05000325/LER-1980-063-03, /03L-0:on 800826,during Testing of Reactor Flow Bias,Three Average Power Range Monitors Were Actuating Out of Spec.Caused by Instrument Drift.Monitors Recalibr & Returned to Svc

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/03L-0:on 800826,during Testing of Reactor Flow Bias,Three Average Power Range Monitors Were Actuating Out of Spec.Caused by Instrument Drift.Monitors Recalibr & Returned to Svc
ML19338D784
Person / Time
Site: Brunswick 
Issue date: 09/16/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19338D749 List:
References
LER-80-063-03L, LER-80-63-3L, NUDOCS 8009230745
Download: ML19338D784 (1)


LER-1980-063, /03L-0:on 800826,during Testing of Reactor Flow Bias,Three Average Power Range Monitors Were Actuating Out of Spec.Caused by Instrument Drift.Monitors Recalibr & Returned to Svc
Event date:
Report date:
3251980063R03 - NRC Website

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LICENSEE EVENT REPORT

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6 80 St CoCKET NyvagR 60 69 EvtNT OATg 74 76 REPORT DATE 80 LVENT DESCRIPTION AND PROBABLE CONSEQUENCES h gl During the perforrance of tesr.ing reactor flow bias, P.T.l.l.7 PC, three APRM's, l

gl ciodel no.145C309AAG001, were founc' actuating out of specification. APRM "A" upscale l o, l alarm / rod block actuated at 110% while the reportable limit is greater than 108%.

l gl AP?li "C" downscale alarci actuated at. 2.95% while the reportable limit is less than l

g {. APRM "F" upscale alarm / rod block indication came in at 109% while the reportable l g[

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