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On 01/01/86 at 0354 thgyunit scrammed from 19 percent power on low reactor water level (level 3).
The low level scram was a result of isolations on both low pressure feedwater heater strings coincident with a failure of the low pressure feedwater heater bypass valve to open.
At 0356 Reactor Core Isolation Cooling was started and used to restore level prior to reaching the initiation level for High Pressure Core Spray.
An investigation into the event was conducted.
It was determined that the probable cause for the isolations was flashing in the level transmitter pots causing high level spikes.
It is believed that the failure of the bypass valve to open was a result of thermal binding causing the motor operator circuit breaker to trip on overload.
There were no safety consequences or implications to the public as a result of this event.
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Aaaovie owe so n-cie.
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, Aot 43' 885*8%*k vgan RIVER BEND STATION 0l0l1 0l1 01 2 0F 0 l3 o ls to lo lc l 4l5 l8 8l 6 rm,-
.ac e u nn On 01/01/86 at 0354 the unit scrammed from 19 percent thermal power on low level (level 3) due to a loss of all feedwater flow.
Apparently a spurious high-high level in the
'A' Sth point low pressure feedwater heater (*HX*) tripped causing condensate flow to the
'A' string to I
isolate.
The
'B' low pressure heater string had previously isolated and gone undetected. It is believed to have been caused by a similar l
spurious signal which may have caused the
'A' heater string to isolate.
The low pressure heater string bypass valve (*V*) failed to I automatically open on either
'A' or
'B' heater string isolation.
Its breaker (*BXR*) was found tripped.
This resulted in a complete isolation of condensate flow to the feed pumps
(*P*) and a loss of feedwater flow to the vessel.
The feedwater pumps are designed to trip on low suction pressure; however, feedwater pump
'A' failed to trip and ran for approximately five minutes before condensate flow was restored.
At 0356 the Reactor Core Isolation Cooling (RJIC)
(*BN*)
l system was started and used to rectore level prior to reaching the initiation level for High Pressure Core Spray (HPCS
(*BG*).
l l
Upon thorough investigation of all associated feedwater heater train instrumentation and logic, with no apparent problems discovered, it was determined the probable cause to be flashing in the level transmitter (*LT*) pots causing high level spikes.
Failure of the low l pressure heater string bypass valve to open was also investigated.
It is possible that during system heat up the bypass val.ve may have thermally bound and caused the motor (*MO*) overload.
l Corrective action has been taken to ensure condensate pots for level transmitters are filled.
These level transmitters have been instrumented with a strip recorder (*LR*) to monitor for similar l
occurrences.
The low pressure heater bypass valve motor overload has been reset from its lower current setting to its upper setpoint.
Additionally, General Operating Procedure (GOP)-0001 "Plant Startup to l Low Power Alarm Point" has been revised to require the bypass valve to be left in the open position until approximately 15 percent power to prevent valve binding during system heatup.
Finally, human factors design changes have been initiated via Modification Requests (MRs) l 86-0015, 0016, and 0017 to highlight heater level alarms and trip indicators for the heater bypass valve.
MR 86-0015, highlighting the heater level alarms, was completed on 8/20/86.
System performance has been satisfactory since completion of the MR.
MRs 86-0016, installation of indicating lights for out of service feedwater system, and 96-0017, a trip indicator for heater bypass valves, has been re-evaluated considering the additional huraan factors draign change.
Based on the decreased probability for human error af ter imnlementation of MR 86-0015 and satisfactory system performance since the reported event, these additional modifications have been determined to be unnecessary and will not be imp.1.emented at this time,
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w i ms4unn There were no safety consequences or implications to the public because the unit was placed in a safe shutdown condition, and water level was quickly restored via the RCIC system.
Furthermore, redundant Emergency Core Cooling Systems (ECCS) were available at all times as an additional source of coolant if necessary.
NOTE:
Energy Industry Identification System Codes are idertified in the test as (*XX*).
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O GULF STATES UTILITIES COMPANY RfVfR BEND STAfiON POST OFFICE Bor 220 ST FRANCISvitLE LOutSIANA '0775 ARE A CODE 504 635 6094 346-8651 June 24, 1988 RBG-28161 File Nos. G9.5, G9.25.1.3 l
U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C.
20555 Gentlemen:
River Bend Station - Unit 1 Docket No. 50-458 Please find enclosed Licensee Event Report No.86-001 Revision 1 for River Bend Station - Unit 1.
This report is being submitted to provide updated information on corrective action.
Sincerely, f.
s J. E.
Booker Manager-River Bend Oversight River Bend Nuclear Group cc:
U.S. Nuclear Regulatory Commission 611 Ryan Plara Drive, Suite 1000 Arlington, TX 76011 NRC Resident Inspector P.O. Box 1051 St. Francisville, LA 70775 INPO Records Center 1100 Circle 75 Parkway Atlanta, GA 30339-3064 I
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| 05000458/LER-1986-001, :on 860101,unit Scrammed from 19% Power on Low Reactor Water Level as Result of Isolations on Both Low Pressure Feedwater Heater Strings.Probably Caused by Flashing in Level Transmitter Pots |
- on 860101,unit Scrammed from 19% Power on Low Reactor Water Level as Result of Isolations on Both Low Pressure Feedwater Heater Strings.Probably Caused by Flashing in Level Transmitter Pots
| | | 05000458/LER-1986-002, :on 860101,total Loss of Offsite Power Occurred When Transformers A,B,C & D Tripped.Caused by Spurious Signals from Hand Held Radios.Shielding on Tone Relaying Equipment Being Installed |
- on 860101,total Loss of Offsite Power Occurred When Transformers A,B,C & D Tripped.Caused by Spurious Signals from Hand Held Radios.Shielding on Tone Relaying Equipment Being Installed
| | | 05000458/LER-1986-003, :on 860101 & 04,unauthorized Jumper Found in Main Control Room Panel 1413-P623 & Unauthorized Lifted Lead Found in Panel 1413-P951,respectively.Cause Undetermined. Affected Sys Immediately Restored |
- on 860101 & 04,unauthorized Jumper Found in Main Control Room Panel 1413-P623 & Unauthorized Lifted Lead Found in Panel 1413-P951,respectively.Cause Undetermined. Affected Sys Immediately Restored
| | | 05000458/LER-1986-004, :on 860103,inadvertent ESF Initiation of Standby Svc Water Sys Occurred.Caused by Electricians Accidentally Striking Switchgear Panel Causing Relay to Close.Relays Reset & Sys Returned to Normal |
- on 860103,inadvertent ESF Initiation of Standby Svc Water Sys Occurred.Caused by Electricians Accidentally Striking Switchgear Panel Causing Relay to Close.Relays Reset & Sys Returned to Normal
| | | 05000458/LER-1986-005, :on 860107,fire Protection Water Curtain Inadvertently Actuated Overloading Floor Drian Sys.Caused by Const Employee Mistaking Solenoid Actuation Switch for Door Latch.Switch Properly labeled.W/870909 1tr |
- on 860107,fire Protection Water Curtain Inadvertently Actuated Overloading Floor Drian Sys.Caused by Const Employee Mistaking Solenoid Actuation Switch for Door Latch.Switch Properly labeled.W/870909 1tr
| | | 05000458/LER-1986-006, :on 860110,discovered Maint Activities Performed on Feedwater Testable Check Valve W/O Performance of Operability Test Prior to Returning Valve to Svc.Caused by Personnel Error.Valve Successfully Tested |
- on 860110,discovered Maint Activities Performed on Feedwater Testable Check Valve W/O Performance of Operability Test Prior to Returning Valve to Svc.Caused by Personnel Error.Valve Successfully Tested
| | | 05000458/LER-1986-007, :on 860115,automatic Reactor Scram Occurred on High Water Level While Attempting to Line Up Feedwater Train B.Caused by Feedwater B Regulator Valve Open W/Controller Indicating Zero Demand |
- on 860115,automatic Reactor Scram Occurred on High Water Level While Attempting to Line Up Feedwater Train B.Caused by Feedwater B Regulator Valve Open W/Controller Indicating Zero Demand
| | | 05000458/LER-1986-008, :on 860107,unqualified Wiring Connecting Control Components in Limitorque Motor Operator Discovered. Caused by Design Change.Valves Declared Inoperable & Wiring Replaced W/Qualified Rockbestos Wire |
- on 860107,unqualified Wiring Connecting Control Components in Limitorque Motor Operator Discovered. Caused by Design Change.Valves Declared Inoperable & Wiring Replaced W/Qualified Rockbestos Wire
| | | 05000458/LER-1986-009, Corrected LER 86-009-00:on 860114,radwaste Liquid Effluent Monitor Sample Pump Not Started During Radioactive Liquid Discharge.Caused by Miscommunication & Procedure Ambiguities.Procedures Revised | Corrected LER 86-009-00:on 860114,radwaste Liquid Effluent Monitor Sample Pump Not Started During Radioactive Liquid Discharge.Caused by Miscommunication & Procedure Ambiguities.Procedures Revised | | | 05000458/LER-1986-010, :on 860116,RWCU Isolation Occurred While Performing Surveillance Test Procedure During Cold Shutdown. Caused by Blown Control Power Fuse When Test Jumper Accidentally Grounded.Fuse Replaced |
- on 860116,RWCU Isolation Occurred While Performing Surveillance Test Procedure During Cold Shutdown. Caused by Blown Control Power Fuse When Test Jumper Accidentally Grounded.Fuse Replaced
| | | 05000458/LER-1986-011, :on 860120,Tech Spec Action Required Sample for Hydrogen Downstream of Recombiners of Offgas Treatment Sys Missed.Caused by Changed Lock on Door to Sample Station. Sampling Performed & Personnel Counseled |
- on 860120,Tech Spec Action Required Sample for Hydrogen Downstream of Recombiners of Offgas Treatment Sys Missed.Caused by Changed Lock on Door to Sample Station. Sampling Performed & Personnel Counseled
| | | 05000458/LER-1986-012, :on 860120,security Notified Control Room That Roving Fire Watches Not Entered in Two Remote Shutdown Panel Rooms for Several Hours.Caused by Personnel Error.Fire Watch Reestablished |
- on 860120,security Notified Control Room That Roving Fire Watches Not Entered in Two Remote Shutdown Panel Rooms for Several Hours.Caused by Personnel Error.Fire Watch Reestablished
| | | 05000458/LER-1986-013, :on 860127,main Steam Line Area Temp Detector 1LDS*RTD4C Failed Channel Check & Declared Inoperable. Caused by Procedure Incorrectly Reflecting Tech Spec Requirements.Procedure Revised |
- on 860127,main Steam Line Area Temp Detector 1LDS*RTD4C Failed Channel Check & Declared Inoperable. Caused by Procedure Incorrectly Reflecting Tech Spec Requirements.Procedure Revised
| | | 05000458/LER-1986-014-01, :on 860128,inadvertent Div 1 Diesel Generator & Standby Gas Treatment Sys Initiation Occurred.Caused by Interruption of Neutral Daisy Chain.Maint Procedure GMP-0042 Revised |
- on 860128,inadvertent Div 1 Diesel Generator & Standby Gas Treatment Sys Initiation Occurred.Caused by Interruption of Neutral Daisy Chain.Maint Procedure GMP-0042 Revised
| | | 05000458/LER-1986-015, :on 860131,containment HVAC Purge Exhaust Valves Failed Local Leak Rate Test.Cause Not Stated.Valve Seats Replaced & Penetration Successfully Retested |
- on 860131,containment HVAC Purge Exhaust Valves Failed Local Leak Rate Test.Cause Not Stated.Valve Seats Replaced & Penetration Successfully Retested
| | | 05000458/LER-1986-017, :on 860205,nonseismically Qualified Tubing Installed in Penetration Valve Leakage Control Sys.Caused by Procedural Deficiency.Tubing Removed,Procedure Revised & Acceptable Designs Installed |
- on 860205,nonseismically Qualified Tubing Installed in Penetration Valve Leakage Control Sys.Caused by Procedural Deficiency.Tubing Removed,Procedure Revised & Acceptable Designs Installed
| | | 05000458/LER-1986-019, :on 860212,turbine Trip/Reactor Scram Occurred from Feedwater Heater Level Problems.Caused by Incorrect Setpoints & Controllers Did Not Respond Efficiently to Level Fluctuations.Setpoints Corrected |
- on 860212,turbine Trip/Reactor Scram Occurred from Feedwater Heater Level Problems.Caused by Incorrect Setpoints & Controllers Did Not Respond Efficiently to Level Fluctuations.Setpoints Corrected
| | | 05000458/LER-1986-021, :on 860301,unit Automatically Scrammed on Low Reactor Water Level.Caused by Transformer Fault & Voltage Transient.Mods to Transformer Encls at Cooling Towers Implemented to Add Addl Walls & Covers |
- on 860301,unit Automatically Scrammed on Low Reactor Water Level.Caused by Transformer Fault & Voltage Transient.Mods to Transformer Encls at Cooling Towers Implemented to Add Addl Walls & Covers
| | | 05000458/LER-1986-022, :on 860312,w/unit at 42% Reactor Power,Full Reactor Scram Occurred.Caused by Pressure Spike in Instrument Line.Station Operating Procedure SOP-0011 Revised |
- on 860312,w/unit at 42% Reactor Power,Full Reactor Scram Occurred.Caused by Pressure Spike in Instrument Line.Station Operating Procedure SOP-0011 Revised
| | | 05000458/LER-1986-024, :on 860325,ESF Actuations Occurred Due to Breaker Failure.On 861224,power to Reactor Protection Sys Bus B Lost Due to Spurious Breaker Trip Resulting in half- Scram.Caused by Malfunctioning Logic Card |
- on 860325,ESF Actuations Occurred Due to Breaker Failure.On 861224,power to Reactor Protection Sys Bus B Lost Due to Spurious Breaker Trip Resulting in half- Scram.Caused by Malfunctioning Logic Card
| | | 05000458/LER-1986-025, :on 860326,RHR Sys Isolation Occurred.Caused by Inadvertent Shorting of Bypass Jumper to Adjacent Test Lead During Performance of Surveillance Test Procedure.Sys Returned to Svc |
- on 860326,RHR Sys Isolation Occurred.Caused by Inadvertent Shorting of Bypass Jumper to Adjacent Test Lead During Performance of Surveillance Test Procedure.Sys Returned to Svc
| | | 05000458/LER-1986-027, :on 860403,reactor Protection Sys Actuation Occurred Due to Loss of Bus B Control Power.Caused by Blown Power Fuse in Elgar Rectifier.Mod of Internal Control Circuits Initiated |
- on 860403,reactor Protection Sys Actuation Occurred Due to Loss of Bus B Control Power.Caused by Blown Power Fuse in Elgar Rectifier.Mod of Internal Control Circuits Initiated
| | | 05000458/LER-1986-029, :on 860405,standby Svc Water Sys Experienced Inadvertent Start.Caused by Electrical Transient.Standby Svc Water Pump Secured |
- on 860405,standby Svc Water Sys Experienced Inadvertent Start.Caused by Electrical Transient.Standby Svc Water Pump Secured
| | | 05000458/LER-1986-031, :on 860418,required Hourly Fire Watch Patrol for Five Inoperative Fire Barriers Inadvertently Cancelled. Caused by Personnel Error & Procedural Deficiency.Control Operating Foreman Counseled |
- on 860418,required Hourly Fire Watch Patrol for Five Inoperative Fire Barriers Inadvertently Cancelled. Caused by Personnel Error & Procedural Deficiency.Control Operating Foreman Counseled
| | | 05000458/LER-1986-032, :on 860423,reactor Scrammed on Water Level 8. Caused by Fouled Connector Pins on Circuit Board Card of Master Controller,Resulting in Erroneous Indication of Automatic Mode.Controller Contacts Cleaned |
- on 860423,reactor Scrammed on Water Level 8. Caused by Fouled Connector Pins on Circuit Board Card of Master Controller,Resulting in Erroneous Indication of Automatic Mode.Controller Contacts Cleaned
| | | 05000458/LER-1986-033, :on 860426,reactor Scrammed Due to Combination of Planned half-scram from Surveillance Test & Unplanned half-scram.Caused by Blown Fuse in Reactor Protection Sys. Fuse Replaced |
- on 860426,reactor Scrammed Due to Combination of Planned half-scram from Surveillance Test & Unplanned half-scram.Caused by Blown Fuse in Reactor Protection Sys. Fuse Replaced
| | | 05000458/LER-1986-034, :on 860516,fuel Bldg Exhaust Radiation Monitor Failed,Initiating Fuel Bldg Filtration Sys Train B.Caused by Mechanical Failure of Monitor.Check Source Lever Arm Properly Positioned & Screw Tightened |
- on 860516,fuel Bldg Exhaust Radiation Monitor Failed,Initiating Fuel Bldg Filtration Sys Train B.Caused by Mechanical Failure of Monitor.Check Source Lever Arm Properly Positioned & Screw Tightened
| | | 05000458/LER-1986-035, :on 860501,reactor Scram Occurred,Resulting in APRM Flow Biased Thermal Trip.Caused by Increased Noise Level on Transmitter a Due to Transmitter B Removed from Svc.Aprm Transmitters Dampened |
- on 860501,reactor Scram Occurred,Resulting in APRM Flow Biased Thermal Trip.Caused by Increased Noise Level on Transmitter a Due to Transmitter B Removed from Svc.Aprm Transmitters Dampened
| | | 05000458/LER-1986-036, :on 860501,Condition Rept CR 86-0539 Initiated, Indicating 31 One Shot Internal Conduit Seals Improperly Located.Walkdown Initiated.Conduit Seals Found in Noncompliance Repaired W/Second Seal |
- on 860501,Condition Rept CR 86-0539 Initiated, Indicating 31 One Shot Internal Conduit Seals Improperly Located.Walkdown Initiated.Conduit Seals Found in Noncompliance Repaired W/Second Seal
| | | 05000458/LER-1986-037, :on 860505,high Reactor Pressure Scram Occurred Due to Turbine Runback Stator Coolant Trouble Alarm.Caused by Low High Stator Water Cooling Temp Setpoint.Temp Switches Recalibr |
- on 860505,high Reactor Pressure Scram Occurred Due to Turbine Runback Stator Coolant Trouble Alarm.Caused by Low High Stator Water Cooling Temp Setpoint.Temp Switches Recalibr
| | | 05000458/LER-1986-041, :on 860614,turbine Tripped on High Vibration at Control Valve 1 Bearing.Caused by Momentary Rise in Vibration.Test Procedure Changed to Bypass High Vibration Trip Function During Valve Testing |
- on 860614,turbine Tripped on High Vibration at Control Valve 1 Bearing.Caused by Momentary Rise in Vibration.Test Procedure Changed to Bypass High Vibration Trip Function During Valve Testing
| | | 05000458/LER-1986-044, :on 860807,reactor Trip Occurred as Result of Turbine Bldg High Temp Isolation Trip Signal.Caused by Failure of Main Steam Moisture Separator Reheater Drain Tank Gasket.Gasket Replaced |
- on 860807,reactor Trip Occurred as Result of Turbine Bldg High Temp Isolation Trip Signal.Caused by Failure of Main Steam Moisture Separator Reheater Drain Tank Gasket.Gasket Replaced
| | | 05000458/LER-1986-046, :on 860611,while Routine Filter & Cartridge Replacement on Monitors performed,wide-range Gas Monitor Found Turned Off.Caused by Min Number of Channels Not Operable.Condition Rept 86-0726 Written |
- on 860611,while Routine Filter & Cartridge Replacement on Monitors performed,wide-range Gas Monitor Found Turned Off.Caused by Min Number of Channels Not Operable.Condition Rept 86-0726 Written
| | | 05000458/LER-1986-047, :on 860731 & 0802,feeder Breaker Tripped Causing Automatic Start of Both Divs of Annulus Mixing, Standby Gas Treatment & Fuel Bldg Ventilation Sys.Caused by Defective Protective Relay.Relay Replaced |
- on 860731 & 0802,feeder Breaker Tripped Causing Automatic Start of Both Divs of Annulus Mixing, Standby Gas Treatment & Fuel Bldg Ventilation Sys.Caused by Defective Protective Relay.Relay Replaced
| | | 05000458/LER-1986-048, :on 860804,discovered That Daily Surveillance Test STP-500-4550 Re Control Sys High & Low Power Setpoint, Not Performed Since 860802.Control Rods Also Pulled.Caused by Poor Scheduling.Schedule to Be Distributed |
- on 860804,discovered That Daily Surveillance Test STP-500-4550 Re Control Sys High & Low Power Setpoint, Not Performed Since 860802.Control Rods Also Pulled.Caused by Poor Scheduling.Schedule to Be Distributed
| | | 05000458/LER-1986-051, :on 860810,RWCU Occurred When Daily Surveillance on Leak Detection Temp Modules Conducted.Caused by Personnel Negligence.Permanent Caution Plaque Mounted Near Read-Set Switches |
- on 860810,RWCU Occurred When Daily Surveillance on Leak Detection Temp Modules Conducted.Caused by Personnel Negligence.Permanent Caution Plaque Mounted Near Read-Set Switches
| | | 05000458/LER-1986-052, :on 860822,main Control Room Ventilation Sys Isolation Occurred.Caused by Induced Signal on Radiation Monitor Due to Maint Work.Noise Suppression Will Be Installed on Preamplifier Power Lines |
- on 860822,main Control Room Ventilation Sys Isolation Occurred.Caused by Induced Signal on Radiation Monitor Due to Maint Work.Noise Suppression Will Be Installed on Preamplifier Power Lines
| | | 05000458/LER-1986-053, :on 860916,thermolag Matl Removed from Equipment Necessary for Safe Shutdown W/O Initiation of Fire Watch Per Tech Spec 3/4.7.7.Caused by Personnel Oversight. Personnel Counseled |
- on 860916,thermolag Matl Removed from Equipment Necessary for Safe Shutdown W/O Initiation of Fire Watch Per Tech Spec 3/4.7.7.Caused by Personnel Oversight. Personnel Counseled
| | | 05000458/LER-1986-054, :on 861005,discovered That on 860921,HPCS Administrative Operability Overlooked.Caused by Inability to Automatically Isolate Injection Path on High Reactor Water Level,Per Tech Spec 3.3.3 |
- on 861005,discovered That on 860921,HPCS Administrative Operability Overlooked.Caused by Inability to Automatically Isolate Injection Path on High Reactor Water Level,Per Tech Spec 3.3.3
| | | 05000458/LER-1986-055, :on 860831,reactor Scrammed Due to Loss of Reactor Protection Sys Bus a Concurrent W/Failure of Sys Backup Scram Circuitry B.Caused by Failure of Cooling Tower Feeder Transformer.Mod Request Generated |
- on 860831,reactor Scrammed Due to Loss of Reactor Protection Sys Bus a Concurrent W/Failure of Sys Backup Scram Circuitry B.Caused by Failure of Cooling Tower Feeder Transformer.Mod Request Generated
| | | 05000458/LER-1986-056, :on 860902,reactor Scrammed on RCIC Initiation. Caused by Entrapped Air in Instrument Sensing Line Following Maint.Air Vented from Instrumentation & Loose Transmitter Connection Reworked & Corrected |
- on 860902,reactor Scrammed on RCIC Initiation. Caused by Entrapped Air in Instrument Sensing Line Following Maint.Air Vented from Instrumentation & Loose Transmitter Connection Reworked & Corrected
| | | 05000458/LER-1986-057, :on 860923,during Surveillance Test Procedure STP-207-4210,RCWU Sys Isolated.Caused by Inadvertent Grounding of Electrical Jumper Resulting in Blown Fuse.Fuse Replaced.Rcwu Isolation Reset |
- on 860923,during Surveillance Test Procedure STP-207-4210,RCWU Sys Isolated.Caused by Inadvertent Grounding of Electrical Jumper Resulting in Blown Fuse.Fuse Replaced.Rcwu Isolation Reset
| | | 05000458/LER-1986-058, :on 861006,during Breaker alignment,1NPS-ACB23 Mistakenly Opened Instead of 1NPS-ACB33,causing 1NNS-SWG2B to Deenergize Which Caused Svc Water Pump 1B to Trip.Caused by Operator Error.All Personnel Counseled |
- on 861006,during Breaker alignment,1NPS-ACB23 Mistakenly Opened Instead of 1NPS-ACB33,causing 1NNS-SWG2B to Deenergize Which Caused Svc Water Pump 1B to Trip.Caused by Operator Error.All Personnel Counseled
| | | 05000458/LER-1986-060, Forwards Info Re Items Identified Subsequent to 861110 Conference Re Insp Rept 50-458/86-36.Addl Info Available in LER 86-60,submitted on 861113 | Forwards Info Re Items Identified Subsequent to 861110 Conference Re Insp Rept 50-458/86-36.Addl Info Available in LER 86-60,submitted on 861113 | | | 05000458/LER-1986-061, :on 861020,cooling Tower Blowdown Radiation Monitor 1RMS-RE108 Experienced Loss of Sample Flow & on 861022,discovered That Grab Samples Required to Be Collected Every 12 H Had Not Been Taken.Test Performed |
- on 861020,cooling Tower Blowdown Radiation Monitor 1RMS-RE108 Experienced Loss of Sample Flow & on 861022,discovered That Grab Samples Required to Be Collected Every 12 H Had Not Been Taken.Test Performed
| | | 05000458/LER-1986-062, :on 861028,automatic Initiation of Div I Standby Gas Treatment Sys & Annulus Mixing Fan Occurred. Caused by Radiation Monitor Susceptability to Electrical Noise.Corrective Action Under Investigation |
- on 861028,automatic Initiation of Div I Standby Gas Treatment Sys & Annulus Mixing Fan Occurred. Caused by Radiation Monitor Susceptability to Electrical Noise.Corrective Action Under Investigation
| | | 05000458/LER-1986-063, :on 861028,unanticipated Isolation Signal Received for RHR During Surveillance Test,Due to Grounded Lead.Caused by Test Procedure Requiring Wiring Termination Activities in Confined Space.Procedure Revised |
- on 861028,unanticipated Isolation Signal Received for RHR During Surveillance Test,Due to Grounded Lead.Caused by Test Procedure Requiring Wiring Termination Activities in Confined Space.Procedure Revised
| | | 05000458/LER-1986-064, :on 861031,grounded Metal Isolation Can Inadvertently Brought Into Contact w/24-volt Dc Power Iodine Cooling Fins of Power Supply B21K613B,resulting in Stated Trips.Caused by Personnel Error |
- on 861031,grounded Metal Isolation Can Inadvertently Brought Into Contact w/24-volt Dc Power Iodine Cooling Fins of Power Supply B21K613B,resulting in Stated Trips.Caused by Personnel Error
| | | 05000458/LER-1986-065, :on 861114,past Interpretation of Leakage Requirements for MSIV Found Incorrect.Memo Issued to Delineate Original Intent of Tech Spec Requirement & Associated Surveillance Procedures Revised |
- on 861114,past Interpretation of Leakage Requirements for MSIV Found Incorrect.Memo Issued to Delineate Original Intent of Tech Spec Requirement & Associated Surveillance Procedures Revised
| | | 05000458/LER-1986-066, :on 861124,discovered That Two Rated Fire Doors Omitted from Any Surveillance Test Procedure (STP) Door List.Caused by Procedural Deficiency.Temporary Change Notice Written to Include Two Doors in Daily STP |
- on 861124,discovered That Two Rated Fire Doors Omitted from Any Surveillance Test Procedure (STP) Door List.Caused by Procedural Deficiency.Temporary Change Notice Written to Include Two Doors in Daily STP
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