ML19339A682

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LER 80-072/01T-0:on 801002,reactor Protection Sys Trip Level Setting Was Adjusted to Nonconservative Level Due to Calculation Error.Procedure 7.4.14 Being Processed to Clearly Delineate Method for Calculating Set Points
ML19339A682
Person / Time
Site: Pilgrim
Issue date: 10/27/1980
From: Holland P
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19339A656 List:
References
LER-80-072-01T, LER-80-72-1T, NUDOCS 8011040521
Download: ML19339A682 (2)


Text

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LICENSEE EVENT REPORT ,

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j 7 4 40 43 coC8C ET NUMgER N 09 EVENT 0 ATE 74 75 REPORT 0 ATE 80 EVENT DESCRIPT1CN AND PROSASLE CONSEQUENCES h j (TTT]l On October 15, 1980 the ORC concurred,following its review,that on October 2,1980 l j ~ .

(y77) l a RPS trip level setting was adjusted to a non-conservative level. The review con- l ,

io,Ai l cluded that as a result of a calculation error the Main Steam Line High Radiaolon l l ,o,3, , Monitors 1705-2A,B,C,D were set to 7.7 times normal full power background. Technical;
I i i a ,, i l Specification Table 3.1.1 indicates that this multiplication factor may not exceed i I

l yo,,yl 7. On October 14 immediately following identification of this error the monitors l.

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-- were recalibrated. l 7 s, so So7E YoE su$CNE CcWPoNENT CoOE SUS :o'C'E 5 E

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$ as 24 as a si ao di 42 42 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS lital l To preclude a repe:1 tion of this event, a revision to orocedure number 7.4.14, en- l i, ,,i ; titled " Source Calibration of Main Steam Line Radiation Monitors" is being processed.I l

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