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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20216H5141999-09-24024 September 1999 Safety Evaluation Supporting Amend 209 to License DPR-16 ML20195C8141999-06-0202 June 1999 Safety Evaluation Supporting Amend 208 to License DPR-16 ML20206U9511999-05-18018 May 1999 Safety Evaluation Supporting Amend 207 to License DPR-16 ML20206P0241999-05-13013 May 1999 Safety Evaluation Supporting Amend 206 to License DPR-16 ML20206P0881999-05-12012 May 1999 Safety Evaluation Supporting Amend 205 to License DPR-16 ML20205A7451999-03-17017 March 1999 Safety Evaluation Supporting Amend 204 to License DPR-16 ML20196E2741998-11-30030 November 1998 Safety Evaluation Supporting Amend 203 to License DPR-16 ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155G9311998-11-0404 November 1998 Safety Evaluation Supporting Amend 201 to License DPR-16 ML20154M6311998-10-15015 October 1998 Safety Evaluation Supporting Amend 200 to License DPR-16 ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20237B7331998-08-13013 August 1998 Safety Evaluation Supporting Amend 196 to License DPR-16 ML20248L1611998-06-0404 June 1998 Safety Evaluation Supporting Amend 195 to License DPR-16 ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20197B4971998-02-11011 February 1998 Corrected Safety Evaluation for Amend 194 to License DPR-16.Page 2 of SE Was Incorrectly Numbered as Page 3 ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20217Q6581997-08-26026 August 1997 Safety Evaluation Supporting Amend 192 to License DPR-16 ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20140H7761997-05-0808 May 1997 Safety Evaluation Supporting Amend 191 to License DPR-16 ML20137X1071997-04-14014 April 1997 Safety Evaluation Supporting Amend 190 to License DPR-16 ML20137D6111997-03-24024 March 1997 Safety Evaluation Supporting Amend 189 to License DPR-16 ML20136D6001997-03-0606 March 1997 Safety Evaluation Supporting Amend 188 to License DPR-16 ML20133E1681997-01-0707 January 1997 Safety Evaluation Re Third 10-yr Interval ISI Plan,Rev 1 to Relief Request R11 for Plant.Proposed Alternative to ASME Requirements Authorized ML20134G2061996-11-0707 November 1996 Safety Evaluation Supporting Amend 187 to License DPR-16 ML20128L1601996-10-0303 October 1996 Safety Evaluation Accepting Third 10-yr Interval Inservice Insp Plan Request for Relief R15 ML20128F4791996-10-0101 October 1996 Safety Evaluation Accepting Rev to Inservice Testing Program Re Leakage Testing of Containment Isolation Valves ML20115F4151996-07-15015 July 1996 Safety Evaluation Supporting Amend 185 to License DPR-16 ML20117K5371996-06-0404 June 1996 Safety Evaluation Supporting Amend 184 to License DPR-16 ML20100Q4231996-03-0404 March 1996 Safety Evaluation Supporting Amend 183 to License DPR-16 ML20092A3011995-09-0606 September 1995 Safety Evaluation Supporting Amend 182 to License DPR-16 ML20087D0531995-08-0707 August 1995 Safety Evaluation Supporting Amend 181 to License DPR-16 ML20087J2831995-05-0101 May 1995 Safety Evaluation Supporting Amend 180 to License DPR-16 ML20081G9711995-03-21021 March 1995 Safety Evaluation Supporting Amend 178 to License DPR-16 ML20080D9851994-12-29029 December 1994 Safety Evaluation Accepting Licensee Requesting to Change TS to Establish Addl Requirements for Availability of LPRM Associated W/Aprm Sys ML20080D9501994-12-29029 December 1994 Safety Evaluation Supporting Amend 176 to License DPR-16 ML20077E7441994-12-0707 December 1994 Revised Page 18 of SE in Accordance W/Actions Described in Section 8.1.3 of OCNGS IPE Submittal Rept ML20077F7081994-11-30030 November 1994 Safety Evaluation Supporting Amend 174 to License DPR-16 ML20076H7361994-10-19019 October 1994 Safety Evaluation Supporting Amend 172 to License DPR-16 ML20076G4911994-10-11011 October 1994 Safety Evaluation Supporting Amend 171 to License DPR-16 ML20071M8121994-07-29029 July 1994 Safety Evaluation Supporting Amend 169 to License DPR-16 ML20029E6021994-05-11011 May 1994 SER Recommends That Licensee Monitor Conditions of Dsw & Bsw at Periodic Intervals to Ensure Continued Functions ML20063M2281994-03-0707 March 1994 Safety Evaluation Supporting Amend 168 to License DPR-16 ML20198Q4311994-01-14014 January 1994 Safety Evaluation Supporting Amend 194 to License DPR-16 ML20062M2811993-12-21021 December 1993 Safety Evaluation Supporting Amend 167 to License DPR-16 ML20057A9221993-09-13013 September 1993 Safety Evaluation Supporting Amend 165 to License DPR-16 ML20056H2651993-08-24024 August 1993 SE Re Inservice Testing Program Requests for Relief ML20056E0911993-08-0404 August 1993 SE Re Util 930614 Response to Bulletin 93-03, Resolution of Issues Related to Reactor Vessel Water Level Instrumentation in Bwrs. Util Justification for Not Implementing Addl Short Term Actions Acceptable ML20046B2301993-07-13013 July 1993 SER Concluding That Licensee pipe-support Anchorages Are in Conformance W/Requirements of NRC Bulletin 79-02 ML20045A4381993-06-0707 June 1993 Safety Evaluation Supporting Amend 164 to License DPR-16 ML20035E4171993-04-0707 April 1993 Safety Evaluation Re Reg Guide 1.97 Involving post-accident Neutron Flux Monitoring Instrumentation for BWRs 1999-09-24
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-011, :on 980914,three Small Bore Pipe Lines Did Not Meet Design Bases for Seismic & Thermal Allowables.Caused by Inadequate Structural Piping Analysis.Two 1/2 Sdcs Lines Were Modified During 17R RFO & 3rd Was Modified During 19991999-09-30030 September 1999
- on 980914,three Small Bore Pipe Lines Did Not Meet Design Bases for Seismic & Thermal Allowables.Caused by Inadequate Structural Piping Analysis.Two 1/2 Sdcs Lines Were Modified During 17R RFO & 3rd Was Modified During 1999
ML20216H5141999-09-24024 September 1999 Safety Evaluation Supporting Amend 209 to License DPR-16 ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With 05000219/LER-1999-001, :on 990208,prolonged Operation of TB with Condenser & Heater Bay Pressure Less than Design Was Noted. Caused by Lack of Clearly Documented Design Description. Placed Alternate Exhaust Fan in Service.With1999-07-29029 July 1999
- on 990208,prolonged Operation of TB with Condenser & Heater Bay Pressure Less than Design Was Noted. Caused by Lack of Clearly Documented Design Description. Placed Alternate Exhaust Fan in Service.With
ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1999-004, :on 990510,determined That Configurations of Two Pipe Supports in Spent Fuel Pool Cooling Sys Do Not Meet Design Requirements for Deadweight Loads.Caused by Inadequate Analysis.Pipes Upgraded.With1999-06-22022 June 1999
- on 990510,determined That Configurations of Two Pipe Supports in Spent Fuel Pool Cooling Sys Do Not Meet Design Requirements for Deadweight Loads.Caused by Inadequate Analysis.Pipes Upgraded.With
ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195C8141999-06-0202 June 1999 Safety Evaluation Supporting Amend 208 to License DPR-16 ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206U9511999-05-18018 May 1999 Safety Evaluation Supporting Amend 207 to License DPR-16 ML20206P0241999-05-13013 May 1999 Safety Evaluation Supporting Amend 206 to License DPR-16 ML20206P0881999-05-12012 May 1999 Safety Evaluation Supporting Amend 205 to License DPR-16 ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1999-003, :on 990402,cable Trays Did Not Meet Separation Criteria.Caused by Inadequate Engineering Review.Fire Watch Was Stationed Immediately Upon Discovery.With1999-04-30030 April 1999
- on 990402,cable Trays Did Not Meet Separation Criteria.Caused by Inadequate Engineering Review.Fire Watch Was Stationed Immediately Upon Discovery.With
05000219/LER-1999-002-01, :on 990330,fire Protection Deluge Sys Isolation Valve Was Found Out of Position.No Root Cause Determined. Technical Assessment Was Performed.With1999-04-29029 April 1999
- on 990330,fire Protection Deluge Sys Isolation Valve Was Found Out of Position.No Root Cause Determined. Technical Assessment Was Performed.With
ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20205A7451999-03-17017 March 1999 Safety Evaluation Supporting Amend 204 to License DPR-16 05000219/LER-1999-001-02, :on 990208,noted Prolonged Operation of TB with Condenser & Heater Bay Pressure.Caused by Loss of Integrity of Ventilation Envelope (Physical Boundaries).Alternate Exhaust Fan Was Placed in Service.With1999-03-0808 March 1999
- on 990208,noted Prolonged Operation of TB with Condenser & Heater Bay Pressure.Caused by Loss of Integrity of Ventilation Envelope (Physical Boundaries).Alternate Exhaust Fan Was Placed in Service.With
ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-016, :on 981028,single DG Start,Occurred.Caused by Loss of One Source of Offsite Power.Generator Relay Surveillance Revised to Eliminate Possibility of Inadvertent Procedural Breaker Trips.With1999-01-0505 January 1999
- on 981028,single DG Start,Occurred.Caused by Loss of One Source of Offsite Power.Generator Relay Surveillance Revised to Eliminate Possibility of Inadvertent Procedural Breaker Trips.With
ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-019, :on 981118,missed TS Required Surveillance Test.Caused by Inadequate Administrative Controls.Revised Related Surveillance Task Descriptions to Provide Improved Ref.With1998-12-18018 December 1998
- on 981118,missed TS Required Surveillance Test.Caused by Inadequate Administrative Controls.Revised Related Surveillance Task Descriptions to Provide Improved Ref.With
ML20196E2741998-11-30030 November 1998 Safety Evaluation Supporting Amend 203 to License DPR-16 ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-017, :on 981027,discovered That Station Battery Racks Did Not Comply with Seismic Design Basis.Caused by Inadequate Engineering Review.Restored Battery Rack Retainer Plates to Appropriate Configuration.With1998-11-25025 November 1998
- on 981027,discovered That Station Battery Racks Did Not Comply with Seismic Design Basis.Caused by Inadequate Engineering Review.Restored Battery Rack Retainer Plates to Appropriate Configuration.With
05000219/LER-1998-018, :on 981023,DG 2 Failed to Start from App R Local Shutdown Panel During Functional Test.Caused by Incorrectly Designed Wiring.Incorrect Wiring Was Modified & Demonstrated by Testing to Be Correct.With1998-11-23023 November 1998
- on 981023,DG 2 Failed to Start from App R Local Shutdown Panel During Functional Test.Caused by Incorrectly Designed Wiring.Incorrect Wiring Was Modified & Demonstrated by Testing to Be Correct.With
ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155G9311998-11-0404 November 1998 Safety Evaluation Supporting Amend 201 to License DPR-16 ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With 05000219/LER-1998-014, :on 980928,noted Failure of Isolation Condenser Tube Bundles.Caused by Thermal Stresses/Tgscc Due to Leaky Valve.Replaced Failed Tubes Bundles & Repaired Condensate Return Valve.With1998-10-29029 October 1998
- on 980928,noted Failure of Isolation Condenser Tube Bundles.Caused by Thermal Stresses/Tgscc Due to Leaky Valve.Replaced Failed Tubes Bundles & Repaired Condensate Return Valve.With
05000219/LER-1998-015, :on 980929,SDC Isolation Occurred Due to Equipment Failure.Caused by Damaged Conduit That Appeared to Have Been Damaged by Personnel Error.Instrument Was Repaired & Bypass Was Removed.With1998-10-28028 October 1998
- on 980929,SDC Isolation Occurred Due to Equipment Failure.Caused by Damaged Conduit That Appeared to Have Been Damaged by Personnel Error.Instrument Was Repaired & Bypass Was Removed.With
05000219/LER-1998-013-01, :on 980926,LLRT Results Indicated That MSIV NS03B Exceeded TS Leak Rate Limit.Caused by Component Wear. Maint Was Performed on Subject Valve to Restore Seat Integrity & as-left LLRT Was Acceptable.With1998-10-26026 October 1998
- on 980926,LLRT Results Indicated That MSIV NS03B Exceeded TS Leak Rate Limit.Caused by Component Wear. Maint Was Performed on Subject Valve to Restore Seat Integrity & as-left LLRT Was Acceptable.With
ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R 05000219/LER-1998-012-01, :on 980916,unplanned Actuation of Esfs Occurred.Caused by Written Communication.Procedure Revised to Include Signature Verifications to Install & Subsequently Remove Ohmmeter1998-10-16016 October 1998
- on 980916,unplanned Actuation of Esfs Occurred.Caused by Written Communication.Procedure Revised to Include Signature Verifications to Install & Subsequently Remove Ohmmeter
ML20154M6311998-10-15015 October 1998 Safety Evaluation Supporting Amend 200 to License DPR-16 05000219/LER-1998-011-01, :on 980914,discovered That Three Small Bore Piping Lines Did Not Meet Design Basis Seismic &/Or Thermal Allowables.Caused by Design Deficiency.Subject Lines Will Be Modified During Present Refueling Outage.With1998-10-15015 October 1998
- on 980914,discovered That Three Small Bore Piping Lines Did Not Meet Design Basis Seismic &/Or Thermal Allowables.Caused by Design Deficiency.Subject Lines Will Be Modified During Present Refueling Outage.With
ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification 05000219/LER-1998-010, :on 980724,DG Switchgear Was Found Beyond Design Bases.Caused by Inadequate Installation During Original Construction.Evaluated Temporary Mod to Determine If It Should Be Reclassified as Permanent Mod1998-08-24024 August 1998
- on 980724,DG Switchgear Was Found Beyond Design Bases.Caused by Inadequate Installation During Original Construction.Evaluated Temporary Mod to Determine If It Should Be Reclassified as Permanent Mod
ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B7331998-08-13013 August 1998 Safety Evaluation Supporting Amend 196 to License DPR-16 ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station 05000219/LER-1997-013, Has Been Canceled1998-06-30030 June 1998 Has Been Canceled 1999-09-30
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WASHINGTON, D.C. 205 %-0001 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO.168 TO FACILITY OPERATING LICENSE N0. DPR-16 GPU NUCLEAR CORPORATION AND JERSEY CENTRAL POWER & LIGHT COMPANY OYSTER CREEK NUCLEAR GENERATING STATION DOCKET NO. 50-219
1.0 INTRODUCTION
By letter dated December 16, 1993, GPU Nuclear Corporation (the licensee) requested an amendment to Facility Operating License No. DPR-16.
The proposed amendment would change certain Oyster Creek Technical Specifications (TS) relating to secondary containment piping penetration isolation requirements.
2.0 DISCUSS _ ION AND EVALUATION 2.1 Secondary Containment Description The Oyster Creek reactor building (RB) completely encloses the reactor and its primary containment. During those reactor operational modes which require primary integrity, the RB serves as a secondary containment for control of fission products which could leak from the primary containment.
During those operational modes for which primary containment integrity is impractical and accidents involving containment pressurization are unlikely (e.g., refueling),
the RB serves as a primary containment.
The RB is provided with a ventilation system (RBVS) system for heating or cooling during normal (non-accident) conditions.
The RBVS contains air supply and exhaust ducts which penetrate the RB walls.. The supply fans are located outside of the RB and supply air to the RB via two supply duct penetrations.
Exhaust air leaves the RB via a single duct penetration.
Redundant automatic isolation dampers (but.terfly valves) are provided in each duct at each RB penetration to automatically isolate the RB under accident conditions.
Under accident conditions, the Standby Gas Treatment System (SGTS) will automatically start, exhausting the RB to the stack to provide a filtered, elevated release of the contaminated RB atmosphere. The RB is designed for a maximum inleakage rate of 200% volume / day.
Failure of the butterfly valves to close tightly could result in excessive RB in-leakage exceeding the capability of the SGTS and thereby causing exfiltration or ground-level,. unfiltered-release of fission products during an accident.
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\\ j 2.2 Changes to Technical Specifications
-l 2.2.1 Definition of Secondary Containment Integrity The Technical Specifications provide a high degree of assurance that the secondary containment will be operable as a fission product control system under accident conditions. TS 1.14 defines three specific requirements necessary for secondary containment integrity. The conditions to be met include:
A.
At least one door at each accus < pening is closed.
B.
The standby gas treatment system is operable.
C.
All reactor building ventilation system automatic i
isolation valves are operable or are secured in the closed 1
position.
i The proposed amendment would change the last requirement to read "All automatic secondary containment isolation valves are operable or are secured in the closed position." This change would provide consistency in terminology and does not change the scope of the TS or any specific Limiting Conditions for Operation (LCOs) or Surveillance Requirements (SRs).
Substitution of the term " secondary containment isolation valves" for " reactor building isolation valves" is acceptable, since, at Oyster Creek, the secondary containment j
boundaries and RB boundaries coincide. The TS 1.14 change is therefore acceptable.
i 2.2.2 Completion times for repair of valves or isolation of penetration i
The more significent of the changes proposed in the licensee's application are intended to permit continued operations when one or more of the butterfly isolation valves is inoperable but integrity of the associated penetration is assured by virtue of another closure device which is not subject to failure to automatically close on demand. TS 3.5.8 currently requires that upon accidental loss of secondary containment integrity (i.e., conditions A, B and C above not met), the licensee must restore secondary containment integrity within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, or:
During power operation:
1 (1) Have the reactor mode switch in the shutdown mode position within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
(2) Cease all work on the reactor or its connected systems in the reactor building which could result in inadvertent releases of radioactive materials.
i
. (3) Cease all operations in, above or around the Spent Fuel Storage Pool that could cause release of radioactive materials.
During refueling:
(1)
Cease fuel handling operations or activities which could reduce the shutdown margin (excluding reactor coolant temperature changes).
(2)
Cease all work on the reactor or its connected systems in the reactor building which could result in the inadvertent releases of radioactive materials.
(3) Cease all operations in, above or around the Spent Fuel Storage Pool that could cause release of radioactive materials.
The above (currently applicable) TS do not acknowledge the use of a single deenergized or locked-closed valve as being sufficient for integrity of a secondary containment penetration.
Should a valve become jammed open, the above action requirements must be followed.
The amendment would revise the above requirements to insert a provision that, after expiration of the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> period with one or more of the automatic secondary containment isolation valves inoperable, the licensee must:
Maintain at least one automatic secondary containment isolation valve in each affected penetration OPERABLE, and Within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> restore the inoperable automatic secondary containment isolation valves (s) to OPERABLE status or isolate each affected penetration with at least one valve secured in the closed position.
The proposed change would provide a 4-hour completion time for the case of two inoperable (open and incapable of automatic closure) valves in a penetration, and an 8-hour. completion time for the case of a single inoperable valve.
After expiration of these completion times the affected penetration (s) must be isolated with at least one secured valve.
When isolated with a secured (i.e.,
deenergized) valve, the penetration is not subject to loss-of leaktightness due to equipment failure or spurious signals.
Thus operations can be continued until repairs can be completed.
The staff has evaluated the potential effects of the proposed TS changes using the STS (Standard Technical Specifications General Electric Plants, BWR/4, NUREG-1433, September 1992) as guidance. The STS specify an 8-hour completion
' time for a single inoperable secondary containment isolation valve in one or
a i more penetrations, and a 4-hour completion time for both secondary containment isolation valves inoperable in one or more penetrations.
The STS also permit continued operations with no time limit, with penetration closure provided by a single closed, deactivated valve.
Based on the STS guidance, and a determination that there are no unique or unusual features of the Oyster Creek design that would preclude use of the STS as guidance, the proposed TS changes are acceptable.
The STS also specify that when a closed and deenergized valve is used to isolate a penetration, the valve position is to be verified every 31 days.
The purpose of this additional requirement is to provide added assurance that the deenergized valve is indeed closed, considering that fact that the valve's control room position indication may also be inoperable.
The licensee has not explicitly included such a requirement with the proposed changes.
The staff discussed this with licensee personnel, and was informed that at Oyster Creek, the RBVS secondary containment isolation valves are coincidentally tested monthly for leak tightness and proper positioning as part of the SGTS surveillance test program.
The monthly SGTS surveillance test involves closure of the RBVS valves while the SGTS draws a negative pressure on the secondary containment.
The monthly SGTS operability test would reveal an improperly positioned valve.
Since the SGTS test interval coincides with the desired interval for verification of proper closure of isolated penetrations, the SGTS surveillance test provides a high degree of assurance of proper secondary containment isolation valve positioning.
Additionally, the licensee's valve tagout administrative procedures include logging of inoperable valves, and the use of red tags at the valve and in the control room to continuously identify valves that are it. operable.
The use of such controls provides added assurance that closed and deenergized (secured) valves remain in the correct position. The proposed changes are thus acceptable notwithstanding the omission of the standard 30-day verification requirement.
2.2.3 Changes to Bases The proposed amendment would add a paragraph to the BASES describing permissible conditions for removal of an RBVS secondary containment isolation valve.
The redundant isolation valves in the two supply duct penetrations are located inside the RB. The redundant isolation valves in the single exhaust duct penetration are located outside the RB. Due to this configuration, it is possible to remove the downstream isolation valves, if the upstream valves are closed, without loss of secondary containment integrity.
Removal of an isolation valve under these conditions is consistent with the Technical Specifications operability requirements and is acceptable.
The staff has reviewed the proposed Technical Specifications changes relating to (a) the definition of secondary integrity, (b) the completion time for actions required when one or more secondary containment piping penetration isolation valves is inoperable, and (c) the removal of an RBVS isolation valve.
The staff has determined that the proposed changes are acceptable.
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3.0 STATE CONSULTATION
in accordance with the Commission's regulations,-the New Jersey State official was notified of the proposed issuance of the amendment. The State official had no comments.
4.0 ENVIRONMENTAL CONSIDERATION
The amendment changes a requirement with respect to installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20.
The NRC staff has determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no i
significant increase in individual or cumulative occupational radiation exposure.
The Commission has previously issued a proposed finding that the amendment involves no significant hazards consideration, and there has been no public comment on such finding (59 FR 4938). Accordingly, the amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9).
Pursuant to 10 CFR 51.2?(b) no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendment.
5.0 CONCLUS108 The Commission has concluded, based on the considerations discussed above, that:
(1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, (2) such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance of the amendment will not be inimical to the common defense and security or to the health and safety of the public.
Principal Contributor:
W. Long Date: fiarch 7, 1994 l
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