05000272/LER-1981-014-03, /03L-0:on 810201,centrifugal Charging Pump 12 Declared Inoperable.Caused by Loss of Oil Overheating Thrust Bearing & Partially Wiping Main Bearing.Bearings Replaced, Oil Reservoir & All Bearing Housing & Oil Lines Flushed

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/03L-0:on 810201,centrifugal Charging Pump 12 Declared Inoperable.Caused by Loss of Oil Overheating Thrust Bearing & Partially Wiping Main Bearing.Bearings Replaced, Oil Reservoir & All Bearing Housing & Oil Lines Flushed
ML18085A931
Person / Time
Site: Salem 
Issue date: 02/19/1981
From: Steele W
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18085A930 List:
References
LER-81-014-03L, LER-81-14-3L, NUDOCS 8102270715
Download: ML18085A931 (3)


LER-1981-014, /03L-0:on 810201,centrifugal Charging Pump 12 Declared Inoperable.Caused by Loss of Oil Overheating Thrust Bearing & Partially Wiping Main Bearing.Bearings Replaced, Oil Reservoir & All Bearing Housing & Oil Lines Flushed
Event date:
Report date:
2721981014R03 - NRC Website

text

NRC FORM 366 (7-771 w. w. r*vw~._,.,,, ***~.....--.. ---*.. --*******-*-*-

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REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

[]JI] f During normal operation on 2/1/81, the #12 Centrifugal Charging Pump was declared

[)))) I inoperable because of oil leakage.

Action Statement 3.5.2.a was entered at 1700

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42 43 44 47 IJ))J I Loss of oil caused the thrust bearing to overheat and the main bearing to partially

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The bearings were replaced.

The oil reservoir, all bearing housings and all oil lines were cleaned and flushed.

A satisfactory surveillance test was performed IJ))] I and the Action Statement was terminated at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on 2/3/81.

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Repott Number:

81-14/03L Report Date:

February 19, 1981 Occurrence Date:

2/01/81 Facility:

Salem Generating Station, Unit 1 Public Service Electric and Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Inoperable ECCS System -

No. 12 Centrifugal Charging Pump CONDITIONS PRIOR TO OCCURRENCE:

Mode 1 -

Rx Power 25% - Unit Load 260 MW DESCRIPTION OF OCCURRENCE:

During normal operation on February 1, 1981, the No. 12 Centrifugal Charging Pump was declared inoperable because of oil leakage.

Action Statement 3.5.2.a was entered at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br /> which requires that an inoperable ECCS subsystem must be made operable within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

This occurrence con-stituted operation in a degraded mode IAW Technical Specification 6.9.1.9.b.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Equipment Failure Oil seals were leaking.

ANALYSIS OF OCCURRENCE:

Loss of oil caused the thrust bearing to overheat and the main bearings to partially wipe.

CORRECTIVE ACTION

The main bearings and thrust bearings were replaced.

All oil lines were cleaned and flushed.

The oil reservoir and all bearing housings were also cleaned and flushed.

A satisfactory surveillance test was performed and the Action Statement was terminated at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on February 3, 1981.

FAILURE DATA:

Pacific Pump -

Model RLlJ-2-1/2"- Serial No. B46617 Part #552 - Stationary Oil Baffle (Inner Bearing) -

Two Replaced Part #

7 - Deflector Ring -

One Replaced

LER 8-l-14/03L Part # 63 Part # 51 Part # 48 Bearing Sleeve Bearing Sleeve Stationary Oil Replaced 2 -

February 19, 1981 Radial -

One Replaced

- Thrust -

One Replaced Baff le (Outboard Bearing) Inner Seal -

One Part# 57 - Thrust Collar -_One Replaced Part #883 -

Oil Control Ring -

One Replaced One set of 12 Thrust Shoes replaced.

Prepared By W. J. Steele SORC Meeting No.

.81-09