ML20024E160

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LER 83-098/03L-0:on 830625,position of Valve Indeterminate Due to Dual Status Indication for Suppression pool-to- Drywell Vacuum Breaker.Caused by Insufficient Limit Switch Plunger Position.Limit Switches adjusted.W/830725 Ltr
ML20024E160
Person / Time
Site: Susquehanna Talen Energy icon.png
Issue date: 07/25/1983
From: Keiser H, Kuczynski L
PENNSYLVANIA POWER & LIGHT CO.
To: Murley T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
LER-83-098-03L, LER-83-98-3L, PLA-1761, NUDOCS 8308090324
Download: ML20024E160 (2)


Text

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EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h IOl2llDuring the performance of a routinely scheduled 31-day surveillance, a dual status l 1013 l l indication for one suppression pool-to-drywell vacuum breakers caused the position l l o l4 l l of the valve to be indeterminate. Since the remaining nine vacuum breakers tested l 10 l5 l l satisfactorily and were available for service, there was minimal impact to the l l 0 l 6 l l health and safety of the general public. l lol7ll l lo18Il '

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.. .4 .. 7 4. et .. 4. .4 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l 110 I h causes of the dual indic ation were an insufficient limit switch plunger posit- l l 1 l 1 l lion and an out-of-adjustment rotary switch contact cam. Both h : switches were l l 112 l l adjusted to provide proper control room indication. The surveillance test was re-l

! 1 I 3 l lpeated. and all valves tested satisfactorily. No further actions are planned. l liI4Il I STAT S  % POW E R OTNER ST Atus isCOVERY DISCOVE R Y D E SCRIPTION l 1 l 5. l.l C l @ l 0 l 0 l Ol@l NA l lBl@l Operator observation l

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N AME OF PREPARER L.A. Kuczynski PHONE:(717)S42-2181 Ex. 3759

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PP&L Pennsylvania Power & Light Company Two North Ninth Street

  • Allentown, PA 18101 = 2151770L5151 July 25, 1983 Dr. Thomas E. Murley Regional Administrator, Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA 19406 SUSQUEHANNA STEAM ELECTRIC STATION LICENSEE EVENT REPORT 83-098/03L-0 ER 100450 FILE 841-23 PLA-1761

Dear Dr. Murley:

Attached is Licensee Event Report No. 83-098/03L-0. This event was determined to be reportable per Technical Specification 6.9.1.9.b, in that, with the unit in Operational Condition 3, one of the suppression pool-to-drywell vacuum breakers was considered inoperable based on dual status indicetion (simultaneous open and closed position indication) in the main control room, f

H.W. Keiser Superintendent of Plant-Susquehanna LAK/pjg cc: G.G. Rhoads Resident Inspector U.S. Nuclear Regulatory Commission P.O. Box 52 Shickshinny, PA 18655 Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555 T

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