LER-1980-032, /01T:on 800724,GE SIL 299 Review Revealed Higher Drywell Ambient Temp than Used for Original Safeguard Yarway Calibrs.Caused by High Temp Due to Inadequate Drywell Cooling.Recalibr & Survey of Drywell Ventilation Conducted |
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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISt!ON (7 77)
LICENSEE EVENT REPORT O
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4 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 1o12l l Review of G.E. SIL 299, as pertaining to Pilgrim Nuclear Power Station, revealed l
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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i, j o; j Drywell temperatures higher than design were the cause of this event. The reason i,,,,l for these temperatures is inadequate drywell cooling. The Yarways were re-cali-l brated to compensate for the existing conditions and an engineering evaluation of l
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c BOSTON EDISON COMPANY PILGRIM NUCI. EAR POWER STATION DOCKET NO. 50-293 Attachment to LER 80-032/01T-0 At 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> on July 24, 1980, PNPS personnel received a preliminary copy of a memo from the SECo. Nuclear Engineering Department to the Nuclear Operations Manager which addressed recommended calibration changes to safety related Yarway level instrumentation.
These calibration changes were necessary to correct for higher reference leg temperatures than initially used to derive calibration data.
This memo was a result of a series of events which began in October of 1979 when PNPS personnel requested an in-depth study of G.E. SIL#299 be conducted by the NOD Plant Support Group.
In the review of SIL#299, the possibility that conditions existing at PNPS warranted further investigation and evaluations of the real potential for " flashing" to occur.
The preliminary review indicat d that even without the small break LOCA condition identified in SIL#299, there app. eared to be higher drywell ambient temperatures than used for original Yarway calibration.
Set point changes were recommended and a Plant Design Change Request was generated to instrument the water level columns to obtain actual operating conditions.
PNPS was conducting 4 refueling outage at this ti=e and it was decided not to make any unsubstancia:ted changes in set points until actual operating conditions were verified, since the potential for inadvertant cold water injections as a result of increasing the set point would create undue ther=al stresses.
i PNPS Instrument and Control personnel gathered infor=ation from the sensors installed during the outage and forwarded the data to the Plant Support Group.
The results of the review of this data was presented to PNPS in draf t form without Nuclear Operations Manager concurrence on July 17, 1980.
Since independent review by the Nuclear Engineering Department and concurrence by the Nuclear Operations Manager had not been conducted, no action was taken at this time.
On July 7.4, 1980 a.'ter independent review by NED and confir=ation with Yarway represer.tatives, a w mo was forwarded to the Nuclear Operations Manager recom-
=ending a zero adjust of five (5) inches.
It was a copy of this me=o which was forwarded to the Instrument and Control Supervisor that initiated actions to re-calibrate the level instruments.
PNPS calibration procedures were revised, reviewed and approved on July 25, 1980 and the zero adjust calibrations were commenced on July 26, 1980.
The station had been shut down on July 25, 1980 to conduct scram testing per II Bulletin 80-17.
While re-calibrations were in progress, the reactor was brought critical and a power ascension was commenced to perform the automatic scram portion of IE Bulletin 80-17.
Calculations were made to determine maximum drywell temperatures that would not violate Yarway setpoints and recording of these temperatures every half hour were commenced.
At approximately 1730 on July 26, the drywell temperature exceeded the calculated maximum values.
The Watch Engineer was not (fied at 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> that the reference leg average temperature had been exceeded d that three of the safeguard yarways were still'not calibrated.
The reactor was scra==ed at 1832 and drywc 1 temperatures below calculated =axi=um by 1930.
The re-es11bration of remaining arways was completed prior to return to power.
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| 05000293/LER-1980-001-01, /01T-0:on 800123,fire Hazard Analysis Determined That Fire in Electrical Raceways in Several Areas of Plant Would Jeopardize Redundant Div of ECCS Sys.Cause Not Stated. Mods Planned to Be Completed by Oct 1980 | /01T-0:on 800123,fire Hazard Analysis Determined That Fire in Electrical Raceways in Several Areas of Plant Would Jeopardize Redundant Div of ECCS Sys.Cause Not Stated. Mods Planned to Be Completed by Oct 1980 | | | 05000293/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000293/LER-1980-002-02, /02T-0:on 800124,cable Separation Inadequacy Discovered Following Review of IE Info Notice 79-32. Affected Automatic Depressurization Sys Cables Will Probably Be Rerouted | /02T-0:on 800124,cable Separation Inadequacy Discovered Following Review of IE Info Notice 79-32. Affected Automatic Depressurization Sys Cables Will Probably Be Rerouted | | | 05000293/LER-1980-002, Forwards LER 80-002/02T-0 | Forwards LER 80-002/02T-0 | | | 05000293/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000293/LER-1980-003-03, /03L-0:on 800108,during Refueling Outage 4,leak Rate Testing of torus-to-reactor Bldg Indicated Valve Leakage in Excess of Limit.Caused by Normal Deterioration of disc-to-seat Mating Surface.Surfaces Lapped | /03L-0:on 800108,during Refueling Outage 4,leak Rate Testing of torus-to-reactor Bldg Indicated Valve Leakage in Excess of Limit.Caused by Normal Deterioration of disc-to-seat Mating Surface.Surfaces Lapped | | | 05000293/LER-1980-004-01, Results of Core Spray Sparger Cracks in Conjunction W/Inservice Insp Program Revealed Several Linear Indications on Each Sparger.Visual Insps Conclude Indications within Criteria | Results of Core Spray Sparger Cracks in Conjunction W/Inservice Insp Program Revealed Several Linear Indications on Each Sparger.Visual Insps Conclude Indications within Criteria | | | 05000293/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000293/LER-1980-005-01, /01T-0:on 800131,measured Concentrations of Sr-90 in Milk Sample Was Greater than 10 Times Concentration in Control Station Sample.Caused by Local Meteorological Conditions.No Corrective Action Taken | /01T-0:on 800131,measured Concentrations of Sr-90 in Milk Sample Was Greater than 10 Times Concentration in Control Station Sample.Caused by Local Meteorological Conditions.No Corrective Action Taken | | | 05000293/LER-1980-005, Revised LER Changing Original Number from LER 80-005/01T to 04T.On 800131,concentrations of Sr-90 in Milk Sample from Indicator Station 2.2 Miles West of Reactor Site 10 Times Greater than Control.Caused by Meteorological Condi | Revised LER Changing Original Number from LER 80-005/01T to 04T.On 800131,concentrations of Sr-90 in Milk Sample from Indicator Station 2.2 Miles West of Reactor Site 10 Times Greater than Control.Caused by Meteorological Conditions | | | 05000293/LER-1980-006-03, /03L-0:on 800115,strut Bushing Insert on RHR Sys snubber,SS-10-10-46,found Turning Freely within Strut.Caused by Lack of Strut to Strut Bushing Weld.Weld Performed to Restore Operable Status | /03L-0:on 800115,strut Bushing Insert on RHR Sys snubber,SS-10-10-46,found Turning Freely within Strut.Caused by Lack of Strut to Strut Bushing Weld.Weld Performed to Restore Operable Status | | | 05000293/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000293/LER-1980-007-03, /03L-0:on 800120,false Detection Alarm,Originating from 4kV Switchgear Room B,Annunciated on Panel C-94 in Control Room.Apparently Caused by Dust from Fire Retardant Beam Coating.Alarm Cleaned | /03L-0:on 800120,false Detection Alarm,Originating from 4kV Switchgear Room B,Annunciated on Panel C-94 in Control Room.Apparently Caused by Dust from Fire Retardant Beam Coating.Alarm Cleaned | | | 05000293/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000293/LER-1980-008-01, /01T-0:on 800308,irradiated Fuel Moved within Fuel Pool W/O Prior Satisfaction of Tech Spec Requirements.Caused by Procedural Inadequacy.Fuel Movement Prohibited & Secondary Containment Leak Rate Testing Initiated | /01T-0:on 800308,irradiated Fuel Moved within Fuel Pool W/O Prior Satisfaction of Tech Spec Requirements.Caused by Procedural Inadequacy.Fuel Movement Prohibited & Secondary Containment Leak Rate Testing Initiated | | | 05000293/LER-1980-008, Forwards LER 80-008/01T-0 | Forwards LER 80-008/01T-0 | | | 05000293/LER-1980-009-04, /04T-0:on 800310,facility Received Analyses Rept from Util Lab Indicating Reportable Concentrations of Cr-51 & Co-60 in Sample of Mussel Taken from Facility Discharge Canal.Cause Not Stated | /04T-0:on 800310,facility Received Analyses Rept from Util Lab Indicating Reportable Concentrations of Cr-51 & Co-60 in Sample of Mussel Taken from Facility Discharge Canal.Cause Not Stated | | | 05000293/LER-1980-009, Forwards LER 80-009/04T-0 | Forwards LER 80-009/04T-0 | | | 05000293/LER-1980-010-03, /03L-0:on 800310,hydrant Hose House 5 Damaged When Hit by Truck.House Wrapped Around Hydrant,Preventing Access. Cause Not Stated.House Rebuilt & Returned to Svc | /03L-0:on 800310,hydrant Hose House 5 Damaged When Hit by Truck.House Wrapped Around Hydrant,Preventing Access. Cause Not Stated.House Rebuilt & Returned to Svc | | | 05000293/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000293/LER-1980-011-01, /01T-0:on 800326,utilizing Approved Station Procedure TP80-37,PNPS Jet Pumps Examined & Jet Pump Beams 1,3 & 15 Found to Have Discontinuities.Caused Not Stated. Flawed Beams & Beam Bolt Assemblies Replaced | /01T-0:on 800326,utilizing Approved Station Procedure TP80-37,PNPS Jet Pumps Examined & Jet Pump Beams 1,3 & 15 Found to Have Discontinuities.Caused Not Stated. Flawed Beams & Beam Bolt Assemblies Replaced | | | 05000293/LER-1980-011, Forwards LER 80-011/01T-0 | Forwards LER 80-011/01T-0 | | | 05000293/LER-1980-012-03, /03L-0:on 800312,while Performing Surveillance Test,Found That Pressure Switch 263-52A Setpoint Had Drifted.Cause Not Stated.Setpoint Drift Is Recurring Problem.Pressure Switch Recalibr | /03L-0:on 800312,while Performing Surveillance Test,Found That Pressure Switch 263-52A Setpoint Had Drifted.Cause Not Stated.Setpoint Drift Is Recurring Problem.Pressure Switch Recalibr | | | 05000293/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000293/LER-1980-013-03, /03L-0:on 800313,while Performing Surveillance Test 8.M.1-5,found Pressure Switch 503D Setpoint Drifted. Cause Not Stated.Drift Is Recurring Problem | /03L-0:on 800313,while Performing Surveillance Test 8.M.1-5,found Pressure Switch 503D Setpoint Drifted. Cause Not Stated.Drift Is Recurring Problem | | | 05000293/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000293/LER-1980-014, Forwards LER 80-014/04T-0 | Forwards LER 80-014/04T-0 | | | 05000293/LER-1980-014-04, /04T-0:on 800418,Yankee Atomic Environ Lab Notified Util That Milk Sample Contained High Concentration of Cs-137.Cause Unknown,Probably Not Result of Plant Effluent | /04T-0:on 800418,Yankee Atomic Environ Lab Notified Util That Milk Sample Contained High Concentration of Cs-137.Cause Unknown,Probably Not Result of Plant Effluent | | | 05000293/LER-1980-015-03, /03L-0:on 800401,during Performance of Surveillance Test,Dry Chemical Fire Protection Sys Failed to Automatically Initiate.Caused by Erratic Pyrotronics, Dtf 190 heat-actuated Device.Unit Replaced | /03L-0:on 800401,during Performance of Surveillance Test,Dry Chemical Fire Protection Sys Failed to Automatically Initiate.Caused by Erratic Pyrotronics, Dtf 190 heat-actuated Device.Unit Replaced | | | 05000293/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000293/LER-1980-016-03, /03L-0:on 800513,while Performing Surveillance Test,Core Spray Pump P215B Failed to Start & Core Spray Valve 14000-24B Failed to Automatically Open.Caused by trip-free Operation & Dirty Contact in Logic Circuit | /03L-0:on 800513,while Performing Surveillance Test,Core Spray Pump P215B Failed to Start & Core Spray Valve 14000-24B Failed to Automatically Open.Caused by trip-free Operation & Dirty Contact in Logic Circuit | | | 05000293/LER-1980-016, Forwards LER 80-016/03L-0 | Forwards LER 80-016/03L-0 | | | 05000293/LER-1980-017-03, /03L-0:on 800505,during 24-h Performance Test of a Diesel Generator Per IE Bulletin 79-23,three Attempts Made Before Satisfactory Conclusion on 800510.Caused by Failure of Potential Transformer in High Voltage Chassis | /03L-0:on 800505,during 24-h Performance Test of a Diesel Generator Per IE Bulletin 79-23,three Attempts Made Before Satisfactory Conclusion on 800510.Caused by Failure of Potential Transformer in High Voltage Chassis | | | 05000293/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000293/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000293/LER-1980-018-03, /03L-0:on 800523,while Performing Surveillance Test 8.7.4.3,isolation valves,5065-11,13 & 23 Declared Inoperable.Cause Not Stated.Valve in Each Affected Sample Line Closed & Position Recorded Daily | /03L-0:on 800523,while Performing Surveillance Test 8.7.4.3,isolation valves,5065-11,13 & 23 Declared Inoperable.Cause Not Stated.Valve in Each Affected Sample Line Closed & Position Recorded Daily | | | 05000293/LER-1980-019-03, /03L-0:on 800519,during Startup of Pnps,Hpci Sys Was Declared Inoperable.Caused by Wiring Attendant to Installation of Alternate Shutdown Panel & Seal Exhaust Leakage Interference.Wiring & Leakage Repaired | /03L-0:on 800519,during Startup of Pnps,Hpci Sys Was Declared Inoperable.Caused by Wiring Attendant to Installation of Alternate Shutdown Panel & Seal Exhaust Leakage Interference.Wiring & Leakage Repaired | | | 05000293/LER-1980-019, Forwards LER 80-019/03L-0 | Forwards LER 80-019/03L-0 | | | 05000293/LER-1980-020-03, /03L-0:on 800426,during Refueling Outage 4,14 Primary Containment Isolation Valves Found to Have Seat Leakage Over Requirements.Caused by Normal Deterioration of Disc to Seat Mating Surface | /03L-0:on 800426,during Refueling Outage 4,14 Primary Containment Isolation Valves Found to Have Seat Leakage Over Requirements.Caused by Normal Deterioration of Disc to Seat Mating Surface | | | 05000293/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000293/LER-1980-021-04, /04T-0:on 800508,algae Sample from Discharge Outfall Area Contained Reportable Concentration of Co-60, According to Yankee Environ Lab 800616 Analysis Rept.Cause Not Stated | /04T-0:on 800508,algae Sample from Discharge Outfall Area Contained Reportable Concentration of Co-60, According to Yankee Environ Lab 800616 Analysis Rept.Cause Not Stated | | | 05000293/LER-1980-021, Forwards LER 80-021/04T-0 | Forwards LER 80-021/04T-0 | | | 05000293/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000293/LER-1980-022-03, /03L-0:on 800527,during Performance of Surveillance Test Re RCIC Steam Line High Temp,Temp Switch 1360-17A Was Found Out of Calibr.Caused by Setpoint Drift | /03L-0:on 800527,during Performance of Surveillance Test Re RCIC Steam Line High Temp,Temp Switch 1360-17A Was Found Out of Calibr.Caused by Setpoint Drift | | | 05000293/LER-1980-023-03, /03L-0:on 800526,during Surveillance Testing, Channel B of Rod Block Monitor Sys Determined to Be Out of Calibr.Caused by Misinterpertation of Tech Specs. Requalification Program Will Include Sys Review | /03L-0:on 800526,during Surveillance Testing, Channel B of Rod Block Monitor Sys Determined to Be Out of Calibr.Caused by Misinterpertation of Tech Specs. Requalification Program Will Include Sys Review | | | 05000293/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000293/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000293/LER-1980-024-03, /03L-0:on 800530,reactor Core Isolation Cooling Sys Was Declared Inoperable.Caused by Faulty Auto Flow Control.Unit Repaired & Returned to Svc | /03L-0:on 800530,reactor Core Isolation Cooling Sys Was Declared Inoperable.Caused by Faulty Auto Flow Control.Unit Repaired & Returned to Svc | | | 05000293/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000293/LER-1980-025-03, /03L-0:on 800602,fire Detection Alarm from HPCI Quadrant Sounded in Control Room on Panel C-94.Roving Fire Patrol Initiated & Immediate Investigation Conducted.Caused by Leak at Flange on HPCI Drain Line Valve AO2301-29 | /03L-0:on 800602,fire Detection Alarm from HPCI Quadrant Sounded in Control Room on Panel C-94.Roving Fire Patrol Initiated & Immediate Investigation Conducted.Caused by Leak at Flange on HPCI Drain Line Valve AO2301-29 | |
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