05000293/LER-1978-057-03, /03L-0 on 781230:while Operating in Full Flow Test,Hpci Tripped.Investigation Revealed Low Level in Oil Sump & Overflow Pit Around Turbine Filled W/Oil.Caused by Disconnected Fitting for Discharge Pressure Gage Oil Pump

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/03L-0 on 781230:while Operating in Full Flow Test,Hpci Tripped.Investigation Revealed Low Level in Oil Sump & Overflow Pit Around Turbine Filled W/Oil.Caused by Disconnected Fitting for Discharge Pressure Gage Oil Pump
ML19259B336
Person / Time
Site: Pilgrim
Issue date: 01/22/1979
From: Mathis C
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19259B334 List:
References
LER-78-057-03L, LER-78-57-3L, NUDOCS 7901260185
Download: ML19259B336 (1)


LER-1978-057, /03L-0 on 781230:while Operating in Full Flow Test,Hpci Tripped.Investigation Revealed Low Level in Oil Sump & Overflow Pit Around Turbine Filled W/Oil.Caused by Disconnected Fitting for Discharge Pressure Gage Oil Pump
Event date:
Report date:
2931978057R03 - NRC Website

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EVENT DATE 74 75 REPORT DAT E 80 EVENT DESCRIPTION AND PROBAULE CONSEQJENCES h lo l 2 l l On December 30, 1978, while operating in full flow test to stir up the condensate I

o 3 l storage tanks' sediment, the HPCI tripped.

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