ML20050D153

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Leaking Fuel Investigation
ML20050D153
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 04/05/1982
From:
ARKANSAS POWER & LIGHT CO.
To:
Shared Package
ML20050D151 List:
References
NUDOCS 8204120078
Download: ML20050D153 (8)


Text

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ARKAiSAS NUCLEAR ONE UNIT 1 LEAKING FUEL INVESTIGATION J

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ARKANSAS POWER & LIGHT COMPANY 1

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8204120078 820405 PDR ADOCK 05000313 p

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- HISTORY OF FAILURES AND DESCRIPTION OF INVESTIGATION PROGRAM

- CONCLUSIONS OBTAINED TO DATE 1

- AP&L PLANS FOR FUTURE EVALUATIONS e

_____________._______________m_,_

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- CONCLUSIONS -

FAILURES NOT MAliUFACTURING RELATED NO INDICATION OF PELLET-CLAD INTERACTION RELATED PHENOMENA MOST PROBABLE CAUSE IS SOME FORM OF EXTERNAL CLAD ATTACK i

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RESULTS OF MANUFACTURING INVESTIGATION

. NO BURNUP DEPENDENCY

- TYPICAL MANUFACTURING RELATED FAILURES ARE SEEN EARLY IN FUEL LIFETIME

- SIMULTANEOUS NATURE OF FAILURES IS INCONSISTENT WITH MANUFACTURING CAUSES

, NO BATCH DEPENDENCY

- 9 BATCH 6

- 6 BATCH 5

- 9 BATCH 4

. NO CORRELATIONS BETWEEN ANY MANUFACTURING RELATED ATTRIBUTES

- NO UNUSUAL INFORMATION FOUND IN EXAMINATION OF RECORDS

  • POWDER
  • PELLETS
  • CLADDING V

- RESULTS OF PCI EVALUATION -

. TYPICALLY PCI OCCURS AS A FUNCTION OF BURNUP AND POWER RAMPS

- ANO-1 LEAKER BURNUP DISTRIBUTION

<2 MWD /T 9

ASSM.

7.6 -

9.1 MWD /T 2

ASSM.

11.4 - 13.7 MWD /T 4

ASSM.

13.7 - 19.0 MWD /T 2

ASSM.

19.8 - 21.4 MWD /T 7

ASSM.

- NO UNUSUAL TRANSIENTS DURING OPERATION

- PLANT OPERATED CONTINUOUSLY 30 DAYS BEFORE LEAKS OCCURRED

- NO SIGNIFICANT ROD MOVEMENTS OR MAJOR SYSTEM IMBALANCES

- REACTOR STARTUPS WERE WITHIN ESTABLISHED SAFE GUIDELINES

. INSPECTION DID NOT REVEAL PCI EFFECTS

- NO UNEXPECTED RIDGING DETECTED FROM DIAMETER MEASUREMENTS

- VISUALLY OBSERVED CLADDING SPLITS WERE NOT INDICATIVE OF PCI

- INTEGRITY OF BURNABLE POISON RODS INTACT l

IDENTICALLY DESIGNED B&W FUEL HAS NO IDENTIFIED PCI FAILURES UNDER SIMILAR OPERATING C0flDITIONS EXPERIMENTAL RAMPING PROGRAMS HAVE NOT RESULTED INPCIUllDERM6RESEVEREOPERATINGCONDITIONS 4

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- CONSIDERATIONS INDICATING EXTERNAL ATTACK -

. NO EVIDENCE OF INTERNAL ATTACK

. NOT IMPOSSIBLE FOR TRANSIENT TO OCCUR OR AGENT TO HAVE ENTERED SYSTEM AT TIME OF FAILURE AND NOT BE DETECTED BY END OF CYCLE WHEN INSPECTIONS WERE PERFORMED

. SIMULTANEOUS NATURE OF FAILURES AND LACK OF BATCH OR BURNUP DEPENDENCE NOTE:

INSPECTIONS OF CHEMISTRY RECORDS HAVE NOT YIELDED ANY EVIDENCE OF ABNORMAL CONDITIONS, I

... ~

FURTHER WORK TO ESTABLISH THE EXACT NATURE OF THE ATTACK IS UNWARRANTED

. PROBABILITY OF SUCCESS VERY LOW AFTER EXTENDED REACTOR AND FUEL RESIDENCE TIME

. THROUGH WALL CRACKS WOULD HAVE EXPERIENCED MASKING DUE TO OXIDIZING, HYDRIDING AND OTHER EFFECTS

. NO CERTAINTY AS TO PRIMARY OR SECONDARY DEFECTS

. INCIPIENT DEFECTS WOULD BE DIFFICULT TO LOCATE

, ADDITIONAL COST CANNOT BE JUSTIFIED

. ACTIVITY LEVELS WERE BELOW TECH SPEC LIMITS

. PRESENT ACTIVITY LEVELS INDICATE NO ADDITIONAL FAILURES

.I

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