05000272/LER-1980-038-03, /03L-0:on 800626,during Routine Insp,Svc Water Found in Charging Pump 12 Lube Oil Reservoir.Pump Declared Inoperable.Caused by Leak in Lube Oil Cooler Due to Tube Failure.Cooler Replaced & Tested Satisfactorily

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/03L-0:on 800626,during Routine Insp,Svc Water Found in Charging Pump 12 Lube Oil Reservoir.Pump Declared Inoperable.Caused by Leak in Lube Oil Cooler Due to Tube Failure.Cooler Replaced & Tested Satisfactorily
ML18082A802
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/23/1980
From: Murphy M
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18082A801 List:
References
LER-80-038-03L, LER-80-38-3L, NUDOCS 8007290844
Download: ML18082A802 (1)


LER-1980-038, /03L-0:on 800626,during Routine Insp,Svc Water Found in Charging Pump 12 Lube Oil Reservoir.Pump Declared Inoperable.Caused by Leak in Lube Oil Cooler Due to Tube Failure.Cooler Replaced & Tested Satisfactorily
Event date:
Report date:
2721980038R03 - NRC Website

text

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((II] I At. oi'oo hours, during routine operation, it was discovered that service water was IIill

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in #12 Charging Pump lube oil reservoir.

The pump was declared inoperable and Action I Statement.3.5.2a was entered (76_;23, 77-34, 77-72, 79-68).

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(([)) I A leak developed in the lube oil cooler due to tube failure.

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replaced and tested satisfactorily.

The Action Statement was terminated at 1445 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.498225e-4 months <br /> on June 27, 1980.

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