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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
ACCELERATED DISTMBUTION DEMONSTRATION SYSTEM
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REGULATORY INFORMATION DISTRXBUTION SYSTEM (RIDS)
ACCESSION NBR:9112300327 DOC.DATE: 91/12/19 NOTARIZED: NO DOCKET FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION FULLER,R.E. Washington Public Power Supply System BAKER,J.W. Washington Public Power Supply System RECXP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 91-032-00:on 911119,reactor scram occurred as result of main turbine governor valve fast closure. Caused by failed capacitor in feedwater summation circuitry. Plant maneuvered to safe shutdown condition.W/911119 ltr.
DISTRXBUTXON CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event. Report (LER), I ciden Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT. COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD 1 1
,ENG,P.L. 1 1 INTERNAL: ACNW -2 2 ACRS AEOD/DOA 1 1 AEOD/DSP/TPAB AEOD/ROAB/DSP 2 2 NRR/DET/ECMB 9H NRR/DET/EMEB 7E 1 1 NRR/DLPQ/LHFB10 NRR/DLPQ/LPEB10 *1 1 NRR/DOEA/OEAB NRR/DREP/PRPBll 2 2 NRR/DST/SELB SD NRR/DST/SICBSH3 1 1 NRR/DPT/S PLBS D1 NRR/DST/SRXB 8E RES/DSIR/EIB 1
1 1
1
-EG RGN5 F~ FILE 01 02 EXTERNAL: EG&G BRYCE,J.H 3 3 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1 p v.~ii'- 73 4 8 ~p iNOTE TO ALL "RIDS" RECII?IEÃIS:
PLEASE HELP US TO REDUCE i'ASTE! CONTACT THE DOCUMENT CONTROL DESK,
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ROOD, I Pl-37 (EXT. 20979) TO ELIIIINATEYOUR NAlvlE FROiM DISTRIBUTION LISTS FOR DOCU<XIENTS YOU DON"T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COP1ES REQUIRED: LTTR 33 ENCL 33
WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 Docket No. 50-397 December 19, 1991 G02-91-231 Document Control Desk U. S. Nuclear Regulatory Commission Washington, D. C. 20555
Subject:
NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO.91-032
Dear Sir:
Transmitted herewith is Licensee Event Report No.91-032 for the WNP-2 Plant. This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
Very truly yours, J. W. Baker (M/D 927M)
WNP-2 Plant Manager
Enclosure:
Licensee Event Report No.91-032 CC: Mr. John B. Martin, NRC - Region V Mr. C. Sorensen, NRC Resident Inspector (M/D 901A)
INPO Records Center - Atlanta, GA Ms. Dottie Sherman, ANI Mr. D. L. Williams, BPA (M/D 399)
NRC Resident Inspector - walk over copy
LICENSEE EVIO REPORT ILERI FACILITY NAME (1) OCKET NUMBER (2) PAGE (3)
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 1 F 8 TITLE (4)
REACTOR SCRAM AND ECCS INJECTION DUE TO FAILURE .OF A FEEDWATER LEVEL CONTROL SYSTEM COMPONENT EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR :;:SEQUENT I AL EVI SION MONTH DAY YEAR FACILITY HAHES OCKET NUHBERS(S)
NUMBER UHBER
- 9 5 0 0 0 1 1 9 9 1 9 1 0 3 2 0 0 1 2 1 9 9 1 5 0 0 0 PERATIHG THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more of the following) (11)
ODE (9) 1 PSJER LEVEL 20.402(b) 0.405(C) 50 '3(a)(2)(iv) 77.71(b)
(10) 20.405(a)(1)(i) 0.36(c)(1) 50.73(a)(2)(v) .73(c) 20.405(a)(1)(ii) 0.36(c)(2) 50.73(a)(2)(vii) THER (Specify in Abstract 20.405(a)(1)(iii) 0.73(a)(2)(i) 50.73(a)(2)(viii)(A) elow and in Text, NRC 20.405(a)(1)(iv) 0.73(a)(2)(ii) 50.73(a)(2)(viii)(B) Form 366A) 20.405(a)(1)(v) 0.73(a)(2)(I II) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER R.E. Fuller REA CODE 5 0 9 7 7 - 4 1 4 8 COHPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEH COMPONENT MANUFACTURER EPORTABLE CAUSE SYSTEM COHPONEHT HANUFACTURER REPORTABLE 0 NPRDS TO NPRDS J 8 C A P B 0 4 Y C A D U Y SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED SUBMISSION MONTH DAY YEAR ATE (15)
YES (If yes, complete EXPECTED SUBMISSION DATE) X NO BSTRACT (16)
On November 19, 1991 at 0741, a reactor scram occurred as a result of Main Turbine Governor Valve Fast Closure initiated by a turbine trip signal from Reactor Pressure Vessel (RPV) high water level signal at Level 8 or +54.5 inches. Later, the High Pressure Core Spray (HPCS)
System automatically injected as RPV level approached Level 2 (-50 inches). The high reactor water level was caused by a component failure in the non-safety related Feedwater Level Control (FWLC) System which resulted in the acceleration of the Reactor Feedwater (RFW) pumps in re-sponse to an erroneous feed-flow/steam-flow mismatch signal. The errone-ous signal was caused by a failed capacitor in a Bailey Type 752 feed flow summation card in the FWLC System, which resulted in opening the 1.0 ampere circuit protection fuse. Low RPV level occurred later as a result of inadequate coolant makeup after the RFW pumps tripped at Level 8.
The immediate corrective action was prompt response by the Plant Opera-tors to maneuver the Plant to a safe shutdown condition and to implement appropriate Plant procedures in a timely manner.
The root cause for failure of the Feed Water Level Control (FWLC) System was a failed capacitor in the feedwater summation circuitry.
LICENSEE EVENT REPORT IlaI TEXT CONTINUATION c FACILITY NAME (1) OCKET NUMBER (2) LER NUMBER (8) PAGE (3)
Year NNEber Rev. No.
Washington Nuclear Plant - Unit 2
'3 0 5 0 0 0 9 7 1 0 3 2 0 0 2 F 8 TITLE (4)
REACTOR SCRAM AND ECCS INJECTION DUE TO FAILURE OF A FEEDWATER LEVEL CONTROL SYSTEM COMPONENT Abstract (cont ')
The corrective action was to replace the FWLC summer board RFW-SUM-615 with a tested board that has been checked for proper amperage draw.
The safety significance .of this event is considered negligible because all safety systems were operable and responded as designed. Adequate core cooling was provided at all times. This event posed no threat to the safety of Plant personnel or the public.
Plant Conditions Power Level - 100:
Plant Mode - 1 Event Descri tion On November 19, 1991 at 0741, a reactor scram occurred as a result of Main Turbine Governor Valve Fast Closure initiated by a turbine. trip signal from Reactor Pressure Vessel (RPV) high water level signal at Level 8 or +54.5 inches. Later, the High Pressure Core Spray (HPCS)
System automatically injected as RPV level approached Level 2 (-50 inches). The high reactor water level was caused by a component failure in the non-safety related Feedwater Level Control (FWLC)
System which resulted in the acceleration of the Reactor Feedwater (RFW) pumps in response to an erroneous feed-flow/steam-flow mismatch signal. The erroneous signal was caused by a Tailed capacitor in a Bailey Type 752 feed flow summation card in 'the FWLC System, which resulted in opening the 1.0 ampere circuit protection fuse. Low RPV level occurred later as a result of inadequate coolant makeup after the RFW pumps tripped at Level 8.
The effect of fuse failure was to cause the summed feedwater flow signal input to the FWLC circuit to indicate zero feedwater flow.
This resulted in a maximum feedwater flow demand signal to the RFW pumps and a transfer of th'e Reactor Recirculation (RRC) pumps from 60 Hz to 15 Hz (fast to slow speed) after a 10 second time delay per design. The decrease in RRC flow resulted in an increase in coolant void formation and a subsequent increase in RPV level. The increased feed to the Reactor Pressure Vessel (RPV) combined with the swell in RPV level from decreased RRC flow caused a level transient which tripped the Main Turbine and the RFW pumps on a Level 8 (+54.5 inches) signal at 07:41:55. The Main Turbine trip at greater than 30% power initiated a Reactor Protection (RPS) System scram due to a decrease in oil supply pressure to the turbine governor valves to less than 1250 psig.
LICENSEE EVENT REPORT INII TEXT CONTINUATION FACILITY NAME (1) OCKET NUMBER (2) LER NUMBER (8) PAGE (3)
Year Number Rev. No.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 91 032 00 3 F 8 TITLE (4)
REACTOR SCRAM AND ECCS INJECTION DUE TO FAILURE OF A FEEDWATER LEVEL CONTROL SYSTEM COMPONENT Reactor power at the time of the scram had decreased to approximately 40: as a result of transfer of the RRC pumps to slow speed. RPV level peaked at +58 inches (Narrow Range) and began decreasing rapidly because the Main Turbine Bypass System was drawing off reactor inven-tory in the form of steam to control reactor pressure. At approxi-mately -20 inches the Reactor Core Isolation Cooling (RCIC) System was manually initiated to regain level control.
Level continued to drop and at 07:42:31 the Main Steam Isolation Valves (MSIVs) closed and other isolations occurred, including closure of Reactor Closed Cooling (RCC) water isolation valves to Drywell cooling when the RPV level reached -43 inches on Wide Range (WR),
instrumentation. At 07:42:43, HPCS initiated with RPV level at -46 inches on WR instrumentation. The lowest RPV level was -48 inches at 07:42:48. Level was then restored by RCIC and HPCS. RRC pump 1A received a Level 2 ATWS trip signal, but RRC pump 1B did not trip because its logic was not satisfied. (Level did not drop below the minimum allowable trip level of -50 inches.)
An Unusual Event was declared at 07:47 due to HPCS Level 2 initiation even though the minimum RPV level indication was -48 inches instead of
-50 inches required by the notification procedure. The appropriate outside agency notifications and Plant announcements were made, including the required immediate notifications via the Emergency Notification System (ENS). HPCS and RCIC restored RPV level to +54 inches. HPCS was then secured and placed in standby status. RCIC injection was inhibited. With the subsequent expansion of the cooler HPCS water,'he RPV level peaked at 77 inches. Direction was then given by the Control Room Supervisor to maintain pressure between 800 and 1000 psig with the Safety Relief Valves (SRV) and RPV level between +13 inches and +54.5 inches with the RCIC system. Also, the
.RPS System scram was reset and cooling to the control rods was re-established.
Drywell cooling had stopped with closure of RCC Drywell cooling isolation valves. Heat was still being transferred .to the Drywell from the RPV and associated piping and. components. This caused an increase in Drywell pressure and temperature. At 08:01:44 a high drywell pressure signal was received and HPCS re-initiated. 'njection was manually prevented by securing the HPCS pump because level was being maintained with RCIC.
LICENSEE EVENT REPORT IIStI TfXT CONTINUATION FACILITY NAME ('I) OCKET NUMBER (2) LER NUMBER (8) PAGE (3)
Washington Nuclear Plant - Unit 2 Year NuIIber 'ev. No.
0 5 0 0 0 3 9 7 1 032 00 4 F 8 TITLE (4)
REACTOR SCRAM AND ECCS INJECTION DUE TO FAILURE OF A FEEDWATER LEVEL CONTROL SYSTEM COMPONENT While attempting to maintain level, SRV cycling caused the RPV level to* fall to +11 inches and resulted in a second RPS scram signal at 08:15. The Control Room Operators (CRO) responded appropriately to the second Reactor Scram and reset the RPS. Recovery from the Drywell high pressure trip was then initiated to re-establish drywell cooling.
The RFW System was reconfigured to route feedwater through the Startup Flow Control Valves (RFW-FCV-10A and RFW-FCV-10B), and the Digital Electro-Hydraulic Control (DEH) System was programmed to reduce RPV pressure within the cool down limits. At 08:52 the CROs,equalized pressure across the MSIVs.," They were then opened to re-establish the condenser as a heat sink. The DEH controlled Main Turbine Bypass valves were used to depressurize the RPV to about 500 psig to facilitate using the condensate booster pumps for level control. The plant secured from the Unusual Event at 09:45.
Immediate Corrective Action The Plant Operators responded promptly to maneuver the Plant to a safe shutdown condition. Appropriate Plant procedures were implemented in a timely manner during response to the transient conditions of the Plant.
Further Evaluation and Corrective Action A. Further Evaluation
- 1. This event 'is reportable per 10CFR50.73 (a) (2) (iv) as a condition that resulted in automatic actuation of the Reactor Protection System (RPS) and an Engineered Safety Feature (ESF). Failure of, a capacitor in a FWLC System summer circuitry caused the circuit protective fuse to open.
This resulted in a high flow demand signal to the RFW pumps which caused a Main Turbine trip on RPV high level and a resulting RPS actuation. The high level caused the RFW turbines to trip which resulted in low RPV level and subsequent HPCS initiation. Also, a high Drywell pressure resulted in a second HPCS initiation and other selected ESF actuations.
- 2. There were no other structures, components, or systems inoperable prior to the event which contributed to the event.
M 4
W
LICENSEE EVENT REPORT. IaI)
TEXT CONTINUATION FACILITY HAHE (1) OCKET HUHBER (2) LER HUMBER (8) PAGE (3)
Year Hunber Rev. Ho.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 91 032 00 5 F 8 TITLE (A)
REACTOR SCRAM AND ECCS INJECTION DUE TO FAILURE OF A FEEDWATER LEVEL CONTROL SYSTEM COMPONENT
- 3. The root cause for failure of the FWLC System which led to the reactor scram was a component failure in the FWLC circuitry. Investigation determined capacitor C-3 on FWLC summer card RFW-SUM-615 failed in the shorted condition.
Excessive amperage draw from the failed capacitor caused the 1 amp circuit protective fuse to open, resulting in a zero feed flow signal to the FWLC System. This caused the erroneous steam-flow/feed-flow mismatch and resultant high flow demand signal to the RFW pumps.
The capacitor which shorted and caused the fuse to blow on the RFW-SUM-615 board was a tantalum capacitor which experience- has shown "shorts" when it fails. These type of capacitors are reliable capacitors with a mean life of 348 years and this particular capacitor was manufactured on the 25th week of 1973. From this information, the failure of this capacitor is considered to be premature.
4 ~ Failure of the RFW-SUM-615 output to zero satisfied the RRC pump logic which requires transfer from fast to slow speed after a 10 second time delay if the feed flow is less than 30:. While this transfer was in progress, a reactor scram occurred from the Main Turbine trip on high RPV level, Level
- 8. Both RRC pumps were at slow speed when a Level 2 ATWS signal caused RRC-P-1A to trip off as designed. Level was within the trip setpoint tolerance band. However, RRC-P-1B remained at slow speed because RPV level did not go low enough to reach the trip setpoint for this pump, but the setpoint was also within the tolerance band. The RPV water level reached -48 inches versus the Level 2 setpoint of -50 inches. Instrument calibration for both trains of RRC were verified to be within the acceptable limits.
LICENSEE EVENT REPORT IlII TEXT CONTINUATION FACILITY NAME (1) OCKET NUMBER (2) LER NUHBER (8) PAGE (3)
Year Rober Rev. No.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 1 032 00 6 F 8 TITLE (4)
REA'CTOR SCRAM AND ECCS INJECTION DUE TO FAILURE OF A FEEDWATER LEVEL CONTROL SYSTEM COMPONENT
- 5. Following the transient, the RRC flow control valve RRC-FCV-60A indicated partially closed because of a blown fuse on the power to the control system. The FCV valve actual position for RRC-P-lA remained unchanged in the open position. When power to the control system is lost, the flow control valve locks in position without any movement.
Failure of the fuse occurred coincident with the transient, but was completely unrelated to the initiating event and provided no influence on the progression or outcome of the transient.
- 6. Using instrument tolerances provided by the Master Data Sheets and the design logic diagrams, it was determined that all NSSSS, ECCS, RRC, RCIC and RFW System responses were consistent with design expectations. Reactor conditions for RPV Level 2 and high Drywell pressure. entered the instrument trip setpoint tolerance band but did not exceed the allowable setpoint. Consequently, the trip logic for all components within the above described systems was not satisfied, and as a result, only part of the components received trip/actuation signals. However, all components receiving trip/actuation signals performed as designed. And those that did not trip were not required to trip nor should have tripped to mitigate the consequences of the accident.
Therefore, all systems performed as designed with consideration of the component failures identified.
- 7. In accordance with the requirements of Technical Specifications 3.5.1, Action (f) and 6.9.2 ,'the following special data .is provided:
Total accumulated ECCS initiation cycles to date equals five (5) .
Current usage factor value remains below 0.70.
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LICENSEE EVENT REPORT )
TEXT CONTINuATION FACILITY NAME (1) OCKET NUMBER (2) LER NUMBER (8) PAGE (3)
Year Number Rev. No.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 1 032 00 7 F 8 TITLE (4)
REACTOR SCRAM AND ECCS INJECTION DUE TO FAILURE OF A FEEDWATER LEVEL CONTROL SYSTEM COMPONENT B. Further Corrective Action
- 1. The FWLC summer board RFW-SUM-615 was replaced with a tested board that has been checked for proper amperage draw.
Safet Si nificance The safety significance of this event is considered negligible because all safety systems were operable and responded as designed. This event was well within the FSAR transient analyses. Adequate core cooling was provided at all times. This event posed no threat to the safety of Plant personnel or the public.
Similar Events LER 87-02 documented a similar event that occurred on March 22; 1987, in which the circuit protection fuse failed on the feed flow summer board RFW-SUM-615 of the FWLC System. This caused a zero feed flow .
signal to the FWLC System and corresponding high flow demand signal to the RFW pumps. The cause of the fuse failure was investigated but was not determinable. Corrective actions to this problem was replacement of the 1/4 amp fuse on this board and boards RFW-SUM-602, 603, 615, and 616 with a 1 amp fuse to increase reliability. Then on October 1, 1991 this same fuse was found blown during start up operations and the fuse was replaced with a 1 amp fuse. Failure of the fuse at this time was attributed to the de-term and re-term work performed in this cabinet during the R-6 outage.
LICENSEE EVENT REPORT (llI TEXT CONTINUATION FAC1L]TY HAME (1) OCKET HUMBER (2) LER HUHBER (8) PAGE (3):
Year NLIIIber Rev. Ho.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 F' 1 032 00 8 T!TLE (4)
REACTOR SCRAM AND ECCS INJECTION DUE TO FAILURE OF A FEEDWATER LEVEL CONTROL SYSTEM COMPONENT EIIS Information Text Reference EIIS Reference
.~Ss tern Reactor Containment II C
Control Rod Drive System AA Turbine Supervisory Control System JJ Main Turbine Control Fluid System TG Emergency Power System for HPCS DG High Pressure Core Spray System BG Reactor Recirculation System AD .FU Low Pressure Core Spray System BM Incore/Excore -Monitoring System IG Main Steam System SB Turbine Bypass System SO Reactor Building NG Reactor Protection System JC Reactor Building Closed Cooling Water System CC Reactor Core Isolation Cooling System BN Feedwater Pump Turbine I&C System JK Reactor Feedwater Control System JB CAP Feedwater System SJ Feedwater Pump Injection System SK RHR/Containment Spray BO Containment & Reactor Vessel Isolation System JM Main Turbine System, TG