ML19259B336

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LER 78-057/03L-0 on 781230:while Operating in Full Flow Test,Hpci Tripped.Investigation Revealed Low Level in Oil Sump & Overflow Pit Around Turbine Filled W/Oil.Caused by Disconnected Fitting for Discharge Pressure Gage Oil Pump
ML19259B336
Person / Time
Site: Pilgrim
Issue date: 01/22/1979
From: Mathis C
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19259B334 List:
References
LER-78-057-03L, LER-78-57-3L, NUDOCS 7901260185
Download: ML19259B336 (1)


Text

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40 41 di 43 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 47 lil0ll Maintenance Personnel discovered the fitting for the discharge pressure gage on the j ii jij latttched oil pump was disconnected. The fitting was reconnected and surveillance I

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