05000272/LER-1981-064-01, /01T-0:on 810715,during Routine Insp,Svc Water Leak Was Discovered on Containment Fan Coil Unit.Caused by Cracked Weld Upstream of Valve 15SW65.Dissimilar Metal Piping Changed to All Stainless Steel

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/01T-0:on 810715,during Routine Insp,Svc Water Leak Was Discovered on Containment Fan Coil Unit.Caused by Cracked Weld Upstream of Valve 15SW65.Dissimilar Metal Piping Changed to All Stainless Steel
ML20010C736
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/11/1981
From: Dickey F
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010C735 List:
References
LER-81-064-01T, LER-81-64-1T, NUDOCS 8108200363
Download: ML20010C736 (1)


LER-1981-064, /01T-0:on 810715,during Routine Insp,Svc Water Leak Was Discovered on Containment Fan Coil Unit.Caused by Cracked Weld Upstream of Valve 15SW65.Dissimilar Metal Piping Changed to All Stainless Steel
Event date:
Report date:
2721981064R01 - NRC Website

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S EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h I o i 21 l On July 15, 1981, during a routine containment inspection, a service water leak was j 15 containment ran i ITTTl i discovered emanating from a 3/4" vent connection pipe weld on no.

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E l service, isolated and action statement 3.6.2.3.a was entered at 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br />.

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