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MONTHYEARML19259D1761979-05-16016 May 1979 Anticipatory Trip Functions for 177 Fuel Assembly Plants Project stage: Other ML19225B2461979-07-13013 July 1979 Forwards Application for Amend to License NPF-3 Revising Tech Specs to Reflect Changes Re Interim Anticipatory Reactor Trip Sys & Auxiliary Feedwater Flow Indications. Class IV Amend Fee Encl Project stage: Request ML15223A5321979-09-0707 September 1979 Requests Addl Info Re Upgrade of Anticipatory Reactor Trip Project stage: Other ML15223A5311979-09-0707 September 1979 Notifies of Review of Responses to IE Bulletin 79-05B. Requests Addl Info Re Proposed Design Description & Implementation Schedule for safety-grade Anticipatory Reactor Trip Project stage: Approval ML19256C7381979-10-0303 October 1979 Forwards Addl Info Re Upgrading of safety-grade Anticipatory Reactor Trip Sys (Arts),In Response to 790907 Request.One Oversize Drawing Available in Central Files Project stage: Other ML19259D1741979-10-0909 October 1979 Forwards Anticipatory Trip Functions for 177 Fuel Assembly Plants Project stage: Other ML19257A9711979-12-20020 December 1979 Forwards Safety Evaluation Approving Preliminary Design for safety-grade Anticipatory Reactor Trip on Loss of Feedwater & Turbine Trip.Requests Addl Info for Final Design Approval Project stage: Approval ML20213D0761979-12-20020 December 1979 Forwards Safety Evaluation Re Preliminary Design for safety- Grade Anticipatory Reactor Trips on Loss of Main Feedwater &/Or Main Turbine Generator Project stage: Approval ML20213D0721979-12-20020 December 1979 Forwards Safety Evaluation Approving Preliminary Design for safety-grade Anticipatory Reactor Trip on Loss of Feedwater & Turbine Trip.Requests Addl Info for Final Design Approval Project stage: Approval ML19257B4161979-12-20020 December 1979 Forwards Safety Evaluation Re Preliminary Design for safety- Grade Anticipatory Reactor Trips on Loss of Main Feedwater &/Or Main Turbine Generator Project stage: Approval ML20214J2801979-12-20020 December 1979 Safety Evaluation Re Preliminary Design for Upgrading Present control-grade Anticipatory Reactor Trip Sys for Loss of Main Feedwater & Turbine Trip to safety-grade Project stage: Approval ML20214J2911979-12-20020 December 1979 Safety Evaluation Re Preliminary Design for safety-grade Anticipatory Reactor Trips on Loss of Main Feedwater &/Or Turbine Trip Project stage: Approval ML19326D9901980-07-21021 July 1980 Notifies That Equipment Being Added to Reactor Protection Sys Cabinets Is of Sufficient Mass as to Require New Seismic Analysis of Cabinets.Analysis Requires Approx 20 Wks.Info Will Be Provided in Time to Allow for Final Design Approval Project stage: Other ML20009B0071981-07-0303 July 1981 Revises Submittal Date to 810814 for Final Design for Safety Grade Anticipatory Reactor Trip & Design Info for Safety Grade Initiation & Flow Indication of Auxiliary Feedwater Sys,Per NUREG-0737,TMI Items II.E.1.2 & II.K.2.10 Project stage: Other ML20009G0981981-07-24024 July 1981 Informs That During Next Refueling Outage in Feb 1982, Anticipatory Reactor Trip Sys Will Be Replaced W/Upgraded Sys.Revised Application Will Be Submitted Project stage: Other ML20010G0141981-09-0808 September 1981 Forwards B&W Rept Auxiliary Feedwater Sys & 36 Oversize Drawings,Per 810703 Commitment to Submit Final Design Info Re NUREG-0737,Items II.K.2.10 & II.E.1.2.Aperture Cards Are Available in PDR Project stage: Other ML20031G5731981-10-19019 October 1981 Responds to Requesting Addl Info Safety Grade Anticipatory Reactor Trip.Forwards Procedure I-111,Revision 9, Reactor Protection Sys Channel Calibr & Procedure I-108A,Revision 17, Reactor Protection Sys Channel a Test Project stage: Other ML20032A6501981-10-21021 October 1981 Ack Receipt of 810908 Rept Re safety-grade Anticipatory Reactor Sys.Requests That Addl Info Per Encl List Be Forwarded within 14 Days Project stage: Other ML20033C8621981-11-25025 November 1981 Application to Amend License NPF-3,revising Tech Specs to Reflect Proposed Changes to Sys Integrity Measurements & Improved Iodine Monitoring Programs & Anticipatory Reactor Trip Sys Project stage: Request ML20033C8651981-11-25025 November 1981 Proposed Tech Specs 6.8.4,3.3.2.3,4.3.2.3 & Tables 3.3-15 & 4.3-15 Re Administrative Controls & Anticipatory Reactor Trip Sys Instrumentation.Safety Evaluation & Bases Encl Project stage: Other ML20033C8541981-11-25025 November 1981 Forwards Application to Amend License NPF-3 Project stage: Request ML20039F5871982-01-0505 January 1982 Responds to Questions Raised at 811208 Meeting W/Nrc & Consultants Re Anticipatory Reactor Trip Sys.Proposed Channel Functional Test Will Include Pressure Switch.Light Indicating Level Bypass Will Clear When Level Bypass Clears Project stage: Meeting ML20041G3811982-03-0505 March 1982 Application to Amend License NPF-3,allowing Rector Startup W/O Trip & Changing Tech Specs for safety-grade Anticipatory Reactor Trip Sys Project stage: Request ML20041G3791982-03-0505 March 1982 Transmits Application for Amend to License NPF-3,extending Length of Fuel Cycle 3 Project stage: Request ML20052H4931982-05-14014 May 1982 Safety Evaluation Re Final Design & Implementation of safety-grade Anticipatory Reactor Trip on Turbine Trip or Loss of Main Feedwater.Design Satisfies Reactor Protection Sys Safety Requirements & Criteria Project stage: Approval ML20054H2231982-06-15015 June 1982 Notifies That Seismic & Environ Qualification Summary Rept for Anticipatory Reactor Trip Sys Complete & Will Be Submitted by 820709 Project stage: Other ML20054M2011982-07-0707 July 1982 Revises 791003 Response to Request for Addl Info Re Operating Bypasses & Bypass Indications,In Support of 811125 Request for Amend to License NPF-3 Project stage: Request ML20063E2211982-07-0808 July 1982 Forwards Seismic Qualification Rept 3394-1..., Anticipatory Reactor Trip Sys Seismic Qualification Test Plan, Seismic Simulation Test Program... & Environ Qualification Rept..., in Response to NRC 820514 Request Project stage: Other IR 05000346/19820191982-07-27027 July 1982 IE Insp Rept 50-346/82-19 on 820713.No Noncompliance Noted. Major Areas Inspected:Followup of Prompt Public Notification/Warning Sys Project stage: Request ML20062F2651982-07-27027 July 1982 Concludes That Anticipatory Reactor Trip Sys Bypasses Classification as Operating Bypass Is Unacceptable Unless Addl Features to Alert Operator to Remove Bypasses Are Added Project stage: Other ML20065H9181982-09-29029 September 1982 Responds to Re NUREG-0737,Item II.K.2.10, Anticipatory Reactor Trip Sys (Arts). Adequate Features Available to Alert Operator to Remove Bypass When Automatic Bypass Removal Not Required Project stage: Other 1981-07-24
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- M December 20, 1979 Docket No. 50-346 Mr. Lowell E. Roe Vice President, Facilities Development Toledo Edison Company Edison Plaza 300 Madison Avenue Toledo, Ohio 43652
Dear Mr. Roe:
SUBJECT:
PRELIMINARY DESIGN APPROVAL FOR THE SAFETY-GRADE ANTICIPATORY REACTOR TRIP SYSTEM (ARTS)
We have reviewed your submittals of May 21 and October 3,1979, in which you forwarded a preliminary design for upgrading the present control-grade anticipatory reactor trip system (ARTS) for loss of main feedwater and turbine trip to safety-grade.
A copy of the staff safety evaluation approv-ing your preliminary design is included as an enclosure to this letter.
As summarized on Attachment 1 to this safety evaluation, additional infor-mation will need to be submitted prior to final design approval by the staff.
Therefore, assure that this information is submitted for review in sufficient time to allow staff review prior to system operation.
If you have any questions regarding this matter, please contact your NRR Operating Reactor Project Manager, Mr. Daniel Garner, on (301) 492-7435.
Sincerely, m
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Robert W. Reid, Chief Operating Reactors Branch '4 Division of Operating Reactors
Enclosure:
Safety Evaluation cc: w/ enclosure l[bb 2bb' See next page 8 001160 Q3$
1
Toledo Edison Company cc w/ enclosure (s):
Mr. Donald H. Hauser, Esq.
Cirector, Technical Assessrent The Cleveland Electric Division Illuminating Company Cffice of Radiation Prograr.s P. O. Box 5000
( AW-459)
Cleveland, Ohio 44101 C. S. Environmental Protection Agency Crystal Mall #2 Gerald Charnoff, Esq.
Arlington, Virginia 20460 Shaw, Pittman, Potts and Trowbridge U. S. Environmental Protection Agency 1800 M Street, N.W.
Federal Activities Branch Washington, D.C.
20335 P.egion V Office A TH:
EIS COORDINATOR Leslie Henry, Esq.
230 South Dearborn Street Fuller, Seney, Henry and Hodge -
Cnicago, Illinois 60604 300 Madison Avenue Toledo, Ohio 43634 Mr. Robert B. Borsum Babcock & Wilcox Chio Der'rtment of Health Nuclear Power Generation Division ATTH:
U1 rector of Health Suite 420, 7735 Old 3eargetown Road 450 East Town Street Bethesda, Marylanc 20014 Columbus, Ohio 43216 Ida Rupp Public Library 310 Madison Street Port Clinton,0hio 43452 President, Board of County Commissioners of Cttawa County Port Clinton, 0 hic 43452 Attorney General Department of Atterr.ey General 30 East Broad Street Columbus, Ohio 43215 Harold Kahn, Staff Scientist Power Siting Commission 361 East Broad Street Columbus, Ohio 43216 Mr. Rick Jagger Industrial Commissicn State of Ohio 2323 est 5:n averus Colurtus, Ohio 422: 9 "r
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'% V SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION EVALUAITON OF PRELIMINARY DESIGN FOR SAFETY GRADE ANTICIPATORY REACTOR TRIPS (ARTS) ON LOSS OF MAIN FEEDWATER AND/0R MAIN TURBINE GENERATOR FOR DAVIS-BESSE, UNIT NO. 1 DOCKET NO. 50-346 I Background Following the accident at Three Mile Island, Unit No. 2, an assessment of feedwater transients in the Babcock & Wilcox (B&W) designed pressurized water reactors was performed.
The results of that review were reported in NUREG-0560.
This report highlighted a concern regarding the challange rate to the power-operated relief valve (PORV) in the B&W design.
In response to I&E Bulletin 79-05B, Toledo Edison Company (TECO or licensee) lowered the existing setpoint for the high pressure reactor trip and raised the setpoint of the PORV.
By inverting these setpoints the challenge rate to the PORV opening, and thus the likelihood of it not reseating following actuation was reduced.
To provide additional margin to the automatic opening setpoi.t of the PORV, the licensee proposed design provisions for direct reactor trip on loss of main feedwater or turbine trip.
This design modification was incorporated as part of the short-term and long-term requirerents of the Comissions' May 16, 1979 Confinnatory Shutdown Order.
In order to achieve a timely implementation of this modification, it was determined that a control-grade design was sufficient for the short-term.
This was implemented by the licensee by installing hardwired, control-grade trips for loss of main feedwater and turbine trip which were independent of the reactor protection system (RPS).
For the long-term, an upgrading of this system to safety-grade is required.
The licensee submitted its proposed safety-grade design in a letter dated May 21, 1979, from J. S. Grant (TECO) to J. G. Keppler (NRC) and later supplemented the design in a letter dated October 3,1979, from L. E. Roe (TECO) to R. W. Reid (NRC).
The following evaluation addres = + M
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b preliminary design of. the Antic Davis-Besse, Unit'No. 1.
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