not be inimical to the common defense and security or to the health and safety of the public.
j Principal Contributor: Alexander W. Dromerick Date: September 6, 1995
.