Letter Sequence Response to RAI |
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EPID:L-2019-LLA-0214, Emergency License Amendment Request: One Time Extension to the TS 3.8.1 Action A.3 Completion Time for an Inoperable Offsite Source (Withdrawn, Closed) |
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MONTHYEARML19276G3132019-10-0202 October 2019 Draft Exigent License Amendment Request - One Time Extension to the TS 3.8.1 Action A.3 Completion Time for an Inoperable Offsite Source Project stage: Draft Request ML19277G0852019-10-0404 October 2019 Emergency License Amendment Request: One Time Extension to the TS 3.8.1 Action A.3 Completion Time for an Inoperable Offsite Source Project stage: Request ML19280A0362019-10-0404 October 2019 NRR E-mail Capture - FitzPatrick Request for Additional Information: Emergency Amendment to Extend Completion Time of Transformer to 21 Days Project stage: RAI ML19280A0052019-10-0404 October 2019 NRR E-mail Capture - (External_Sender) FitzPatrick Emergency Amendment Public Conference Call Discussion Points - 4 Project stage: Request ML19277D5522019-10-0404 October 2019 Draft James A. FitzPatrick Nuclear Power Plant - Emergency License Amendment Request - One Time Extension to the TS 3.8.1 Action A.3 Completion Time for an Inoperable Offsite Source Project stage: Draft Request ML19280A0392019-10-0505 October 2019 NRR E-mail Capture - FitzPatrick Additional Request for Additional Information: Emergency Amendment to Extend Completion Time of Transformer to 21 Days Project stage: RAI ML19280A0372019-10-0505 October 2019 NRR E-mail Capture - FitzPatrick Revised Request for Additional Information: Emergency Amendment to Extend Completion Time of Transformer to 21 Days Project stage: RAI ML19279A0012019-10-0606 October 2019 Response to Request for Additional Information by the Office of Nuclear Reactor Regulation to Support Review of an Emergency License Amendment Request for One Time Extension to the TS 3.8.1 Action ... Project stage: Response to RAI ML19281A9962019-10-0808 October 2019 Withdrawal of Emergency License Amendment Request for One Time Extension to the TS 3.8.1 Action A.3 Completion Time for an Inoperable Offsite Source Project stage: Withdrawal ML19282A4502019-10-10010 October 2019 Withdrawal of Emergency License Amendment Request Project stage: Withdrawal ML19291A0022019-11-0101 November 2019 10/03-10/08/2019 Summary of Meetings with Exelon Generation Company, LLC, on Emergency Amendment Request Regarding One-Time Extension to Technical Specifications 3.8.1 Action A.3 Completion Time for Inoperable Offsite Source (EPID L-2019-LL Project stage: Meeting 2019-10-05
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Category:Letter
MONTHYEARIR 05000333/20230042024-02-0707 February 2024 Integrated Inspection Report 05000333/2023004 and Independent Spent Fuel Storage Installation Inspection Report 07200012/2023001 ML24037A0102024-02-0606 February 2024 Requalification Program Inspection ML24018A0012024-01-18018 January 2024 Notification of Commercial Grade Dedication Inspection (05000333/2024010) and Request for Information ML24004A2302024-01-0808 January 2024 Project Manager Reassignment ML23356A0832024-01-0404 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0058 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML23278A1292023-12-14014 December 2023 Units 1 & 2; Limerick, Units 1 & 2; Nine Mile Point, Units 1 & 2; and Peach Bottom, Units 2 & 3 -Revision to Approved Alternatives to Use Boiling Water Reactor Vessel and Internals Project Guidelines JAFP-23-0065, License Amendment Request to Revise Technical Specifications to Adopt TSTF-529, Clarify Use and Application Rules, Revision 4, and Administrative Changes to the Technical Specifications2023-12-14014 December 2023 License Amendment Request to Revise Technical Specifications to Adopt TSTF-529, Clarify Use and Application Rules, Revision 4, and Administrative Changes to the Technical Specifications IR 05000333/20234012023-12-0808 December 2023 Cybersecurity Inspection Report 05000333/2023401 (Cover Letter Only) RS-23-126, Request for Exemption from 10 CFR 2.109(b)2023-12-0707 December 2023 Request for Exemption from 10 CFR 2.109(b) JAFP-23-0069, Supplemental Response to Part 73 Exemption Request Withdrawal of Request for Exemption from 10 CFR 73, Subpart B, Preemption Authority Requirements2023-12-0707 December 2023 Supplemental Response to Part 73 Exemption Request Withdrawal of Request for Exemption from 10 CFR 73, Subpart B, Preemption Authority Requirements JAFP-23-0057, and Independent Spent Fuel Storage Installation - Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-11-22022 November 2023 and Independent Spent Fuel Storage Installation - Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation JAFP-23-0064, Emergency Plan Document Revision2023-11-15015 November 2023 Emergency Plan Document Revision JAFP-23-0063, Registration of Spent Fuel Cask Use2023-11-13013 November 2023 Registration of Spent Fuel Cask Use IR 05000333/20230032023-11-13013 November 2023 Integrated Inspection Report 05000333/2023003 ML23317A1192023-11-10010 November 2023 Constellation Energy Generation, LLC - 2023 Annual Report - Guarantees of Payment of Deferred Premiums IR 05000333/20230102023-10-26026 October 2023 Biennial Problem Identification and Resolution Inspection Report 05000333/2023010 JAFP-23-0059, Registration of Spent Fuel Cask Use2023-10-24024 October 2023 Registration of Spent Fuel Cask Use IR 05000333/20233012023-10-19019 October 2023 Initial Operator Licensing Examination Report 05000333/2023301 RS-23-097, Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans2023-10-12012 October 2023 Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans JAFP-23-0050, Physical Security Plan, Revision 242023-08-31031 August 2023 Physical Security Plan, Revision 24 JAFP-23-0048, Supplemental Information for License Amendment Request to Update the Technical Specification Bases to Change the Fuel Handling Accident Analysis2023-08-31031 August 2023 Supplemental Information for License Amendment Request to Update the Technical Specification Bases to Change the Fuel Handling Accident Analysis IR 05000333/20230052023-08-31031 August 2023 Updated Inspection Plan for James A. FitzPatrick Nuclear Power Plant (Report 05000333/2023005) JAFP-23-0047, Correction to the 2022 Annual Radioactive Effluent Release Report2023-08-30030 August 2023 Correction to the 2022 Annual Radioactive Effluent Release Report ML23228A1342023-08-16016 August 2023 Licensed Operator Positive Fitness-For-Duty Test IR 05000333/20230022023-08-0707 August 2023 Integrated Inspection Report 05000333/2023002 RS-23-087, Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor2023-08-0404 August 2023 Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor JAFP-23-0040, License Amendment Request to Update the Technical Specification Bases to Change the Fuel Handling Accident Analysis2023-08-0303 August 2023 License Amendment Request to Update the Technical Specification Bases to Change the Fuel Handling Accident Analysis JAFP-23-0043, 10 CFR 50.46 Annual Report2023-07-31031 July 2023 10 CFR 50.46 Annual Report JAFP-23-0038, License Amendment Request to Modify Technical Specification Surveillance Requirement (SR) 3.4.3.1 Safety Relief Valves (S/Rvs) Setpoint Lower Tolerance2023-07-28028 July 2023 License Amendment Request to Modify Technical Specification Surveillance Requirement (SR) 3.4.3.1 Safety Relief Valves (S/Rvs) Setpoint Lower Tolerance ML23208A1622023-07-27027 July 2023 Operator Licensing Examination Approval IR 05000333/20234022023-07-26026 July 2023 Security Baseline Inspection Report 05000333/2023402 IR 05000333/20230112023-07-25025 July 2023 Post-Approval Site Inspection for License Renewal - Phase 4 Inspection Report 05000333/2023011 IR 05000333/20235012023-07-20020 July 2023 Emergency Preparedness Biennial Exercise Inspection Report 05000333/2023501 JAFP-23-0033, License Amendment Request - Technical Specifications (TS) Section 3.3.1.2, Source Range Monitors (SRM) Instrumentation2023-06-28028 June 2023 License Amendment Request - Technical Specifications (TS) Section 3.3.1.2, Source Range Monitors (SRM) Instrumentation IR 05000333/20234202023-06-26026 June 2023 Security Baseline Inspection Report 05000333 2023420 RS-23-077, Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations2023-06-16016 June 2023 Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations ML23164A0322023-06-13013 June 2023 Request for Information for a Biennial Problem Identification and Resolution Inspection; Inspection Report 05000333/2023010 ML23152A0042023-06-0101 June 2023 Information Request for the Cyber Security Baseline Inspection, Notification to Perform Inspection 05000333/2023401 RS-23-042, Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling2023-05-25025 May 2023 Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling JAFP-23-0025, 2022 Annual Radiological Environmental Operating Report2023-05-10010 May 2023 2022 Annual Radiological Environmental Operating Report IR 05000333/20230012023-05-0303 May 2023 Integrated Inspection Report 05000333/2023001 ML23117A2172023-05-0101 May 2023 Safety Evaluation for Quality Assurance Program Manual Reduction in Commitment ML23114A2522023-04-28028 April 2023 Request to Use a Provision of a Later Edition of the ASME Boiler & Pressure Vessel Code, Section XI JAFP-23-0023, 2022 Annual Radioactive Effluent Release Report2023-04-27027 April 2023 2022 Annual Radioactive Effluent Release Report IR 05000333/20230122023-04-13013 April 2023 Quadrennial Fire Protection Inspection Report 05000333/2023012 ML23095A3722023-04-0505 April 2023 2023 Updated Final Safety Analysis Report, Technical Specification Bases and Technical Requirements Manual Changes Transmittal RS-23-049, Constellation Energy Generation, LLC, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-23023 March 2023 Constellation Energy Generation, LLC, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations IR 05000333/20220042023-03-20020 March 2023 Integrated Inspection Report 05000333/2022004 JAFP-23-0010, 2022 REIRS Transmittal of NRC Form 52023-03-20020 March 2023 2022 REIRS Transmittal of NRC Form 5 ML23061A1632023-03-0303 March 2023 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch 3 2024-02-07
[Table view] Category:Response to Request for Additional Information (RAI)
MONTHYEARJAFP-22-0032, Response to Request for Additional Information for James A. FitzPatrick Nuclear Power Plant to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b..2022-06-16016 June 2022 Response to Request for Additional Information for James A. FitzPatrick Nuclear Power Plant to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b.. RS-22-027, Constellation, Response to Request for Additional Information Regarding Application to Revise Technical Specifications to Adopt TSTF-541 Revision 2, Add Exceptions to Surveillance Requirements for Valves and Dampers Locked in the Actuated2022-02-23023 February 2022 Constellation, Response to Request for Additional Information Regarding Application to Revise Technical Specifications to Adopt TSTF-541 Revision 2, Add Exceptions to Surveillance Requirements for Valves and Dampers Locked in the Actuated P NMP1L3447, Constellation Energy Generation, LLC - Response to Request for Additional Information - Proposed Relief Request Associated with Reactor Pressure Vessel Water Level Instrumentation Partial Penetration Nozzle Repairs2022-02-0202 February 2022 Constellation Energy Generation, LLC - Response to Request for Additional Information - Proposed Relief Request Associated with Reactor Pressure Vessel Water Level Instrumentation Partial Penetration Nozzle Repairs JAFP-22-0008, Response to Request for Supplemental Information by the Office of Nuclear Reactor Regulation to Support Review of a License Amendment Request to Eliminate Selected Response Time Testing for Reactor Protection System and Primary2022-01-14014 January 2022 Response to Request for Supplemental Information by the Office of Nuclear Reactor Regulation to Support Review of a License Amendment Request to Eliminate Selected Response Time Testing for Reactor Protection System and Primary JAFP-21-0087, Response to Request for Additional Information Regarding Request for Approval of Transfer of Licenses and Conforming Amendments2021-09-16016 September 2021 Response to Request for Additional Information Regarding Request for Approval of Transfer of Licenses and Conforming Amendments JAFP-21-0073, Response to Request for Additional Information Regarding Application to Revise the James A. FitzPatrick Nuclear Power Plant Limiting Condition for Operation (LCO) 3.5.1, ECCS - Operating Surveillance.2021-08-0909 August 2021 Response to Request for Additional Information Regarding Application to Revise the James A. FitzPatrick Nuclear Power Plant Limiting Condition for Operation (LCO) 3.5.1, ECCS - Operating Surveillance. JAFP-21-0044, Response to Request for Additional Information Regarding Request for Approval of Transfer of Licenses and Conforming Amendments2021-06-11011 June 2021 Response to Request for Additional Information Regarding Request for Approval of Transfer of Licenses and Conforming Amendments ML21138A0132021-05-18018 May 2021 NRC Response to Request for Additional Time to Respond to James A. Fitzpatrick Nuclear Power Plant: Final Significance Determination of a White Finding with Assessment Follow Up and Notice of Violation-Inspection No. 05000333/2021090 JAFP-21-0032, Response to Request for Additional Information - Proposed Alternative Concerning ASME Section XI Repair/Replacement Documentation for Replacement of Pressure Retaining Bolting2021-04-20020 April 2021 Response to Request for Additional Information - Proposed Alternative Concerning ASME Section XI Repair/Replacement Documentation for Replacement of Pressure Retaining Bolting JAFP-21-0008, Supplement to Application to Revise Surveillance Requirement (SR) 3.5.1.62021-02-18018 February 2021 Supplement to Application to Revise Surveillance Requirement (SR) 3.5.1.6 JAFP-21-0005, Response to Request for Additional Information to Support Review of License Amendment Request - Application to Modify Technical Specifications 3.6.1.3 Primary Containment Isolation Valves2021-01-26026 January 2021 Response to Request for Additional Information to Support Review of License Amendment Request - Application to Modify Technical Specifications 3.6.1.3 Primary Containment Isolation Valves ML20315A2452020-11-10010 November 2020 Response to Request for Additional Information to Support Review of License Amendment Request - Application to Modify Technical Specifications 3.6.1.3 Primary Containment Isolation Valves JAFP-20-0030, Response to Request for Additional Information in Support of License Amendment Request - Proposed Changes to the Technical Specifications to Primary Containment Hydrodynamic Loads2020-04-0606 April 2020 Response to Request for Additional Information in Support of License Amendment Request - Proposed Changes to the Technical Specifications to Primary Containment Hydrodynamic Loads JAFP-20-0026, Response to Request for Additional Information to Support Review of a License Amendment Request to Revise the Allowable Value for Reactor Water Cleanup (RWCU) System Primary Containment Isolation2020-03-31031 March 2020 Response to Request for Additional Information to Support Review of a License Amendment Request to Revise the Allowable Value for Reactor Water Cleanup (RWCU) System Primary Containment Isolation JAFP-20-0020, Response to Request for Additional Information to Support Review of a License Amendment Request to Revise the Allowable Value for Reactor Water Cleanup (RWCU) System Primary Containment Isolation2020-02-21021 February 2020 Response to Request for Additional Information to Support Review of a License Amendment Request to Revise the Allowable Value for Reactor Water Cleanup (RWCU) System Primary Containment Isolation JAFP-20-0008, Response to Request for Additional Information Associated with the License Amendment Request for Application of the Alternative Source Term for Calculating Loss-of-Coolant Accident Dose Consequences2020-01-16016 January 2020 Response to Request for Additional Information Associated with the License Amendment Request for Application of the Alternative Source Term for Calculating Loss-of-Coolant Accident Dose Consequences JAFP-19-0105, Response to Request for Supplemental Information by the Office of Nuclear Reactor Regulation to Support Review of a License Amendment Request to Revise the Allowable Value for Reactor Water Cleanup (Rwcu)...2019-11-0606 November 2019 Response to Request for Supplemental Information by the Office of Nuclear Reactor Regulation to Support Review of a License Amendment Request to Revise the Allowable Value for Reactor Water Cleanup (Rwcu)... ML19279A0012019-10-0606 October 2019 Response to Request for Additional Information by the Office of Nuclear Reactor Regulation to Support Review of an Emergency License Amendment Request for One Time Extension to the TS 3.8.1 Action ... JAFP-19-0057, Response to Request for Additional Information - Proposed Alternative to Utilize Code Cases N-878 and N-8802019-06-0404 June 2019 Response to Request for Additional Information - Proposed Alternative to Utilize Code Cases N-878 and N-880 NMP1L3279, Response to Request for Additional Information - Proposed Alternatives to Utilize Code Cases N-878 and N-880 for Plants2019-05-0101 May 2019 Response to Request for Additional Information - Proposed Alternatives to Utilize Code Cases N-878 and N-880 for Plants JAFP-19-0009, End of Interval Relief Request Associated with the Fourth Ten-Year Inservice Inspection (ISI) Interval2019-01-15015 January 2019 End of Interval Relief Request Associated with the Fourth Ten-Year Inservice Inspection (ISI) Interval JAFP-19-0006, Response to Request for Additional Information - Proposed Alternative to Utilize Code Cases N-878 and N-8802019-01-0808 January 2019 Response to Request for Additional Information - Proposed Alternative to Utilize Code Cases N-878 and N-880 JAFP-18-0068, Response to Request for Additional Information: License Amendment Request to Adopt Emergency Action Level Schemes Pursuant to NEI 99-01, Revision 6, Development of Emergency Action Levels for Non-Passive Reactors2018-07-12012 July 2018 Response to Request for Additional Information: License Amendment Request to Adopt Emergency Action Level Schemes Pursuant to NEI 99-01, Revision 6, Development of Emergency Action Levels for Non-Passive Reactors RS-18-067, Response to Request for Additional Information Regarding Generic Letter 2016-012018-05-29029 May 2018 Response to Request for Additional Information Regarding Generic Letter 2016-01 JAFP-18-0038, Response to Request for Additional Information Application to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control, Revision 22018-04-19019 April 2018 Response to Request for Additional Information Application to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control, Revision 2 JAFP-18-0029, Response to Request for Additional Information by the Office of Nuclear Reactor Regulation to Support Review of James A. FitzPatrick Nuclear Power Plant to Address Secondary Containment Personnel Access Door Openings2018-03-15015 March 2018 Response to Request for Additional Information by the Office of Nuclear Reactor Regulation to Support Review of James A. FitzPatrick Nuclear Power Plant to Address Secondary Containment Personnel Access Door Openings JAFP-18-0014, Response to Request for Additional Information on Submittal of Relief Request JAF-15R-05 Concerning Nozzle-to-Vessel Weld and Inner Radii Examinations (Use of Code Case N-702)2018-03-0202 March 2018 Response to Request for Additional Information on Submittal of Relief Request JAF-15R-05 Concerning Nozzle-to-Vessel Weld and Inner Radii Examinations (Use of Code Case N-702) ML18025A7992018-01-25025 January 2018 Response to Request for Additional Information Regarding Generic Letter 2016-01 JAFP-18-0012, Supplemental Response Concerning License Amendment Request to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control, Revision 22018-01-22022 January 2018 Supplemental Response Concerning License Amendment Request to Revise Technical Specifications to Adopt TSTF-542, Reactor Pressure Vessel Water Inventory Control, Revision 2 ML17346A1532017-12-11011 December 2017 Submittal of Response to Request for Additional Information on Relief Requests Associated with the Fifth Inservice Inspection (ISI) Interval JAFP-17-0029, Revision to Entergy'S Expedited Seismic Evaluation Process Report (CEUS Sites) Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of Near-Term Task Force Review of Insights...2017-04-27027 April 2017 Revision to Entergy'S Expedited Seismic Evaluation Process Report (CEUS Sites) Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of Near-Term Task Force Review of Insights... JAFP-17-0005, Response to 03/12/2012 Request for Information Regarding Recommendations of the Near-Term Task Force Review of Insights from the Fukushima Daiichi Accident, Recommendation 9.3 for Emergency Preparedness2017-01-23023 January 2017 Response to 03/12/2012 Request for Information Regarding Recommendations of the Near-Term Task Force Review of Insights from the Fukushima Daiichi Accident, Recommendation 9.3 for Emergency Preparedness JAFP-16-0182, Spent Fuel Pool Evaluation, Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident2016-12-22022 December 2016 Spent Fuel Pool Evaluation, Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident ML16335A1042016-11-29029 November 2016 Independent Spent Fuel Storage Installation, Response to Request for Additional Information Regarding Application for Order Approving Transfer F Renewed Facility Operating License and Proposed Conforming License Amendment JAFP-16-0170, Response to Request for Additional Information (RAI) Regarding License Amendment Request to Revise Technical Specifications Section 5.5.6 for Extension of Type a and Type C Leak Rate Test Frequencies - Supplement 12016-11-21021 November 2016 Response to Request for Additional Information (RAI) Regarding License Amendment Request to Revise Technical Specifications Section 5.5.6 for Extension of Type a and Type C Leak Rate Test Frequencies - Supplement 1 JAFP-16-0165, Response to Generic Letter 2016-01 - Monitoring of Neutron Absorbing Materials in Spent Fuel Pools2016-11-0303 November 2016 Response to Generic Letter 2016-01 - Monitoring of Neutron Absorbing Materials in Spent Fuel Pools JAFP-16-0142, Revision to Technical Specification (TS) Administrative Controls for Staffing and Training Upon Permanent Cessation of Operation (CAC No. MF7280) - Supplement 22016-09-19019 September 2016 Revision to Technical Specification (TS) Administrative Controls for Staffing and Training Upon Permanent Cessation of Operation (CAC No. MF7280) - Supplement 2 JAFP-16-0131, Response to Request for Additional Information Regarding Request for Approval of a Certified Fuel Handler Training and Retraining Program2016-08-18018 August 2016 Response to Request for Additional Information Regarding Request for Approval of a Certified Fuel Handler Training and Retraining Program JAFP-16-0130, License Amendment Request to Revise the Emergency Plan to Address the Permanently Defueled Condition - Supplement 22016-08-10010 August 2016 License Amendment Request to Revise the Emergency Plan to Address the Permanently Defueled Condition - Supplement 2 JAFP-16-0113, License Amendment Request to Revise the Emergency Plan to Address the Permanently Defueled Condition - Supplement 12016-07-0606 July 2016 License Amendment Request to Revise the Emergency Plan to Address the Permanently Defueled Condition - Supplement 1 JAFP-16-0114, Response to Request for Additional Information for Proposed Inservice Inspection Program Alternative in Accordance with 10 CFR 50.55a(z)(2), RR-202016-06-27027 June 2016 Response to Request for Additional Information for Proposed Inservice Inspection Program Alternative in Accordance with 10 CFR 50.55a(z)(2), RR-20 JAFP-16-0077, Response to Request for Additional Information (RAI) Regarding Revision to Technical Specification (TS) Administrative Controls for Staffing and Training Upon Permanent Cessation of Operation (CAC No. MF7280) - Supplement 12016-06-0303 June 2016 Response to Request for Additional Information (RAI) Regarding Revision to Technical Specification (TS) Administrative Controls for Staffing and Training Upon Permanent Cessation of Operation (CAC No. MF7280) - Supplement 1 JAFP-16-0078, Response to Request for Additional Information (RAI) Regarding Request for Approval of Certified Fuel Handler Training and Retaining Program2016-06-0303 June 2016 Response to Request for Additional Information (RAI) Regarding Request for Approval of Certified Fuel Handler Training and Retaining Program CNRO-2016-00016, Entergy - Response to RAI Questions and Submittal of Relief Request EN-ISI-15-1 (Updated)2016-06-0202 June 2016 Entergy - Response to RAI Questions and Submittal of Relief Request EN-ISI-15-1 (Updated) ML16071A4412016-03-0707 March 2016 Entergy Fleet Relief Request No. RR-EN-15-1-Proposed Alternative to Use ASME Code Case N-789-1 - E-mail from G.Davant to R.Guzman - Response to Second RAI (MF6340 - MF6349) CNRO-2016-00005, Response to Request for Additional Information Pertaining to a Change to the Entergy Quality Assurance Program Manual (QAPM)2016-02-25025 February 2016 Response to Request for Additional Information Pertaining to a Change to the Entergy Quality Assurance Program Manual (QAPM) CNRO-2016-00002, Entergy - Relief Request Number RR EN-15-1, Rev. 1 - Proposed Alternative to Use ASME Code Case N-789-1, Alternative Requirements for Pad Reinforcement of Class 2 and 3 Moderate Energy Carbon Steel Piping for Raw Water Service, Secti2016-01-29029 January 2016 Entergy - Relief Request Number RR EN-15-1, Rev. 1 - Proposed Alternative to Use ASME Code Case N-789-1, Alternative Requirements for Pad Reinforcement of Class 2 and 3 Moderate Energy Carbon Steel Piping for Raw Water Service, Section Xl, CNRO-2015-00002, Entergy Operations, Inc. - Response to RAI Questions and Submittal of RR EN-15-2, Rev. 12015-12-0404 December 2015 Entergy Operations, Inc. - Response to RAI Questions and Submittal of RR EN-15-2, Rev. 1 JAFP-15-0094, Response to Request for Additional Information for Expedited Seismic Evaluation Process Report2015-08-0404 August 2015 Response to Request for Additional Information for Expedited Seismic Evaluation Process Report 2022-06-16
[Table view] |
Text
200 Exelon Way Kennett Square, PA 19348 www.exeloncorp.com 10 CFR 50.90 10 CFR 50.91(a)(5)
October 6, 2019 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 James A. FitzPatrick Nuclear Power Plant Renewed Facility Operating License No. DPR-59 NRC Docket No. 50-333
SUBJECT:
Response to Request for Additional Information by the Office of Nuclear Reactor Regulation to support Review of an Emergency License Amendment Request for One Time Extension to the TS 3.8.1 Action A.3 Completion Time for an Inoperable Offsite Source
References:
- 1. Letter from D. Gudger (Exelon Generation Company, LLC) to U.S.
Nuclear Regulatory Commission, "Emergency License Amendment Request - One Time Extension to the TS 3.8.1 Action A.3 Completion Time for an Inoperable Offsite Source dated October 4, 2019
- 2. Electronic mail from S. Lee (Project Manager, U.S. Nuclear Regulatory Commission) to C. Williams (Exelon), FitzPatrick request for additional information: Emergency amendment to extend completion time of transformer to 21 days (EPID: L-2019-LLA-0214)," October 4, 2019.
5:01 PM
- 3. Electronic mail from S. Lee (Project Manager, U.S. Nuclear Regulatory Commission) to C. Williams (Exelon), FitzPatrick request for additional information: Emergency amendment to extend completion time of transformer to 21 days (EPID: L-2019-LLA-0214)," October 5, 2019, 7:18 AM
- 4. Electronic mail from S. Lee (Project Manager, U.S. Nuclear Regulatory Commission) to C. Williams (Exelon), FitzPatrick request for additional information: Emergency amendment to extend completion time of transformer to 21 days (EPID: L-2019-LLA-0214)," October 5, 2019.
9:49 AM By letter dated October 4, 2019, (Reference 1) Exelon Generation Company, LLC (Exelon) requested a one-time change to the James A. FitzPatrick (JAF) Technical Specifications (TS) under an emergency basis in accordance with 10 CFR 50.91(a)(5). The proposed amendment request would apply the one time change to the Completion Time for TS 3.8.1, required Action A.3 from 7 days to 21 days.
Response to Request for Additional Information by the Office of Nuclear Reactor Regulation to support Review of an Emergency License Amendment Request for One Time Extension to the TS 3.8.1 Action A.3 Completion Time for an Inoperable Offsite Source October 6, 2019 Page2 By electronic mail dated October 4 and October 5, 2019 (References 2, 3 and 4), the NRC identified areas where additional information was necessary to complete the review.
Attachment 1 to this letter contains the NRC's request for additional information immediately followed by Exelon's response.
Exelon has reviewed the information supporting a finding of no significant hazards consideration and the environmental consideration provided to the NRC in Reference 1.
The information attached to this letter does not affect the bases for concluding that the proposed license amendment does not involve a significant hazards consideration.
Furthermore, the information attached to this letter does not affect the bases for concluding that neither an environmental impact statement nor an environmental assessment needs to be prepared in connection with the proposed amendment.
There are no commitments contained in this response.
If you should have any questions regarding this submittal, please contact Christian Williams at 610-765-5729.
I declare under penalty of perjury that the foregoing is true and correct. Executed on the 61h day of October 2019.
Respectfully, Jr._ -J T. J__,,,}0-'-
David T. Gudger Acting Director, Licensing Exelon Generation Company, LLC
Attachment:
- 1. Request for Additional Information and Exelon Response cc: Regional Administrator - NRC Region I w/ attachments NRC Senior Resident Inspector- JAF "
NRC Project Manager, NRA - JAF "
A. L. Peterson, NYSERDA "
Attachment 1 Page 1 of 4 ATTACHMENT 1 Request for Additional Information and Exelon Response James A. FitzPatrick Nuclear Power Plant Renewed Facility Operating License No. DPR-59 NRC Docket No. 50-333 RAI-EICB-1 For Surveillance 3.3.5.1.3, associated with Technical Specification (TS) table 3.3.5.1-1, functions 4.e and 5.e., and 3.3.5.1.6, associated with TS 3.3.5.1-1, functions 3.f and 3.g, what historical evidence is there to show that performance is satisfactory? For example, for Surveillance Requirement (SR) 3.3.5.1.3, have the most recent past several surveillances shown that the As-Found condition of the instruments is consistently within the As-Found Tolerance limits, and within the Allowable Value, especially when the Calibration Surveillance falls within the grace period? For SR 3.3.5.1.6, have the results of the Logic System Functional Test been consistently achieving the test acceptance criteria? Is there any other evidence that would indicate that these instrument channels have been performing reliably? Also, what does the LAR mean, exactly, when it says:
o The A and B Emergency Diesel Generators and their associated cooling water pumps and power supplies will be protected.
o The 4160V emergency buses will be protected.
o HPCI and Reactor Core Isolation Cooling (RCIC) will be protected.
o Both trains of Residual Heat Removal (RHR) and CSP will be protected.
EXELON RESPONSE:
Surveillance requirement 3.3.5.1.3 is demonstrated as being meet through the completion of ISP-6A, ISP-22-2 and ST-22C. Previous completion review of these activities was conducted.
ISP-6A (through Sept 2017) was reviewed and as-found test results were in specification and no adjustment has been required. ISP-22-2 (last 3 performances) was reviewed and as-found test results were in specification and no adjustment has been required. Surveillance Requirement 3.3.5.1.6 is also partially met by ST-22C, ADS Logic System Functional Test. The last performance of ST-22C (November 2018) was completed satisfactorily with no corrective actions.
The intent of protecting systems and components is to provide additional administrative barriers to guard against inadvertently rendering a component or system, which is important to unit risk and nuclear safety, inoperable or unavailable. It is also applicable to those systems and activities that pose a potential risk to generation.
Attachment 1 Page 2 of 4 RAI-EMIB-1 SRs 3.5.1.2, 3.5.2.5, 3.5.3.2, 3.6.1.9.1, 3.6.2.3.1, 3.7.1.1 - Explain why it is acceptable to delay these valve position verifications.
EXELON RESPONSE:
The referenced Surveillance Requirements are satisfied by procedures which contain activities other than valve position verifications based on control room panel indication. Procedure ODSO-4, Shift Turnover and Log Keeping, requires a documented verification of all Technical Specification related switch and controller positions once per shift. The completed form is reviewed by a shift SRO and any out-of-normal positions are reviewed by the Shift Manager.
RAI-EMIB-2 SR 3.5.1.7 - Discuss whether or not the core spray and LPCI pumps have shown degradation in past surveillances.
EXELON RESPONSE:
Response for Core Spray: Based on the trending for Core Spray pumps performed per quarterly frequency ST-3PA and ST-3PB, there have been no failures or degrading trends in the past four surveillances. In addition, the last 24-month comprehensive pump test was completed satisfactorily for each pump.
Response for LPCI: Based on the trending for LPCI pumps performed per quarterly frequency ST-2AM and ST-2AL, there have been no failures or degrading trends in the past four surveillances. In addition, the last 24-month comprehensive pump test was completed satisfactorily for each pump.
RAI-EMIB-3 SRs 3.5.1.8 and 3.5.1.9 - Discuss whether or not the HPCI pump has shown degradation in past surveillances.
EXELON RESPONSE:
Based on the trending for HPCI pumps performed per quarterly frequency ST-4N, there have been no failures or degrading trends in the past four surveillances. In addition, the last 24-month comprehensive pump test was completed satisfactorily.
RAI-EMIB-4 SR 3.6.1.3.5 - Discuss whether or not any valves have shown degradation in past surveillances.
Attachment 1 Page 3 of 4 EXELON RESPONSE:
ST-4N, HPCI Quick Start, Inservice, and Transient Monitoring; and ST-2AM, RHR Loop B Quarterly Operability Test, in part, satisfy the PCIV SR 3.6.1.3.5. There have been no failures or degrading trends identified in the past four performances.
RAI-EMIB-5 SRs 3.6.1.9.2 and 3.6.2.3.2 - Discuss whether any RHR pump has shown degradation in past surveillances.
EXELON RESPONSE:
Based on the trending for RHR pumps performed per quarterly frequency ST-2AM and ST-2AL, there have been no failures or degrading trends in the past four surveillances. In addition, the last 24-month comprehensive pump test was completed satisfactorily for each pump.
RAI-EMIB-6 SRs 3.8.1.4, 3.8.3.1, 3.8.3.2, 3.8.3.4 - Explain why it is acceptable to delay these SRs.
EXELON RESPONSE:
The referenced Surveillance Requirements are satisfied by procedures which contain activities other than visual observations of EDG support systems (lube oil, fuel oil, and starting air pressure). These activities have the potential to introduce FME into the subject systems or require the operation of the EDGs. EDG fuel oil in both underground fuel oil storage tanks and fuel oil day tanks, as well as lube oil and air starting pressures, are monitored and recorded daily during operator rounds. Operator Rounds are reviewed and approved by the on-shift SRO to ensure any out-of-specification readings are evaluated and corrective actions initiated.
RAI-SCPB-1 Provide specific information for the NRC staff to adequately determine that delaying SRs 3.8.1.4 and 3.8.1.5 would have no adverse impact on the Emergency Diesel Generators (EDGs), if EDG operation becomes necessary during the extended surveillance period.
EXELON RESPONSE:
The referenced Surveillance Requirements are associated with the EDG fuel oil day tanks. EDG fuel oil day tank level is monitored and recorded daily during Operator Rounds. Operator Rounds are reviewed and approved by the on-shift SRO to ensure any out-of-specification readings are evaluated and corrective actions initiated. The potential for water intrusion into the fuel is minimal as evidenced by the fact there have been no failures to meet ST-9AA acceptance criteria during the last 24 months. Additionally, fuel oil would normally only be transferred from the underground fuel oil storage tank to the day tank follow an EDG run which will not be scheduled during the extended surveillance period.
Attachment 1 Page 4 of 4 RAI-EEOB-1 In the LAR, Attachment 1, Page 7, the licensee stated: The preferred resolution is to restore the installed transformer to service based on the age and limited functionality of the replacement transformer.
Please explain the term limited functionality of the alternative of replacement transformer. List the major differences between the installed transformer and the replacement transformer. Please explain whether the replacement transformer will have an On-Load Tap Changer. If not, whether it will impact the current licensing basis.
EXELON RESPONSE:
The limited functionality refers to the fact that the replacement transformer does not have an On-Load Tap Changer. This is the only major functional difference between the installed transformer and the replacement transformer. The current licensing basis will be reviewed as part of the engineering modification process and updated if required. An agreement between JAF and National Grid will ensure compliance with NERC reliability standard NUC-001-3, Nuclear Plant Interface Requirements (NPIRs), and JAF requirements for grid voltage.
RAI-EEOB-2 Section 8.4.3 of the JAF UFSAR states: The 345 kV system is capable of supplying all loads on the emergency buses to maintain the plant in the shutdown condition. As the 345 kV backfeed power will be used only during plant outages, a LOCA is not postulated. Please provide an estimate of time which will be required to establish the 345 kV backfeed power, after the plant is tripped.
EXELON RESPONSE:
FitzPatrick has previously implemented the 345kV back-feed configuration to support outage tasks. Based on plant experience, approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> would be required to place the station in a 345kV back-feed configuration following a unit trip.
RAI-STSB-1 The Risk Management Actions (RMAs) proposed in pages 10 and 11 of Attachment 5 of the LAR reference two 115kV transmission lines. The second RMA specifically identifies that Nine Mile Point Lines #1 and #4 will be controlled such that maintenance and switching on the lines will be done in emergency situations only. Per the Final Safety Analysis Report as updated in section 8.3.2.4 it describes that the line terminates at Nine Mile Point Nuclear Station Unit 1 before being connected to the National Grids South Oswego Substation. Does the RMA described above include controlling any work in the switchyard associated with Nine Mile Point Unit 1? If so please describe. If not will controls be put in place in the switchyard associated with Nine Mile Point Unit 1?
Attachment 1 Page 5 of 4 EXELON RESPONSE:
The Nine Mile Point Unit 1 115kV switchyard is protected in accordance with OP-AA-108-117, Protected Equipment Program. The switchyard will remain protected until the 115kV transformer 71T-3 is returned to service.