Nuclear Svc Site Ofc Rept 59 for 770916-1009ML20085A480 |
Person / Time |
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Site: |
Davis Besse, Three Mile Island |
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Issue date: |
10/10/1977 |
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From: |
Faist F BABCOCK & WILCOX CO. |
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To: |
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References |
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TASK-05, TASK-06, TASK-07, TASK-11, TASK-5, TASK-6, TASK-7, TASK-GB GPU-0487, GPU-487, NUDOCS 8307060524 |
Download: ML20085A480 (5) |
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Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20236W9961998-06-0909 June 1998 1998 Quadrennial Simulator Certification Rept ML20217P8041998-04-0707 April 1998 11RFO OTSG ECT Insp Scope ML20210P4461997-08-31031 August 1997 Update 2 to TMI-2 Post-Defueling Monitored Storage Sar ML20210T3411997-08-31031 August 1997 Rev 0 to TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20199E5841997-08-18018 August 1997 Limited Liability Company Agreement of Amergen Energy Co, LLC Among PECO Energy Co,British Energy PLC & British Energy,Inc ML20133D8771996-12-23023 December 1996 Rev 2 to TMI-1 Evaluation of Thermo-Lag Fire Barriers ML20196B8951996-12-16016 December 1996 First Amended & Restated Master Decommissioning Trust Agreement Dtd as of 961216 Between Cleveland Electric Illuminating Co & Mellon Bank ML20196B8771996-12-16016 December 1996 First Amended & Restated Master Decommissioning Trust Agreement Dtd as of 961231 Between Toledo Edison Co & Mellon Bank ML20137F1301996-08-27027 August 1996 Rev 0 to Auxiliary Bldg Sump Sludge Prevention (Regulatory Required) ML20117H6621996-07-20020 July 1996 Rev 1 to TR 094 TMI-1 Evaluation of Thermo-Lag Fire Barriers ML20129G9291996-06-17017 June 1996 TMI-1 Reload Design & Setpoint Methodology ML20134D7821996-05-0808 May 1996 Rev 1 to Instrument Drift Data Analysis Methodology & Assumptions ML20148F0831996-04-0202 April 1996 Rev 0 to EDG 1B Air Start 2 Reservoir Tank ML20148F0611996-04-0202 April 1996 Rev 0 to SQ-TI-EG-T-0001B-1, EDG 1B Air Start 1 Reservior ML20098B1291995-09-19019 September 1995 Rev 1 to Pages 3 & 30 of TMI-1 USI A-46 Seismic Evaluation Rept ML20091S4311995-08-31031 August 1995 USI A-46 Seismic Evaluation Rept. W/61 Oversize Drawings ML20100L6581995-05-25025 May 1995 Div 1/2 Mod Design Description for New TMI-1 Radwaste Demineralizer Sys Three Mile Island Unit 1,Nuclear Generating Station, Rev 2 ML20087J5281995-05-11011 May 1995 Nonproprietary Page 2 of TMI Unit 1 USI A-46 Seismic Evaluation Rept ML20082G4191995-03-22022 March 1995 Rev 0 to Topical Rept 093, TMI-1 Reactor Bldg Twenty Yr Tendon Surveillance (Insp Period 6) ML20082Q8051995-03-10010 March 1995 TMI-1 Core Thermal-Hydraulic Methodology Using VIPRE-01 Computer Code ML20082G4441995-02-22022 February 1995 Vols I & II 20th Yr Physical Surveillance of TMI-1 Containment Bldg ML20100L6321994-08-0303 August 1994 Shipment of Miscellaneous Waste Evaporator Concentrates ML20138J1411994-02-28028 February 1994 Rev 0 to IPEEE,A-46 & Design In-Structure Response Spectra for Selected Bldgs at Dbnps ML20059M2181993-11-30030 November 1993 Amend 19 to Pdms Sar ML20148F1011993-10-28028 October 1993 Rev 0 to Air Accumulator for FW-V-16B ML20148F0931993-10-28028 October 1993 Rev 0 to Air Accumulator for FW-V-16A ML20059F0471993-08-31031 August 1993 Amend 18 to Post-Defueling Monitored Storage (Pdms) Sar. W/Rev 2 to List of Pdms Requirements & Commitments ML20067D3311993-08-31031 August 1993 Technical Evaluation Rept,Evaluation of B&Wog Pressurizer Surge Line Thermal Stratification Program to Address NRC Bulletin 88-11 ML20056E5921993-07-31031 July 1993 Conservative Design In-Structure Response Spectra for Resolution of USI A-46 for Tmi,Unit 1 ML20059D7351993-02-0707 February 1993 Review of Offsite Response to Site Area Emergency Incident at Three Mile Island Nuclear Station ML20126D2831992-12-18018 December 1992 Criticality SAR for TMI-2 Reactor Vessel ML20114B9631992-08-0808 August 1992 Rev 3 to Criticality Safety Evaluation of TMI Fuel Storage Facilities W/Fuel of 5% Enrichment ML20058F6561992-07-31031 July 1992 Companion Sample Exams ML20058F6481992-01-31031 January 1992 Metallographic & Hardness Exams of TMI-2 Lower Pressure Vessel Head Samples ML20091P5721991-10-31031 October 1991 Reactor Containment Bldg Integrated Leak Rate Test Including,Type A,B & C Periodic Test Results ML20070Q1911991-03-25025 March 1991 NRC Form 474 Simulation Facility Certification ML20066K3591991-01-31031 January 1991 Rev 0 to Rept on 1990 Eddy Current Exams of TMI-1 OTSG Tubing ML20216K1251990-10-31031 October 1990 Amend 9 to Post-Defueling Monitored Storage Sar ML20217A4251990-09-11011 September 1990 Rev 3 to Licensing Rept for Spent Fuel Pool Mod of Pool a: TMI Unit I ML20058L1891990-08-0101 August 1990 Dcrdr Human Engineering Discrepancy Repts 1988 Summary Addendum 1,Vol 1 ML20058M7251990-08-0101 August 1990 Rev 2 to Div Technical Evaluation Rept for Processed Water Disposal Sys ML20056A0091990-07-26026 July 1990 TMI-1 Trust Agreements ML20043A2341990-05-0202 May 1990 Rev 0 to TMI-1 Reactor Bldg 15-Yr Tendon Surveillance (Insp Period 5). ML20055C9461990-03-31031 March 1990 Final Rept, TMI - Unit 2 Safety Advisory Board, for Mar 1981 - Dec 1989 1999-08-31
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20195H0751999-06-0808 June 1999 Drill 9904, 1999 Biennial Exercise for Three Mile Island ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209G0351999-05-31031 May 1999 TER on Review of TMI-1 IPEEE Submittal on High Winds,Floods & Other External Events (Hfo) ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With ML20210C0161999-03-0101 March 1999 Forwards Corrected Pp 3 of SECY-98-252.Correction Makes Changes to Footnote 3 as Directed by SRM on SECY-98-246 ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20207A9291998-12-31031 December 1998 1998 Annual Rept for TMI-1 & TMI-2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20196G4661998-12-31031 December 1998 British Energy Annual Rept & Accounts 1997/98. Prospectus of British Energy Share Offer Encl ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20203G1211998-10-30030 October 1998 Informs Commission About Staff Preliminary Views Concerning Whether Proposed Purchase of TMI-1,by Amergen,Inc,Would Cause Commission to Know or Have Reason to Believe That License for TMI-1 Would Be Controlled by Foreign Govt ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20155E7511998-10-15015 October 1998 Rev 1 to Form NIS-1 Owners Data Rept for Isi,Rept on 1997 Outage 12R EC Exams of TMI-1 OTSG Tubing 1999-09-30
[Table view] |
Text
-
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' BABCOCK & WILCOX
. Md E7.rcli Q2 7FD' LID [!!T NUCLEAR SERVICE
.3 &tl. A. C' DDL"J' J SITE OFFICE REPORT- T3.3.1
. pg g P2 PORT NUISER j59 . DATE 10/10/TT U.R -M Edisen Cencany LOCATION / UNIT Davis-3 esse Unit I : , _. /) , p OP EATIC55191*ACER Y Fred R. Faist Fred R. Faist u I *:GP SCFIDULE RCS HYDRO S C g let MHFT g hg FUELLOADg%%7 100% FP gags.te4 i SII".;TE 1 Sta* T Fi .ish lRCS HYDRO 9/UT6 HFI 3.inish
/10/77 FUEI. I,0ADg737777 ,100% FP y773
.T I::CLUSIVE DATES 9/16/77 - 10/9/77 -
. TNMEr, 15 TO INCLLJE THE FOLLOUING INFORMATION: MAJOR EVENTS, ACTIVITIES, PROBLEMS, SCHEDULE,
- 9;ca IvE TS: .
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1 Plant at 532*F 2155 psig on 9/16/77, all (18) Main Steam'SafetIy Valves (Dresser) reset. ~~~
) 2. CRDM stator in location N-8 determined to have failed. Stator changed out with spare on 9/16/77 - 9/19/77.
- 3. ~.eactor critical on 9/19/TT. Turbine on line with 2x power apprcxi=ately 155 entire ;
veek. .
l 4
Tests completed at 15%, Unit Load Steady State, TP 800.12; Core Pcver Dist:ibution, TP 800.11; Incore Detector Test, TP 800.24
- 5. 9/2h/77 - Plant experienced an uncontrolled rapid depressurization due to PZR electrenatic relief valve sticking open. See' details below. Plant in r.aintenance j outa$e through 10/10/7T.
l ACTIVITIES:
l.
1 On 9/16/77 all 18 Main Steam Safety Valves (Dresser) were reset. Valves were fcund to be set lov (as =uch as 50 psig) pr* =-117 due to high room temperature and an error in the hydroset curves supplied by Dressen. SPR 363.
- 2. Failed Stator - S?R 365 - On 9/16/77, the CROM stator in location N-8 was dete s ~e to have an internal short between 3 is C phases. Atte= pts to d y out stater failed end on 9/17/77 preparations were in progress to change the stater cut with a spare in the CTIC b1dg.
i RCS vas at 532*F, 2155 psig, as:1 a decision to ecolde ~ to 360 -
380*F was made to reduce heatup rate on the CRDM stators with cooling v=cer secured.
Prchlens with seating the new stater, ?I tube adjustment, fining COJ 1eaks end in-l experienced, unfa=iliar =aintenance personnel extended the jcb until 9/19/77. During the PI tube adjustnent, =sintenance d'.= aged the threads and helicoil on the PI tube and hc.i to send a =echenie into the service structure to re=cve the helicoil frc=
the PI positiening stud en the stacor. SPR #36h. Scb $nith of DP3Co on si:e to 0' assis t.
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- Site Office Report #59 620-0014
- October 10, 1977 Page 2 0 .
- 3. Plant Testing -
- a. Reactor achieved criticality on 9/19/7T. Core Pcver at 15% on 9/20/T7, 0600.
Generator output approxi=ately 100 W. Only 1/2 the cire water syste= vas operable (only 1/2 the condensor available). ,,
- b. Turbine Overspeed Trip on '9/20/T7 vith the reactor at 75 FP. Three atte= pts were =ade, all unsuccessfcily. Adjustments vill be =ade and further atte= pts vill be cade after physics testing at 15%.
- c. Reactor returned to 15% FF on 9/21/TT, 0330, 'avaiting equilibriu= Xenen for core power distribution. During this time period, perfor=ed the fol. lowing:
- 1. NSS Heat Balance , TP 800.22, results acceptable. ,
- 2. NI Calibration, TP 800.02, results acceptable. -
- 3. Unit Load Steady State, TP 800.12 (data being reviewed).
- h. Core Power Distribution, TP 800.11, results- acceptable.
~
- 5. Incore Detector Test, TP 800.24, results acceptable.
- 6. ICS Tuning, TP 800.08, to be continued on return to power.
L. RCS - rapid depiessurication O o= 9/2'/TT. 1eco, a te - 1e x betwee= *se *==*t=e e-ver='r v 1ve e= a= *==bi=e oce. red, necessitating turbine shutdevn. Reactor power /as being reduced to 6 - 7% power (re=ain in Mode 1) until stea= leaks could be repaired.
APproximately 213k on 9/2h/TT, with reactor 'at 9% FP - the following sequence of events occurred:
- a. SFRCS for unkncvn reasons shut the S/U W control valve to #2 0'ISG.
- b. #2 OTSG level dropped causing RCS Tave, pressure to incre'ase. SFRCS actuated on lov OTSG level. ,
- c. SFRCS actuation bottled up both OTSG's initiating Aux. N to both. '!he Aux.
W pu=p to #2 OTSG failed to ec=e up to speed due to gove=nor prcble=s , thus causing #2 CTSG to go dry.
- d. PZR level reached 290 in. and the reactor was tripped =anually.
- e. Prior to reactor trip, the RCS pressure had increased to greater than 2255 psis, causing the electrc=stic relief valve to open. A seal-in relay was later deter-r.ined to be missing frc= the relay cabinet, thus causing the valve to cycle cpen and closed abouc 2255 psig. It was deter =ined that the valve cycled 9 times within h5 see. before the pilot valve was da= aged causing the electrc=atic re'.icf to stick open. ,
- "P.'~R7I.GI dI O.- '
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Site Office Report #59
, . 620-0014 October 10, 1977 '
Page 3
- f. RCS pressure decreased and at 1600 psig, the SFAS actuated. CD2 isolation and h?I. Isolating = cst of the CT:C cut off cooling vater to the Quench Tank.
,; . With the electro =atic relief valve still open, and the Quench Ta=k unable to quench stes=, the quench tank rupture disc blev out da= aging a ventilating duct and blowing approx 1=ately 200 sq. ft. of mirror insulation off the OTSO.
- h. An esti=ated 20 =inutes vent by before the electro =atic relief isolation block val.re was closed.
- i. During the transient, 2 RCP's were tripped le'aving a 1/1 co=bination, HPI was secured and restated, two =akeup pu=ps were operating si-"Ttaneously t
during par.t of the ti=e, PZR level indication vent greater than 320 in, and as 1cv as 10 in. Approxi=ately 6000 - 8000 gallons du= ped into CDE. .
RCS pressure /te=perature was such, that stea= for=ed in th'e RCS loops , co=-
ponents, etc. -
Da=are:
a., Quench Tank rupture disc.
b Ventilating duct.
O e. orso 1= u1 *1e=-
- d. PZR heater cables (high hu=idity - lov =eggar readings).
- e. Potential danage to EW supplied equipr.ent, such as =ajor co=ponents, RCP, RCPM, RCP seals, etc. , has been evaluated and deter =ined not to be a proble=,
however, =ccitering of RCP perfor=ance during startup vill be required. See SPR's 369 and 372 for details.
Meetings between TICo/3G/NRC vere conducted to revbv th 1 transient. NRC re-stricted DB-I to operatien below 200'F (less than Mode h; until all proble=s could be resolved. On 10/7/77, NRC released DB-I to startup.
- 5. RCP Initial Runs after transient: .
3-J representatives and John De=psey of BW vere on site 10/5/77 -.10/7/77 to 4
vitness ths initial RCP runs after the transient. RCS pressure approxi=ately 225 pais, te=perature approximately 100'F, a series of short RCP runs were con-ducted on all h RCP's. Data fr== these runs indicated goed RCP seal perfor--ce.
Salance of RCP data to be taken when RCS is greater than 1300 psig.
- 6. Makeup and Purification Pu=ps:
On 10/8/77 and,10/9/77, atte= pts to run a =akeup pu=p .resulted in va*- 'ad age out the inboard seal. This seal had just been replaced by TECo maintencace the previous veek. The seal was i= properly installed, an "C" ring had be.en rolled -
during installation. P.:=p vas declared operable en 10/10/77, in preparation to h run RCP's for hen up. !.'U ~'u :p proble= vas an offspring of the bearing housing oil lech prcble= reported in SpH 368.
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. 620-0014 October 10, 1977 Page 4 0 .
- 7. Feedvater Cleanup started on 10/6/77.
- 3. Ceeputer Repairs -
During the past several.veeks, the 855 had been stalling and reinitiallising frequently. The outage during the last two weekn pe:mitted I&C and BMCo per-sonnel to take the computer out of service to locate proble=s , replace " marginal" IC chips , r.odules , etc. Troubleshooting vill continue into the week of 10/10/77 On 9/22/77, proble=s with the NSS calculations, PDO, delayed physics testing Approxi=stely 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
PROBI.D'S
- 1. SPR 372 - for the past two weeks the major problem has been t:-Ag to reconst: tet, evaluate the transient that occurred on 9/2k/77. NRC has per=itted DB-I to start up, however, TECo made several co==itt=ents in order to obtain this pe=ission.
- 2. :.7-1 Source Range Instru=entatica - during the past two veeks the source range'has failed icv 3 or k ti=es. The count rate amplifier was changed out , but the results
.ere the sa=e - TECo is setting up monitoring equip =ent to dete=ine cause.*SPR 342.
(M.
v SPR's - Status Since Previous Report - -
- a. Eleven (11) new SPR's have been written:
- 363 - S. G. Code Relief Setpoint Drift '
- 364 - Da= aged Threads & Helicoil on PI Tube & Stator ~
- 365 - Short in CRDM Stator at N-8
- 366 - Errors in CRDM Manual Use of Wrong Lube *
- 367 - Reactor Trip
- 368 - 011 Leak en M.U. Pu=p Bearing Rousing
- 369 - Electrc=atic Relief valve Damage ,
- #370 - Rose =ount k1hE & 414F RTD Bridges
- 371 - FC #97 Installation
- 372 - SFRCS Trip / Reactor Trip / Coolant Spill
- 373 ' Inboard Water Seal Le**g -
- b. Seven (T) SPR's have been cleared. *
- c. Sixty-five (65) re=ain open.
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' Site Office Report #59 620-001h October 10, 1977
, . Page 5 SGEOULE 1.
Reactor Critical - estimated 10/12/TT 2
Finish 15% power testing, including turbine overspc .d tr'.p te$ ting, unit shutdevn test, - anticipated completion 10/14/77.
3.
PES to h05 pcver to start 10/16/TT. Reach h0% power 10/19/77.
FEFf0ZEL F. R. Fais t , SOM I. D. Green, ROE
- 2. L. Flood, Sec'y. -
J. E. Anderson .
- 3. F..Snith ....
C. C. England ,
1 L. Nelson D. L. Allison D. 2. Shaffer, 3MCo PSS
, psTS TOPS bei -
9/16/77 +- Bin Nielsen, 3&W, reactimeter operator 9/1T/TT - Mike Boesch, 3MCo, computer 9/18/TT.- Bob S=ith, DPSCo, service .CarM .
9/21/TT - Garden Markley, B&W, inspection .
9/2k/TT - Mike 3cesch, BMCo, computer 9/27/TT - Norm Infott, 3&W, audit for Isley-9/27/77 - W. R. Conroy, Crosby Valve, service 9/27 & 28/TT - J. J. Keny, 3&W, data evaluation .
9/29/77 & Joe Lauer, George Meyer, John Dempsey, Art McBride, 9/30/77 '
Frank Levendoski - all B&W - meeting with. TICo on SFRCS 10/3/TT - W. D. Ssith, 3MCo - computer service 10/3/77 - Roger Kunes, EMCo - co=puter service (still on site).
i 10/k/TT - Tis Grubaugh, 3MCo - service (meeting with PSS).
10/5/TT - W. J. Lollis, 3.J. Pu p - service -
10/5/TT - Larry Wong, B.J. P=p - service .
10/7/TT - Carl roledzy, 3&W, = aster services
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