05000325/LER-1980-077-03, /03L-0:on 801120,snubber 1-E41-2SS105 Found Not to Be Connected to Pipe Clamp on HPCI Sys Main Pump Discharge Piping.Caused by Personnel Error.Personnel to Be Reinstructed

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/03L-0:on 801120,snubber 1-E41-2SS105 Found Not to Be Connected to Pipe Clamp on HPCI Sys Main Pump Discharge Piping.Caused by Personnel Error.Personnel to Be Reinstructed
ML19340D449
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 12/19/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19340D435 List:
References
LER-80-077-03L-01, LER-80-77-3L-1, NUDOCS 8012300590
Download: ML19340D449 (2)


LER-1980-077, /03L-0:on 801120,snubber 1-E41-2SS105 Found Not to Be Connected to Pipe Clamp on HPCI Sys Main Pump Discharge Piping.Caused by Personnel Error.Personnel to Be Reinstructed
Event date:
Report date:
3251980077R03 - NRC Website

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8 60 61 COCK ET %M9ER 63 69 EVENT DATE 14 d5 REPO9TDATE 80 EVENT DESCRIPTION AND PROB ABLE CONSECUENCES h toj2] l During the performance of visual inspection of accessible snubbers on safety-related I

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