LER-1981-015, /03L-0:on 810531,twelve Penetrations Were Found Leaking Excessively.Ten Caused by Normal Wear & Two by Improper Limitorque Operation.Valve Repairs Performed |
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t Mr. K. V. Seyfrit, Director June 30, 1981 Page 2.
Initial leakage was found to be.39 cfh. The established limit is 0.1 scfh. aCAD-1311 Limitorque motor operator was adjusted. After adjust-ment the leakage was reduced to.08 scfh. The leaking valves are Anchor 1" gate valves with Limitorque motor operators.
X-14 RWCU, Inlet to RWCU System.
RWCU-M0-15 (supply inboard isolation) and RWCU-MO-18 (supply outboard isolation).
Initial leakage was found to be 39.67 cfh. The established limit is 2.0 scfh.
RWCb-MO-15 and RWCU-MO-18 were disassembled and gates removed and lapped, seals cleaned and reassembled. After reassembly, the leakage check was 39.6 scfh. The leakage was determined to be from RWCU-M0-15.
3 ove the established limit, further repair b
Even though the leakage wat was not initiated because of the safety margin in the established limits.
Primary containment would be maintained by the outboard isolation valve.
RWCU-MO-15 and M0-18 are Anchor 6" gate valves.
i X-13A RHR Loop "A" Supply to RPV.
RRR-MO-25A (loop "A" inboard injection block) and RHR-M0-27A (1)op "A" outboard injection block).
Initial leakage was found to be 34.12 cfh. The established limit is 10 scfh. RHR-M0-25A was disassembled and the seats were lapped, seal rings replaced and reassembled. After repair of RHR-M0-25A, the leakage was 0 scfh.
RHR-M0-25A is an Anchor 24" gate valve.
X-8 Main Steam Line Drain. MS-MO-74 (inboard isolation valve) and MS-MO-77 (outboard isolation valve).
Initial leakage was found to be 18.28 cfh. The established limit is 1.5 scfh. MS-MO-74 was disassembled, the disc removed and lapped, the seats were cleaned, and valve reassembled. After repair, the leakage was.23 scfh. MS-M0-74 is an Anchor 3" gate valve.
X-205 ACAD Porge Supply Line to the Suppression Chamber. ACAD-1303MV (out-Soard isolation valve) and ACAD-1304MV (inboard isolation valve).
The initial leakage was too rapid to determine an initial leak rate.
The established Timit is.1 scfh. The gate was removed and lapped, the seats were cleaned, and the valve reassembled. Retest indicated ACAD-1303MV was not shutting tightly. A new Limitorque was installed cn *E valve. After replacement of the Limitorque, the leak rate was reJ"ceu to.007 scfh. ACAD-1304MV was not repaired or adjusted. Therefore, primary containment would have been maintained by the inboard isolation valve ACAD-1304MV. The leaking valve is an Anchor 1" gate valve with a Limitorque operator.
8107280631 810630 PDR ADOCK 05000290 S
PDR
- M*:. K. V. Ocy'rit, Director June 30,'1981 Page 3.
L-212 RCIC Turbine Exhaust to the Suppression Chamber, RCIC-15CV and RCIC 37.
Initial leakage was found to be 9.3 cfh. The established limit is 1.0 scfh. RCIC-37 was disassembled for repair and indicated rough seating surfaces. The seats were lapped and the disc cleaned and valve reas-sembled. After rep..ir to RCIC-37, the leakage rate was 2.3 scfh. Even though the leakage was above established limit, further repair was not initiated because of the safety margin in the established limits. RCIC-37 is an 8" Anchor globe valve.
X-210B and X-211B RHR to Suppression Pool.
RHR-M0-34B (supprassion pool cooling inboard)
RHR-M0-38B (suppression pool inboard spray) and RHR-M0-29B (suppression pool cooling and spray outboard block valve).
Initial leakage was found to be 210 cfh. The established limit is 8.0 scfh. RHR-M039B was disassembled, the seats and gate were lapped, and a new bonnet gasket installed.
rhe valve was reassembled and tested.
After repair of RHR-MO-39B, ne leakage was 1.68 cfh. RHR-HV-34B and RHR-MO-38B were not repaireo or adjusted. RHR-M0-39B is an Anchor 18" gate valve.
X-220 Primary Containment Purge and Vent Exhaust From Suppression Chamber.
PC-M0-230 (inboard isolation valve) PC-AO-245 (outboard isolation valve). PC-57MV (inboard isolation bypass) and ACAD-1308MV (ACAD torus vent).
The initial leakage was too u
- termine an initial leak rate.
The established limit is 5.0 scfh.
FC-A0-245 was disassembled and the rubber seating ring replaced. After repair, the leakage was 2.8 scfh.
PC-230MV and PC-57MV were not repaired or adjusted. Therefore, primary contcinment would have been maintained by the inboard isolation valves.
PC-245AV is - 24" Allis-Chalmers butterfly valve.
X-221 1
RCIC Vacuum Pump Discharge to Suppression Chamber The test volume for this penetration is between RCIC-12CV and manual valve RCIC-42.
Initial leakage was found to be 2.23 cfh. The estab-i lished limit is.1 scfh. FCIC-12CV was disascembled~and was found to have a dirty seat causing improper seating. The seat was cleaned and valve reassembled. After reassembly and retest, the leakage was.09 scfh. RCIC-12CV is an Anchor 2", 600# check valve.
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Mr. K. V. Scyfrit, Dirsctor June 30, 1981 Page 4.
X-223B Core Spray Pump "B" Minimum Flow Recirc Isolation.
The test volume for this penetration is between CS-MOV-M05B and CS-V-25.
Initial leaking tests showed a leak rate of 7.86 cfh. The established limit is 1.0 scfh. CS-MO-5B and CS-V-25 were both disassembled. New seat rings were installed in CS-MOV-5B and the gate was lapped followed by blue check of seats. The stem and seats of CS-V-25 were cleaned and reassembled with new gasket. After repair to the two valves, the retest leakage was.13 scfh. CS-MOV-M05B is an Anchor 3" gate valve and CS-V-25 is an Anchor 3" globe valve.
Per Section 4.7.A.2.f of the Technical Specifications, all valves were tested at > 58 psig with the exception of the MSIV's.
Pressure decay or water collection was used to determine the leakage. The total as-found leakage was approximately 505.8 cfm.
Of this, the uncontained leakage was determined to be less than 132.8 scfh. This leak rate does not exceed the equivalent of.6 La (189 scfh) of the primary _ containment volume per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> at 58 psig as addressed in Technical Specification Section 4.7.A.2.a. Page 160. After repair of the leaking valves, the leak rate was reduced to less than 136.5 scfh.
4 Sincerely,
- - v-m L. C. Lessor Station Superintendent Cooper Nuclear Station LCL:cg
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ARC FORM 366 U. S. NUCLEAR REGULATORY s JMMISSION
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H 60 61 DOCKET NUMBER 68 69 EVENT DATE 14 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o l 2 l l While performing local leak rate test procedure 6.3.1.1, twelve penetrations were 1 [o l3l lfound leaking excessively. Technical Specifications Section 3.7.4 requires the l
1014 l l primary containment leakage to be less than 189 scfh (.6 La).
The uncontained I
l o I s l I leakane was less than 132.8 scfh. UE 75-22 and LER's 77-57, 79-9 and 80-12 I
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There was no significant occurrence as I
l o 17 l l a result of this event. There were no adverse effects to public health and i
I O Ia l ! safety.
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33 34 35 36 JI 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l i l U l l Ten leaks were caused by normal valve wear, two by improper Limitorque operation.
I i i l Valve repairs were performed on one 24" AC butterfiv, one 24" Anchor gate, one 18" l li121lArchor gate, one 6" Anchor gate, two 3" Anchor gates, one 1" Anchor gate, one 8" l
l i l a i I Anchor niobe. one 3" Anchor clobe and one 2" Anchor check valve. One Limitorque l
najn= coa. Final leakage was less than 136.5 scfh.
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NAME OF PREPARER PHONE:
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| 05000298/LER-1981-001-03, /03L-0:on 810102,hydraulic Shock Suppressor RF-S4 Discovered Inoperable.Caused by Improper Installation. Suppressor Reoriented Properly | /03L-0:on 810102,hydraulic Shock Suppressor RF-S4 Discovered Inoperable.Caused by Improper Installation. Suppressor Reoriented Properly | | | 05000298/LER-1981-001, Forwards LER 81-001/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-001/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-002, Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-002-03, /03L-0:on 810213,brass Filings Found in Oil Sump of Outboard Motor Bearing of RHR Svc Water Booster Pump. Caused by Loose Inboard Motor Fan & Set Screw.Fan Repaired & Second Set Screw Added | /03L-0:on 810213,brass Filings Found in Oil Sump of Outboard Motor Bearing of RHR Svc Water Booster Pump. Caused by Loose Inboard Motor Fan & Set Screw.Fan Repaired & Second Set Screw Added | | | 05000298/LER-1981-003-03, /03L-0:on 810223,RHR-MO-26B Motor Amps Increased & Remained Excessively High When Valve Reached Closed Position.Caused by Limit Switch on Limitorque SMB-O Valve Motor Operator Not Opening & de-energizing Starter | /03L-0:on 810223,RHR-MO-26B Motor Amps Increased & Remained Excessively High When Valve Reached Closed Position.Caused by Limit Switch on Limitorque SMB-O Valve Motor Operator Not Opening & de-energizing Starter | | | 05000298/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000298/LER-1981-004-03, /03L-0:on 810306,during Normal Operation,Relay 27x3/1G Found de-energized.Cause Unknown.Relay Replaced. Operation Verified.Corresponding Relay for Redundant Sys Found Operable | /03L-0:on 810306,during Normal Operation,Relay 27x3/1G Found de-energized.Cause Unknown.Relay Replaced. Operation Verified.Corresponding Relay for Redundant Sys Found Operable | | | 05000298/LER-1981-005, Forwards LER 81-005/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-005/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-005-03, /03L-0:on 810320,reactor Bldg Closed Cooling Water Pump 1D Tripped During Start.Caused by Installation of Undersized Fuse.Fuses Replaced | /03L-0:on 810320,reactor Bldg Closed Cooling Water Pump 1D Tripped During Start.Caused by Installation of Undersized Fuse.Fuses Replaced | | | 05000298/LER-1981-006, Forwards LER 81-006/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-006/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-006-03, /03L-0:on 810414,during Normal Surveillance Testing of Scram Discharge Header Cms,Three of Four Channels Installed Failed.Caused by Component Failure.Marginal Crystals Used in Transmitter Replaced by Manufacturer | /03L-0:on 810414,during Normal Surveillance Testing of Scram Discharge Header Cms,Three of Four Channels Installed Failed.Caused by Component Failure.Marginal Crystals Used in Transmitter Replaced by Manufacturer | | | 05000298/LER-1981-007, Forwards LER 81-007/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-007/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-007-03, /03L-0:on 810426,diesel Generator 1 Cylinder Temp Increased During Surveillance Procedure 6.5.12.1 W/Reactor in Cold Shutdown.Caused by Temporary Air Pressure Test Gauge Which Fell Off Control Air Supply | /03L-0:on 810426,diesel Generator 1 Cylinder Temp Increased During Surveillance Procedure 6.5.12.1 W/Reactor in Cold Shutdown.Caused by Temporary Air Pressure Test Gauge Which Fell Off Control Air Supply | | | 05000298/LER-1981-008-03, /03L-0:on 810426,reactor Vessel Level Switch LIS-72C,Switch-4,caused Continuous Annunciator 9-3-1/8-2 Alarm.Caused by Failure of Yarway Model 4418C Level Indicating Switch,Due to Film Buildup Between Contacts | /03L-0:on 810426,reactor Vessel Level Switch LIS-72C,Switch-4,caused Continuous Annunciator 9-3-1/8-2 Alarm.Caused by Failure of Yarway Model 4418C Level Indicating Switch,Due to Film Buildup Between Contacts | | | 05000298/LER-1981-008, Forwards LER 81-008/03L-0.Detailed Event Analysis Encl | Forwards LER 81-008/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-009-03, /03L-0:on 810503,two Pacific Scientific Model PSA-10 Mechanical Shock Suppressors Found Inoperable.Cause Under Evaluation.Snubber Replaced | /03L-0:on 810503,two Pacific Scientific Model PSA-10 Mechanical Shock Suppressors Found Inoperable.Cause Under Evaluation.Snubber Replaced | | | 05000298/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000298/LER-1981-010-03, /03L-0:on 810505,static Inverter 1A Spike Suppressor Capacitor Failed Causing Inverter to Become Inoperable.Caused by Aging & Effects of High Ripple Charger | /03L-0:on 810505,static Inverter 1A Spike Suppressor Capacitor Failed Causing Inverter to Become Inoperable.Caused by Aging & Effects of High Ripple Charger | | | 05000298/LER-1981-011, Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-011-03, /03L-0:on 810528,during Insp of Unexpected Alarm, CS Header Break Detection Instrument Switches Found Piped to Incorrect Lines.Caused by Connection to Wrong Line at Drywell Penetration.Instruments Connected to Proper Lines | /03L-0:on 810528,during Insp of Unexpected Alarm, CS Header Break Detection Instrument Switches Found Piped to Incorrect Lines.Caused by Connection to Wrong Line at Drywell Penetration.Instruments Connected to Proper Lines | | | 05000298/LER-1981-012, Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-012-03, /03L-0:on 810519,during Testing HPCI-PS-68D Tripped at 89 Psig Instead of 100 Psig Tech Spec Limit. Caused by Random Instrument Drift.Instrument Immediately Recalibr & Returned to Svc | /03L-0:on 810519,during Testing HPCI-PS-68D Tripped at 89 Psig Instead of 100 Psig Tech Spec Limit. Caused by Random Instrument Drift.Instrument Immediately Recalibr & Returned to Svc | | | 05000298/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-013-03, /03L-0:on 810528,during Testing of Station Battery Rated Load Test W/Plant in Cold shutdown,125 Volt Batteries 1A & 1B Discharged at Rate Greater than Required.Caused by Error in Reading Procedure.Procedure Will Be Revised | /03L-0:on 810528,during Testing of Station Battery Rated Load Test W/Plant in Cold shutdown,125 Volt Batteries 1A & 1B Discharged at Rate Greater than Required.Caused by Error in Reading Procedure.Procedure Will Be Revised | | | 05000298/LER-1981-014, Forwards LER 81-014/03L-0.Detailed Event Analysis Encl | Forwards LER 81-014/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-014-03, /03L-0:on 810608,during Testing,Hpci Pump Turbine Tripped on Overspeed Prior to Reaching Rated Sys Flow.Sys Declared Inoperable.Caused by Improper Valve line-up Procedure.Valve Throttled & Tested | /03L-0:on 810608,during Testing,Hpci Pump Turbine Tripped on Overspeed Prior to Reaching Rated Sys Flow.Sys Declared Inoperable.Caused by Improper Valve line-up Procedure.Valve Throttled & Tested | | | 05000298/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Also Submitted | Forwards LER 81-015/03L-0.Detailed Event Analysis Also Submitted | | | 05000298/LER-1981-015-03, /03L-0:on 810531,twelve Penetrations Were Found Leaking Excessively.Ten Caused by Normal Wear & Two by Improper Limitorque Operation.Valve Repairs Performed | /03L-0:on 810531,twelve Penetrations Were Found Leaking Excessively.Ten Caused by Normal Wear & Two by Improper Limitorque Operation.Valve Repairs Performed | | | 05000298/LER-1981-016, Forwards LER 81-016/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-016/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-016-03, /03L-0:on 810610,core Thermal Power Calculation Performed by Process Computer Found Incorrect Due to Incorrect Feedwater Flow Value in Computer.Caused by Personnel Error in Changing Conversion Coefficient | /03L-0:on 810610,core Thermal Power Calculation Performed by Process Computer Found Incorrect Due to Incorrect Feedwater Flow Value in Computer.Caused by Personnel Error in Changing Conversion Coefficient | | | 05000298/LER-1981-017-03, /03L-0:on 810613,reactor Core Isolation Cooling Sys Steam Supply Valve RCIC-MOV-M016 Failed to Open.Caused by Improperly Wired Motor Operator Circuit.Jumper Installed | /03L-0:on 810613,reactor Core Isolation Cooling Sys Steam Supply Valve RCIC-MOV-M016 Failed to Open.Caused by Improperly Wired Motor Operator Circuit.Jumper Installed | | | 05000298/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-018-03, /03L-0:on 810625,pressure Switch NBI-PS-52A Found W/Trip Point Less Conservative than Tech Spec.Apparently Caused by Setpoint Drift.Switch Readjusted.Setpoints for Switches Reset | /03L-0:on 810625,pressure Switch NBI-PS-52A Found W/Trip Point Less Conservative than Tech Spec.Apparently Caused by Setpoint Drift.Switch Readjusted.Setpoints for Switches Reset | | | 05000298/LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-019-03, /03L-0:on 810728,during Surveillance to Prove Operability of Diesel Generator 1,fuel Supply Hose Developed Leak.Caused by Excessive Localized Flexure & Vibration. Hose Replaced | /03L-0:on 810728,during Surveillance to Prove Operability of Diesel Generator 1,fuel Supply Hose Developed Leak.Caused by Excessive Localized Flexure & Vibration. Hose Replaced | | | 05000298/LER-1981-019, Forwards LER 81-019/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-019/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-020, Forwards LER 81-020/03L-0. Detailed Event Analysis Also Submitted | Forwards LER 81-020/03L-0. Detailed Event Analysis Also Submitted | | | 05000298/LER-1981-020-03, /03L-0: on 810728, During Procedure Returning Diesel Generator 1 to Svc After Flexible Fuel Line Leak, Control Air Line Fitting Failed Causing Generator to Shut Down. Caused by Broken Air Line Due to Crimped Ferrule | /03L-0: on 810728, During Procedure Returning Diesel Generator 1 to Svc After Flexible Fuel Line Leak, Control Air Line Fitting Failed Causing Generator to Shut Down. Caused by Broken Air Line Due to Crimped Ferrule | | | 05000298/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Rept Submitted | Forwards LER 81-021/03L-0.Detailed Event Rept Submitted | | | 05000298/LER-1981-021-03, /03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced | /03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced | | | 05000298/LER-1981-022-03, /03L-0:on 810912,blown Fuse in Valve Motor Circuit Disabled Valve & Reactor Core Isolation Cooling Sys.Caused by Motor Grounded by Grease That Penetrated Defective Seal in Valve Operator & Into Armature.Motor & Seal Replaced | /03L-0:on 810912,blown Fuse in Valve Motor Circuit Disabled Valve & Reactor Core Isolation Cooling Sys.Caused by Motor Grounded by Grease That Penetrated Defective Seal in Valve Operator & Into Armature.Motor & Seal Replaced | | | 05000298/LER-1981-022, Forwards LER 81-022/03L-0.Detailed Event Analysis Also Submitted | Forwards LER 81-022/03L-0.Detailed Event Analysis Also Submitted | | | 05000298/LER-1981-023-03, /03L-0:on 811026,uncalibr Temp Switch Installed in MS-TS-1480 During 1981 Refueling Outage.Caused by Technician Error.Technicians Counseled.Will Color Code Switches & Revise Surveillance Procedure | /03L-0:on 811026,uncalibr Temp Switch Installed in MS-TS-1480 During 1981 Refueling Outage.Caused by Technician Error.Technicians Counseled.Will Color Code Switches & Revise Surveillance Procedure | | | 05000298/LER-1981-023, Forwards LER 81-023/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-023/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-024-03, /03L-0:on 811106,safety Relief Valve 71-D Failed to Close After Test.Caused by Failure of Solenoid Plunger to Drop Out When Solenoid de-energized.Solenoid Replaced | /03L-0:on 811106,safety Relief Valve 71-D Failed to Close After Test.Caused by Failure of Solenoid Plunger to Drop Out When Solenoid de-energized.Solenoid Replaced | | | 05000298/LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-025-04, /04T-0:on 811224,during Full Power,Discharge Was Made from Floor Drain Sample Tank W/O Adequate Sampling & Analysis of Batch.Caused by Personnel Error.Liquid Discharge Procedures Being Revised.Personnel Reprimanded | /04T-0:on 811224,during Full Power,Discharge Was Made from Floor Drain Sample Tank W/O Adequate Sampling & Analysis of Batch.Caused by Personnel Error.Liquid Discharge Procedures Being Revised.Personnel Reprimanded | | | 05000298/LER-1981-025, Forwards LER 81-025/04T-0.Detailed Event Analysis Encl | Forwards LER 81-025/04T-0.Detailed Event Analysis Encl | |
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