05000397/LER-1990-028, :on 901023,degradation of Primary Containment Pressure Boundary Caused Plant Shutdown,Due to Cracks on HPCS Small Bore Piping
| ML17286A514 | |
| Person / Time | |
|---|---|
| Site: | Columbia |
| Issue date: | 12/04/1990 |
| From: | Baker W, Washington S WASHINGTON PUBLIC POWER SUPPLY SYSTEM |
| To: | |
| Shared Package | |
| ML17286A513 | List: |
| References | |
| LER-90-028, LER-90-28, NUDOCS 9012140238 | |
| Download: ML17286A514 (10) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(e)(2) 10 CFR 50.73(a)(2)(ii) |
| 3971990028R00 - NRC Website | |
text
NRC FOII,M 356 (Se9)
V.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LERI FACILITYNAME (1)
Washington Nuclear Plant - Unit 2 PAGE 3I DOCKET NUMBER (2) o 5
o o
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an Shutdown Oue to Cracks on High Pressure Core Spray Small Bore Piping MONTH OAY YEAR YEAR EVENT DATE ISI'ER NUMBER (6)
REVISION
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NUMBER MONTH DAY YEAR REPORT DATE 17)
DOCKET NUMBER(SI 0
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FACILITYNAMES OTHER FACILITIES INVOLVED(SI 0
9 2 8 0 0 1
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Beginning on October 23,
- 1990, four related reportable events or conditions occurred.
- First, on October 23, 1990 a hairline crack was discovered on a small bore drain line pipe off of the High Pressure Core Spray (HPCS) Suppression Pool Test Return Line.
This condition was considered a degradation of the Primary Con-tainment.
- Second, on October 31, 1990 the HPCS System, a single train safety
- system, was de'clared inoperable due to a linear indication on a small bore pipe (weld) attached to the HPCS Injection Line.
- Third, on November 2, 1990'at 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br /> Plant Engineers determined that the linear indication was a crack (not a
through the pipe wall crack).
At the time this condition was considered a more significant degradation of the Primary Containment pressure boundary and at 1726 hour0.02 days <br />0.479 hours <br />0.00285 weeks <br />6.56743e-4 months <br />s-a Plant shutdown was initiated and an Unusual Event declared.
The Plant was manually scrammed at 2153 hours0.0249 days <br />0.598 hours <br />0.00356 weeks <br />8.192165e-4 months <br />.
The fourth reportable event occurred when a
Reactor Protection System (RPS) actuation occurred due to a HLow" Reactor water level trip.
At the time of the event Plant Operators were reducing Reactor pressure so that water could be fed to the Reactor using a Condensate Booster Pump.
y01214023 '01204 PDI-ADOCK 0500035'7 F'DC NRC Form 366 (6e9)
~
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9 On October 23, 1990 immediate corrective-action was taken to isolate the drain line from both Primary Containment and the HPCS System.
Other HPCS small bore pipe welds were examined.
Engineering analysis determined that the linear indication found on the drain line attached to the HPCS Injection Line on October 31, 1990 would not affect the integrity of the Primary Containment pressure boundary.
The root cause of the HPCS Injection Line pipe crack event is indeterminate in that the cause for the initiation of the crack can not been determined.
The root cause of the Test Return Line vent and drain line cracks is believed to be fatigue.,The root cause of the RPS actuation due to the Low Vessel Water Level event is per-formance based in that the Reactor mass input/output was not balanced.
Corrective Actions include-replacing the HPCS Injection Line drain line pipe, and redesign and replacement of the Test Return Line drain and vent line connections.
Regarding the RPS actuation, Plant Operations Management is reviewing the event with each each Operations Crew.
Plant Conditions
a)
Power Level - 1005 b)
Plant Mode -
1 (Power Operation)
Event Descri tion Beginning on October 23, 1990, four related reportable events or conditions occurred.
On October 23, 1990 at 0513 hours0.00594 days <br />0.143 hours <br />8.482143e-4 weeks <br />1.951965e-4 months <br />, a Plant Equipment Operator (non-licensed) dis-covered a hairline crack in a socket weld joining a small bore (3/4H) pipe drain line (HPCS-V-36 drain valve) to the 12H HPCS Suppression Pool Test Return Line.
The crack was discovered because it was a through the wall crack and a small amount of water was leaking through the crack.
At the time of this discovery, the Equipment Operator was closing the Suppression Pool Test Return Line Manual Isolation Valve (HPCS-V-64) due to the inoperability of the Test Return Line Automatic Isolation Valve (HPCS-V-23)(See LER 90-25).
Closing HPCS-V-64 isolated the cracked pipe from the Primary Containment pressure boundary.
At 0850 hours0.00984 days <br />0.236 hours <br />0.00141 weeks <br />3.23425e-4 months <br />, the HPCS Suppression Pool Test Return Automatic Isolation Valve, HPCS-V-23, was closed and tagged to prevent it from being opened.
This isolated the cracked line from the HPCS System.
An investigation was initiated by Plant Management to review other HPCS small bore piping welds which had previously been identified as having a
some probability of failure due to HPCS System vibration and pipe configuration.
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On October 31, 1990, during nondestructive examinations, using magnetic particle and dye penetrant techniques, Supply System Engineers found a linear indication on the socket weld joining the small bore (3/4" ) piping for drain valves HPCS-V-21 and HPCS-V-22 to the 12H HPCS Injection-Line.
A Plant Operating Committee (POC
) Irane-diate Disposition was approved to allow continued operation, because a linear indi-cation is not necessarily an indication of a crack, there was no leakage at reactor pressure (approximately 1000 psi),
and engineering analysis showed that the drain line would remain intact during and after a design basis seismic event and a Loss of Cooling Accident (LOCA).
Since the affect of operating the HPCS System on the pipe could not be character ized by engineering analysis the HPCS System was declared inoperable and all HPCS pump starts disabled.
Also on October 31,
- 1990, a second linear indication was found on the small bore pipe connection for a 3/4" vent line attached to the HPCS Suppression Pool Test Return Line directly above the drain line found cracked on October 23, 1990.
No action was required since HPCS-V-64 and HPCS-V-23 were previously closed isolating this section of pipe from the Primary Containment pressure boundary and from the HPCS System.
On November 2, 1990 at 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br /> Supply System Engineers, using ultrasonic non-destructive testing techniques determined that the linear indication found on the drain line attached to the HPCS Injection Line was a crack.
Since Primary Contain-ment integrity could not be assured, at 1726 hours0.02 days <br />0.479 hours <br />0.00285 weeks <br />6.56743e-4 months <br /> a Plant Shutdown was initiated and an Unusual Event Declared due to a Technical Specification (Containment Integrity 3.6.1.1) forced shutdown.
Plant operators using the General Operating Procedure (PPM 3.2.1),
Normal Shutdown to Cold Shutdown, at 2153 hours0.0249 days <br />0.598 hours <br />0.00356 weeks <br />8.192165e-4 months <br /> manually scrammed the reactor.
At the time of the
- scram, reactor power was 20%, the Main Turbine/Generator was off-line, and reactor vessel level was being controlled by the Startup Level Controller (RFM-LIC-620) using the Startup Flow Control Valves (RFW-FCV-1 OA and 1 OB).
Mhen the reactor was scrammed the vessel level dropped rapidly due to void collapse and then recovered as inventory accumulated.
At 2157 hours0.025 days <br />0.599 hours <br />0.00357 weeks <br />8.207385e-4 months <br /> a Reactor Vessel Mater Level "High" (Level 8) trip occurred at +54 inches.
This, by design, caused the Reactor Feedwater Drive Turbine (RFW-DT-lA) to trip which in turn caused a the operating Reactor Feedwater Pump (RFW-P-lA) to shut down.
At the time of the Feedwater Turbine trip Reactor pressure had decayed to approxi-mately 650 psig which was below the pressure control setpoint of the Digital Electro-Hydraulic (DEH
) (Main Turbine) Control System and the Main Turbine Bypass Valves were closed.
Over the next 26 minutes, reactor pressure slowly increased from 650 psig to 700 psig and water level slowly decreased to +41 inches.
At 2223 hours0.0257 days <br />0.618 hours <br />0.00368 weeks <br />8.458515e-4 months <br /> P'Iant Operators began to reduce Reactor pressure by decreasing the DEH pres-sure control setpoi nt which opened the Main Turbine Bypass Valves.
The Operators were reducing reactor pressure to approximately 600 psig so that water could be added to the Reactor Pressure Vessel (RPV) using a Condensate Booster Pump.
Opening~
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9 the Bypass Valves allowed the Reactor water level to decrease along with Reactor pressure.
Just prior to the event Plant Operators increased the DEH depressurization rate from 16 psi g/minute to 25 psi g/minute.
At 2231 hours0.0258 days <br />0.62 hours <br />0.00369 weeks <br />8.488955e-4 months <br />, when reactor pressure reached 620 psig and reactor vessel level had dropped to +15
- inches, feedflow was established to the vessel and level began to increase.
How-ever, at approximately that same time changes in the Feedwater Startup Flow Control Valve (FCV) position caused the level to decrease again and a Reactor Vessel Low Level
(+13 inches) trip occurred at 2234 hours0.0259 days <br />0.621 hours <br />0.00369 weeks <br />8.50037e-4 months <br />.
The changes in the Startup FCV are attributed to the change in the deprressurization rate.
On November 3, 1990 at 0856 hours0.00991 days <br />0.238 hours <br />0.00142 weeks <br />3.25708e-4 months <br />, the Unusual Event terminated as the Plant reached Operational Mode 4 (Cold Shutdown).
Immediate Corrective Action
The immediate corrective actions taken during the event are included in the event
description
above.
There were no immediate corrective action associated with'the RPS actuation because there was no actual Control Rod movement since they were already fully inserted into the core, and Reactor pressure had decreased to the point where makeup flow could be provided by the Condensate System.
Further Evaluation and Corrective Action A.
Further Evaluation l.
This event is being reported per the requirements of four 10CFR50. 73 criteria.
Per 10CFR50. 73(a)(2)(i)(A) as a completion of a Plant Shutdown required by Technical Specifications.
Reported verbally per 10CFR50.72(b)(l)(i)(A) at 1742 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.62831e-4 months <br /> on November 2, 1990.
Per 10CFR50.73(a)(2)(ii) as a condition that seriously degraded a primary safety barrier (Primary Containment).
Reported per 10CFR50.72(b)(l)(ii) at 0612 hours0.00708 days <br />0.17 hours <br />0.00101 weeks <br />2.32866e-4 months <br /> on October 23, 1990 and at 1742 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.62831e-4 months <br /> on November 2, 1990.
The second event reported, the crack found on the drain line on the HPCS Injection Line identified on November 2, 1990, was later downgraded to not reportable when it was determined by engineering analysis that the line would not have failed during normal or accident conditions.
Per 10CFR50. 73(a)(2 )(iv) as an automatic actuation of the Reactor Pro-tection System..
Reported per 10CFR50.72(b)(2)(ii) at 2317 hours0.0268 days <br />0.644 hours <br />0.00383 weeks <br />8.816185e-4 months <br /> on November 2,
1990.
Per 10CFR50. 73(a)(2 )(v) as an a condition which prevented a safety system from accomplishing its function.
The HPCS System is a single train system which was taken out of service during this event.
Reported per 1 OCFR50. 72( b)(2)( iii )(D ) at 001 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> on November 1, 1 990.(64) 9)
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Washington Nuclear Plant - Unit 2 TEXT fffmoro sOsso r9 rooofrsd, oss sddio'onsl ffi(C Form 3NA'sI (17) 0 s
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9 2.
There were no structures,
- systems, or components inoperable prior to this event which contributed to the event except for mechanical problems with the Feedwater regulator and opening pressure booster on RFW-FCV-TOA/B.
These problems had previously been identified and may have contributed to the Low Vessel Water Level RPS actuation event.
As discussed in LER 90-25, the HPCS Automatic Isolation Valve, HPCS-V-23, was inoperable during this event, it did not contribute to this event.
3.
Upon shutdown of the plant, the drain line pup piece was removed from HPCS-V-21 for metallurgical evaluation.
The linear indication was cut open to expose the fracture surface.
It was determined upon examination that the crack was caused by fatigue.
Subsequent scanning electron microscopy (SEI<) examination determined the fatigue was due to inter-mittent loading, based on the presence of "beach" marks.
This initialized a testing program on the HPCS system to define loading conditions at the drain line location.
The HPCS-V-21 and HPCS-V-22 drain line and HPCS Injection Line directly above the drain connection was instrumented with five accelerometers.
Three accelerometers were mounted (tri-axially) on-the large bore piping and two accel erometers (horizontal plane) were mounted on HPCS-V-22.
Utilizing the described instrumentation, five
" system tests were performed as follows: 1)
HPCS surveillance, PPN 7'.4.5.1.11, simulating throttling HPCS-V-23 in the Suppression Pool Test, Return Line; 2)
HPCS injection to the RPV (stroking open the HPCS Injection Valve (HPCS-V-4) under full pump differential pressure; 3)
HPCS-V-4 LLRT utilizing a positive.displacement hydro pump simulating yearly 950 psid leakage testing; 4)
HPCS-V-4 surveillance testing involv-ing valve stroking while simulating the RPV at rated pressure;
- 5) Static stroking of HPCS-V-4.
The results from this dynamic testing revealed that significant loads are generated from the RPV ihjection event when the HPCS-V-4 valve begins opening with full pump discharge pressure differential across it.
These loads were then digitized and applied to a dynamic model of the HPCS-V-21/22 drain line to establish a stress field for subsequent frac-ture mechanics analysis.
A fracture mechanics model was developed using the actual crack configur-ation.
The stresses developed by the HPCS injection to the RPV were used as input into the model.
Based upon the results of the number of cycles developed during the HPCS injection and comparing the crack growth between "beach'arks, it was determined that intermittent crack growth was due to HPCS injections.
Therefore, correlation between actual system loads and measured crack propagation was established.
One indeterminate factor exists dealing with the crack initiation event.
Computer modeling assumes a crack has been initiated by some unknown mechanism.
(Possibly an initial construction defect.)(64)9)
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6.
7.
Engineering analysis of the HPCS system tests concluded that the number of HPCS injections incurred to date would not have initiated the crack, but rather would have only propagated the crack initiated by some other mechanism.
- Further, analysis has shown that roughly an additional 60 HPCS injections would be required to propagate an initiated crack into a through-wall fatigue crack.
Concur rent with the fracture mechanics and HPCS system tests, liquid pene-trant examinations were being conducted on selected vent and drain line connections which performed a Containment integrity function or were within a small break LOCA boundary which could not be isolated from the RPV, and were contained in pump driven systems.
Between October 23, 1 990 and November 8,
1990 104 fillet welds on 40 vent/drain line connections were nondestructively examined.
After the results of the fracture mechanics
- analysis, the scope of NDE examination was narrowed to include all
- HPCS, Low Pressure Core Spray System(LPCS),
Residual Heat Removal System (RHR)
Low Pressure Core Injection Mode, and Reactor Core Isolation Cooling (RCIC) injection line connections immediately downstream of the injection isolation valves which open against full pump differential pres-sure.
No indications were found using fluorescent liquid penetrant non-destructive testing techniques.
Plant Operations Management has evaluated the Operations Crew management of reactor pressure and water level following the manual scram.
The RPS actuation was due to the establishment of an RPV mass removal mechanism (steam flow through the bypass valves) which exceeded the inservice makeup capability of the Control Rod Drive System inflow. It was assumed an RPV feed source of sufficient capacity would become available prior to reach-ing the RPS "LowH water level setpoint.
A combination of the Feedwater Startup FCV control speed and level fluctuations frustrated determination of level margin available to preclude actuation.
The root cause of the pipe crack on the drain line attached to the HPCS Injection Line is indeterminate.
Engineering analysis has established the cause of the crack propagation but no event analyzed would have been suf-ficient to initiate the crack.
Therefore, it is believed that the flaw has existed since the original weld was made.
The root cause evaluation of the cracks on the vent and drain lines on the Test Return Line is not yet complete;
- however, they are believed to be fatigue cracks.
If the final root cause is different a Supplemental LER will be sent.
The preliminary root cause of the RPS actuation event is the situation analysis by the Operating Crew was less than adequate in that they did not balance the mass input and output to the RPV. If the final root cause is different a Supplemental LER will be sent.
A contributing cause was the mechanical problems associated with RFW-FCV-10A/B.
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Further Corrective Action 2.
The HPCS-V-21 and HPCS-V-22 drain line was replaced.
- Further, these welds will be redesigned and replaced during the next Refueling Outage.
Both the HPCS-V-36 drain'ine and the HPCS-V-74 vent line have been
'edesigned and replaced.,
3.
A plant modification is planned to reduce the vibration in the HPCS Suppression Pool Test Return Line.
The design is scheduled to be completed by June 1991 and installation is planned for Refueling Outage R7 (Spring 1992).
4.
Further evaluations will be conducted to determine if other small bore pipe configurations shoul'd be modified, and if other design modifications need to -be made to reduce the vibration or loading on these small bore pipes; When appropriate, nondestructive testing will be performed until the above evaluations and modifications have been completed.
5.
Corrective maintenance was performed on RFW-FCV-10A/B.
6.
Plant Operations Management is reviewing this event with each of the six Operation Crews.
The discussion focuses on Management's expectations with regards to Reactor pressure and water level control strategies.
Safet Si nificance There is a minimal safety significance risk associated with the cracks on the vent and drain lines attached to the HPCS Suppression Pool Test Return Line.
It i s the opinion of Plant Engineers that without planned Test Return Line modifications both of these lines would have eventually failed.
The Test Return Line redesign is scheduled to be completed by June 1991 and installation is planned for Refueling Outage R7 (Spring 1992).
If the vent or drain line did fail it most likely would occur during HPCS testing when the high vibration condition occurs.
If the failure did occur during testing, there is no safety significance because the lines can be isolated.
Also, it is unlikely that(,failures would occur during accident conditions because the HPCS Suppression Pool Test Return Automatic Isolation Valve HPCS-V-23 closes whenever the HPCS System is initiated and there would be no flow in the line.
There is no safety significance associated with the crack found in the HPCS-V-21/22 drain line which was determined by engineering analysis to be capable of withstanding 60 more cycles before the line would have failed.
This 60 cycles bounds the expected number of times this event(64) 9)
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TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENTBRANCH (P r)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555. AND TO 1HE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON. DC 20503 FACILITYNAME 111 DOCKET NUMBER (2I LER NUMBER (6)
PAGE (3)
Washington Nuclear Plant - Unit 2 TEXT (// more 4/Mseis required, use eddrr/ons/1YRC Form 366r4'4/ (12) osooo YEAR
~g@
9 0 SEGUENTIAL AS NUMBER 0
2 8
REVISION NUMSER 0 0 0 8oF0 9
would be expected to occur during the remaining Plant License lifetime.
There is no safety significance associated with the HPCS System being out-of-set vice.
The length of time the System was out of service was within the Technical Specification allowable HPCS outage time.
- Further, the RCIC System (non-safety system) was available for high pressure water injection to'he RPV.
The Automatic Depressurization System (ADS) whose'function is to depressurize the RPV in the event that no high pressure source of injection water is available was also available.
There is no safety significance associated with the RPS actuation since all Control Rods were already full inserted prior to the event and reactor water level was promptly recovered.
Similar Events
LER 89-15 describes an event where a vent line broke off of the HPCS Suppression Pool Test Return Line.
Corrective actions
committed to in LER 89-15 are still being implemented.
Installation of a design modification to reduce vibration on the HPCS Suppression Pool Test Return Line is planned for Refueling Outage R7 in the Spring of 1992.
Both the small bore pipes found cracked had previously been identified as high vibration locations.
Both welds were examined during the Refuel.ing Outage R4 (spring 1989) with no indications identified.
LER 85-1 1-00 and LER 85-11-01.
There have been several events associated with level fluxuations at WNP-2 (LERs86-038, 87-002,88-001 and 88-003).
- However, none of these LERs were associated with events specific to control of level during a controlled shutdown.
EIIS Information Text Reference E I IS Reference
~Sstem
~tom onent High Pressure Core Spray System(HPCS)
HPCS Suppression Pool Test Return Line Primary Containment HPCS Injection Line Reactor Protection System Condensate Booster Pump HPCS Drain Valve 36 (HPCS-V-36)
HPCS Supression Pool Test Return Automatic Isolation Yalve (HPCS-V-23)
HPCS Suppression Pool Test Return Manual Isolation Valve (HPCS-V-64)
HPCS Drain Valve 21 (HPCS-V-21)
HPCS Drain Valve 22 (HPCS-Y-21)
HPCS Pump Main Turbine/Generator BG BG C
BG JC SD BG BG BG BG BG BG TA/TB PSP PSP P
V V
Y V
P TRB/GENr (64)9)
U.S. NUCLEAR REGULATORYCOMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION t
APPROVED OMB NO. 31504))04 EXPIRES: 4/30/92 ESTIMATED BURDEN PER
RESPONSE
TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS, FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENTBRANCH (P.530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO
'IHE PAPERWORK REDUCTION PROJECT (31504)104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON,DC 20503, FACILITYNAME (1)
DOCKET NUMBER 12)
YEAR LER NUMBER (6)
SEOUENTIAL r%%:
NUMBE R REVISION NUMBER PAGE (3)
Washington Nuclear Plant - Unit 2 TEXTllfmors s/MC ~ is rsr)oirsd, oss sdditions/NRC Form 3MA'4/(17),
I OF 0
Startup Feedwater Level Controller (RFW-LIC-620)
Feedwater Startup Flow Control Valve (RFW-FCV-10A/B)
Reactor Feedwater Drive Turbine,lA (RFW-DT-1A)
Reactor Feedwater Pump lA (RFW-P-1A)
Digital Electro Hydraulic System (DEH)
Main Turbine Bypass Valves Control Rod Condensate System Reactor Pressure Vessel(( RPV)
HPCS Injection Valve (HPCS-V-4)
HPCS Vent Valve (HPCS-V-74)
Low Pressure Core Spray System (LPCS)
Reactor Core Isolation Cooling (RCIC)
Automatic Depressurization System (ADS)
JB SJ JJ SO AA SD AC BG BG BM BO BN BG LIC
~
FCV TRB V
V