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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
[Table view] |
Text
ACCESSION NBR:9304260154 DOC.DATE: 93/04/22 NOTARIZED: NO DOCKET FACZL,50-260 Browns Ferry Nuclear Power Station, Unit 2, Tennessee 05000260
'AUTH. NAME AUTHOR .AFFILIATION HSIEH,C.S.'ennessee Valley Authority ZERINGUE,O.J. Tennessee Valley Authority RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 93-003-00:on 930323,main steam safety/relief valves exceeded TS setpint limits to open as result of disc/seat bonding.MSRVs will be replaced w/recertified Target Rock safety/relief valves from Unit 3.W/930422 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR i ENCL SIZE: /
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident pt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT 'COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-4 1 1 HEBDON,F 1 1 ROSS,T. 1 1 INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 NRR-.DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 EG XKE 02 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG!EG BRYCEPJ.H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHYPG.A 1 1' NSIC POOREPW. 1 1 NUDOCS FULL TXT 1 4QTE TQ ALL "R!DS" REC!?/EH~I ASE:-: .' US TQ REDUCE 'Pi.~STE! CONTACT T!!E DQCU'lE.iT CONTROL DESi.
RQQ!!? I-S"i (EX .. 5~'.-20o5) TQ E';! 'tiN.q. > QUR NA,".>E: RQ!! D!STR.oUTiQY L STS I QR DQCU~!" YQU DQi>'T FEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 .ENCL 32
Il 0 Tennessee Valley Authority, Post Dlfice Box 2000. Decatur, Alabama 35609.2000 O. J. "Ike'eringue Vice President, Browne Ferry Nuclear Plant APR 22 1993 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555
Dear Sir:
TVA BROWNS FERRY NUCLEAR PLANT (BFN) UNITS 1, 2, AND 3 DOCKET NOS ~ 50-259, 260, AND 296 FACILITY OPERATING LICENSE DPR-33, 52, AND 68 LICENSEE EVENT REPORT LER'0-260/93003 The enclosed report provides details concerning main steam safety/relief valves exceeding the technical specifications setpoint limit during bench
-testing.
This report is submitted in accordance with 10 CFR 50.73(a)(2)(i)(B).
Sincerely,
( J.I Zeringueu~if(k'.
Enclosure cc: See page 2 26i"OJ'v 9304260i54 930422 PDR ADOCK. 05000260
~age 8 PDR I(
0
." U.S. Nuclear Regulatory Commission cc (Enclosure):
INFO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, Georgia 30339 Paul Krippner American Nuclear Insurers Town Center, Suite 300S 29 South Main Street West Hartford, Connecticut 06107 NRC Resident Inspector Browns Ferry Nuclear Plant Route 12, P.O. Box 637 Athens, Alabama 35609-2000 Regional Administrator U.S. Nuclear Regulatory Commi'ssion Region II 101 Marietta Street, Suite 2900 Atlanta, Georgia 30323 Thierry M. Ross U.S. Nuclear Regulatory Commission One White Flint, North 11555. Rockville Pike Rockville, Maryland 20852
0 0 NRC Form 366 . NUCLEAR REGULATORY COMMISSION Approved OHB No. 3150-0104 (6-89) Expires 4/30/92 LICENSEE EVENT REPORT (LER)
FACILITY NAME (1) iDOCKET 'NUMBER (2) (
wn Fr FN ni TITLE (4) Main Steam Safety/Relief Valves Exceeded the Technical Specifications Setpoint Limit to Open as Result f Di in V N I. I I ISEqUENTIAL I IREVISIONI I I I FACILITY NAHES ]DOCKET NUHBER(S)
I Y Y Y A
~l l OPERATING I
I I
'ITHIS I
REPORT I
IS SUBMITTED I I I I I I PURSUANT TO THE RE()UIREHENTS OF 10 CFR fl 5:
HODE I I mr h i l20.402(b) l20.405(c) ,) [50.73(a)(2)(iv) 173.71(b)
POMER (20.405(a)( 1)(i) (50.36(c)( 1) ) [50.73(a)(2)(v) (73.71(c)
LEVEL )20.405(a)( l)(ii) (50.36(c)(2) ) [50.73(a)(2)(vii) )OTHER (Specify in (20".405(a)( 1)(i ii ) (50.73(a)(2)(i)(B)) [50.73(a)(2)(viii)(A) Abstract below and in
) l20.405(a)( 1)(iv) (50.73(a)(2)(ii) ( (50.73(a)(2)(viii)(B) Text, NRC Form 366A)
.4 1 v TH NAME I AREA CODE I H i MP T R A P N iREPORTABLEt I I I IREPORTABLEI I I P NT HAN T I I V T I I NT P T 14 EXPECTED I T I I SUBMISSION I .I I T 0 M T 1 Y 1 P ABSTRACT (Limit to 1400 spaces, i.e., approximately fifteen single-space typewritten lines) (16)
On March 23, 1993, TVA was notified that of the first six of the thirteen Unit 2 main steam safety/relief valves bench-tested at Wyle Laboratories five failed the setpoint test acceptance criteria. On March 26, 1993, 'with the testing of all thirteen Unit 2 main steam safety/relief valves completed, a total of eleven valves had failed to open within one-percent of their setpoints. This event is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by the plant's technical specifications.
The apparent cause was corrosion bonding of the valve pilot disc/seat interface resulting in an upward setpoint drift. This bonding resulted in an increase in the valve opening pressure due to the need for additional opening force above the setpoint value. Corrosion is be'i'ng attributed to radiologically produced oxygen
~
collecting at the disc/seat interface.
TVA plans to use the Unit 2 main steam safety/relief valves on Unit 3. The out-of-tolerance valves will .be refurbished, retested, and recert'ified prior to the startup of Unit 3 cycle 6 The Unit 2 main steam safety/relief valves will be
~
replaced with the recertified, safety/relief valves from Unit 3 prior to the restart of Unit 2 from its current cycle 6 refueling outage.
TVA will continue to participate in BWROG's Evaluation on the long term solution concerning the SRV setpoint drift problem.
NRC Form 366(6-89)
0 V,
NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OHB No. 3150-0104 (6-89) Expires 4/30/92 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME '(1) )DOCKET NUHBER (2)
I' I I I I SE()UEN TIAL I I REVISION I I I Browns Ferry Unit 2 I A N H I I I I TEXT (If more space is required, use additional NRC Form 366A's) (17)
PLANT CONDITIONS Browns Ferry Units 1, 2, and 3 were shutdown and in a defueled condition. Unit 2 was in a refueling outage with all of its main steam [SB] safety/relief valves (SRVs) [RV] removed for testing and recertification by Wyle Laboratories.
II- DESCRIPTION OF EVENT A. jb~rt:
On March,23, 1993, TVA was notified by Wyle Laboratories that the results of bench-testing the first six of the thirteen Unit,2 main steam SRVs (Target Rock Two-Stage SRV Model No. 7576F) showed five SRVs failed the setpoint -test acceptance criteria. On March 26, 1993, with the testing of the remaining seven main steam SRVs completed, an additional six valves failed. Altogether, eleven valves failed to open within one-percent of their setpoints.
Technical Specifications (TS) 4.6.D.1 requires that approximately one-half of al'1 SRVs be bench checked or replaced with a bench checked valve each operating cycle (normally every 18 to 24 months). During the current Unit 2 refueling outage, the thirteen SRVs in the Unit 2 nuclear system pressure relief system were removed and shipped to Wyle Laboratories for testing and recertification.
Wyle Laboratories informed TVA that only two opened within the TS (2.2.A)'imit of +/- one-percent (11 psig) setpoint tolerance.
Nine valves opened at pressures outside the one-percent setpoint tolerance limit. Two completely failed to open with testing pressure ramped to 1250 psig nuclear system design pressure.
Also, one valve was found leaking excessively. The attachment to this LER provides specific data of the SRV test results.
NRC Form 366(6-89)
0 NRC Form 366A U.S. NUCLEAR REGULATORY COHHISSION Approved OHB No. 3150-0104 (6-89) Expires 4/30/92 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAHE (1) IDOCKET NUHBER (2)
I (SEQUENTIAL / )REVISION/
Browns Ferry Unit 2 I ] I I I I 0
TEXT (If more space is required, use additiona1 NRC Form 366A's) (17) reported this in accordance with 10 CFR '50.72(b)(2)(i) as a condition, found while the reactor is shutdown that, had it been TVA found while'he reactor was in operation, would have resulted in the nuclear power plant, including its principal safety barriers, being in an unalyzed condition that significantl'y compromises plant safety and 10 CFR 50.72(b)(2)(iii) as a condition that alone could have prevented the fulfillment of the safety function of the structure or systems required to control the release of radioactive material. However, after further evaluation, TVA is reporting this event in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by the plant's TS.
B. Ja~~b t t t t t t t t t t~~gt:
None.
C.
March 23, 1993 Wyle Laboratories notified TVA of the SRV test results.
March 23, 1993 at 1630 TVA made a four-hour nonemergency hours CST notification,to NRC in accordance with 10 CFR 50.72(b)(2)(i) and 10 CFR 50.72(b)(2)(iii).
March 26, 1993 Wyle Laboratories completed SRVs bench tests and reported additional SRV failures.
D. th None.
E. t The deviations of SRV pressure setpoints were identified during the scheduled performance of valve bench testing at Wyle Laboratories in Huntsville, Alabama.
None.
NRC Form. 366(6-89)
0 NRC Form 366A U.S. NUCLEAR REGULATORY COHHISSION Approved OHB No. 3150-0104 (6-89) Expires 4/30/92 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAHE (1) IDOCKET NUHBER (2) 3 I I I I SEQUENTIAL I IREVISIONI I I I I Browns Ferry Uni t 2 I. NH 4 F TEXT (If more space is required, use additional NRC Form 366A's) (17)
G t t None.
III CAUSE OF THE EVENT
&mc5ixQt~QQK" The immediate cause of this event was the deviation of relief valve setpoints outside the testing setpoint limit of +/-
one-percent tolerance.
B. t The apparent cause of this event is corrosion bonding of Target Rock two-stage SRV pilot disc/seat interface. The bonding results in an upward setpoint drift (except for valves 1-31 and 1-42 which had a -2.1 percent and +2.0 percent deviation, respectively, that may have been due to a normal mechanical dri'ft problem for "inservice" valves). Corrosion bonding causes an increase in the SRV opening pressure due to the need for additional opening force above the setpoint value.
Corrosion is being attributed to radiologically produced oxygen collecting at the valve pilot disc/seat interface. For repeated actuation of each individual valve, the test data shows general trend in decreasing pressure relief setpoints required to induce relief valve actuation. This is consistent with that which has been seen in the past with corrosion bonding in other SRV pilot valve failures.
C.
None.
NRC Form 366(6-89)
0 NRC Form 366A U.S: NUCLEAR REGULATORY COHHISSION Approved OHB No. 3150-0104 (6-89) Expires 4/30/92.
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAHE (1) iOOCKET NUHBER (2) H I / SE()UENTIAL i /REVISIONS Browns Ferry Unit 2 I I I I I TEXT (If more space is required, use additiona1 NRC Form 366A's) (17)
'V.
ANALYSIS 'OF THE EVENT There are thirteen main steam relief valves (MSRVs) on the main steam piping which perform the safety/relief function for the primary reactor system. Each valve is designed to open at, a pressure sensed in the valve body of 1105, 1115, or 1125 psig providing a safety/relief function. Each MSRV also has a pneumatic operator which allows for remote manual action of the valve. Six of these valves serve as Automatic Depressurization System (ADS) valves and can be remotel'y actuated (via the pneumatic operator) by emergency core cooling system .logic in the event of a loss of coolant accident in which high pressure makeup is inadequate. The manual and ADS actuation of the valves was not affected.
The safety/relief function of the MSRVs is to limit primary reactor system pressure to <1375 psig in the event of a pressurization transient resulting from a turbine trip or a main steam isolation
~alve (MSIV) closure. The cycle specific limiting pressurization transient analysis for Unit 2 cycle 6 (MSIV closure with flux scram) was reperformed assuming a spectrum of MSRV failures and setpoint drifts. The bounding case assumed four inoperable (i.e., completely failed to open) MSRVs with the remainder operating ten percent above setpoint. TVA's analysis conservatively shows that had this limiting design basis transient occurred, the .primary reactor system pressure would not have exceeded 1355 psig. This is within the safety limit of 1375 psig given in TS section 1.2.A (i.e., ten percent over vessel design of 1250 psig and twenty percent over piping design of 1148 psig.) Therefore, the plant and the public safety would not have been adversely affected and the 'safety of plant personnel was not compromised.
V. CORRECTIVE ACTIONS A. V
,Since TVA plans to use the Unit 2 MSRVs on Unit 3, there are no immediate corrective actions to refurbish/recertify the.
out-of-tolerance valves during the present, Unit 2 refueling outage. Instead, the eleven out-of-tolerance Target Rock valves will be 'refurbished, retested, and recertified prior replaced to the startup of Unit 3 cycle 6. The Unit 2 MSRVs will be with the recertified Target Rock safety/relief valves from Unit 3.
This replacement will be completed prior to the restart of Unit 2 from its current cycle 6 refueling outage.
NRC Form 366(6-89),
0 NRC,Form 366A U.S. NUCLEAR REGULATORY CONHISSION Approved OHB No. 3150-0104 (6-89) Expires 4/30/92 LICENSEE EVENT REPORT (LER)
TEXT 'ONTINUATION FACILITY NAME (1)
Browns Ferry Uni t 2' I I I ISEqUENTIAL I
~
IREVISIONi I I I I TEXT (If more space is required', use additional NRC Form 366A's) (17)
B. r tv t t Setpoint drift of this type: SRV is being investigated by the Boiling Water Reactor Owners'roup (BWROG) SRV Drift 'Fix Development Committee and the manufacturer, Target Rock Corporation. The setpoint drift is' generic concern experienced by all utilities using this brand of SRV in boiling water reactors.
TVA is presently evaluating the Committee's recommendation of replacing the existing Stellite 6B pilot disc with a 0.3 percent platinum alloyed Stellite or installing'everal parts 'in the pilot disc/seat area with catalyst plated platinum alloy to act as a recombi'ner of excess oxygen, thereby reducing the oxygen available for corrosion. In addition, TVA is also reviewing the use of redundant pressure switches/transmitters that would'ontrol the opening of the SRUs.
VI. ADDITIONAL INFORMATION Target Rock Two-Stage SRUs Model No., 7567F.
B. v Since the early 1980s, TVA has tested SRVs at Wyle Laboratories and .received data that indicated Target Rock SRVs failed to open within the allowable range of the as-found set pressure. TVA has previously issued several LERs concerning MSRVs setpoint,drift due to disc/seat corrosion bonding. At the present time, both BWR owners'roup and the valve manufacturer are actively pursuing corrective actions for the disc/seat corrosion bonding problem.
Either corrective actions previously discussed should help toward decreasing future setpoint deviation problem on the SRVs.
NRC Form 366(6-89)
0 lh NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104'xpires (6-89) 4/30/92 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) 100CKET NUMBER (2)
I I I SEQUENTIAL I (REVISION)
Browns Ferry Uni t 2 I Y I I I I TEXT (If more space is required, use additional NRC Form 366A's)'17),
VII. COMMITMENTS
- 1. TVA will have the eleven out-of-tolerance Target Rock SRVs refurbished, retested and recertified prior to the startup of Unit 3 cycle 6..
- 2. TVA will replace the Unit,2 NSRVs with the recertified Target Rock safety/relief valves from, Unit 3 prior to the restart of Unit 2 from its current.,cycle 6 refueling outage.
- 3. TVA will continue to participate in BWROG's Evaluation on the long term solution concerning the SRV setpoint drift problem.
Energy Industry Identification System '(EIIS) codes are identified'n the text as [XX].
NRC Form 366(6-89)
0 NRC Form 366A U.ST NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (6-89) Expires 4/30/92 LICENSEE EVENT 'REPORT (LER)
TEXT CONTINUATION FACILITY NAHE (1) IDOCKET NUMBER (2)
I I I, I SEQUENTIAL I IREVISION I I I I I Browns Ferry Unit 2 I I I I I TEXT (If more space is required, use additional NRC Form 366A's) (17)
ATTACHMENT TO LER 260/93003 Valve Valve As Found Setpoint Pressure Deviation Cartridge ID (psig) .(psig)
SLH 1014 1-80 1185 1125 +5.3X 1117 -0.71K 1114 -0.98K 1015 1-41 1180 1125 +4.9X 1138 +1.15K 1135 +0. 9X 1134 +0.8X 1132 +0.6X 1016 1-4 1172 1125 +4.2X 1149 +2.1X 1138 +1.15K 1020, 1-31 ADS 1082 1105 -2.1X 1076 -2.6X 1074 -2.
8'>12.1X 1021 1-5 ADS did not '1115 open at 1250 1022 1-19 ADS did not 1105 +>13.1X open at 1250 1026 1-179 1136 1125 +0.98K 1128 +0. 26'X 1123 -'0. 18K 1028 1-30 'ADS 1194 111'5 +7.1X 1143 +2 'X 1130 +1.3X 1126 +0.99K 1131 +1.4X 1118 +0.27K 1110 -0.45K 1111 -0.36K NRC Form 366(6-89)
0 NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (6-89) Expires 4/30/92 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION IOOCKET NUMBER (2)
I I I I SEQUENTIAL I I REV IS ION I I I I I Browns Ferry Unit 2' lx I I I I I.alalol TEXT (If more space is required, use additional NRC Form 366A's) (17) 1031 1-23 1168 1105 +5. 7X 1110 +0. 5't, 1117 +1.1X 1120 +1.36K 1'104 -0.1X 1103 -0 1 8'Fo
~
1098 -0.63K 1032 1-42 1148 1125 +2.0X 1162 +3.3X 1137 +1.07K 1033 1-34 ADS 1250 1105 (severe leak) +13.1X 1145 +3.6X 1133 +2.5X 1076 1-22 ADS 1108 1115 -0.63K 1106 -0.81K 1110 -0.45K 1079 1-18 1176 1115 +5.
5'0.18K 1117 1112 -0.27K 1114 -0.09K NRC Form'366(6-89)