LER-1979-074, /03L-0:on 791019,reactor Scram Received from High Radiation Signal on Main Steam Line High Radiation Monitors. Caused by Resin Injection from Reactor Water Cleanup Sys.Sys Depressurized |
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LICENSEE EVENT REPORT CONTROL BLOCK:
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8 60 61 DOCKET NUM8ER 6d 69 EVENT DATE 14 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Ml During nor-,1 full cover coeration. a reactor scram was received due to a high l
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1 radiation signal on the Main Steam Line High Radiation Monitors. After the scram,l 0
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the nonitors returned to a normal reading and all MSIV's were onened. No stack l
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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 1 O l The c,n=e for the reactor scram was a resin iniection from the RWCU system. The LLL'_J l stm =yara una han, otit of service for aooroximately six hours prior to the scrami i 2 I
fnr system -nintenance.
Durine this ceriod. it is believed'that the filter cake l
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A METPOOF F ACILITY DISCOVERY OISCOVERY DESCRIPTION 32 STATUS *
% POWER OTHERSTATUS
(,Ijh 1lololhl NA l l Al@l Reactor Scram l
1 5 ACTIVITY CO TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE M W @ d@l NA l NA l
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NUY8ER OESCRIPTION IT R Iololol@l NA l
7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY
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8 9 10 80 ISSUE OE SC RiPTION e
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8 3 10 68 69 80 5 NAME OF PREPARER A. C. Tollison, Jr.
919-457-9521 2
PHONE:
, _. LER CONTINUATION -- RO# l-79-74:
Facility: BSEP Unit # 1 Event Date: 10-19-79 EVENT DESCRIPTION AND PROBAh:E CONSEQUENCES (Cont'd)
Slight Increase No Change Power (APRM)
Core a P
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Vessel Pressure Vessel Level Core Flow "B" Feed Flow "A" Feed Flow Throttle Pressure Total Steam Flow Gross Megawatts Turbine Vibration Events noted during and after the scram were as follows:
1.
- 1 Diesel Generator did not start on the lov level (-38") initiation signal at the time of the scram.
2.
While trying to go into torus cooling and later, shutdown cooling, on "B" RHR heat exchanger, no a T could be developed across the heat exchanger.
3.
After being used intermittently throughout the day for ves cl level control, the RCIC turbine could not be started on the afternoon of the scram.
4.
Vessel chemistry exceeded 2 umho for approxtsately 31.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, reaching a maximum value of 6.63 umho.
5.
The CRD scram discharge volume drain line was found to have several pipe supports damaged from an apparent water hammer event.
Technical Specifications 6.9.1.9b l j '/ 4 J
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- - 3 LER CONTINUATION - RO# l-79-74 Facility: BSEP Unit # 1 Event Date: 10-19-79 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (Cont'd)
RWCU pump was started. Approximately one minute later, the reactor scrammed.
Resin injected into the vessel caused a change in coolant viscosity and surface tension resulting in flow and pressure disturbances.
This imbalance in vessel chemistry results in a release of N-16 which carries over with the steam. The N-16 high energy gamma caused the scram.
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The faLI.ure of the #1 Diesc1 Generator was due to a split metallic bellows on the lube oil diverting valve actuator, causing a loss of control air.
The diverting valve actuator was replaced with a new vender modified design on all diesel generators. Diesel generator control air pressure has been added to the auxiliary operators Daily Surveillance Report to be checked once per shift.
The anti-rotation device on the RHR heat exchanger inlet valve F047B allowed the stem to rotate without moving the valve disk. The anti-rotation device was adjusted and the valve tested satisfactorily. This is considered an isolated event.
Disassembly of the RCIC steam exhaust check valve showed that the stud and nut on the back of the disk had broken and the disk had separated from the hinge and had lodged in the valve inlet. A new valve has been ordered and will be installed upon arrival. Engineering has been tasked to determine the cause of the failure.
Vessel conductivity increase to 6.63 umho was due to the resin injection and resin breakdown due to temperature and neutron flux. The vessel was cleaned to less than 2 gmho in approximate'ly 31.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. Operating Procedure 14, RWCU, has been revised to direct the RWCU effluent to the condenser after precoating or an. extended shutdown until a chemical analysis is run on the effluent.
Also, the revision requires that (1) double valve isolation of the filter /
demineralizer be used when going.co " Hold / Start", (2) always backwash and precoat the filters when RWCU has been depressurized for greater than thirty minutes, and (3) F042, the RWCU injection valve, will not be opened until the system is completely pressurized and stable.
The CRD scram discharge volume drain line had esveral of its supports damaged by water hammer during the scram. This water hammer is believed to have been caused by the excessively long closing time of the drain line isolation valve.
This problem has been corrected by replacement of the solenoid valve which operates the drain and vent valves. The damaged supports were also replaced and an evaluation is underway to determine if additional support is required.
PT inspections will be conducted on all welds on this line. The drain lines on the other unit were inspected with no detectable damage noted.
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| 05000324/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000324/LER-1979-001-03, /03L-0 on 790102:instrument B21-LIS-N017B Found Out of Calibr;Switch Actuated at 1.13 Inches.Switch Out of Calibr Due to Setpoint Drift.New Instrument Ordered; Existing Instrument Showed Excessive Deadbeat in Indicator | /03L-0 on 790102:instrument B21-LIS-N017B Found Out of Calibr;Switch Actuated at 1.13 Inches.Switch Out of Calibr Due to Setpoint Drift.New Instrument Ordered; Existing Instrument Showed Excessive Deadbeat in Indicator | | | 05000325/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000325/LER-1979-001-03, /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing | /03L-0 on 790104:HPCI Sys Failed Response Time Periodic Test.Testing to Be Done Again After Reactor Startup,When Steam Is Available.Event Cause & Corrections to Be Submitted After Satisfactory Testing | | | 05000325/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000324/LER-1979-002-03, /03L-0 on 790115:generator Failed to Produce Output Voltage.Caused by Failure of Generator Field Reset Switch to Make Good Contact | /03L-0 on 790115:generator Failed to Produce Output Voltage.Caused by Failure of Generator Field Reset Switch to Make Good Contact | | | 05000324/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000325/LER-1979-002-03, /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset | /03L-0 on 790123:standby Liquid Control Relief Valve C41-F029 Lifted at Pressure of 1300 Psig,Below Tech Spec Min.No Mechanical Reason Found.Valve Reset | | | 05000324/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000324/LER-1979-003-03, /03L-0 on 790130:reactor Scrammed on Average Power Range Monitor High Flux.Caused by stem-disc Separating, Causing a Momentary Pressure Spike.Repairs to Appropriate Valve Will Be Made | /03L-0 on 790130:reactor Scrammed on Average Power Range Monitor High Flux.Caused by stem-disc Separating, Causing a Momentary Pressure Spike.Repairs to Appropriate Valve Will Be Made | | | 05000325/LER-1979-003-03, /03L-0 on 790117:steamline Low Pressure Isolation Instrument Actuated Below Tech Spec Min.Caused by Loose Clamp Block Allowing Instrument Torque Shaft to Slip | /03L-0 on 790117:steamline Low Pressure Isolation Instrument Actuated Below Tech Spec Min.Caused by Loose Clamp Block Allowing Instrument Torque Shaft to Slip | | | 05000325/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000325/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000325/LER-1979-004-03, /03L-0 on 790105:containment Atmospheric Dilution Tank Contained Less than Tech Spec Limit.Operator Misread Conversion Graph,Resulting in Higher than Actual Nitrogen Reading.Tank Indicators to Be Marked W/Specific Limit | /03L-0 on 790105:containment Atmospheric Dilution Tank Contained Less than Tech Spec Limit.Operator Misread Conversion Graph,Resulting in Higher than Actual Nitrogen Reading.Tank Indicators to Be Marked W/Specific Limit | | | 05000324/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000324/LER-1979-004-03, /03L-0 on 790110:chart Recorder for CAC-AT-1259 Was Reading Inaccurately,Since Sample Pump for Drywell Monitor CAC-AT-1259 Was Producing Poor Flow,Due to Malfunction | /03L-0 on 790110:chart Recorder for CAC-AT-1259 Was Reading Inaccurately,Since Sample Pump for Drywell Monitor CAC-AT-1259 Was Producing Poor Flow,Due to Malfunction | | | 05000325/LER-1979-005-03, /03L-0 on 790104:1A Recirculation Pump Tripped W/Reactor at 97% power.1B Pump Then Reduced to Approx 50% Speed.Caused by 1A Pump Motor Generator Set Low Lubrication Oil Pressure Signal & Missing Locknut.New Locknuts Put in | /03L-0 on 790104:1A Recirculation Pump Tripped W/Reactor at 97% power.1B Pump Then Reduced to Approx 50% Speed.Caused by 1A Pump Motor Generator Set Low Lubrication Oil Pressure Signal & Missing Locknut.New Locknuts Put in | | | 05000325/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000324/LER-1979-005-03, /03L-0 on 790109:RHR Pump Discharge Pressure Switch E11-PS-N020D Failed,Causing Pump Running Annunciator. Caused by Contact Plunger Stem Corrosion | /03L-0 on 790109:RHR Pump Discharge Pressure Switch E11-PS-N020D Failed,Causing Pump Running Annunciator. Caused by Contact Plunger Stem Corrosion | | | 05000324/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000325/LER-1979-006-03, /03L-0 on 790316:during Refueling Outage,Condenser Tube Leaks Allowed Chlorides to Enter Condensate Sys.Cfd in Svc Became Depleted Due to Entrained Oxygen.Condenser Vacuum Broken & Cfds & Cdds Placed in Svc to Clean Sys | /03L-0 on 790316:during Refueling Outage,Condenser Tube Leaks Allowed Chlorides to Enter Condensate Sys.Cfd in Svc Became Depleted Due to Entrained Oxygen.Condenser Vacuum Broken & Cfds & Cdds Placed in Svc to Clean Sys | | | 05000324/LER-1979-006-03, /03L-0 on 790131:while Performing High Drywell Pressure Functional Check of Core Spray HPCI & LPCI a Loop RHR Logic Failure Alarm Received.Caused by Blown Fuse in P617 | /03L-0 on 790131:while Performing High Drywell Pressure Functional Check of Core Spray HPCI & LPCI a Loop RHR Logic Failure Alarm Received.Caused by Blown Fuse in P617 | | | 05000325/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000324/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000325/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000325/LER-1979-007-03, /03L-0 on 790109:during Sys Component Test, Residual Heat Removal Pump D Would Not Start.Caused by Motor Switch Being in Off Position | /03L-0 on 790109:during Sys Component Test, Residual Heat Removal Pump D Would Not Start.Caused by Motor Switch Being in Off Position | | | 05000324/LER-1979-007-01, /01T-0 on 790227:during Reactor Annulus Pressurization Analysis,Pipe Whip Restraint in Each Unit Did Not Conform.Caused by Improper Design of Restraint.Architect & Owner Will Design Addl Restraint | /01T-0 on 790227:during Reactor Annulus Pressurization Analysis,Pipe Whip Restraint in Each Unit Did Not Conform.Caused by Improper Design of Restraint.Architect & Owner Will Design Addl Restraint | | | 05000324/LER-1979-007, Forwards LER 79-007/01T-0 | Forwards LER 79-007/01T-0 | | | 05000325/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000325/LER-1979-008-03, /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown | /03L-0 on 790112:unacceptable Levels of Pump Differential Sys & Vibration Noted During Test of 1B Pump. Cause Unknown | | | 05000324/LER-1979-009-03, /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced | /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced | | | 05000324/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000325/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000325/LER-1979-010-03, /03L-0 on 790123:main Turbine Control Valve Response Time Test Failed to Meet Tech Spec Response Time. Caused by Slow Actuation Time on Installed Switch | /03L-0 on 790123:main Turbine Control Valve Response Time Test Failed to Meet Tech Spec Response Time. Caused by Slow Actuation Time on Installed Switch | | | 05000324/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000324/LER-1979-012-03, /03L-0 on 790219:Snubber 2-E11-89SS480 Was Fully Extended.Caused by Loose Pipe Clamp.Snubber & Clamp Were Repositioned & Bolted Into Place | /03L-0 on 790219:Snubber 2-E11-89SS480 Was Fully Extended.Caused by Loose Pipe Clamp.Snubber & Clamp Were Repositioned & Bolted Into Place | | | 05000324/LER-1979-013-03, /03L-0 on 790220:after Maint,Calibr on Suppression Pool Level Transmitter CAC-LT-2601 Found to Be 1/2 Inch Below Spec.Caused by Transmitter Being Out of Calibr. Instrument Recalibr | /03L-0 on 790220:after Maint,Calibr on Suppression Pool Level Transmitter CAC-LT-2601 Found to Be 1/2 Inch Below Spec.Caused by Transmitter Being Out of Calibr. Instrument Recalibr | | | 05000324/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000325/LER-1979-014-03, /03L-0 on 790519:operator Noted Containment Atmosphere Dilution Less than 4,350.Caused by Frozen Pressure Control Valve.Regulator on Pressure Control Valve Adjusted | /03L-0 on 790519:operator Noted Containment Atmosphere Dilution Less than 4,350.Caused by Frozen Pressure Control Valve.Regulator on Pressure Control Valve Adjusted | | | 05000325/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000325/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000325/LER-1979-017-03, /03L-0 on 790417:while Auxiliary Operator Was Hanging Clearance on RHR Pumps 2A & 2C,control Operator Noticed Pumps Were Still Energized.Caused by Clearance Listing Unit 1 Instead of Unit 2.Clearance Was Corrected | /03L-0 on 790417:while Auxiliary Operator Was Hanging Clearance on RHR Pumps 2A & 2C,control Operator Noticed Pumps Were Still Energized.Caused by Clearance Listing Unit 1 Instead of Unit 2.Clearance Was Corrected | | | 05000325/LER-1979-018, Forwards LER 79-018/03X-1 | Forwards LER 79-018/03X-1 | | | 05000325/LER-1979-018-03, /03X-1 on 790414:main Steam Relief Valve 1B21-F013J Opened at 520 Psi During Plant Startup.Valve Immediately Reseated.Possible Cause May Be Excessive Pilot or Second Stage Seat Leakage | /03X-1 on 790414:main Steam Relief Valve 1B21-F013J Opened at 520 Psi During Plant Startup.Valve Immediately Reseated.Possible Cause May Be Excessive Pilot or Second Stage Seat Leakage | | | 05000325/LER-1979-019-03, /03L-0 on 790520:operator Noted Recorder 1-CAC-TR-1258 for Printing Containment Pressure Was Not Working.Caused by Burned Gould Part TF255-C-C & Stuck Contacts in K-3 Relay.Relay Replaced | /03L-0 on 790520:operator Noted Recorder 1-CAC-TR-1258 for Printing Containment Pressure Was Not Working.Caused by Burned Gould Part TF255-C-C & Stuck Contacts in K-3 Relay.Relay Replaced | | | 05000325/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000324/LER-1979-021-03, /03L-0 on 790702:steam Line Snubber,Pump Suction Snubber & Main Steam Relief Smubbers Found Inoperable. Caused by Seal Failure.Snubbers Rebuilt,Functionally Tested & Reinstalled | /03L-0 on 790702:steam Line Snubber,Pump Suction Snubber & Main Steam Relief Smubbers Found Inoperable. Caused by Seal Failure.Snubbers Rebuilt,Functionally Tested & Reinstalled | | | 05000324/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000325/LER-1979-022-03, /03L-0 on 790723:linear Heat Generation Rate Found to Be 0.29 Kw/Ft Above Limit During Daily Core Parameter Check After Reaching 99% Power.Caused by Faulty Computer Reading.After Evaluation 1-3% Power Derate Imposed | /03L-0 on 790723:linear Heat Generation Rate Found to Be 0.29 Kw/Ft Above Limit During Daily Core Parameter Check After Reaching 99% Power.Caused by Faulty Computer Reading.After Evaluation 1-3% Power Derate Imposed | | | 05000325/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | |
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