LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl |
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CNSS810747 December 3, 1981 p
7 W (b[./[f} [D Mr. K. V. Seyfrit, Director U.S. Nuclear Regulatory Commission
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(1 Office of Inspection and Enforcement k
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611 Ryan Plaza Drive Qr%
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Suite 1000 Arlington, Texas 76011
Dear Sir:
D This report is submitted in accordance with Section t,.7.2.B.2 of the Technical Specifications for Cooper Nuclear Station and discusses a reportable occurrence that was discovered on November 6, 1981. A li-censee event report form is also enclosed.
Report No.:
50-298-81-24 Report Date:
December 3, 1981 Occurrence Date: November 6, 1981 Facility:
Cecper Nuclear Station Brownville, Nebraska 68321 Identification of Occurrence:
A condition which led to operation in a degraded mode permitted by a limiting condition for operation established in Paragraph 3.6.D.1 of the Technical Specifications.
Conditions Prior to Occurrence:
The reactor was operating at approximately 3% of rated thermal power during a startup.
Reactor pressure was approximately 150 psig.
Description of Occurrence:
While performing Surveillance Procedure 6.3.2.1, (SRV Manual Ac-j tuation) Safety Relief Valve (SRV) 71-D failed to close after the 150 psig test.
Designation of Apparent Cause of Occurrence:
The apparent cause of this occurrence was a shift of drop-out pressure of the solenoid valve.
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Mr. K. V. Seyfrit December 3, 1981 Page 2.
Analysis of Occurrence:
SRV 71-D is one of eight (8) Target Rock pressue relief valves on the reactor vessel. These particular Target Rock valves are pilot operated valves each with an auxiliary air operator solenoid valve.
Six (6) of the eight SRV's are also part of the Automatic Depres-surization System (ADS).
SRV 71-D, however, is not one of the ADS valves.
While performing a surveillance procedure on the SRV's.during reactor startup, SRV 71-D failed to close. At tne time of the failure, reactor pressure was_at approximately 150 psig and in-strument air pressure was approximately 115 psig.
Several attempts were made to close SRV 71-D by cycling the control switch on con-trol room panel 9-3;-however, the valve did not close. After the
- - control switch was cycled with unsuccessful results, the Shift Supervisor removed the solenoid control fuse, de-energizing the solenoid.
SRV 71-D still would.not close.
After the above attempts to close SRV 71-D failed, a reactor shut-down was initiated so that the problem could be further investi-gated and corrected.
Subsequent to the reactor shutdown, a review of the SRV temperature recorder indicated that SRV 71-D closed at a reactor pressure of approximately 15-20 psig. The reactor vessel cooldown rate due to the SRV not closing was witian Technical Specification vessel cooldown limits. During the drywell entry following shutdown, it was discovered that with the control switch in the close position and the solenoid control fuse removed, in-strument air was continuously venting from the control solenoid.
This indicated that the solenoid had not dropped out when de-energized.
The solenoid removed from SRV 71-D was subsequently disassembled and inspected visually by CNS personnel. With the exception of a damaged 0-ring, the inspection revealed no apparent cause of the malfunction.
Following the CNS inspection, the SRV solenoid was returned to the manufacturer, Target Rock Corp., for inspection and investigation into the malfunction of the subject solenoid. The results of the investigation revealed that the minimum drop-out pressure of the solenoid had shifted from 135 psig minimum to a drop-out pressure of approximately 118 psig. No other conclusive evidence as to the failure of the solenoid could be ascertained by the vendor.
r-a Mr. K. V. Seyfrit December 3, 1981 Page 3.
During the Spring 1981 Refueling Outage, each of the eight (8) SRV I
solenoids and air operators were removed, disassembled, inspected, and subsequently tested with satisfactory results. This evaluation I
was in response to NRC IE Bulletin No. 80-25.
The 0-rings which were installed during reassembly were lubricated with Neo-lube per the vendor's recommendations.
SRV 71-D was inoperable less than one day following reactor start-up.
During the' period of inoperability, the pressure relief feature of SRV 71-D was still operable. Additionally, the other seven (7)
SRV's were operational if needed and the low pressure emergency core cooling systems were available if needed. This occurrence presented no -adverse consequences. from the standpoint of public health and safety.
Corrective Action
The safety / relief valve solenoid was immediately removed and re-placed with a spare solenoid.
Surveillance Procedure _6.3.2.1 (SRV Manual Actuation) was again performed on the subject valve with satisfactory results. We have discussed this problem with our valve supplier and the valve manufacturer.
It is our understanding that our supplier is pursuing a generic fix.
Sincerely, L. C. Lessor Station Superintendent Cooper Nuclear Station LCL:cg Attach.
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| 05000298/LER-1981-001-03, /03L-0:on 810102,hydraulic Shock Suppressor RF-S4 Discovered Inoperable.Caused by Improper Installation. Suppressor Reoriented Properly | /03L-0:on 810102,hydraulic Shock Suppressor RF-S4 Discovered Inoperable.Caused by Improper Installation. Suppressor Reoriented Properly | | | 05000298/LER-1981-001, Forwards LER 81-001/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-001/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-002, Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-002-03, /03L-0:on 810213,brass Filings Found in Oil Sump of Outboard Motor Bearing of RHR Svc Water Booster Pump. Caused by Loose Inboard Motor Fan & Set Screw.Fan Repaired & Second Set Screw Added | /03L-0:on 810213,brass Filings Found in Oil Sump of Outboard Motor Bearing of RHR Svc Water Booster Pump. Caused by Loose Inboard Motor Fan & Set Screw.Fan Repaired & Second Set Screw Added | | | 05000298/LER-1981-003-03, /03L-0:on 810223,RHR-MO-26B Motor Amps Increased & Remained Excessively High When Valve Reached Closed Position.Caused by Limit Switch on Limitorque SMB-O Valve Motor Operator Not Opening & de-energizing Starter | /03L-0:on 810223,RHR-MO-26B Motor Amps Increased & Remained Excessively High When Valve Reached Closed Position.Caused by Limit Switch on Limitorque SMB-O Valve Motor Operator Not Opening & de-energizing Starter | | | 05000298/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000298/LER-1981-004-03, /03L-0:on 810306,during Normal Operation,Relay 27x3/1G Found de-energized.Cause Unknown.Relay Replaced. Operation Verified.Corresponding Relay for Redundant Sys Found Operable | /03L-0:on 810306,during Normal Operation,Relay 27x3/1G Found de-energized.Cause Unknown.Relay Replaced. Operation Verified.Corresponding Relay for Redundant Sys Found Operable | | | 05000298/LER-1981-005, Forwards LER 81-005/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-005/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-005-03, /03L-0:on 810320,reactor Bldg Closed Cooling Water Pump 1D Tripped During Start.Caused by Installation of Undersized Fuse.Fuses Replaced | /03L-0:on 810320,reactor Bldg Closed Cooling Water Pump 1D Tripped During Start.Caused by Installation of Undersized Fuse.Fuses Replaced | | | 05000298/LER-1981-006, Forwards LER 81-006/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-006/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-006-03, /03L-0:on 810414,during Normal Surveillance Testing of Scram Discharge Header Cms,Three of Four Channels Installed Failed.Caused by Component Failure.Marginal Crystals Used in Transmitter Replaced by Manufacturer | /03L-0:on 810414,during Normal Surveillance Testing of Scram Discharge Header Cms,Three of Four Channels Installed Failed.Caused by Component Failure.Marginal Crystals Used in Transmitter Replaced by Manufacturer | | | 05000298/LER-1981-007, Forwards LER 81-007/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-007/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-007-03, /03L-0:on 810426,diesel Generator 1 Cylinder Temp Increased During Surveillance Procedure 6.5.12.1 W/Reactor in Cold Shutdown.Caused by Temporary Air Pressure Test Gauge Which Fell Off Control Air Supply | /03L-0:on 810426,diesel Generator 1 Cylinder Temp Increased During Surveillance Procedure 6.5.12.1 W/Reactor in Cold Shutdown.Caused by Temporary Air Pressure Test Gauge Which Fell Off Control Air Supply | | | 05000298/LER-1981-008-03, /03L-0:on 810426,reactor Vessel Level Switch LIS-72C,Switch-4,caused Continuous Annunciator 9-3-1/8-2 Alarm.Caused by Failure of Yarway Model 4418C Level Indicating Switch,Due to Film Buildup Between Contacts | /03L-0:on 810426,reactor Vessel Level Switch LIS-72C,Switch-4,caused Continuous Annunciator 9-3-1/8-2 Alarm.Caused by Failure of Yarway Model 4418C Level Indicating Switch,Due to Film Buildup Between Contacts | | | 05000298/LER-1981-008, Forwards LER 81-008/03L-0.Detailed Event Analysis Encl | Forwards LER 81-008/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-009-03, /03L-0:on 810503,two Pacific Scientific Model PSA-10 Mechanical Shock Suppressors Found Inoperable.Cause Under Evaluation.Snubber Replaced | /03L-0:on 810503,two Pacific Scientific Model PSA-10 Mechanical Shock Suppressors Found Inoperable.Cause Under Evaluation.Snubber Replaced | | | 05000298/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000298/LER-1981-010-03, /03L-0:on 810505,static Inverter 1A Spike Suppressor Capacitor Failed Causing Inverter to Become Inoperable.Caused by Aging & Effects of High Ripple Charger | /03L-0:on 810505,static Inverter 1A Spike Suppressor Capacitor Failed Causing Inverter to Become Inoperable.Caused by Aging & Effects of High Ripple Charger | | | 05000298/LER-1981-011, Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-011/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-011-03, /03L-0:on 810528,during Insp of Unexpected Alarm, CS Header Break Detection Instrument Switches Found Piped to Incorrect Lines.Caused by Connection to Wrong Line at Drywell Penetration.Instruments Connected to Proper Lines | /03L-0:on 810528,during Insp of Unexpected Alarm, CS Header Break Detection Instrument Switches Found Piped to Incorrect Lines.Caused by Connection to Wrong Line at Drywell Penetration.Instruments Connected to Proper Lines | | | 05000298/LER-1981-012, Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-012-03, /03L-0:on 810519,during Testing HPCI-PS-68D Tripped at 89 Psig Instead of 100 Psig Tech Spec Limit. Caused by Random Instrument Drift.Instrument Immediately Recalibr & Returned to Svc | /03L-0:on 810519,during Testing HPCI-PS-68D Tripped at 89 Psig Instead of 100 Psig Tech Spec Limit. Caused by Random Instrument Drift.Instrument Immediately Recalibr & Returned to Svc | | | 05000298/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-013-03, /03L-0:on 810528,during Testing of Station Battery Rated Load Test W/Plant in Cold shutdown,125 Volt Batteries 1A & 1B Discharged at Rate Greater than Required.Caused by Error in Reading Procedure.Procedure Will Be Revised | /03L-0:on 810528,during Testing of Station Battery Rated Load Test W/Plant in Cold shutdown,125 Volt Batteries 1A & 1B Discharged at Rate Greater than Required.Caused by Error in Reading Procedure.Procedure Will Be Revised | | | 05000298/LER-1981-014, Forwards LER 81-014/03L-0.Detailed Event Analysis Encl | Forwards LER 81-014/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-014-03, /03L-0:on 810608,during Testing,Hpci Pump Turbine Tripped on Overspeed Prior to Reaching Rated Sys Flow.Sys Declared Inoperable.Caused by Improper Valve line-up Procedure.Valve Throttled & Tested | /03L-0:on 810608,during Testing,Hpci Pump Turbine Tripped on Overspeed Prior to Reaching Rated Sys Flow.Sys Declared Inoperable.Caused by Improper Valve line-up Procedure.Valve Throttled & Tested | | | 05000298/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Also Submitted | Forwards LER 81-015/03L-0.Detailed Event Analysis Also Submitted | | | 05000298/LER-1981-015-03, /03L-0:on 810531,twelve Penetrations Were Found Leaking Excessively.Ten Caused by Normal Wear & Two by Improper Limitorque Operation.Valve Repairs Performed | /03L-0:on 810531,twelve Penetrations Were Found Leaking Excessively.Ten Caused by Normal Wear & Two by Improper Limitorque Operation.Valve Repairs Performed | | | 05000298/LER-1981-016, Forwards LER 81-016/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-016/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-016-03, /03L-0:on 810610,core Thermal Power Calculation Performed by Process Computer Found Incorrect Due to Incorrect Feedwater Flow Value in Computer.Caused by Personnel Error in Changing Conversion Coefficient | /03L-0:on 810610,core Thermal Power Calculation Performed by Process Computer Found Incorrect Due to Incorrect Feedwater Flow Value in Computer.Caused by Personnel Error in Changing Conversion Coefficient | | | 05000298/LER-1981-017-03, /03L-0:on 810613,reactor Core Isolation Cooling Sys Steam Supply Valve RCIC-MOV-M016 Failed to Open.Caused by Improperly Wired Motor Operator Circuit.Jumper Installed | /03L-0:on 810613,reactor Core Isolation Cooling Sys Steam Supply Valve RCIC-MOV-M016 Failed to Open.Caused by Improperly Wired Motor Operator Circuit.Jumper Installed | | | 05000298/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-018-03, /03L-0:on 810625,pressure Switch NBI-PS-52A Found W/Trip Point Less Conservative than Tech Spec.Apparently Caused by Setpoint Drift.Switch Readjusted.Setpoints for Switches Reset | /03L-0:on 810625,pressure Switch NBI-PS-52A Found W/Trip Point Less Conservative than Tech Spec.Apparently Caused by Setpoint Drift.Switch Readjusted.Setpoints for Switches Reset | | | 05000298/LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-019-03, /03L-0:on 810728,during Surveillance to Prove Operability of Diesel Generator 1,fuel Supply Hose Developed Leak.Caused by Excessive Localized Flexure & Vibration. Hose Replaced | /03L-0:on 810728,during Surveillance to Prove Operability of Diesel Generator 1,fuel Supply Hose Developed Leak.Caused by Excessive Localized Flexure & Vibration. Hose Replaced | | | 05000298/LER-1981-019, Forwards LER 81-019/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-019/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-020, Forwards LER 81-020/03L-0. Detailed Event Analysis Also Submitted | Forwards LER 81-020/03L-0. Detailed Event Analysis Also Submitted | | | 05000298/LER-1981-020-03, /03L-0: on 810728, During Procedure Returning Diesel Generator 1 to Svc After Flexible Fuel Line Leak, Control Air Line Fitting Failed Causing Generator to Shut Down. Caused by Broken Air Line Due to Crimped Ferrule | /03L-0: on 810728, During Procedure Returning Diesel Generator 1 to Svc After Flexible Fuel Line Leak, Control Air Line Fitting Failed Causing Generator to Shut Down. Caused by Broken Air Line Due to Crimped Ferrule | | | 05000298/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Rept Submitted | Forwards LER 81-021/03L-0.Detailed Event Rept Submitted | | | 05000298/LER-1981-021-03, /03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced | /03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced | | | 05000298/LER-1981-022-03, /03L-0:on 810912,blown Fuse in Valve Motor Circuit Disabled Valve & Reactor Core Isolation Cooling Sys.Caused by Motor Grounded by Grease That Penetrated Defective Seal in Valve Operator & Into Armature.Motor & Seal Replaced | /03L-0:on 810912,blown Fuse in Valve Motor Circuit Disabled Valve & Reactor Core Isolation Cooling Sys.Caused by Motor Grounded by Grease That Penetrated Defective Seal in Valve Operator & Into Armature.Motor & Seal Replaced | | | 05000298/LER-1981-022, Forwards LER 81-022/03L-0.Detailed Event Analysis Also Submitted | Forwards LER 81-022/03L-0.Detailed Event Analysis Also Submitted | | | 05000298/LER-1981-023-03, /03L-0:on 811026,uncalibr Temp Switch Installed in MS-TS-1480 During 1981 Refueling Outage.Caused by Technician Error.Technicians Counseled.Will Color Code Switches & Revise Surveillance Procedure | /03L-0:on 811026,uncalibr Temp Switch Installed in MS-TS-1480 During 1981 Refueling Outage.Caused by Technician Error.Technicians Counseled.Will Color Code Switches & Revise Surveillance Procedure | | | 05000298/LER-1981-023, Forwards LER 81-023/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-023/03L-0.Detailed Event Analysis Submitted | | | 05000298/LER-1981-024-03, /03L-0:on 811106,safety Relief Valve 71-D Failed to Close After Test.Caused by Failure of Solenoid Plunger to Drop Out When Solenoid de-energized.Solenoid Replaced | /03L-0:on 811106,safety Relief Valve 71-D Failed to Close After Test.Caused by Failure of Solenoid Plunger to Drop Out When Solenoid de-energized.Solenoid Replaced | | | 05000298/LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | | | 05000298/LER-1981-025-04, /04T-0:on 811224,during Full Power,Discharge Was Made from Floor Drain Sample Tank W/O Adequate Sampling & Analysis of Batch.Caused by Personnel Error.Liquid Discharge Procedures Being Revised.Personnel Reprimanded | /04T-0:on 811224,during Full Power,Discharge Was Made from Floor Drain Sample Tank W/O Adequate Sampling & Analysis of Batch.Caused by Personnel Error.Liquid Discharge Procedures Being Revised.Personnel Reprimanded | | | 05000298/LER-1981-025, Forwards LER 81-025/04T-0.Detailed Event Analysis Encl | Forwards LER 81-025/04T-0.Detailed Event Analysis Encl | |
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