ML20091L024

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Pressurizer Nozzle Level Tap LBB Assessment
ML20091L024
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 12/29/1990
From: Moore K, Ouellette G
BABCOCK & WILCOX CO.
To:
Shared Package
ML19344C240 List:
References
86-E-0074-87, 86-E-74-87, NUDOCS 9201270210
Download: ML20091L024 (4)


Text

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., ewmoao.6 weg h hH L ENGINEERING INFORMATION RECORD Document Identifier 51 __12022n-00 Title ANO-1_Pressuriger Nortle 1,evel Tan LBB Assu n cnL PREPARED BY: REVIEWED BY:

Name c.t h r. Name CA ouellene _

Signature _._d.82M4hc i_._ Date f Signaturedd A/aMM . Date.d2,h.v Technical Manager Statement: initial 4/M$

Reviewer is independent.

R: marks:

1.0 EVff. gig The purpose of this document is to evaluate the potential for Leak-Before-Break in the rem ining ANO-1 precouriser instrument nostles (level taps).

2.0 BAcr.cROUND One of the ANO-1 pressuriser level taps located in the vapor space has been subjected to NDE following discovery of a small leak. An axially oriented crack about 0.4 inch long has been detected in the nozzle bore within- 0.2 inch and 0.6 inch of the end of the nogale.

All seven of these nozzles were fabricated from the same heat of SB 166 Alloy 600s Allegheny Ludlum Steel Corp. Heat No. 26471. This material has a yield strength of 47.5 kai and a carbon concentration of 0.069 w/o.

The baratock was hot rolled and annealed; the annealing temperature has not been determinnd The preliminary review of n.anuf acturing records indicates the nostles were installed prior to stress relief. The stress relief heat treatment ie believed to have been -10 hr at 1100-1150*r.

l Four of these nozzles are located below the normal liquid level; the other 3 are in the vapor space.

The cracking mechanism is strongly suspected to be pure water stress corrosion' cracking (PWsec). PWscc refers to intergranular stress corrosion cracking (ICSCC) in the primary water environment of PWRs. The laboratory demonstration of PWSCC in Inconel 600 was first report.ed by coriou almost 30 years ago. The studies of PWSCC in Inconel 600 have been well documented. However, the mechanism for PWSec in Inconel 600 is still not well understood. In PWRs. PWSCC of Inconal 600 was first reported in steam generator tubing. Laboratory and service experience indicates SCC can be hastened at elevated temperatures. This is believed to be the 9201270210 920121

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l reason the majority of the PWR nozzle f ailures have occurred in pressuris-ers. The evidence also suggests certain (possibly all) product forms of Alloy 600 are susceptible in pressuriser applications. Residual and applied stresses in some instances are sufficient to initis e SCC.

3.0 srRVIcr ExprRIENCE '

There have been numerous f ailures of Alloy 600 pressuriser nozzles and heater sleeves in the U.S. and in Europe. These occurrences have been well documented; one of the most recent updates is contained in a study performed for the B&W Owners Group'. The following is a summary of these occurrences:

1. Southern California Edison detected a small pressure boundary leak on February 27, 1986, in a 3/4-inch diameter pressurazer level instrument nottle at San onofre Unit 3. A PT inspection c! the leak revealed an axial crack that extended from the end of the nozzle inside the pressuciter for a length of 5/8-inch outward through the pressure boundary. The cracked nostle was removed for metallurgical ,

analysis, and the f ailure mechanism was identified as PWsCC; axial, intergranular cracks were observed. The failure has been attributed to an unf avorable material heat treat condition and to environmental conditions, including an operating temperature greater than 650*r.

This nozzle was replaced. In January 1987, southern California Edison decided to replace additional nozzles two upper nottles in the vapor space that were from the same susceptible heat of material. Florida Power & Light has also replaced pressurizer instrument nozzles at St. Lucie Unit 2 (see 3. below); theso were manuf actured from the same heat of material used at San onofre Unit 3.

2. In April, 1987, Arkansas Power & Light discovered leakage from two pressuriser heaters and sleeves at Arkansas Nuclear One, Unit 2. A heater sheath had ruptured, allowing the insulation to swell as a result of the absorbed coolant. This caused the sheath to press against the nearby heater sleeve, which cracked under exposure to the coolant and the resulting increase in stress, subsequent failure analyses of the heater sheaths indicated that PWsCC had occurred and that the material used to f abricate the heater sleeves had characteristics (nonuniform carbide distribution and very little intergranular carbide preelpitation) that would indicate cuecepti-bility to SCC; axial cracks were observed. In addition, these heaters were manufactured by swaging the Alloy 600 tubing onto the heater elements without a final anneal. Thus, the surf ace was cold

'C. A. Quellette and S. Fyfitch, " Alloy 600 susceptibility ccoping study of Components at Crystal River 3." BWNS Document $1-1201160-00, November 29, 1990.

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$1-1202275-00 worked and relatively high residual stresses were imparted to the material. All heaters were replacad, while the sleeves were restored and welds repaired. Boric acid damage below the pressuris-er was also repaired.

3. Four instrumentation nottles at the top of the pressuriser were replaced (with Alloy 600 material believed to be more resistant to pWsCC) at st. Lucie Unit 2 during a refueling outage in october, 1987. Although extensive metallurgical examination was not performed, two of the nozzles were observed to have txial cracks.

These nortles were f abricated from the same material used for the SONGS-3 nozzles (see 1. above), which had a high yield strength and susceptible microstructure; therefore, PWsCC was suspected. Time-to-f ailure estimates were calculated for six remaining Alloy 600 nozzles; these nozzles were left in the system until completion of that current operating cycle, after which it was decided to leave the nozzles in service.

4. In a refue: . ag outage at Shearon Harris in July,1988, two of three steam generators were observed to have boric acid deposits on the lower channel heads. The channel head drain pipes were examined through eddy current testing, and were found to have throughwall, axial cracks up to 1.5 inches long. Residual stresses obtained through a rolling operation (unique to Shearon Harris) were concluded to have made the pipes susceptible to PWsCC. The drain pipes were repaired by cutting each pipe at the outer surf ace, then ,

a coupling (which issued to connect two pipes) was welded to Inconal cladding, which had been applied to the outer curf ace of the steam generator head psnatration area. The two sections of the drain pipe, inside and outside the steam generator, were then reconnected.

5. During a refueling shutdown at Baltimore cas & Electric Company's (BGEE) Calvert Clif f s Unit 2, it was discovered on May 4,1989, that boric acid deposits had accumulated around 20 of-the 120 penetra-tions where the heater sleeves enter the bottom of the pressurizer.

These same 20 heater sleeves were identified by PT indications as ,

failed. Failure analyses performed on two sleeves removed from the '

pressurizer indicate that PWSCC had occurred in the base material.

The racks were axial and confined to a region within 2 inches of the top end of the heater sleeve (at the I.D. of the pressurizer shell). None of these cracks extended across the wall or HAZ.

Again, the heat of material used for fabricating these heater s'eeves was concluded to be susceptible to SCC duo to its micro-structure and initially high yield strength. Also, it is known that the f ailed heater sleeves were reamed during installation which induced residual stresses in the material. The cracks occurred in the reamed area. All 120 sleeves were replaced with heat treated M sy 690 sleeves. some of the sleeves in Unit 1 (which were made ul 4e same heat of material as Unit 2 sleeves) were inspected for W3 1ar cracks, but none were observed; it was determined that Page 3 of 4

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51-1202275-00 although the Unit 2 sleeves were reamed before welding, those at Unit I were teamed af ter the ww1 ding process, and to a lesser degree than the Unit 2 sleeves. Thus, the sleeves at Unit I were concluded to possess a lower degrees of susceptibility to acc.

6. BG&E also detected cracking in a leaking level tap at calvert Clif f a '

Unit 2 using liquid penetrant and eddy current techniques. The cracking in a vapor space level tap was axial and in the same general location as found at SONCS-3 and St. Lucio-2. Axial cracks were detected in 4, 5, and 9 o' clock orientations. The yield strength of the nozzle heat was 36 kei; in this case, its suscepti-bility was attributed to stresses and material conditions caused by the rework (repair welding) required on this nozzle.

7. A number of pressurizer instrumentation nozzles have bo9n reported ,

to have failed at two PWRs in Europe. It has been reported that a susceptible material was used and that the nozzle surf aces were cold worked (in a rolling process); these two conditions were determined to have caused the sec. The cracks were located in the rolled area and predominantly axially oriented. However, some circumferenital cracking was also observed. This was attributed to the rolling operation. Long term plans include the replacement of all Alloy 600 pressurizer penetrations with components made from stainless steel.

4.0 EVALUATION The information presented above is evidence that f ailure of Alloy 600 componente due to PWSCC occurs as a result of the propagation of axial  ;

cracks; no such failures have been attributed to circumferential crack propagation. At the ANO-1 pressurizer nozzle, this axial-crack mechanism is believed to have occurred, resulting in the throughwall crack which initiated at the ID of the nozzle and which was confined within the pressurizer shell-to-nozzle penetration, should PWSCC occur in the other nozzles, all prior experience and the ANO-1 nozzle crack information demonstrate that the cracking will be axially oriented. Thus, given the inherent toughness of Alloy 600 and the location of the nozzle within the shall (confined), a leak-before-break mode of failure would result from the axial crack propagation which is characteristic to PWSCC f ailure.

Each of the failures described above has been attributed to presumebly unique material and/or 13.sta11ation characteristics, similar findings may be rervealed as the iM lure investigation proceeds on the ANO-1 cracked nozzle.

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