05000272/LER-1981-054-01, /01T-0:on 810521,vendor Advised That Regulatory Requirements Could Be Violated by Failure of Vol Control Tank Level Control Sys & Subsequent Loss of Suction to Centrifugal Charging Pump W/Failure of Remaining Pump

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/01T-0:on 810521,vendor Advised That Regulatory Requirements Could Be Violated by Failure of Vol Control Tank Level Control Sys & Subsequent Loss of Suction to Centrifugal Charging Pump W/Failure of Remaining Pump
ML20004E718
Person / Time
Site: Salem PSEG icon.png
Issue date: 06/04/1981
From: Espey J
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004E716 List:
References
LER-81-054-01T, LER-81-54-1T, NUDOCS 8106150105
Download: ML20004E718 (1)


LER-1981-054, /01T-0:on 810521,vendor Advised That Regulatory Requirements Could Be Violated by Failure of Vol Control Tank Level Control Sys & Subsequent Loss of Suction to Centrifugal Charging Pump W/Failure of Remaining Pump
Event date:
Report date:
2721981054R01 - NRC Website

text

NRC FON 366 U. S. NUCLEAR REGULATORY COMMISSION 87 77) '

LICENSEE EVENT REPORT CONTROL BLOCK: l l

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l l lh IPLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI Nia is I cl hl il@ln I n lI n i n l o l n I n l_ in i n l@lc li l il ili l@l I

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4 40 Si DOCKET NUMSER 88 89 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCR:? TION AND PROB ABLE CONSEQUENCES h lol2l l We have been informed by Westinghouse of a nostulated niant oneratine concit rinn I

gg which could result in a violation of current regulatory requirements. The assumption l gl involves a failure of the volume control tank (VCT) level control system and a sub-l jo,3; ; sequent loss of su u ton to an operating centrifugal charging pump coupled with a l

g] single random failure of the remaining centrifugal charging pump. Loss of makeup to l

o;7, l the VCT and continued charging flow could lead to draining of the VCT and loss of l

l c !s I I suction with consequential pump damage.

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