05000293/LER-1979-036-01, /01T-0:on 791001,discovered That Portion of SSW Loop Piping B Could Be Overstressed During Seismic Event. Caused by Design Error.Plant Design Change Request Initiated to Reduce Stress to Acceptable Limits

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/01T-0:on 791001,discovered That Portion of SSW Loop Piping B Could Be Overstressed During Seismic Event. Caused by Design Error.Plant Design Change Request Initiated to Reduce Stress to Acceptable Limits
ML19253B426
Person / Time
Site: Pilgrim
Issue date: 10/09/1979
From: Whitney G
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19253B424 List:
References
LER-79-036-01T, LER-79-36-1T, NUDOCS 7910150538
Download: ML19253B426 (1)


LER-1979-036, /01T-0:on 791001,discovered That Portion of SSW Loop Piping B Could Be Overstressed During Seismic Event. Caused by Design Error.Plant Design Change Request Initiated to Reduce Stress to Acceptable Limits
Event date:
Report date:
2931979036R01 - NRC Website

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60 61 DOCKET NUMBER 68 t/J EVENT DATE 14 IS HEPORT DATE 80 EVENT DESCRIPTION AND PROBAOLE CONSEQUENCES h 1012 l l On October 1, 1979, Pilgrim Station was informed by it 2 Engineering Department j

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