|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
[Table view] |
Text
j. mj.~ms'i'Y ACCELERATED RIDS PROCESSING) l REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)'CCESSION NBR:9410050054 DOC.DATE: 94/09/29 NOTARIZED: NO DOCKET FACIL:50-260 Browns Ferry Nuclear Power Station, Unit 2, Tennessee 050002'60 AUTH. NAME AUTHOR AFFILIATION HSIEH,C.S. Tennessee Valley Authority MACHON,R.D.
RECIP-NAME
'ennessee Valley Authority RECIPIENT AFFILIATION
SUBJECT:
LER 94-006-00:on 940831,received alarms that indicated loss of Unit 2 ECCS instrumentation. Caused by random failure of ECCS division I, ATU inverter.ATU inverter was replaced by replacing shorted SCR.W/940929 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED-LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), ncident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-4-PD 1 1 WILLIAMS,J. 1 1 INTERNAL: ACRS 1 1 QO~ROAB/=DS~ 2 2 AEOD/SPD/RRAB 1 1 FIXATE CENTER 1 1 NRR/DE/EELB 1 1 /D EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRSS/PRPB 2 2 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 NRR/PMAS/IRCB-E 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL 'EG &G BRYCE i J H 2 2 L ST LOBBY WARD 1 1 NOAC MURPHY,G.A 1 1 NOAC POORE,W. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 BLAME NOTE TO ALL RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE iVASTE! CONTACI'THE DOCL'MENT CONTROL DESK. ROOKI Pl -37 (EXT. 504-2083 ) TO ELDIINATEYOI.'R PRO~I DISTRIBUTION LISTS I'OR DOCL'MENTS YOU DON"I'L'ED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF -COPIES REQUIRED: LTTR 27 ENCL 27
4>
f I
Tennessee Vattey Avthorlty.,Post Office Box 2000. Decatur, Atabama 35609-2000 R. D. (Rick) Machon Vice President, Browns Feny Mtctear Rant September 29, 1994 U.S. Nuclear Regulatory Commission 10 CFR 50.73 ATTN: Document Control Desk Washington, D.C. 20555
Dear Sir:
BROWNS FERRY NUCLEAR PLANT (BFN) - UNITS 1g 2p AND 3 - DOCKET NOS ~ 50-259~ 50-260'ND 296 - FACILITY OPERATING LICENSE DPR-33~ 52@ AND 68 - LICENSEE EVENT REPORT 50-260/94006 The enclosed report provides details concerning a loss of instrumentation input logic for the plant's Division I Emergency Core Cooling System caused by a fault (i.e., short) in the Analog Trip Unit inverter silicon controlled rectifier. The inverter supply breaker tripped as a result of the short.
The. report is submitted pursuant to 10 CFR 50.73(a)(2)(i)(B),
and 50.73(a)(2)(vii).Section VII of the enclosure describes the .commitment made in this report.
Sincerely, Site ce President Enclosure cc: See page 2 9410050054 94092'st PDR'DOCK 05000260 S PDR
4l U.S.,Nuclear Regulatory Commission Page 2 September 29, 1994 cc,(Enclosure):
INPO Records 'Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 Paul Krippner.
American Nuclear Insurers Town Center, Suite 300S:
29 South Main Street West Hartford, Connecticut 06107
,NRC Resident Inspector Browns Ferry Nuclear Plant
.Route 12, Box 637 Athens, Alabama 35611 Regional Administrator U.S. Nuclear Regulatory Commission Region 101 II Marietta Street, -NW, Suite 2900 Atlanta, Georgia 30323 Mr. J. F,. Williams, Project Manager U.S. Nuclear Regulatory Commission
'One White Flint, North 11555 Rockville Pike Rockville, Maryland '20852
1 4l
'I I
NRC FORM 366 U.S. NUCLEAR REGULATORY C(NIIISSION APPROVED BY (X(B NO. 3150-0104
,(5-92) EXPIRES 5/31/95 EST IHATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER) FORWARD COHHENTS REGARDING BURDEN ESTIMATE TO THE INFORHATION AND RECORDS MANAGEMENT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COHMISSIQN, (See reverse, for required number of digits/characters for each block) WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3140.0104), OFFICE OF MANAGEHENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAHE (1) DOCKET NINGIER (2) PAGE (3)
Browns Ferr Nuclear Plant BFN Unit 2 05000260 1 OF 6 TITLE (4) Entry into Technical Specification 1.C.1 due to a loss of Emergency Core Cooling System Division I instrumentation from a short in the Analog Trip Unit Inverter EVEN DATE 5 LER NINBER 6 REPORT DATE 7 OTHER FACILITIES INVOLVED 8 HONTH DAY YEAR YEAR SEQUENTIAL REVISION MOHTH DAY YEAR FACILITY NAHE N/A DOCKET NUHBER HUHBER NUMBER 08 31 '4 94 006 00 09 29 94 FACILITY NAME 'N/A DOCKET NUMBER OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR : Check one or mor e 11
,MCDE (9) N 20.402(b)- 20.C05(c) 50.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1)(i) 50.36(c)(1) 50.73(a>(2)(v) 73.71(c)
LEVEL (10) 93 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405(a)(1)(iii) 50.73(a)(2)(i)(B) 50.73(a)(2)(viii)(A) (Specify in 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50 '3(a)(2)(viii)(B) Abstract below and in Text,
'0.405(a)(1>(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) NRC Form 366A LICENSEE CONTACT FOR THIS LER 12 NAHE TELEPHONE HUHBER (Include Area Code)
Clare S. Hsieh, Compliance Engineer (205)729-2635 4 C(NPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13 REPORTABLE REPORTABLE CAUSE STSTEH COHPONENT MANUFACTURER CAUSE SYSTEH COMPONENT MANUFACTURER TO NPRDS TO NPRDS X AD SCR A080 N X AD. INVT N431 SUPPLEMENTAL REPORT EXPECTED 1C EXPECTED HONTH DAY YEAR YES SUBMISSION X
(I f yes, -conpiete. EXPECTED SUBHISSION DATE) ~
NO DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On August 31, 1994, at 1248 hours0.0144 days <br />0.347 hours <br />0.00206 weeks <br />4.74864e-4 months <br /> CDT, at approximately 93 percent power, control room operators received alarms that indicated a loss of Unit 2, Division I Emergency Core Cooling Systems (ECCS) instrumentation. The operators declared Division I of ECCS instrumentation inoperable and entered Technical Specification (TS) 1.C.1 (i.e., Standard TS 3.0.3) which requires that the UIIit be placed in Hot Standby within six hours and Cold Shutdown within 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />. Troubleshooting determined that the event was initiated from a shorted Silicon Controlled Rectifier (SCR) in the ECCS Division I, Analog Trip Unit (ATU) inveiter. The short caused the inverter supply breaker to trip, which resulted in a loss of power to the inverter and loss of input logic signals from the affected systems to the control room instrumentation. TVA determined the root cause to be a random failure of the, inverter. Contributing to the event is the ECCS ATU design which lends itself to the loss of an entire ECCS division from a single component failure. The ATU inverter was repaired by replacing the shorted SCR, and a search of previous similar events has not found any other incidents with the same root cause. TVA will evaluate the present design on the ECCS ATU power distribution to determine if design enhancements can be made.
NRC FORM (
- )
NRC FORH 366A U.S. NUCLEAR REGULATORY CQNIISS ION APPROVED BY (NS NO. 3150-0104 (5-92) EXPIRES. 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY UITH THIS INFORMATION COLLECTION REOUEST: 50.0 NRS. FORUARD COMHENTS REGARDING BURDEH ESTIMATE TO THE INFORMATION AND RECORDS MANAGEHENT LICENSEE EVENT REPORT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COMHISSION, TEXT CONTINUATION NASNINGTON, DC 20555-0001, AND TO THE PAPERlJORK REDUCTION PROJECT (3150 0104), OFFICE OF MANAGEHENT AND BUDGET, NASHINGTON DC 20503 FACILITY NAKE (1) DOCKET NlÃBER (2) LER NWSER (6) PAGE (3)
YEAR, SEQUENTIAL REVISION NUHBER NUMBER Browns Ferry Unit 2 05000260 94 006 00 2 of 6 TEXT If more s ce is r uired use edd tionsl co ies of NRC Form 366A (17)
Z ~ PLANT CONDZTIONS Unit 2 was in end-of-cycle coastdown at approximately 93 percent power (3080 megawatts thermal). Units 1 and 3 were shutdown and defueled.
ZI. DESCRIPTION OF EVENT A. Events On August 31, 1994, at 1248 hours0.0144 days <br />0.347 hours <br />0.00206 weeks <br />4.74864e-4 months <br /> Central Daylight Time (CDT), the Unit 2 Control Room operators received alarms that indicated a loss of Division I Instrumentation for the plant's Emergency Core Cooling System (ECCS). High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCZC) steam flow, reactor level and pressure, and drywell pressure input signals were lost to the instrumentation logic for the following ECCS subsystems:
~ HPCI [BJ]
~ RCIC [BN]
~ Core Spray (CS), Division I [BG]
~ Anticipated Transient Without Scram (ATWS), Division. I [JC]
~ Residual Heat Removal (RHR), Division I [BO]
~ Automatic Depressurization System (ADS),,Division I [JC]
Additionally, instrumentation which operates the suppression pool to Reactor Building Vacuum Breakers [VB] was rendered inoperable.
ECCS Division ZZ instrumentation remained operable and was available for initiation of both divisions of the affected systems with the exception of RCIC, which had also lost power to its flow controller. The event did not require plant operators to take any actions other than initiation of troubleshooting activities.
Plant operators declared the subsystems or division of subsystems inoperable. Because there was no single TS (Technical Specifications) Limiting Conditions for Operation (LCO) which enveloped the event, plant operators entered TS 1.C.1 (i.e.,
Standard TS 3.0.3). TS 1.C.l requires the unit be placed in Hot Standby within six hours and Cold Shutdown within 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
Il Qi NRC FORM 366A U.S. NUCLEAR REGULATORY LXSIIISSION APPROVED BY (NS NO 5150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEH PER RESPONSE TO COMPLY IJITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT LICENSEE EVENT REPORT SRANCH (MHBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, TEXT CONTINUATION WASHINGTON, DC 20555-0001, AHD TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON DC 20503 FACILITY NiULE (1) DOCKET NLNLSER (2) LER NLNBER (6) PAGE (3)
TEAR SEQUEN1'IAL REVISION NUMBER NUMBER Browne Ferry Unit 2 05000260 94 006 00 3 of 6 TEXT If more s ce is r uired use sdditionaL co ies of NRC Form 3 66A (17)
Troubleshooting of the ECCS Division I Instrumentation logic determined that the event was initi.ated from a short in the ECCS Division I, Analog Trip Unit (ATU) inverter Silicon Controlled
'ectifier (SCR). The short caused the inverter supply breaker to trip, resulting in a loss of power supply to the ATU inverter and loss of input logic signals from the affected systems to the control room instrumentation.
TVA repaired the inverter by replacing the shorted SCR and declared the associated instruments and systems operable at 1350 hours0.0156 days <br />0.375 hours <br />0.00223 weeks <br />5.13675e-4 months <br /> on August 31, 1994. TS 1.C.1 was exited before having to initiate actions required to achieve Hot Standby.
TVA determined this event to be reportable pursuant to 10 CFR 50.73(a),(2)(i)(B) as a condition prohibited by TS due to entry into TS 1.C.l. Additionally, this event is reportable in accordance with 10 CFR 50.73(a)(2)(vii) as any event where a single cause or condition caused at least one independent train or channel to become inoperable in multiple systems.
B. Zno erable Structures Com onents or S stems that, Contributed to the Event!
None.
C. Dates and A roximate Times of Ma or Occurrences:
August 31, 1994 at 1248 CDT Division I ECCS Instrumentation was lost due to a short in the ATU inverter SCRI LCO 1.C.1 was entered.
1336 CDT The ATU inverter was repaired; Division I ECCS ATU inverter was reeneigized.
1350 CDT Associated instruments and systems were declared operable; LCO 1.C.1 was exited.
NRC FORH 366A U. S NUCLEAR REGULATORY CQIIISS I ON APPROVED BY (HBI" NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY llITH THIS INFORHATIOII COLLECTION REQUEST: 50.0 HRS ~ FORWARD COHHENTS REGARDING BURDEN 'ESTIHATE TO THE INFORNATION AND RECORDS HANAGEHEHT LICENSEE EVENT REPORT BRANCH (HNBB 7714), U.S. 'NUCLEAR REGULATORY COHHISSION, TEXT CONTINUATION WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF NANAGEHEHT AND 'BUDGET,
'WASHINGTON, DC 20503 FACILITY NAHE (1) DOCKET NINBER (2) LER NLSSER (6) PAGE (3)
YEAR SEQUEHT IAL REVI SI OH HUNGER HUNGER Browns Ferry Unit 2 05000260 94 006 00 4 of 6 TEXT If more s ce is r ired use additions( co ies of NRC Form 366A (17)
DE Other S stems or Seconda Functions Affected'one.
E. Method of Discove This event was immediately discovered at 1248 hours0.0144 days <br />0.347 hours <br />0.00206 weeks <br />4.74864e-4 months <br /> on August 31, 1994, when control room alarms indicated ECCS Division I instrumentation problems. Primary among the alarms received was the ECCS ATU Trouble Alarm.
F. 0 erator Actions:
There were no TS safety system initiations required of control room operators. The steps taken to identify the problem and initiate maintenance actions were appropriate.
- 0. Safet S stem Res onses:
None.
ZIZZ CAUSE OF THE EVENT A. Immediate Cause:
The immediate cause of the event was due to a short in the SCR of the ECCS Division I, ATU .inverter.
B. Root Cause:.
'TVA determined that the root cause was a random failure of the ECCS Division I, ATU inverter. The short in the ATU inverter SCR caused the inverter supply breaker to trip.
C. Contributin Factors:
The design of the ECCS ATU power supply system lends itself to the loss of an entire division of ECCS instrumentation from a single component failure.
,Each ECCS ATU power distribution panel is fed from a 250 VDC reactor motor-operated-valve board through an ATU inverter to two 24 VDC redundant power supplies. This inverter is a single failure point. The loss of an ATU inverter results in the loss of an entire division of ECCS instrumentation.
i( i V
NRC FORM 366A U.S. NUCLEAR REGULATORY C(HBIISSIOH APPROVED BY (NS NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY llITH THIS REQUEST: 50.0 HRS.
INFORMATION'OLLECTION FORHARD COMMENTS REGARDIHG BURDEH ESTIMATE TO THE INFORMATION AHD RECORDS MANAGEMENT LICENSEE EVENT .REPORT BRANCH (MHBB 7714), U.S. NUCLEAR REGULATORY COMMISSION/
TEXT CONTINUATZON NASHINGTON, DC 20555-0001, AND TO THE PAPERNORK REDUCTION (3150-0104), OFFICE OF MANAGEMENT AHD BUDGET, 'ROJECT HASHINGTON, DC 20503 FACILITY NAME (1) DOCKET NLBIBER (2) LER IRNBER (6) PAGE (3)
YEAR SEQUENTIAL 'EVISION NUMBER NUMBER Browns Ferry Uni.t 2 05000260 94 006 00 5 of 6 TEXT If more s ce >s r uired use additions( co ies of HRC Form 3 66A (17)
IV. ANALYSIS OF THE EVENT This event did not result in any plant transient described in the BFN FS&, Chapter 14 accident analyses nor did health and safety of plant personnel or the public.
it adversely affect the The short in the ECCS 'Division I, ATU inverter SCR caused the inverter supply breaker to trip, resulting in a loss of power supply to the inverter and loss of RCIC and HPCI steam flow, reactor level and pressure, and drywell pressure input signals from the HPCI, RCIC, CS, RHRg ATWS ADS, and vacuum breakers to their respective i.nstrumentati.on
~
logic systems. However, Division ZI instruments remained operable during the event and were available to Control Room operators for initiation of both divisions. The rel'iabi.lity and redundancy of the controls and instrumentation for the ECCS ensure that no failure of a single initiating sensor would either prevent or falsely start the initiation of these cooling systems. Additionally, no single control failure prevents the combined cooling systems from providing the core with adequate cooling.
V . CORRECTIVE ACTIONS A. Immediate Corrective Actions:
TVA repaired the ECCS Division I, ATU inverter by replacing the shorted SCR in the inverter.
B. Corrective Actions ta Prevent Recurrencel A search of TVA trending databases has not found any other previous SCR failures. Thus, TVA considers this failure to be a random event. Preventive Maintenance (PM) inspections are currently performed on the ATU inverter in accordance with vendor recommended guidelines. These PM inspecti:ons include calibration of the meters, cleaning of the inverter internals, maintenance of the circuit breakers, insulation testing of the transformer and inductor coi.ls, and visual inspections of the inverter components.
Additionally, the electrolytic capacitors of the inverter are replaced periodically.
Since this event affected an entire division of ECCS instrumentation from the loss of an ATU inverter, TVA will evaluate the present design of the ECCS ATU power distribution to determine i.f design enhancements can be made.
l C
4l gi L
II
/ ~
~,
NRC FAtH 3t4h U.S. NUCLEAR REGULATORY CDIIISSION APPROVED BY (HEI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY MITH THIS INFORMATION COLLECTIOH RE(tUEST: 50.0 HRS. FORNARD COHHEHTS REGARDING BURDEH EST IHATE TO THE IHFORHATIOH AND RECORDS HANAGEHENT LICENSEE EVENT REPORT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, TEXT CONTINUATZON llASHINGTOH, DC 20555-0001, AND TO THE PAPERNORK REDUCTION PROJECT (3150 0104) ~ OFFICE OF HANAGENEHT AND BUDGET ~
'WASHINGTOH DC 20503 FACILITY NAHE (1) DOCKET NIHIBER (2) LER NIMBER (6) PACE (3)
YEAR SEQUENTIAL REVI SIOH NUHBER HUNGER
'Browns Ferry Unit 2 05000260 94 006 00 6 of 6 TEXT If more s ce is r ired use edditionet co ies of NRC Form 366A (17)
VIE ADDITIONAL INFORMATION Ar Failed Com onentsI
~ SCR, 1 kV, 68 Amp, 15 microsecond, Part No. TD42F1000, Manufactured by AEG-Telefunken
~ ATU Znverter, Part No. 6841310, Manufactured by HDR Power Systems, Znc.
B. Previous LERs on Similar Events:
TVA has reviewed previous BFN LERs to determine have occurred. There have been previous LERs involving the loss if similar events of an ECCS ATU inverter (i e LERs 260/83028 260/83034@
~
260/94001). However, none of the previous LERs resulted from a shorted SCR.
VII. Commitments
+A will evaluate the present design on the ECCS ATU power distribution to determine if design enhancements can be made. This evaluation will be completed by November 30, 1994.
Energy Industry Identification, System (EIIS) system and component codes are identified in the text with brackets (e.g., (XX]).
Oi
'I fy