ML20036C343

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Insp Repts 50-321/93-06 & 50-366/93-06 on 930411-0508. Violations Noted.Major Areas Inspected:Unit 1 Loss of Shutdown Cooling Flow & Continued Review of Activities Associated W/Unit 2 Fuel Leakage & Surveillance Testing
ML20036C343
Person / Time
Site: Hatch  
Issue date: 05/26/1993
From: Christnot E, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20036C336 List:
References
50-321-93-06, 50-321-93-6, 50-366-93-06, 50-366-93-6, NUDOCS 9306160139
Download: ML20036C343 (26)


See also: IR 05000321/1993006

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA STREET, N.W.

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ATi.ANTA, GEORGI A 30323

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Report Nos.: 50-321/93-06 and 50-366/93-06

Licensee: Georgia Power Company

P.O. Box 1295

Birmingham, AL 35201

Docket Nos.:

50-321 and 50-366

License Nos.: DPR-57 and NPF-5

Facility Name: Hatch Nuclear Plant

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Inspection Conducted: April 11 - May 08, 1993

Inspectors:

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Leon rd D.

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Jr., Sr. Resident Inspector

Date Signed

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Edward F. L

tpt,ResidentInspector

Date Signed

Accompanying Inspecto . Bob Ho broo,'C

Approved by:

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Pi6rce H. Skinner Chief, Project Section 3B

Date Signed

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Division of Reacto,r Projects

SUMMARY

Scope:

This routine, announced inspection involved inspection on-site in

the areas of operations including a Unit I loss of shutdown

cooling flow and continued review of activities associated with

Unit 2 fuel leakage, surveillance testing, maintenance activities

including a walkdown of drywell conditions, Unit I refueling

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outage activities including modifications, Temporary Instruction

2515/119 (Water Level Instrumentation Errors During and After

Depressurization Transients), and review of open items.

Results:

Two violations and one non-cited violation were identified:

The first violation addressed a loss of shutdown cooling flow

during loading of fuel into the Unit I reactor vessel.

Maintenance activities in a control room panel resulted in a short

circuit and subsequent blown fuse. The blown fuse resulted in

isolation of the injection valve in the operable shutdown cooling

loop. Both loops of shutdown cooling were inoperable for

approximately two hours. A minimal decay heat load and the

availability of numerous other cooling systems resulted in the

safety significance of the particular event being small. Several

concerns were noted regarding the length of time required before

the loss of flow was identified. The licensee's immediate

corrective actions after the problem was identified were

9306160139 930601

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appropriate (Violation 50-321/93-06-01:

Failure to Comply With

Shutdown Cooling Technical Specification Requirements, paragraph

2b.).

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The second violation involved a failure to comply with emergency

diesel generator alarm response procedures during testing. The

generator outboard bearing temperature increased to above the

value at which the procedure directed that the diesel was to be

shutdown. The inspectors identified the violation during

observation of TS required testing (Violation 50-321/93-06-02:

Failure to Follow Diesel Generator Alarm Response Procedures,

paragraph 3.b.).

The non-cited violation involved a dosimetry technician who failed

to perform portions of a testing procedure on a pocket ion chamber

but recorded in the procedure that the test had been performed

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satisfactorily (NCV 50-321,366/93-06-03: False Documentation of

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Portions of a Dosimeter Calibration Test, paragraph 2.c.).

Two examples of incidents in which a more aggressive questioning

attitude on the part af operating personnel may have reduced the

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significance of or prevented an event were noted.

During the loss

of shutdown cooling flow, an operator observed indications of a

possible short circuit but failed to report or follow up on the

information. During attempts to start a reactor water cleanup

pump, an unexpectedly closed discharge valve was not adequately

pursued before additional pump starts were attempted. Other

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examples involving insufficient questioning of indications by

operators have been noted in recent months (paragraph 2.b.).

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

J. Betsill, Unit 2 Operations Superintendent

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C. Coggin, Training and Emergency Preparedness Manager

D. Davis, Plant Administration Manager

  • P. Fornel, Maintenance Manager
  • 0. Fraser, Safety Audit and Engineering Review Supervisor
  • G. Goode, Engineering Support Manager

J. Hammonds, Regulatory Compliance Supervisor

  • W. Kirkley, Health Physics and Chemistry Manager
  • J. Lewis, Operations Manager

C. Moore, Assistant General Manager - Plant Operations

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  • D. Read, Assistant General Manager - Plant Support
  • P. Roberts, Outages and Planning Supervisor
  • K. Robuck, Manager, Modifications and Maintenance Support
  • H. Sumner, General Manager - Nuclear Plant

J. Thompson, Nuclear Security Manager

  • S. Tipps, Nuclear Safety and Compliance Manager
  • P. Wells, Unit 1 Operations Suparintendent

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Other licensee employees contacted included technicians, operators,

mechanics, security force members and staff personnel.

NRC Resident Inspectors

  • L. Wert
  • E. Christnot

Accompanying Inspector

B. Holbrook

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  • Attended exit interview

Acronyms and abbreviations used throughout this report are listed in the

last paragraph.

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2.

Plant Operations (71707) (92701) (93702)

a.

Operational Status

Unit I remained in the cycle 14 refueling outage during the entire

reporting period.

Unit 2 was returned to RTP on April 6, 1993 following a forced

outage due to leaking fuel bundles. On April 13, 1993, plant

management directed that unit power be decreased to approximately

75 percent RTP. Although offgas radiation levels were still

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within TS limits, the levels had increased to above expected

values, apparently due to continued problems with fuel leakage.

Reactor power was subsequently decreased to approximately 55

percent RTP. Reactor engineering conducted flux tilt testing

activities and determined that one of the four fuel bundles

associated with control rod 46-23 was the most probable location

for the leaking fuel. Control rods insertions were performed to

provide flux suppression for the suspected leaking fuel bundle (s).

On April 28, 1993, reactor power was slowly increased to just less

that 75 percent RTP. Additional monitoring and evaluations of the

offgas levels was conducted. At the end of this reporting period

Unit 2 reactor power was being maintained at approximately 74

percent RTP. Offgas sampling and analyses are being conducted at

12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> intervals. The inspectors will continue to monitor the

licensees actions associated with the reactor power increase and

offgas monitoring activities.

Paragraph 2.d of this report

contains additional details of the activities.

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, TSs,

and administrative controls. Control room logs, shift turnover

records, temporary modification logs, LC0 logs and equipment

clearance records were reviewed routinely. The inspectors

periodically monitored activities on the refueling floor

associated with the movement of irradiated fuel and in-vessel

maintenance activities. Discussions were conducted with plant

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operations, maintenance, chemistry, health physics, I&C, reactor

engineering, and NSAC personnel.

Activities within the control rooms were monitored on an almost

daily basis.

Inspections were conducted on the day and night

shifts, during weekdays, and on weekends. Observations included

control room manning, access control, operator professionalism and

attentiveness, and adherence to procedures.

Instrument readings,

recorder traces, annunciator alarms, operability of nuclear

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instrumentation and reactor protection system channels,

availability of power sources, and operability of the SPDS were

monitored.

Control Room observations also included ECCS system

lineups, containment integrity, reactor mode switch position,

scram discharge volume valve positions, and rod movement controls.

Numerous informal discussions were conducted with the operators

and their supervisors.

Several inspections were made during shift

change in order to evaluate shift turnover performance. Actions

observed were conducted as required by the licensee's

administrative procedures. The complement of licensed personnel

on each shift met or exceeded the requirements of TS.

The inspectors performed additional reviews regarding the

operability of the SPDS. The system engineers and STAS have been

collecting data and monitoring the online times of the system. A

review of the data indicated that the reliability of the SPDS was

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considered as being very high by the licensee. The inspector

reviewed NUREG 0660 (Item I.D.2) and various correspondence in

attempts to identify a specific SPDS reliability requirement.

Discussions with licensee personnel indicated that the

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installation of the SPDS, in accordance with NUREG 0660, was

adequate. Discussions were held with other NRC personnel familiar

with SPDS and NUREG 0660 requirements.

No regulatory requirements

for SPDS reliability were identified. The system is maintained in

an operable status by continuous monitoring and when a problem or

potential problem is identified corrective action is initiated to

restore the system. The inspectors concluded that the current

system meets the requirements committed to by Hatch. The licensee

has recently discontinued collection of SPDS performance data and

reliability assessments.

On April 21, 1993, during monitoring of CR activities, an

inspector observed operator actions during a decreasing fuel pool

level incident. The Unit 1 CB0 noted that the spent fuel pool

cooling pump 1G41-C001B had tripped on low level. The inspector

noted that the CB0 immediately contacted an operator and ordered

that the draining down of the volume between the reactor cavity

gate and the Unit I spent fuel pool gate be stopped. The

inspector observing the control room activities then proceeded to

the refuel floor and observed some of the recovery activities

there. The inspector immediately noted that the spent fuel pool

level indicated 22 feet. This is above the TS minimum of 21 feet

above the fuel.

Inspection Reports 321,366/90-26 and 92-18 both

contain discussions involving previous spent fuel pool water level

problems.

Both incidents involved pool overflows and problems

with the level indication / alarm systems. The inspectors had

concluded that repetitive problems with the alarms were a

contributing factor to the overflows. Additional review of this

instance identified that the air supply hose used to inflate the

spent fuel pool gate bladder (at the gates between the pool and

the cavity) was not connected properly and resulted in the bladder

not being inflated. The " snap in" connection on the air supply

line had not been fully engaged.

Because the supply air pressure

gage was sensing pressure on the supply side of the connection,

the gage did not indicate the depressurized lines to the bladder.

This in turn allowed water to leak past the gate and into the

volume area being drained down.

The inspector concluded from reviews, observations, and

discussions with licensee personnel that the control room operator

was aware of the plant conditions as well as ongoing evolutions

and took immediate effective action to stop the fuel pool drain

down. The method of connection of the air supply line and location

of the pressure gage contributed to this issue.

It was also noted

that no TS violation occurred. An ongoing followup review by the

inspector involves the status of the fuel pool skimmer tank alarm

system. The pump has a 9 psig low suction pressure trip setpoint.

The skimmer tank low level alarm set point is 222 feet and the low

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alarm set point is 219 feet. At the close of the inspection

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period, the inspectors and the licensee were reviewing the

incident to determine if the alarms should have actuated before

the pump tripped. The inspectors will continue their review of

this issue.

Plant tours were performed throughout the reporting period on a

routine basis. The areas toured included the following:

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Reactor Buildings

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Station Yard Zone within the Protected Area

Turbine Building

Intake Structure

Diesel Generator Building

Fire Pump Building

Unit 1 Drywell

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Unit 1 Torus (area) and Torus (proper)

During the plant tours, ongoing activities, housekeeping,

security, equipment status, and radiation control practices were

observed. No significant problems were noted. Minor housekeeping

and personnel safety issues were resolved as they were identified.

During tours of the lower torus area of the Unit 1 RB, the

inspectors noted several indications of tobacco expectorant

beneath areas of maintenance activities. The inspectors informed

the RB coordinator and outage and planning management of the

observations.

Emphasis was placed on adherence to radiological

work practices during meetings with supervisory and craft

personnel over the next several days. During several tours inside

the torus (proper) area, the inspectors noted that excellent

housekeeping controls and a high level of overall cleanliness

existed in the torus. Some of the ECCS strainers were also

examined with no problems noted.

b.

Hatch Unit 1 Loss of Shutdown Cooling Flow

On April 14, 1993, RHR system shutdown cooling flow was lost on

Unit 1 for a period of almost 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />.

Reloading of irradiated

and new fuel bundles had been initiated at about 6:00 am EST. At

the time that the loss of SDC flow was identified, fuel movement

was in progress with 20-25 bundles having been placed into the

vessel. The refueling cavity was flooded up and one train of the

fuel pool cooling system was providing cooling of the cavity

water.

During modification work on a CR panel (the PCIS display panel),

manipulation of wiring in that panel resulted in fuse 1A718-F22

blowing. This fuse powers logic circuitry which provides input to

several valves including IE11-F015B (the "B" loop of SDC injection

. valve). When the fuse blew, valve IE11-F015B closed.

Since the

Qinimum flow valve is shut during SDC alignment (to prevent a

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flowpath from the cavity to torus), this shut off the discharge

flowpath of the "B"

and "D" RHR pumps ("B" SDC loop).

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The problem was identified by a CR operator performing a required

surveillance procedure.

In accordance with procedure 34GO-0PS-

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015-1S: Maintaining Cold Shutdown or Refuel Condition, cold

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shutdown parameters are monitored at least once every four hours.

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One of these parameters is reactor coolant flow, which under these

conditions, is obtained by reference to the RHR system flow chart

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recorder. The flow was identified as indicating zero flow. The

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operators then observed that IE11-F015B was shut and attempted to

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reopen it. The valve traveled open and then reclosed. The SS

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directed that the "D" RHR pump be secured (it had been running-

with the "B" pump in standby). Fuel movement was stopped. This

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was about 10:10 am EST.

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After investigation, replacement of the fuse, and other recovery-

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actions, the pump was restarted at 11:43 am EST. A PE0 was

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stationed at the pump during restart and maintenance personnel

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obtained vibration indications on the running pump.

No problems

were noted. The licensee contacted the pump vendor for additional

information. The vendor' recommended that the pump's performance

be checked against the head curves furnished for the pump. This

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was completed and it was concluded that the pump was not damaged.

The inspectors performed independent reviews 'of the associated

chart recorder indications for flowrates and temperatures.

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Additional discussions were held with the operators-involved in

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the event. The following information was obtained:

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From the time that the F015B valve shut until SDC flow was

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restored was almost three hours total.

For just under one

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and a half hours, the pump was running with the discharge

path secured (before identification). Approximately one and'

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one half. hours were required to restore SDC after the

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situation was identified.

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The inspectors examined the temperature transient in-detail.

Additional information was obtained by correlating the time

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that valve IE11-F015 was stroked open (obtained from the RHR

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flow chart) to the temperature chart. At the time the valve

was stroked, the temperature chart (RHR HX inlet temp)

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showed a " spike" in temperature from 95 degrees F to about

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110-115 degrees F and then a-decrease over about 5 minutes

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to about 105 degrees F.

The inspectors concluded that this.

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is indicative of the warmed pump discharge fluid (no flow

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conditions for about I hour) flowing through the line as the

valve was opened. The temperature sensor (E11-N0048) is

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located in the RHR pump discharge about 50 feet from the

pump and 15 feet before the inlet to the RHR HX. The

temperature trace was steady for the next 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, then-

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decreased to just under-100 degrees F very rapidly as the

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RHR pump was restored. After the immediate drop, the

temperature decreased to 95 degrees in less than 15 minutes.

The inspectors concluded that the reactor vessel water may

not have increased in temperature at all during the event.

Since there is no direct indication, it is difficult to-

determine exactly what the vessel temperatures response was.

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The inspectors also concluded that the licensee had neither

neglected preplanning nor took inappropriate risks regarding

the modification that was in progress that caused the 1 Ell-

F015 valve to shut. The circumstances which resulted in the

problem were not reasonably foreseeable. Care was being

exercised in handling of the CR panel. A wooden support

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frame had been constructed to facilitate the work.

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There is no annunciator or alarm to warn the operators of

such an occurrence. By procedure, the checks of cold

shutdown parameters are only required once every four hours.

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Additionally, the inspectors noted that the personnel

working on the panel probably partially blocked the

operator's view of the RHR system mimic where the IE11-F015B

valve position is indicated. During initial follow-up

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discussions some information indicated that the modification

workers had noted an electrical spark (apparently when the

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wires were shorted) and reported it to a nearby operator,

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but did not report this to onshift management.

The safety significance of this particular event is very small.

Numerous backup systems to cool or maintain the inventory of the

cavity were available. 'These included: FPC system (one train was

in service to the cavity during the event, the other was aligned

to the spent fuel pool),

"B" CS system, an alternate (temporary)

fuel pool cooling system, PSW, demineralized water, CRD system,

and CST makeup. Attachment 2 of 34AB-Ell-001-IS:

Loss of

Shutdown Cooling, provides a graph of " vessel and cavity boil-off

time" (the amount of time required for boiling to cause reactor

level to decrease to the ECCS setpoint) vs number of days since

core last critical. The graph assumes all fuel is still in the

core, all cooling is lost, and initial temperature is 150 degrees

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F.

In this case, only 20-25 bundles were loaded, and all cooling

had not been lost. The reactor had been scrammed on March 16,

1993. Using 30 days as an entry point on the graph, the

inspectors noted that it would require at least 150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br /> to reach

boil-off to the ECCS setpoint, even without accounting for the

numerous conservatisms of this example. Approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

would be required before boiling would start to occur in the core

area. The inspectors also noted that 2 of the 3 EDGs were

operable and both offsite power sources were operable during the

event.

Information provided in draft NUREG 1449:

Shutdown and

Low Power Operation at Commercial Nuclear Power Plants in the

United States, was used to assess the safety significance.

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Additional followup reviews and observation by the inspector

indicated that when the short circuit occurred, an operator,

(acting as an assistant plant operator and performing ECCS status

checks) and the modification implementing crew had noted

indications that a circuit had been shorted (a small arc).

However, aggressive action was not taken to investigate possible

problems that might have occurred. The CBO, plant operator, or

shift management was not informed that a potential grounding of a

control panel circuit had occurred. The inspectors noted that

step 8.11.5.2 of procedure 30AC-0PS-003-0S:

Plant Operations,

states that the Assistant Plant Operator is required to keep the

SS and Plant Operator informed on plant problems and activities.

Although more aggressive pursuance of the observed indications may

have reduced the time required to identify the loss of flow, the

inspectors concluded that the failure to report this particular

observation was not a violation of these procedural requirements.

While it was not unreasonable for this operator, given the ongoing

activities, to characterize the observed "small electrical spark"

as not a " plant problem," it would have been more prudent to

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inform the CB0.

The inspectors noted that another incident which did involve a

clear failure to conduct proper followup of an observed problem

occurred on April 28, 1993. Operators attempted to start the "1A"

RWCU pump after it had been secured for the reactor vessel

pressure test.

The pump tripped and the discharge valve was found

shut. The valve was reopened and the pump was restarted and

tripped again. Subsequent-investigation indicated that the pump,

which the shift had considered to be in a " standby" condition, had

been fully secured. Cooling water had been isolated. The

inspectors' review of the incident indicated that the problem was

not caused by any direct failures to follow procedures.

Miscommunications and a lack of questioning on the part of the

operators were the primary causes.

The inspectors concluded that

the lack of additional followup after the discharge valve was

found unexpectedly closed was a weakness on the part of the

involved operators. As noted in the loss of the SDC flow

incident, more aggressive followup actions may have prevented or

reduced the significance of the problem. The inspectors noted

that operations management issued a memo which addressed the role

that a lack of a questioning attitude played in these events.

Other examples of inadequate followup actions have been noted in

the recent months, some identified by the licensee, others

identified by the inspectors. The Senior Resident Inspector

discussed these examples of inadequate questioning and

insufficient followup with the General Manager.

While the loss of SDC flow situation was not considered to be of a

large safety significance, the event did highlight a vulnerability

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of Hatch (and similar BWRs) due to the unavailability of a strong

indication of a loss of SDC system flow. The inspectors noted

that the licensee had placed the plant in more limiting

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circumstances during the reactor vessel disassembly prior to

unloading the core. One train.of RHR was available, the cavity

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was not flooded, and decay heat-loads were considerably higher.

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If this loss of cooling had occurred under these conditions, the

safety significance could have been much more significant.

Several other differences were noted between the plant conditions

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during the actual cooling loss and those during vessel

disassembly. The plant computer was operable during vessel

disassembly and a increasing temperature indication should have

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been more noticeable. The outage " safety assessment" had listed

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decay heat removal as a " red" condition (primarily due to the

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unflooded cavity) so more attention may have been focused on the

SDC system. Under those conditions, if SDC flow had been lost for

almost 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />, a significant. temperature increase would have

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occurred. The licensee is considering stricter monitoring

requirements on the SDC system under certain conditions.

In addition to the restoration actions, the licensee initiated an

operations crder requiring more frequent control room panel

walkdowns. The event was reported to the NRC Operations Center

due to the actuation of the Group 2 isolation valves. A detailed

review of the event was conducted by the licensee, and additional

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corrective' actions are being considered. This issue is identified

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as Violation 50-321/93-06-01:

Failure to Comply with Shutdown

Cooling TS Requirements.

c.

Failure to Perform Dosimetry Leakage and Calibration Test.

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During an investigation performed in an effort to resolve a

discrepancy between an individual's TLD and PIC dose recordings,

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portions of a calibration check of the PIC were documented as

completed, when in actuality, they had not been performed.

Section 7.5 of 62RP-RAD-001-OS: Dosimetry Issuance and Tracking,.

contains requirements associated with assessment of a worker's

exposure. One of the requirements is to initiate an investigation

when the difference between the TLD and PIC measured exposures'is

greater than 25 percent.

In this case, the difference was-greater

than the allowable amount and an assessment was required. A " Dose

Discrepancy Investigation" form (Attachment 17 of the procedure)

was completed and the " investigation finding" of "possible drift"

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of the PIC was indicated. The next step is typically to

investigate / test the PIC to identify any problems.

Section 7.3 of 62HI-0CB-012-OS:

Pocket Dosimeter Use and

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Performance Test, provides guidance on calibration. -In accordance

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with this procedure, a " Charge-Leakage" test was performed

satisfactorily by a dosimetry technician. Another technician was

then supposed to perform the " Dosimetry Calibration" (Section

7.3.2).

This test involves exposure of the PIC to a source.- The

test was not performed. The technician falsified portions of the

" Dosimetry Leakage and Calibration" form by recording data that

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indicated the test was performed. Another worker in the

department informed the foreman of suspicions that the test had

not been performed. Checks of RWP records and source check-out

records supported the accusation. When confronted, the worker

admitted falsifying the test. Subsequently, a test of the PIC was

satisfactorily performed.

The involved worker has been assigned to these " dosimetry" duties

since 1987. Typical duties are primarily administrative and

include whole body checks and dosimetry records maintenance. This

worker was not involved in activities such as surveys or HP

coverage of activities. Most of the tasks that were performed by

this worker are routinely reviewed by additional personnel.

During discussions with licensee supervision, the inspectors were

informed that this worker has a very good work record.

The inspectors noted that the involved procedures are safety

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related. Administrative TS requirements address this type of

testing and documentation. The inspectors noted that the licensee

promptly informed the inspectors of the event, conducted

investigations, and interviews and disciplinary actions were

taken. The importance of honesty and accountability was re-

emphasized to all plant personnel. A memo on this subject

recently written by the Hatch Vice President was recirculated.

After review of the licensee's corrective actions in this matter,

the inspectors concluded that.the actions were appropriate. This

issue will not be subject to enforcement actions because the

licensees's efforts in identifying and correcting the violation

meet the criteria in Section VII.B of the Enforcement Policy, for

non-cited violations. After discussions with NRC management, it

was determined that this issue is a violation of 10 CFR 50.9.

This issue is identified as NCV 50-321,366/93-06-03:

False

Documentation of Portions of a Dosimeter Calibration Test.

d.

Hatch Unit 2 Continuing Fuel Leaking Incident

Unit 2 power was increased to RTP on April 9,1993, following a

forced outage to conduct fuel sipping and inspection to identify

possible leaking fuel. The unit remained at nearly RTP until

April 13,1993. As expected, during the power increase, offgas

radioactivity levels increased. However, a chemistry sample

conducted on April 12, 1993, indicated the " sum of the sixes" (TS

required noble gas samples of Xe-133, Xe-135, Xe-138, Kr-85, Kr-

87, and Kr-88) indicated possible fuel leakage. The offgas levels

were well below the regulatory limits but were increasing to a

level greater than expected for the current plant conditions. On

April 13, 1993, plant management directed that unit power be

decreased to approximately 75 percent RTP.

Reactor power was

eventually decreased to approximately 55 percent RTP.

Reactor

Engineering began flux tilt inspection activities of the reactor

core. The licensee determined that one of the four fuel bundles

associated with control rod 46-23 were the major suspects for fuel

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10

leakage.

Control rod 46-23 and two adjacent control rods, 46-19

and 50-23, were intentionally inserted to "00" (full in). One

additional control rod, 42-23, which was at "00" due to the

existing control rod pattern, was being maintained at the "00"

<

full in position. These control rods serve as shielding or

neutron flux suppression for the suspected leaking fuel bundles.

At 6:40 p.m. EST, on April 28, 1993, the licensee decided to

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slowly increase reactor power to just below 75 percent RTP, and

conduct additional monitoring and evaluations of the offgas

levels. Written instructions were provided to the operating

shifts as to the methodology to be used in power ascension.

Sampling of the offgas continued, and the value of the " sum of the

sixes" appeared to be satisfactory for the power increase. This

power level will be maintained until the licensee collects

additional data and conducts further evaluations of the offgas

releases. At the present reactor power level (74 percent) the

offgas levels for gross gamma radioactivity rate of noble gases is

well below the TS limit. Currently the value of the " sum of the

sixes" is approximately 13 percent of the TS limit. At the end of

this reporting period Unit 2 reactor power was being maintained at

approximately 74 percent RTP and offgas sampling and analysis are

being conducted at 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> intervals.

The inspectors have reviewed the TS requirements, monitored the

day to day activities in the CR, and completed some independent

reviews of the offgas sampling results.

The inspectors will

continue to review the licensees actions associated with the

reactor power increase and offgas monitoring activities.

.

e.

Unit 1 Reactor Water Level Instrument Anomalies

At 1:15 p.m. EST, May 1, 1993, during the heat up and

pressurization stage of the reactor vessel pressure test, the unit

received a full scram and a 1/2 group 2 isolation signal from low

reactor water level. The reactor temperature was approximately

180 degrees F and pressure was 100 psig.

Following the scram the

operators verified reactor water level at approximately +175

inches and steady.

Following further investigation it was

determined that all level instruments attached to reference leg

D004A were reading low. This would usually be indicative of a

problem associated with the variable leg.

Operators were dispatched to the reactor building to inspect the

instrument racks and tubing associated with these level

instruments. No discrepancies were identified.

Personnel were

then dispatched into the DW to walkdown the instrument tubing,

from the DW penetration to the reactor vessel, and investigate for

leaks. No leaks or other problems were identified. Various

trouble shooting activities were initiated. This included

lowering reactor water level to verify the accuracy of the other

available instruments (IB21-R605 and IC32-R655).

I&C connected

digital differential pressure gauges to check the response of the

.

f

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11

instrument legs and theorized that air bubbles must be in the

i

instrument lines. The instrument lines were then back filled.

Further investigation found that the equalization valve for

instrument 1821-N035 was slightly cracked open.

It was postulated

that this could allow air from the pressure test to be injected

into the variable legs and produce the level responses that were

being observed. The equalizing valve was closed and the reactor

vessel pressure test was resumed.

When the reactor recirculation pumps were used to increase core

flow (as part of the reactor vessel heatup process) the level

-

instruments in question again began to read low. Once the core

flow was stopped, the instruments would trend back up to .

.'

approximately normal position. The reactor vessel pressure test

was again stopped and further investigation was conducted.

I&C

checked the various instruments that could be leaking-by, either

through the equalizing valve or through a ruptured diaphragm. The

following instruments were checked for possible leakage:

1821-

N085, NO38, N070, and NO36. The instruments were isolated and

returned to service individually while the instrument and level

responses were monitored.

Following this investigation, it was

concluded that instruments N085 and NO38 were not the cause of the

,

problem. However, N070 and NO36 showed signs of some leakage.

With N070 and NO36 isolated, the shift began the reactor vessel

pressure test again. The level instruments displayed the same

anomalies. The test was again terminated.

Following additional discussions with I&C, it was determined the

variable legs of the instruments had not been properly back

filled. At 11:57 a.m. EST, May 2, 1993, a manual scram was

initiated (to aid in the filling of the instrument legs) and I&C

proceeded to back fill both the reference and variable legs of the

instruments.

I&C technicians reported that during the process of

back filling the reference legs (using a hydro pump) the reference

leg pressure increased to approximately 350-400 psig, and then

suddenly decreased. This response indicated that there had been

some type of blockage in the reference leg.

Instruments N070 and

NO36 were calibrated by I&C and placed back in service, and all

water level instruments indicated normal. At 1:40 p.m., May 2,

1993, the reactor vessel test was continued. The licensee

conducted further investigation and review of outage work that

could have affected the reactor water level instruments.

During the outage, a DCR was completed to correct the slope of the

instrument legs associated with condensing chamber D003A and

D004A. These lines did not have the specified minimum slope. As

discussed in GL 92-04, the modification would have decreased the

probability of erroneous water level indications. This

modification required cutting out and rewelding sections of the

reference leg piping.

In order to complete this work, a temporary

plug was installed in reactor vessel penetration N12A. Apparently

the plug did not provide a completely water tight seal and the

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reference leg could not be completely drained and maintained dry.

In order to perform a dry weld on the reference leg, the welding

.

supervisor directed the welders to plug the reference leg (near

the weld location) with " rice paper."

The rice paper was rolled

up (approximately a five inch roll) and forced up into the

reference leg. This " rice paper" is actually soluble purge dam

material referred to as "Dissolvo WLD-35."

It is designed to

i

absorb a liquid, and after a time period, completely dissolve into

t

the liquid.

It is commonly used as a dam during inert gas welding

evolutions. Discussions with plant management indicated the use

of rice paper was standard practice. The inspectors noted that

the use of rice paper had been recorded on the modification work

i

package.

It was learned that the rice paper had been in place for

'

approximately 21 days prior to the reactor level anomalies.

The ERT investigating the event theorized the rice paper had not

I

dissolved completely (due to the length of the roll) and perhaps

air had been trapped on the downstream side of the roll which

prevented the paper from becoming saturated. When the I&C

technicians had pressurized the reference leg with the hydrostatic

test pump, the roll was forced through the reference leg into the

reactor vessel. The investigating team had a model of the

reference leg piping fabricated, plugged the leg with rice paper

and with a high pressure air supply and a hydrostatic test pump

'

simulated back filling the leg.

It was determined the rice paper

could be moved up through the reference leg and could provide the

same type of response as was seen during the back filling

evolutions. Additionally, a standing water column was placed on a

tightly rolled section of the paper which was jammed into a

transparent column. The inspectors observed that over a period of

6 days, the water had migrated through less than half of the

rolled paper mass.

It was concluded that the dissolution of the

paper depends on sufficient exposure to water. Tightly packed

large accumulations of the paper prevented some of the paper from

being dissolved. The inspectors also noted that chemistry samples

of the reactor coolant (after the hydrostatic pump was used)

supported the postulation that the rice paper had been discharged

into the reactor water and had dissolved (an increase in

sulfates).

One of the inspectors closely followed the licensee actions

dealing with the reactor water level anomalies. Two different

phone conversations were held late in the evening of May 1, and

onsite review was performed early in the morning of May 2,1993,

to follow up on the actions. The inspector observed that there

were adequate reactor water level indications and that the

operators were closely monitoring the level. No TS violations

occurred. The inspector verified that the reactor scram was reset

and the group isolation was reset and valve positions were

correct. The operations shift management, STA, 1&C technicians

and the hydro test engineer were actively pursuing the level

.

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13

problem.

P&ID's and procedures were being utilized for guidance

during the trouble shooting.

During discussions with plant management and ERT personnel, the

inspectors noted that there are no specific guidelines as to how

much or how large a quantity of rice paper should be used during

maintenance activities. The requirements of the job being worked

generally would dictate how much would be used.

Skill of the

worker was relied upon for installation. The inspectors concluded

that the licensee actions dealing with the reactor water level

anomalies were appropriate. At the close of the inspection

report, the licensee's ERT was still reviewing the issue for

further corrective actions. More controls on the use of the paper

are being considered to preclude recurrence of such an event.

One violation and one non-cited violation were identified.

3.

Surveillance Testing (61726)

a.

Surveillance tests were reviewed by the inspectors to verify

procedural and performance adequacy. The completed tests reviewed

were examined for necessary test prerequisites, instructicns,

acceptance criteria, technical content, authorization to begin

work, data collection, independent verification where required,

handling of deficiencies noted, and review of completed work. The

tests witnessed, in whole or in part, were inspected to

determine that approved procedures were available, test

equipment was calibrated, prerequisites were met, tests were

conducted according to procedure, test results were acceptable and

systems restoration was completed.

The following surveillances were reviewed and witnessed in whole

or in part:

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1.

42SV-R43-030-IS:

1A EDG 24 Hour Run/LOSP LSFT

2.

421T-C11-001-05: Control Rod Drive Friction Testing

3.

42SV-R43-021-IS:

Loss of Site Power / Loss of Coolant

Accident Test

4.

42SV-TET-003-15:

Primary Containment Integrated Leak Rate

Test

On April 15, 1993, the inspectors observed portions of the EDG 1A

22.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> post maintenance run (after cylinder liner replacement).

The inspector was present when a leak occurred due to the failure

of the flexible hose in the cooling water system between the

expansion tank and coolers.

The hose was replaced and the post

maintenance test was completed.

The licensee determined that the

'

hose failed due to age and will inspect the hoses of the other

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14

EDGs. This test included loading the EDG and maintaining 3550 KW

for one half hour. There were no other discrepancies identified.

'

The inspectors monitored Unit 1 Control Rod Drive Friction Testing

activities. The monitoring included observations of operator

activities in the CR.

Procedural usage, control rod

'

manipulations, work practices, communications between the various

test personnel, and administrative activities were observed. The

inspectors also monitored activities locally in the reactor

building and discussed test results with the test engineers and

I&C technicians. There were no discrepancies identified.

The inspectors also observed and reviewed the activities

associated with the Unit 1 CILRT. This included independent

reviews of the preparation, initial pressurization and

stabilization. The inspector noted that test personnel

demonstrated awareness of the minimum and maximum pressurization

requirements for the test, the parameters necessary to declare

stabilization, and the verification requirements. The inspector

will perform additional reviews of the final data. The test was

performed in accordance with the approved procedure.

b.

IA EDG Outboard Generator Bearing High Temperature

During the performance of the Diesel Generator IA 24-Hour Run/LOSP

LSFT surveillance test, conducted on April 21, 1993, the

inspectors observed the pre-job briefing, procedure review, and

discussions which were conducted by two system engineers for the

operations group. The control board operator (to start and

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monitor the EDG from the CR) and two PE0's (to locally monitor the

EDG and record data during the EDG run) were present. The

inspectors observed the initial starting and loading of the 1A EDG

from the CR and observed EDG operations and data taking activities

locally at the EDG building. One of the inspectors, after

reviewing the data that was being recorded by the PEO, observed

that the EDG outboard bearing temperature was greater than the

expected band (100-170 degrees F) as indicated on the surveillance

data sheet. The inspector verified locally (temperature indicator

1R43-R767A) that the EDG outboard temperature was 184 degrees F

and increasing. The inspectors determined that the alarm response

procedure, 34AR-652-Il3-IS: Diesel Generator IA Inboard /0utboard

Bearing Temperature High, states that an alarm actuates upon high

temperature. The inspectors verified that this alarm had actuated

in the CR at 180 degrees F.

The operator actions of the alarm

response procedure directed personnel to confirm that a high

bearing temperature condition existed on temperature indicators

1R43-R767A or 1R43-768A, and if IA EDG was in " test," to shutdown

the diesel per the system operating procedure or applicable

surveillance procedure. After observing that the EDG was still in

operation, and following discussions with operations personnel in

the CR, it was determined that the SOS had directed that the 1A

EDG not be shutdown until the bearing temperature reached 190

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15

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degrees F.

Additionally, the inspectors verified that instrument

setpoint or procedure change requests that would allow the EDG to

be operated with elevated bearing temperatures had not been

implemented. The inspectors discussed their observations with

operations management (above the SOS level) who indicated that

they were not aware of the present bearing temperature problem.

However, they did state that they were aware of a previous problem

that had occurred during a similar EDG run and vaguely remembered

that a vendor representative stated a bearing temperature of 205

degrees F or less would be satisfactory. When the bearing

temperature reached 190 degrees F, the operators shutdown the EDG.

The inspectors determined that, prior to shutdown, the EDG was in

operation for approximately two and one half hours with the

outboard bearing temperature greater than 180 degrees F.

Failing

to shutdown the 1A EDG with the outboard bearing temperatura

greater than the value indicated in the alarm response procedure

l

was discussed in a meeting with plant management.

Plant

management at this time stated they expected the operators to

comply with the written procedures or use the correct

administrative process to have the procedures changed. The

following is a brief account of the EDG runs and maintenance

activities initiated after the outboard bearing high temperature

indications:

,

On April 22, 1993, following the initial outboard bearing

high temperature indication, the 1A EDG bearing oil system

was flushed. The 1A EDG was run and again was required to

be shutdown due to an outboard bearing temperature reaching

180 degrees F.

Maintenance activities were initiated to

replace the outboard bearing.

It was also determined that

the thermocouple sensing this bearing temperature was of the

wrong type.

The type of thermocouple that was installed

("J" type) resulted in indicated temperatures being 10

degrees F higher than values indicated by the correct type

of thermocouple ("S" type).

On April 23, the 1A EDG was run again and was required to be

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shutdown due to the outboard bearing high temperature

problem.

It was learned during the subsequent maintenance

activities (to again replace the bearing), that during the

first bearing replacement the oil port to the bearing had

been partially blocked. A metal gasket had been rotated

such that the oil port did not align with the oil supply

system.

On April 24, 25, and 26, additional testing of the 1A EDG

was conducted, and additional shutdowns were necessary due

to the outboard bearing temperature approaching or reaching

180 degrees F.

Activities following the unsuccessful runs

included maintenance inspections by plant maintenance

personnel and vendor representatives and coupling alignment

i

adjustments.

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.

On April 27, the licensee initiated a temporary procedure

change to the EDG post maintenance procedure, procedure

42SV-R43-030-IS: Diesel Generator IA 24-Hour Run/LOSP LSFT,

and alarm response procedure 34AR-652-113-IS: Diesel

Generator IA Inboard / Outboard Bearing Temperature High.

These temporary procedure changes allow operation of the EDG

with an outboard bearing temperature increase to 205 degrees

F.

The 1A EDG was again run and the outboard bearing

temperature increased to between 195-196 degrees F.

The

inspectors observed that during subsequent post maintenance

test runs and during the required 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run, the EDG

bearing temperature indicated between 164 and 168 degrees F.

.

Additional reviews and observation by the inspectors, as well as

discussions with licensee personnel, indicated the following:

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A total of six EDG runs were made on a daily basis, observed

periodically by the inspectors, between April 21-28, 1993.

Each run indicated outboard generator bearing high

temperatures.

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The April 15, 1993, liner replacement maintenance activities

and maintenance run of the EDG had been completed with no

deficiencies identified.

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The wrong type thermocouple was replaced with a correct type

and the other four EDG were verified as having the correct

type.

.

A discussion with the EDG vendor indicated that a grounded

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thermocouple could contribute to a high temperature due to a

heating effect.

Licensee personnel insulated the bearing

'

thermocouple.

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The generator bearing was changed out two times with two new

bearings.

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The rotation of the metallic gasket that blocked the oil

supply to the bearing housing did not contribute to the

bearing high temperature experienced on April 23, 1993. The

oil level in the bearing oil sump was maintained at a high

level .

Consequently the oil ran through the bearing and

into the bearing housing. However, this activity did

demonstrate a poor work practice.

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The licensee formed an engineering team to review the

circumstances involved with the bearing high temperature

problem.

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The EDG completed a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> TS run on May 2, 1993.

No

bearing high temperature problems were observed.

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17

The inspectors will continue to monitor and review the licensee's

activities in this area. The principle issues involved correct

placement of the thermocouple sensors in relation to the bearing

races. Additional review of this aspect is being conducted by the

licensee.

It appears that the situation could have been resolved

by more realistic temperature limits in the procedures. An

additional factor in this issue is that, due to work completed on

the EDGs during the outage, the EDGs were being run with reactive

loading in excess of previous testing. While considerable

troubleshooting and maintenance activities were required to

correct the problems, the inspectors concluded that the problems-

did not involve operability of the EDGs. The inspectors also

questioned if indications of a failed or failing bearing had been

precluded by the thermocouple sensors being placed too far away

from the bearing surface.

The failure to shutdown the 1A DG when the outboard bearing

temperature exceeded 180 degrees F, as required by the alarm

response procedure, is identified as Violation 321/93-06-02:

Failure to Follow EDG Alarm Response Procedures.

>

One violation was identified.

4.

Maintenance Activities (62703)

a.

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures in use adequately described

work that was not within the skill of the trade. Activities,

procedures, and work requests were examined to verify; proper

authorization to begin work, provisions for fire hazards,

cleanliness, exposure control, proper return of equipment to

service, and that limiting conditions for operation were met.

The following maintenance activities were reviewed and witnessed

in whole or in part:

1.

MWO 1-93-1906: Replace Outboard Bearing on IA EDG

Alternator

2.

MWO 1-92-5048:

1A Diesel, Alternator and Accessories

Inspection

3.

MWO 1-93-309:

1A EDG Major Internals Components Inspection

4.

MWO 1-92-6685:

IST Leak Rate Test of Valve 1E41-F005 (HPCI

Discharge Check Valve)

The inspector reviewed and observed the licensee's activities

involved with the 1A EDG. Additional discussion is provided in

paragraph 3.a of this report. The inspector noted effective use

of two procedures, 51GM-MNT-032: Component Alignment of Rotating

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18

Equipment, and 52CM-R43-002-OS: Alternator Major

Inspection /0verhaul. The local leak rate testing of the HPCI

check valve was conducted in accordance with the IST procedure.

The licensee informed the inspectors that during EQ qualification

testing of MSIV solenoids (three solenoids attached to a housing

block), Wyle laboratories reported finding a small (1/8 inch)

particle of non-magnetic metal in one of the solenoid blocks.

These solenoids had not been installed in the plant. Wyle

laboratories then proceeded to dissemble and inspect five

additional solenoid blocks and no discrepancies were noted.

Additionally, four other solenoid blocks were inspected and again

no discrepancies were noted. The licensee stated that the small

piece of nonmetallic metal in one solenoid block seemed to be an

isolated incident and, after reviewing the results of the

additional testing that was performed, was confident about the

qualification and operability of the solenoid valves. The newly

inspected solenoid valves have been installed on each of the eight

MSIV's and have been tested satisfactorily. The inspectors

completed an independent review of procedure 34SV-B21-002-IS:

Main Steam Isolation Valve Trip Test, the regulatory requirements,

acceptance criteria and test results. There were no discrepancies

identified. The inspectors will continue to monitor the

performance of the solenoid valves.

b.

Drywell Inspection

,

'

Due to some deficiencies noted during previous outage DW tours and

the significant amount of insulation material that the inspectors

,

had noted removed for work during the outage, the inspectors

examined conditions in the DW at the end of the outage. The

inspectors reviewed General Electric specification 21All82:

" Standard Requirements For Reactor Vessel Insulation" and the

associated drawings for the insulation installation and procedure

52GM-MME-007: Drywnll Closeout.

Even though the DW was not ready

for official closeout, the inspectors conducted an inspection of

the Unit 1 DW to assess the general conditions and observe work

activities associated with closecut preparation. The inspectors

viewed the general areas for cleanliness and assessed the amount

of scaffolding, tools and equipment yet to be removed.

Additionally, the inspectors inspected piping, valves and

connections for apparent deterioration, damage or leakage; and

observed the general condition and installation of the reactor

vessel insulation. The general areas were relatively clean and

most of the tools, equipment and scaffolding were removed. There

were no apparent valve or component leakage or damage identified.

,

The inspectors observed that, except for three or four pieces of

insulation around the main steam line penetrations, the reactor

vessel insulation was in place.

It was noted that several of the

fasteners used to hold the insulation in place were either damaged

or missing. The areas of insulation that were to be secured by

the damaged or missing fasteners were held together by wire.

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was also noted that a metal band which would. aid in holding the

insulation in place encircled the reactor vessel on the outside of

the insulation. The insulation showed many signs of dents and

scrapes, but these did not appear to affect the serviceability of

the insulation. There were some small gaps observed, but none

that seemed to be in excess of the specification guidelines.. It

3

was noted that three of the four pieces of insulation that were.

not installed were either placed on the grating or leaning against

l

the reactor vessel. Step 5.7.8 of GE specification 21A1182:

" Standard Requirements For Reactor Vessel Insulation," indicates

?

that the pieces of removable insulation would be placed on

I

hangers. Discussions with licensee personnel and a review of

procedure 52GM-MNT-018-OS: Removal, Storage'and Installation of

Reflective Insulation, indicated that insulation removed at Hatch

is not normally placed on hangers.

Instead, the procedure directs

i

establishing temporary storage a: close to the work area as-

.

practical. The three or four pieces of insulation observed by the

!

inspectors were placed very near the location where they would be

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reinstalled. The procedure also requires that barricades or signs

!

be installed to prevent personnel from climbing over.or standing

'

on the removed insulation while it is in temporary storage. .The

inspectors did not. observe any signs or barricades erected to

'

protect the pieces of insulation that were not installed. The

inspectors were informed that management is reviewing this issue-

!

and considering other storage methods which would reduce the

,

!

probability of damage to removed insulation.

'

5.

Outage Activities and Modifications (37701) (37828) (62703)

The inspector continued to review, observe and discuss specific

modifications completed, started and tested for the Unit 1 outage and

for Unit 2.

The specific modifications involved were :

1

DCR 89-278:

SBGT Hardened Vent Pipe Bypass

DCR 91-135:

SRVs Electrical Overpressure

i

DCR 92-011:

EHC System Logic Modifications

DCR 92-170:

Refueling Floor HVAC, Unit.2

3

The review consisted of the DCR packages, including the 50.59 reviews,

.i

individual design drawings within the DCR packages, and applicable

design drawing notes. The observations included the installation work

procedures of the Unit 2 refueling floor HVAC and post modification

testing of DCR's92-170 and 89-278. The discussions included attendance

at meetings, interfacing with licensee personnel and contractors,. and

discussing field observations and reviews with cognizant personnel.

j

!

The inspector closely reviewed DCR 92-011:

EHC System Logic

Modifications. This modification was implemented to remove the one of

one logic for turbine trips on low EHC fluid pressure, shaft low oil

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pressure, and stator cooling high outlet water temperature. The

implemented logic is 2 out of 3 for the parameters. The inspector

i

concluded that this modification did not impact the RPS trips from the

main turbine. The inspector was informed that this DCR was initiated

and sent to the field for implementation by the A/E, and not the vendor.

The inspector was also informed that the vendor has a modification

available which would provide the same 2 out of 3 logic. The vendor's

modification has a feature that the current modification does not have.

This feature would ensure that the system would fail in a safe

direction. Modifications management indicated that the DCR, as

implemented, would remain, and that during a future outage the

modification would be changed to incorporate the vendor's features.

The inspector reviewed modification, DCR 92-144:

Intake Structure

.

Ventilation Fans. This modification was initiated to eliminate a' single

failure vulnerability of the intake structure ventilation fans.

Fan

IX41-C009C was to be powered from a Unit 2 electrical source and fans

'

IX41-C009A and B were to remain powered from a Unit 1 power source. The

modification also required that each fan have their own control station,

consisting of a control switch and positions HAND-0FF-AUTO, and RED and

GREEN indicating lights, and a thermostat. The inspectors follow up

actions will consist of a review of the installation and testing of the

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DCR.

One Unit 2 modification was reviewed.

DCR 92-170 was implemented to

eliminate the ability to use four control switches for dampers, 2T41-

F023A/B and 2T41-F023A/B, to override the automatic closure of these

refueling floor ventilation system dampers. Control switch logic for

the dampers was modified to eliminate the OPEN position of the switches.

The positions were changed from AUTO-0 PEN to CLOSE-AUTO.

If the

switches are moved from the normal position AUTO they will be placed in

the safe position of CLOSE. The inspector reviewed the DCR package,

observed installation of the modification, and post maintenance testing.

The inspectors also attended several of the post Unit I refueling outage

training classes which discussed the modifications implemented on both

units during the Unit 1 outage. The inspector noted that the classroom

discussions and the handout information indicated that for DCR 92-051,

,

the internals of PSW valve IP41-F363 had been removed. This

modification was performed as a result of IPE information.

The

inspectors had noted that the entire valve was removed and replaced with

a spool piece. The inspector discussed this with the Unit 1 operations

manager to ensure that correct information was being provided to the

plant operations personnel.

All modification activities observed were carried out in accordance with

procedures, instructions and drawings and with adequate engineering

support.

No violations or deviations were identified

.

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21

6.

Reactor Water level Training (GL 92-04, TI 2515/119)

The inspector followed up on the licensee's response to GL 92-04,

" Resolution of the Issues Related to Reactor Vessel Water Level

Instrumentation in BWRs Pursuant to 10 CFR 50.44 (f)." The inspector

used Appendix A of TI 2515/119 as a checklist of licensee activities.

Additionally, the inspection consisted of review of classroom attendance

records, shift briefing records and discussions with licensed operators.

The discussions with licensed operators indicated the operators had

attended training, were aware of the water level issues and were

familiar with the Emergency Operating Procedures that dealt with the

uncertainties associated with reactor water level indications. The

inspector conducted discussions with operator licensing training

instructor and reviewed lesson plan LR-IH-50002-01:

Noncondensible Gas

Effects on Reactor Water Level Indication. The lesson plan contained

interim policies to follow following rapid reactor depressurizations

(less that 450 psig at greater than 100 degrees F per hour) to verify

that the cold-reference leg instruments had not been affected.

Basically, this consisted of comparing the different level recorders and

verifying that the difference in indication was less that 10 inches.

If

the difference in the level recorders indication was less that 10

inches, it could be assumed that non-condensible gases had not evolved

in the reference legs

The inspector determined that training had not

developed a specific simulator scenario to exercise these particular

anomalies. Since the issue was still under investigation by the BWROG,

the licensee had not developed simulator software to model .the

phenomenon. However, the inspector verified that there were 3 or 4

other simulator scenarios that would require the operators to evaluate

the operability of level indications. The scenarios consisted of events

that caused rapid reactor depressurization, high DW temperatures, and

complete or partial loss of reactor level indications.

Based upon these-

events, the operators would be required to perform reactor pressure

vessel flooding, and/or containment flooding.

The inspectors have also walked down the physical arrangement of most of

the reactor vessel level indication piping in both DWs during previous

outages. Discussions were held with the engineer responsible for the

licensee's overall actions in response to the GL. Several modifications

have been completed and additional work is under consideration.

Information indicates that Hatch has not observed the level indication

" notching" effect, although some level oscillations have been noted

under low pressure conditions.

The inspectors concluded, based upon the areas inspected, the actions

taken by the licensee were adequate and met the criteria of GL 92-04 and

TI 2515/119.

No violations or deviations were identified.

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6.

Inspection of Open items (92700) (90712) (92701)

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The following item was reviewed using licensee reports, inspections,

record reviews, and discussions with licensee personnel, as appropriate:

a.

(Closed)

IFI 50-321/92-29-02:

Inspection of Unit 1 Shroud Access-

Hole Covers.

During the recent outage, DCR 93-002 was

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4

implemented. This design change replaced the welded Inconel Alloy

600 circular access hole covers, located in the core shroud area,

with bolted covers. This item is closed for Unit 1 and remains

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open for Unit 2.

7.

Exit Interview

The inspection scope and findings were summarized on May 12, 1993, with

those persons indicated in paragraph 1 above. The inspectors described

the areas inspected and discussed in detail the inspection findings.

Dissenting comments were received in two areas. The licensee took israe

with the statement "that if the loss of SDC flow would have occurred

under certain conditiont which existed earlier in the outage, a more

significant safety concern could have resulted." The licensee also

questioned the appropriateness of citing the dosimetry calibration issue

under 10 CFR 50.9 instead of 10 CFR 50.5.

The licensee did not identify

as proprietary any of the material provided to or reviewed by the

inspectors during this inspection.

Item Number

Status

Description and Reference

,

321/93-06-01

Open

VIO - Failure to Comply With

Shutdown Cooling TS Requirements,

paragraph 2.b

321/93-06-02

Open

VIO - Failure to Follow EDG Alarm

Response Procedures, paragraph 3.b

NCV 321,366/93-06-03

Open and

NCV - False Documentation of

Closed

Portions of a Pocket Dosimeter

Calibration Test, paragraph 2.c

8.

Acronyms and Abbreviations

ADS - Automatic depressurization System

A/E - Architect Engineer

AGM-P0- Assistant General Manager - Plant Operations

AGM-PS- Assistant General Manager - Plant Support

AHC - Access Hole Covers

AHU

Air Handling Unit

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APRM - Average Power Range Monitor

ATWS - Anticipated Transient Without Scram

BWR - Boiling Water Reactor

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BWROG- Boiling Water Reactors Owners Group

CB0 - Control Board Operator

Code of Federal Regulations

CFR

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CILRT - Containment Integrated Leakrate Test

CR

- Control Room

CRD - Control Rod Drive

CS

Core Spray

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CST

Condensate Storage Tank

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DC

- Deficiency Card

DCR - Design Change Request

.

DW

- Drywell

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ECCS - Emergency Core Cooling System

EDG - Emergency Diesel Generator

EDT - Eastern Daylight Time

Electro Hydraulic Control System

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EHC

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EQ

- Equipment . Qualification

ERT - Event Review Team'.

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ESF - Engineered Safety Feature

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EST - Eastern Standard Time

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F

- Fahrenheit

Fire Hazards Analysis

FHA

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FPC - Fuel Pool Cooling

-*

FSAR - Final Safety Analysis Report

GE

- General Electric Company

i

Generic Letter

GL

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GPM - Gallons per Minute

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HP

- Health Physics

HPCI - High Pressure Coolant Injection System-

HVAC - Heating, Ventilation and Air Conditioning

Heat Exchanger

.:

HX

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I&C -

Instrumentation and Controls

!

IFI - Inspector Followup Item

l

IN

- Information Notice

1

IPE - Individual Plant Examination

i

IRM -

Intermediate Range Monitor

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IST - Inservice. Testing

!

Kilowatt

!

KW

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LC0 - Limiting Condition for Operation

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LER - Licensee Event Report

!

LOCA - Loss of Coolant Accident

~j

LOSP - Loss of Site Power

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LPRM'- Local Power Range Monitor

l

LSFT - Logic System Functional Test

j

-MFP - Main Feed Pump

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MSIV - Main Steam Isolation Valve

MWE - Megawatts Electric.

!

MWO - Maintenance Work Order

!

Non-cited Violation

i

NCV

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NRC ' - Nuclear Regulatory Commission

NRHX - Non Regenetive Heat Exchanger

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NRR - Office of Nuclear Reactor Regulation

NSAC - Nuclear Safety and Compliance

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PCIS - Primary Containment Isolation System

PE0

Plant Equipment Operator

-

PIC - Pocket Ion Chamber

P&ID - Piping and Instrumentation Drawing

PM

- Preventive Maintenance

psig - Pounds Per Square Inch Gauge

PSW - Plant Service Water System

RB

- Reactor Building

RBM - Rod Block Monitor

RCIC - Reactor Core Isolation Cooling System

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RFP - Reactor Feed Pump

RFPT - Reactor Feed Pump Turbine

RHR - Residual Heat Removal

RHRSW- Residual Heat Removal Service Water System

RPS - Reactor Protection System

RTD - Resistance Temperature Detector

RTP - Rated Thermal Power

RWCU - Reactor Water Cleanup System

RWM - Rod Worth Minimilar

RWP - Radiation Work Permit

RX

- Reactor

SAER - Safety Audit and Engineering Review

SBGT - Standby Gas Treatment System

SBLC -

Standby Liquid Control System

SCS - Southern Company Services

SDC - Shutdown Cooling

.

SER - Safety Evaluation Report

SFP - Spent Fuel Pool

SNC - Southern Nuclear Company

SOR - Significant Occurrence Report

SOS - Superintendent of Shift (Operations)

SPDS - Safety Parameter Display System

SR0 - Senior Reactor Operator

-

SRV - Safety Relief Valve

SS

- Shift Supervisor

STA - Shift Technical Advisor

SUT - Startup Transformer

TI

- Temporary Instruction

TLD - Thermal Luminescent Dosimetry

TS

- Technical Specifications

URI

- Unresolved Item

WPS - Work Process Sheets

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