ML17059B940
| ML17059B940 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 03/20/1998 |
| From: | Doerflein L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17059B938 | List: |
| References | |
| 50-220-98-01, 50-220-98-1, 50-410-98-01, 50-410-98-1, NUDOCS 9803310055 | |
| Download: ML17059B940 (80) | |
See also: IR 05000220/1998001
Text
U.S. NUCLEAR REGULATORYCOMMISSION
REGION I
Docket/Report Nos.:
50-220/98-01
50-41 0/98-01
License Nos.:
NPF-69
Licensee:
Niagara Mohawk Power Corporation
P. O. Box 63
Lycomnin, NY 13093
Facility:
Nine Mile Point, Units
1 and 2
Location:
Scriba, New York
Dates:,
January 4- February 14, 1998
Inspectors:
B. S. Norris, Senior Resident Inspector
T. A. Beltz, Resident Inspector
R. A. Skokowski, Resident Inspector
Approved by:
Lawrence T. Doerflein, Chief
Projects Branch
1
Division of Reactor Projects
9803310055
980320
ADQCK 05000220
6
TABLEOF CONTENTS
page
TABLEOF CONTENTS
EXECUTIVE SUMMARY
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SUMMARYOF ACTIVITIES'........... ~.....
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Niagara Mohaw'k Power Corporation (NMPC) Activities
Nuclear Regulatory Commission (NRC) Staff Activities...
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Conduct of Operations ..................................
01.1
General Comments......,............,............
01.2
Initiation of a Unit 2 Plant Shutdown due to Inoperable Containm
Atmospheric Gaseous/Particulate
Radiation Monit'ors........
01.3
Identification of a Reactor Fuel Leak at Unit 2...........:.
01.4
Inadequate Shift Turnover for Unit 1 Rea'ctor Operator.......
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Operational Status of Facilities and Equipment
02.1
Inadequate Separation Between Conduits for Safety-Related
Temperature Elements
02.2
Control of Catch Containments at Unit 1
02.3
Review of Unit 1 Extended Markup/Holdout Quarterly Report ..
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Miscellaneous Operations Issues ...........................
08.1
(Closed) LER 50-410/98-01: Entry'into TS 3.0.3 Due to Contain
Atmospheric Gaseous/Particulate
Radiation Monitors Inoperable
I I ~ MAINTENANCE
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Conduct of Maintenance ~.................
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M1.2
Replacement of Leaking Fuel Delivery Valve on a Unit 2 EDG
M2
Maintenance and Material Condition of Facilities and Equipment .....
M2.1
Unit 1 Liquid Poison System Surveillance Testing Deficiency
M8
Miscellaneous Maintenance Issues..........................
M8.1
Administrative Closure of Escalated Enforcement Items ......
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Conduct of Engineering ~... ~.......
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E2
Engineering Support of Facilities and Equipment
E2.1
Maintenance on Unit 1 Service Water Valve Violated Secondary
Containment Integrity............ ~...................
E2.2
Longstanding Holdout on Temperature Control Valve for Unit 1
Control Room Emergency Ventilation System
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Miscellaneous Engineering Issues.............................
E8.1
(Closed) LER 50-410/97-05-01:
High Pressure
Core Spray System
Inoperable Due to Failed,Unit Cooler
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Table of Contents (cont'd)
E8,2
E8.3
E8.4
E8.5
E8.6
E8.7
E8.8
E8.9
E8.10
(Closed) LER 50-220/97-10-01:TS
Required Shutdown Due to
Emergency Cooling Condenser Tube Leak
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(Closed) LER 50-410/97-13:
Prior to 1992, Emergency Switchgear
Not Seismically Qualified With Breakers Racked Out ..........
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(Closed) LER 50-410/97-16:
Missed TSSR 4.3.4.1.2 for ATWS-RPT
T'ip of LFMG .. ~.................. ~.............
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(Closed) VIO 50-220/96-07-03:
UFSAR Drawing Changed Without
Performing a 10 CFR 50,59 Safety Evaluation.............
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(Closed) 10 CFR 21 Notification: Potentially Defective Diesel
Generator Air Start Solenoid Valves... ~....
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(Opened) 10 CFR 21 Notification: Potentially Defective GE SBM-Type
Switches Unit 1
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(Closed) URI 50-220/96-05-03:
Lack of 10CFR50.59 Safety
Evaluation for the Modification to Restore the Unit 1 Blowout Panels
to Compliance with UFSAR................
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(Closed) Unit 2 Special Report:
Division I Standby EDG Non-valid
Test and Non-valid Failure..........
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Administrative Closure of Escalated Enforcement Items ........ 25
IV. PLANT SUPPORT
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Radiological Protection and Chemistry, Controls
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R1.1
Potentially Contaminated Truck Released from Unit 1.....,
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Miscellaneous RPRC Issues.............................
R8.1
Administrative Closure of Escalated Enforcement Items ...
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Status of Fire Protection Facilities and Equipment
F2.1
Unit 1 Unplanned Fire Alarms and Preaction Sprinkler System
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Exit Meeting Summary ................................
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ATTACHMENT
ATTACHMENT1 -
Partial List of Persons Contacted
Inspection Procedures
Used
Items Opened, Closed, and Updated
List of Acronyms Used
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EXECUTIVE SUMMARY
Nine lVlile Point Units 1 and 2
50-220/98-01 5. 50-41 0/98-01
January 4 - February 14, 1998
This NRC inspection report includes reviews of licensee activities in the functional areas of
operations, engineering, maintenance,
and plant support.
The report covers a six-week
period of inspections and reviews by the resident staff.
PLANT OPERATIONS
Unit 2 operators responded appropriately to the failure of the Division II containment
atmosphere
gaseous/particulate
radiation monitor that occurred while the Division I monitor
was inoperable for maintenance.
Station Operations Review Committee members
maintained the proper safety focus during the meeting to discuss the basis for requesting
Routine monitoring of the Unit 2 fuel reliability index allowed NMPC to identify a reactor
'uel
leak early, before it degraded any further. The flux tilting and power suppression
evolution was methodical and well-controlled due, in part, to good communication and
coordination among all involved organizations.
NMPC took aggressive actions to prevent
further leak degradation.
During an inspection in the Unit 2 residual heat removal pump rooms, the inspectors
identified inadequate
separation between conduits for safety-related temperature elements
of different divisions.
(NCV) A breakdown in communications between an Assistant
Station Shift Supervisor and a system engineer resulted in a one week delay in recognizing
the impact that inadequate conduit separation
had on the operability of safety-related plant
equipment.
Most catch containments installed in Unit 1 were adequately installed and maintained.
However, many designated
as "permanent" did not have an engineering evaluation to
determine if a plant change or modification was required.
(NCV) The most recent semi-
annual catch containment review lacked depth, in that NMPC failed to fully evaluate
whether catch containments should be removed or that those designated
as "permanent"
had the required engineering evaluation.
The quarterly reviews of extended markups at Unit 1 were weak in that the reviewers
failed to identify numerous markup discrepancies that were later identified by the
inspectors.
Unit 1 management was aware of the weaknesses,
and proposed corrective
actions appeared
appropriate.
MAINTENANCE
NMPC appropriately evaluated the impact of a leaking fuel delivery valve on the operability
of the Unit 2 emergency diesel generator.
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Executive Summary (cont'd)
Based upon the NRC inspectors'uestions,
NMPC management
declared the Unit 1 liquid
poison system inoperable.
Portions of the system piping had not been periodically flow
tested and NMPC was unable to readily ascertain whether the piping'from the liquid poison
tank to the pump suction valves was obstructed.
NMPC's decision to declare the liquid
poison system inoperable and commence
a shutdown was conservative,
and the actions
taken to test the system were appropriate. The special evolution brief was thorough.
Although the pievious Unit 1 liquid poison system surveillance testing met technical
specification requirements, the testing was inadequate to verify system operability.
(VIO)
ENGINEERING
As a result of a good questioning attitude by a system engineer, NMPC identified that
maintenance
on the Unit 1 service water drag valve in the reactor building violated
secondary containment integrity. Past maintenance
on the valve exceeded the allowable
limiting condition for operation outage time, and a reactor shutdown had not been initiated
in accordance with the technical specification requirements.
(NCV) The inspectors
identified that NMPC failed to perform a design change for permanently installed
(NCV)
The inspectors identified that the temperature control valve for the Unit 1 control room
emergency ventilation system had been inoperable since 1983. The administrative controls
to disposition the failed valve had not been properly implemented; i.e., the controlled
drawings did not indicate the inoperable valve, nor was an engineering evaluation
performed, as required by procedures, to determine if continued operation with the
degraded condition was acceptable.
(VIO)
Prior to April 30, 1992, Unit 2 operated with circuit breakers in the racked out position,
and failed to recognize the adverse impact on switchgear seismic qualification and,
therefore, switchgear operability.
(NCV) Although NMPC took appropriate actions in 1992
to preclude future operations with breakers in the racked out position, they failed to
recognize that they were in an unanalyzed, condition, and that the condition was
reportable.
(NCV)
NMPC identified that a portion of the Unit 2 testing for the recirculation pump trip in
response to an anticipated transient without scram was not completed in accordance with
the technical specifications.
(NCV) Specifically, the logic system functional testing failed
to include the high reactor pressure trip of the low frequency motor generator.
In addition,
the failure to specify an acceptability range for the low frequency motor generator time
delay in the subsequent
procedure change procedure indicated weaknesses
in the
procedure and in the review of the associated
procedure change.
Furthermore, in
December 1996, NMPC missed an opportunity to identify the inadequate
surveillance test
due to a non-conservative interpretation of the Updated Final Safety Analysis Report.
The licensee's actions at both units to address
an industry concern with potentially
defective emergency diesel generator air start solenoid valves was timely and technically
sound.
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Executive Summary (cont'd)
NMPC responded quickly and appropriately to a vendor notification related to a possible
failure of spring-return switch'es used in the emergency cooling and containment spray
systems at Unit 1
~ Control room operators were aware of the potential failure mode;
however, the associated
operating procedures
had not been revised to include a
precautionary note related to the concern.
PLANT SUPPORT
Control room and fire brigade personnel appropriately responded to numerous Unit 1 fire
alarm actuations,
and the investigation effort appeared
adequately coordinated.
The failure
to fully investigate and resolve previous similar false fire protection system actuations was
a weakness
and likely contributed to the recent event.
Although Unit 1 fire suppression
system operability did not appear to be affected by degraded components, the impact of
the deficiencies could hinder plant personnel responding to an in-plant fire due to potential
multiple false alarms.
REPORT DETAILS
Nine Mile Point Units 1 and 2
50-220/98-01
8L 50-41 0/98-01
January 4 - February 14, 1998
SUMMARYOF ACTIVITIES
Niagara Mohawk Power Corporation (NMPC) Activities
Unit 1
Nine Mile Point Unit 1 (Unit 1) started the inspection period at full power.
On the morning
of January 21, 1998, the licensee commenced
a unit shutdown due to the liquid poison
system being inoperable (Section M2.1 of this report).
Reactor power was reduced to
approximately 70% when the operability of the liquid poison system was confirmed; full
power was achieved later that day.
The unit remained at full power throughout the
remainder of the inspection period.
Unit 2
Nine Mile Point Unit 2 (Unit 2) started the inspection period at 95% power, limited to 95%
due to the moisture separator reheaters
being removed from service.
On January 7, 1998,
the licensee commenced
a unit shutdown due to both drywell radiation monitors being out-
of-service (Section 01.2 of this report); reactor power was lowered to approximately 50%.
During the power reduction, NMPC requested,
and was granted, enforcement discretion by
the NRC. The unit was returned to 95% power on January 8.
On January 24, reactor
power was again reduced to approximately 50% to identify the source of a potential fuel
leak (Section 01.3 of this report).
The unit was returned to 95% on January 30.
On
February 14, reactor power was lowered to approximately 81% to perform a rod pattern
adjustment, and this power level was maintained through the remainder of the inspection
period.
Mana ement Reor anization
On January 23, 1998, Mr. John H. Mueller assumed the position of Senior Vice President
and Chief Nuclear Officer of NMPC. Mr. Mueller succeeded
Mr. B. Ralph Sylvia.
Nuclear Regulatory Commission (NRC) Staff Activities
Ins ection Activities
The NRC resident inspectors conducted inspection activities during normal, backshift, and
deep backshift hours.
The results of the inspection activities are contained in the
applicable sections of this report.
U dated Final Safet
Anal sis Re ort Reviews
While performing the inspections discussed
in this report, the inspectors reviewed the
applicable portions of the Updated Final Safety Analysis Report (UFSAR) related to the
0
areas inspected.
The inspectors verified that the UFSAR wording was consistent with the
observed plant practices, procedures
and/or parameters.
Exceptions noted were:
(1) the
conduit for safety-related residual heat removal temperature elements of different electrical
divisions were in contact, although the Unit 2 UFSAR specifies a minimum conduit-to-
conduit physical separation of ~/z-inch (Section 02.1 of this report); and (2) the logic
sy'tem functional testing of the anticipated transient without scram-recirculation pump trip
of the low frequency motor generator on high pressure
had not been performed due to a
non-conservative interpretation of the Unit 2 UFSAR (Section E8.3 of this report).
I. OPERATIONS
01
Conduct of Operations (71707)
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General Comments
Using NRC Inspection Procedure 71707, the resident inspectors conducted frequent
reviews of ongoing plant operations to verify that the units were operated safely:
and in accordance with licensee procedures
and regulatory requirements.
The
reviews included tours of both accessible
and normally inaccessible
areas of both
units, verification of engineered
safeguards features
(ESF) system operability,
verification of adequate control room and shift staffing, verification that the units
were operated in conformance with technical specifications, and verification that
logs and records accurately identified equipment status or deficiencies.
In general,
the conduct of operations was professional and safety-conscious;
specific events
and noteworthy observations
are detailed in the sections below.
01.2
Initiation of a Unit 2 Plant Shutdown due to Ino erable Containment Atmos heric
Gaseous
Particulate Radiation Monitors
a.
Ins ection Sco
e
The inspectors assessed
NMPC's performance in response to a failure of the.
Division II containment atmosphere gaseous/particulate
radiation monitor concurrent
with the Division I monitor being inoperable for preplanned maintenance.
The
inspectors observed Unit 2 control room troubleshooting activities and initiation of
the reactor shutdown,
The inspectors reviewed the Station Shift Supervisor's
(SSS)
logs, applicable procedures,
and technical specifications (TS), and discussed
related
issues with on-duty operators, technicians,
and management.
In addition,
discussions were held with NRC management
and technical staff members from the
Region
I Office and the Office of Nuclear Reactor Regulations (NRR) with regard to
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Topical headings such as 01, MB, etc., are used in accordance with the NRC standardized reactor inspection report outline.
Individual reports are not expected to address all outline topics.
The NRC inspection manual procedure or temporary instruction
(Tl) that was used as inspection guidance is listed for each applicable report section.
Observations
and Findin s
On January 7, 1998, at 4:41 a.m., Unit 2 experienced
a failure of the Division II
containment atmosphere gaseous/particulate
radiation monitor (2CMS"CAB10B).
At the same time, the redundant Division I radiation monitor (2CMS"CAB10A) was
out-of-service for maintenance to replace
a portion of the heat trace circuitry. With
both divisions of containment radiation monitoring inoperable, the Unit 2 operators
entered TS 3.0.3, which required actions be initiated within one hour to shutdown
the reactor, and to place the mode switch in STARTup within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. At
5:35 a.m., the operators commenced
a reactor shutdown.
Attempts to return 2CMS"CAB10Ato service were unsuccessful.
The licensee's
initial troubleshooting determined that both divisions of containment radiation
monitoring failed due to moisture intrusion.
NMPC determined that they would not
be able to return the monitors to an operable status within the 6-hours allowed by
TS before having to complete the reactor shutdown.
Therefore, NMPC notified the
NRC and requested enforcement discretion to delay the shutdown during restoration
of the equipment, and avoid an unnecessary
plant shutdown.
NMPC continued to
reduce reactor power and, at 11:23 a.m., with the reactor at 50% power, Region
I
verbally granted enforcement discretion from the TS requirements until 9:00 a.m. on
January 8, 1998. The enforcement discretion was granted provided that during the
discretionary period:
(1) drywell atmospheric grab samples would be taken and
analyzed every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, and (2) primary containment floor and equipment drain
leakage detection systems would be monitored every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
Subsequently,
on
January 9, 1998, a written Notice of Enforcement Discretion (NOED) was issued.
Further licensee troubleshooting determined that 2CMS"CAB10B(Division II) failed
due to a defective flow control transducer board, and not due to moisture-intrusion.
The board was replaced, and the monitor was calibrated and returned to service on
January 7, 1998, at 6:20 p.m.
Restoration of the Division II monitor allowed
NMPC'o
exit the TS shutdown actions and eliminated the continued need for NRC
2CMS "CAB10Awas returned to an operable status on
January 9, 1998.
The inspectors observed control room activities shortly after Unit 2 operators
identified that 2CMS "CAB10B had failed. The operators'ctions
were consistent
with the licensee's procedures
and TSs,
Troubleshooting and repair activities were
methodical.
The inspectors observed the Unit 2 Station Operating Review
Committee (SORC) meeting that discussed the basis for requesting enforcement
discretion and noted that the SORC members maintained the proper safety focus
throughout the meeting.
In addition, during the period enforcement discretion was
granted, the inspectors verified that the drywell atmospheric grab samples were
taken and analyzed every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, and that the primary containment floor and
equipment drain leakage detection system were monitored every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.
Conclusion
Unit 2 operators responded appropriately to the failure of the Division II containment
atmosphere
gaseous/particulate
radiation monitor that occurred while the Division I
monitor was inoperable for maintenance.
SORC members maintained the proper
safety focus during the meeting to discuss the basis for requesting-enforcement
discretion.
Identification of a Reactor Fuel Leak at Unit 2
Ins ection Sco
e
The inspectors assessed
NMPC's identification of a reactor fuel leak at Unit 2, and
subsequent
actions to address the leak.
The inspectors reviewed plant operating
data, licensee procedures,
and other related documentation, including the Unit 2
UFSAR. The inspectors observed portions of the flux tilting and power suppression
evolution. Additionally, the inspectors discussed the issue with the Unit 2 Plant
Manager and Operations Manager, and members of the reactor engineering and
radiation monitor calibration groups.
Observations
and Findin s
On January 16, 1998, NMPC concluded that a reactor fuel leak had developed at
Unit 2. This was based on a small increase in the fuel reliability index (FRI). The
FRI is an analysis of xenon isotopes present in offgas samples,
and is used to
provide indication of fuel failure. The FRI is performed weekly at both units.
The
FRI on January 10, 1998, was 75 microcuries per second (pCI/sec), which was a
significant increase over the previous readings that ranged between 10 and
20 pCI/sec.
However, offgas activity remained relatively steady.
NMPC discussed
the indications with General Electric (GE) and, on January 16, concluded that a
small fuel leak existed and had probably developed late in December 1997.
Based on the increase
in FRI, NMPC initiated the "Level 1" actions, as described in
Procedure
FRG-1, "Fuel Reliability Guidelines."
The initiation of Level
1 actions
was conservative since FRG-1 defines a Level
1 condition as a FRI greater than
100 pCI/sec above the cycle baseline.
Plans were developed to locate the fuel
leak(s) and to suppress the power in the vicinityof the leak(s).
During the interim,
control rod movement at Unit 2 was minimized to avoid aggravating the leak.
To facilitate locating the leaking fuel, NMPC connected
a continuous on-line isotopic
monitor. The isotopic monitor alleviated the need to obtain and analyze chemistry
samples, therefore minimizing the time between control rod manipulations.
The on-
line isotopic monitoring equipment required changes to the Unit 2 UFSAR sections
associated with the plant radiation monitors.
The changes were reviewed in
accordance with Title 10 of the Code of Federal Regulations, Part 50.59 (10 CFR 50.59)
~ Additionally, NMPC Procedure. N2-REP-31, "Power Suppression Testing,"
was revised to incorporate the use of the on-line isotopic monitoring,equipment.
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The inspectors reviewed these changes,
including the 10 CFR 50,59 safety
evaluation, and found them acceptable.
On January 23, Unit 2 operators commenced
a down power to 55% and began
power suppression testing in accordance with Procedure N2-REP-31.
The purpose
of the test was to identify the location of the fuel leaks by varying power through
control rod movement and observing offgas radiation changes.
NMPC considered
this test a special evolution, as defined in Procedure GAP-SAT-03, "Control of
Special Evolutions." The inspectors ob'served that appropriate management
oversight was present during the test.
The inspectors also observed that the test
was conducted
in a methodical manner and was well-controlled due, in part, to
good communication and coordination among all involved organizations.
The testing was completed on January 27, and data indicated that only one location
within the core had fuel rod leakage.
The suspected
location was between control rods 18-27, 14-27 and 14-23, with the greatest indications near control rod 18-27.
Following the testing, these three control rods were left completely inserted to
suppress the power in the location of the fuel leak.
Subsequently,
reactor power
was slowly returned to full power (95%), so as not to further aggravate the fuel
leak.
The next weekly FRI was within the normal 10 to 20yCi/sec range, indicating
that the power suppression was successful.
Historically, BWRs are normally operated with a symmetric control rod pattern.
This
was necessary to determine reactor core thermal power, since the computer
program used core mirror imaging in the calculations.
However, operating with
three adjacent control rods inserted to suppress the fuel leak resulted in an
asymmetric control rod pattern.
Unit 2 had previously updated their three
dimensional reactor core monitoring (3D Monicore) computer program to the
"Baseline 94" version.
This allowed the 3D Monicore program to automatically
account for asymmetric rod patterns.
The inspectors discussed the unusual rod
pattern with Unit 2 reactor engineering personnel and reviewed supporting
documentation from GE, and no concerns were identified.
Conclusion
Routine monitoring of the Unit 2 fuel reliability index allowed NMPC to identify a
reactor fuel leak early, before it degraded
an'y further. The flux tilting and power
suppression
evolution was methodical and well-controlled due, in part, to good
communication and coordination among all involved organizations.
NMPC took
aggressive actions to prevent further leak degradation.
Inade
uate Shift Turnover for Unit 1 Reactor 0 erator
During a tour of the Unit 1 control room soon after shift turnover, chief station
operator (CSO), a licensed reactor operator (RO), was questioned by the inspectors
as to the status of 4122 emergency cooling (EC) condenser radiation monitor,
which was inoperable due to a failed surveillance test.
The CSO had not been
informed by the off-going CSO during the shift turnover that the monitor was
r
The inspectors discussed this'weakness with the SSS and the Unit 1
Operations Manager.
Both concurred with the inspectors conclusion that the shift
turnover by the off-going CSO was weak.
02
Operational Status of Facilities and Equipment (71707)
02.1
Inade
uate Se
aration Between Conduits for Safet -Related Tem erature Elements
a 0
Ins ection Sco
e
During a visual inspection of equipment within the Unit 2 residual heat removal
(RHR) pump rooms, the inspectors questioned the physical separation between
conduits for safety-related temperature elements of different electrical divisions.
The inspectors assessed
the licensee's
actions to correct the condition, and
reviewed the applicable sections of the UFSAR and associated
plant drawings.
b.
Observations
and Findin s
On January 30, 1998, the inspectors identified that the conduit for temperature
element
2RHS "TE49Awas touching the conduit for temperature element
2RHS "TE49B. These temperature elements are powered from Division I and
Division II, respectively, and provided containment isolation signals for shutdown
cooling valves (Group 5) and reactor core isolation cooling (RCIC) steam supply
valves (Group 10). The inspectors were concerned that a fault in one division could
potentially impact the other division due to the inadequate separation.
This concern
was discussed with the on-watch Assistant Station Shift Supervisor (ASSS).
The initial response was that the Unit 2 system engineers concluded no problem
existed.
The inspectors questioned the basis for this conclusion, and learned that
there was a breakdown in communications between the ASSS and th'e system
engineers.
Specifically, the system engineers understood the problem to be with
the temperature elements and not with the conduit.
On February 6, the system
engineering staff identified the location where the conduits were touching and
informed the control room. The on-watch operators declared the two temperature
elements inoperable, and took the actions required by the TS.
In addition, NMPC
notified the NRC in accordance with 10 CFR 50.72. Work order (WO) 98-01546-00
was generated
and proper separation was established.
The inspectors reviewed the applicable plant drawings with members of the system
engineer staff and determined that a fault impacting both divisions would be no
worse than a fault impacting only one division. This was because:
(1) each
temperature element provided a signal to both containment isolation groups (Groups
5 and 10);
(2) the containment isolation system logic only required one signal for
actuation; and (3) the containment isolation system logic was designed
as fail safe.
The Unit 2 UFSAR, Section 8.3.1.4.2,,"Physical Separation," specified a minimum
conduit-to-conduit separation of ~/~-inch. The failure to maintain the Unit 2 plant
configuration in accordance with the specification provided within the UFSAR is a
violation of 10 CFR 50 Appendix B, "Quality Assurance Criteria for Nuclear Power
Plants and Fuel Reprocessing
Plants," Criterion III, "Design Control." This failure
constitutes
a violation of minor significance and is being treated as a Non-Cited
Violation (NCV), consistent with Section IV of the NRC Enforcement Policy.
(NCV 50-410/98-01-01)
C.
Conclusion
During an inspection in the Unit 2 residual heat removal pump rooms, the inspectors
identified inadequate separation between conduits for safety-related temperature
elements of different divisions.
(NCV) A breakdown in communications between
an Assistant Station Shift Supervisor and a system engineer resulted in a one week
delay in recognizing the impact that inadequate conduit separation
had on the
operability of safety-related plant equipment.
02.2
Control of Catch Containments at Unit 1
a 0
Ins ection Sco
e
The inspectors reviewed the catch containment tracking log maintained in the Unit 1
control room and performed a random sampling of catch containments installed in
the plant to assess
the adequacy of administrative controls for catch containment
installation and removal.
Issues were subsequently discussed with operations
personnel.
b.
Observations
and Findin s
During routine plant walkdowns of the Unit 1 reactor and turbine buildings, the
inspectors examined installed catch containments.
A catch containment is a device
installed below plant equipment to divert or contain water typically resulting from
component leakage or condensation.
The inspectors observed that, generally, catch
containments were adequately installed and maintained in accordance with NMPC
Procedure GAP-OPS-04, "Control of Catch Containments."
The inspectors reviewed the catch containment tracking log maintained in the Unit 1
control room and identified that the log accurately reflected the catch containments
installed in the plant. The inspectors observed that many of the catch containments
in the log were greater than five years old; approximately one-half of the current
fifty-fourcatch containments were installed between 1990 and 1993. These older
catch containments were installed either to collect condensation
or were awaiting
disposition as a "permanent" plant change.
GAP-OPS-04, Section 3.1.4, required that a catch containment designated
as
"permanent" be assessed
by system engineering to determine if a plant change was
desired and to initiate a modification as required.
The procedure required a
determination as to the continued need for each catch containment.
The inspectors
identified that many of the catch containments designated
as "permanent" did not
have documented engineering evaluations performed to determine if a plant change
0
or modification was required.
This failure to perform an engineering evaluation as
required by GAP-OPS-04 constitutes
a violation of minor significance and is being
treated as a Non-Cited Violation consistent with Section IV of the NRC Enforcement
Policy.
(NCV 50-220/98-01-02)
The inspectors identified that the required semi-annual catch containment review
had last been performed in October 1997. The inspectors considered the review to
lack sufficient depth, in that the licensee failed to fully evaluate whether catch
containments should be removed or that those catch containments designated
as
"permanent" had the required engineering evaluation performed.
Operations staff
acknowledged that catch containments were not being effectively removed or
adequately evaluated for permanent installation.
A Deviation/Event Report (DER
1-98-0078) was issued to address this concern, and the licensee performed a
detailed catch containment review. The Unit 1 Operations Manager directed that
the catch containment tracking log be updated and modified to ensure better
personnel responsibility and accountability for each log entry, and to provide
sufficient information for determining the status of engineering evaluations.
Subsequently,
approximately twenty-two catch containments were removed from
the reactor and turbine buildings.
Conclusions
Most catch containments installed in Unit 1 were adequately installed and
maintained.
However, many designated
as "permanent" did not have
an'ngineering
evaluation to determine if a plant change or modification was required.
(NCV) The most recent semi-annual catch containme'nt review, lacked depth, in that
NMPC failed to fully evaluate whether catch containments should be removed or
that those designated
as "permanent" had the required engineering evaluation.
Review of Unit 1 Extended Marku
Holdout Quarterl
Re ort
Ins ection Sco
e
The inspectors reviewed the Unit 1 extended markup/control tag/holdout quarterly
audit report and discussed findings with the Shift Technical Advisor (STA);
Observations
and Findin s
The inspectors reviewed the Unit 1 quarterly audit report of extended markups,
control tags, and holdouts.
The quarterly audit was used to determine the
continued need and applicability of each current markup on file and to ensure that
discrepancies
are documented.
Unit 1 Procedure N1-PM-Q2, "Periodic Review of
Hazardous Energy and Configuration Tagging System," provided the administrative
controls for completing the quarterly audit, which was last completed on
January 15, 1998.
/
The inspectors discussed the results with the STA, who was responsible for
coordinating the review and maintaining the quarterly audit report.
The inspectors
~
~
e
noted many weaknesses
in the maintenance of the audit report, such as:
(1) the
associated
work documents were not current, (2) the individual responsible for
completing the required work was either not listed or the name was not current, and
(3) the expected work completion date was either incomplete or indeterminate.
The
Unit 1 Plant Manager informed the inspectors that most equipment with
longstanding unavailability was not receiving engineering reviews or Plant Manager
concurrences,
as required by NMPC Procedure NIP-ECA-01, "Deviation/Event
Report." A specific example of this is a longstanding holdout on the control room
emergency ventilation system, as discussed
in Section E2.2 of this inspection
report.
I
The inspectors discussed the program implementation weaknesses
with the Unit 1
Operations Manager.
The Operations Manager was aware of the weaknesses,
which also included the administrative tracking of control room deficiencies,
operator work-arounds, and catch containments
(previously discussed
in Section
02.2). The Operations Manager issued an internal memorandum to Unit 1
management
and Operations department supervisors that delegated the
responsibility for tracking these issues to the STAs. Also, a meeting was held to
discuss past programmatic weaknesses
in tracking of longstanding holdouts.
A
draft revision to the quarterly audit report was presented
at this meeting, and
included a tracking mechanism for ensuring applicability reviews and safety
evaluations were completed.
The inspectors considered these changes to be
appropriate.
C.
Conclusions
The quarterly reviews of extended markups at Unit 1 were weak in that the
reviewers failed to identify numerous markup discrepancies that were later identified
'by the inspectors.
Unit 1 management was aware of the weaknesses,
and
proposed corrective actions appeared. appropriate.
08
Miscellaneous Operations Issues
(92901)
08.1
Closed
LER 50-410 98-01: Entr
into TS 3.0.3 Due to Containment Atmos heric
Gaseous
Particulate Radiation Monitors Ino erable
The technical issues associated with this licensee event report (LER) were described
in Section 01.2 of this inspection report.
The inspectors verified that the LER was
completed in accordance with the requirements of 10 CFR 50.73.
Specifically, the
description and analysis of the event, as contained in the LER, were consistent with
the inspectors'nderstanding
of the event.
The root cause, and corrective and
preventive actions as described in the LER were reasonable.
This LER is closed.
10
II. MAINTENANCE
M1
Conduct of Maintenance (61726, 62707)
M1
~ 1
General Comments
Using NRC Inspection Procedures
61726 and 62707, the resident inspectors
periodically observed plant maintenance activities and the performance of various
surveillance tests.
As part of the obseivations, the inspectors evaluated the
activities with respect to the requirements of the Maintenance
Rule, as detailed in
Title 10 of the Code of Federal Regulations, Part 50.65 (10 CFR 50.65).
In general,
maintenance
and surveillance activities were conducted professionally, with the
work orders (WOs) and necessary
procedures
in use at the work site, and witlithe
appropriate focus on safety.
Specific activities and noteworthy observations
are
detailed in the inspection report.
The inspectors reviewed procedures
and observed
all or portions of the following maintenance/surveillance
activities:
~
WO 94-101-01
TCV 210.1-56 to be Retired in Place
~
WO 98-00279-00
Repair Leaky Delivery Valve on Division I EDG
~
WO 98-509-02
~
N1-MMP-072-247
Clean Reactor Building
Service Water Temperature Control Valve TCV-72-146
(RBCLC) and TCV-72-147 (TBCLC) Maintenance
~
N1-MAP-MAI-0301
Scaffold Control
~
N2-OSP-ENS-M001
4.16 kV Emergency Bus Under and Degraded Voltage
Functional Test
~
N2-ISP-RDS-Q106
Quarterly Functional/Calibration of Control Rod Block
Scram Discharge Volume High Water Level Instrument
Channel
~
N2-ISP-CMS-M@001
Suppression
Pool Water Temperature Calibration
M1.2
Re lacement of Leakin
Fuel Deliver
Valve on a Unit 2 EDG
a.
Ins ection Sco
e
The inspectors observed the Unit 2 maintenance activities associated with the
replacement of a leaking fuel delivery valve on the one emergency diesel generator
2 Surveillance activities are included under
Maintenance."
For example, a section involving surveillance observations might
be inciuded as a separate sub-topic under Ml, "Conduct of Maintenance."
0
11
(EDG). Additionally, the inspectors reviewed the applicable WO and discussed
related issues with the SSS, system engineer, and maintenance
supervisor.
b.
Observations
and Findin s
On January 6, 1998, Unit 2 operators declared the Division I EDG inoperable for
pre-planned maintenance.
TS 3.8.1.1 allows the Division I EDG to be inoperable
provided that it is restored to operable within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />; otherwise, the plant is to be
in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
Due to unforeseen events,
including an unexpected trip of the EDG due to a failed optical isolator transmitter
board (see Section E8.9), the maintenance
activities were not completed until the
morning of January 9.
During the post-maintenance
surveillance test of the EDG,
one of the fuel delivery valves developed
a leak. Although the surveillance test was
considered satisfactory, the SSS decided that the EDG would remain inoperable
until the valve was replaced and tested.
This decision was made about the same
time the 72-hour portion of the TS limiting condition for operation (LCO) expired.
NMPC determined that no immediate actions would be necessary to shutdown the
reactor, since the time to replace and test the valve was expected to be short.
The inspectors observed the valve replacement.
The activity was completed in
accordance with WO 98-00279-00.
Proper Quality Assurance
(QA) and
management
oversight were noted during the activity. Upon completion of a
satisfactory post-maintenance
test, the SSS declared the EDG operable and exited
the LCO action statement.
The Unit 2 EDG system engineer informed the inspectors that cracking of fuel
delivery valves was an industry concern, initiallyidentified in May 1996. As a
result, NMPC initiated DER 2-96-1275 to evaluate the consequences
of delivery
valve failures and determined there was no adverse impact on EDG operability.
NMPC had planned to replace all the suspect valves in October 1996, but the
valves of newer design were not available for installation.
Since then, NMPC has
received the new valves, and plans to install them during the next refueling outage.
The inspectors reviewed DER 2-96-1275 and the associated
engineering supporting
analysis (ESA), which justified EDG operability with the suspect valves, and the
inspectors considered the licensee's actions to be acceptable.
C.
Conclusion
NMPC appropriately evaluated the impact of a leaking fuel delivery valve on the
operability of the Unit 2 emergency diesel generator.
0
12
M2
Maintenance and Material Condition of Facilities and Equipment (61726)
M2.1
Unit 1 Li uid Poison S stem Surveillance Testin
Deficienc
Ins ection Sco
e
NMPC initiated a normal reactor shutdown of Unit I based on the liquid poison
system being declared inoperable due to a section of piping not being previously
tested.
The inspectors discussed the issue with the Unit 1 Operations Manager and
the system engineer, and reviewed the event notification.
b.
Observations
and Findin s
In the summer of 1997, the inspectors had monitored a monthly surveillance test of
the Unit 1 liquid poison system.
The inspectors, through discussions with operators
and the inservice testing (IST) supervisor, identified that all current liquid poison
system surveillance tests were performed with the liquid poison pumps taking a
suction from a test tank filled with demineralized water.
This system configuration
maintained the pump suction valves closed, and isolated the section of piping from
the liquid poison tank to the pump suction valves.
The inspectors questioned the
IST supervisor as to whether the liquid poison system had been periodically tested
to confirm adequate flow through this piping. The supervisor was unable to
determine whether that section of piping had ever been previously tested.
NMPC initiallydid not question system operability. This determination was based
upon the current surveillance testing meeting the requirements
in the TSs and
UFSAR, that the system design included tank heaters
and temperature indicators,
and that the piping under concern was insulated and heat-traced.
However, the IST
supervisor informed the inspectors that Unit 2 TSs required periodic flow verification
through the section of piping from the liquid poison tank to the pumps, at least
every eighteen months, to ensure the system was unobstructed.
The IST
supervisor also contacted other nuclear facilities to determine if this section of
piping was periodically tested throughout the industry.
Based upon this further
information from these facilities, the IST supervisor informed the inspectors that a
procedure would be developed to periodically take suction from the liquid poison
tank, and that the procedure would most likely be conducted during the next
refueling outage.
In January 1998, the inspectors queried Unit 1 staff as to the status of the
proposed liquid poison system surveillance test procedure.
The inspectors question
received a higher level of NMPC management attention.
After subsequent
management
review, NMPC concluded that the ability to readily ascertain whether
the piping from the liquid poison tank to the pump suction valves was unobstructed
was in question, and the system was declared inoperable on January 21, at
7:35 a.m.
The licensee commenced a,normal orderly shutdown within one hour of
declaring the system inoperable, as required by Unit 1 TS 3.1.2.e.
The inspectors
considered the licensee's decision to declare the liquid poison system inoperable
13
and commence
a shutdown to be conservative,
and the actions to test the system
to be appropriate.
In parallel with the shutdown, the licensee developed and approved
a surveillance
test to verify system flow when taking suction from the liquid poison tank.
The
inspectors observed the special evolution brief conducted prior to performing the
test.
The senior manager and the principal test engineer for the brief were the
Unit 1 Operations Manager and an off-shift Senior Reactor Operator, respectively.
The inspectors considered the special evolution brief to be thorough, in that it
detailed the purpose of the test and emphasized
procedural adherence,
communications,
and abort criteria.
The inspectors monitored the special evolution
locally in the reactor building, and determined that NMPC personnel performed the
test adequately.
The test results confirmed that no obstruction existed, and that
the liquid poison system could establish adequate flow when taking suction from
the liquid poison tank.'he test results received
a timely and adequate
supervisory
review and the liquid poison system was declared operable at 2:30 p.m. The
shutdown was discontinued and power ascension
commenced, with full power
achieved at 4:35 p.m.
The Operations Manager informed the inspectors that routine performance of this
test would occur on a cyclic basis.
The inspectors agreed with NMPC that the
testing requirements for the liquid poison system, as discussed
in Unit 1 TSs and
the UFSAR, had been met.
However, the lack of a questioning attitude to routinely
demonstrate that the entire liquid poison system was capable of performing the
required function was considered
a weakness.
The failure to periodically verify that
the liquid poison system was operable from the liquid poison tank to the pump
suction valves is a violation of 10 CFR 50, Appendix 8, Criterion XI, "Test Control,"
which requires that a test program be established to assure that all testing required
to demonstrate
a system willperform satisfactorily in service is identified and
performed in accordance with written procedures.
(VIO 50-220/98-01-03)
Conclusions
Based upon inspectors questions,
NMPC management declared the Unit 1 liquid
poison system inoperable.
Portions of the system piping had not been periodically
flow tested and NMPC was unable to readily ascertain whether the piping from the
liquid poison tank to the pump suction valves was obstructed.
NMPC's decision to
declare the liquid poison system inoperable and commence
a shutdown was
conservative,
and the actions taken to test the system. were appropriate. The
special evolution brief was thorough.
Although the previous Unit 1 liquid poison
system surveillance testing met technical specification requirements, the testing
was inadequate to verify system operability.
(VIO)
M8
Miscellaneous Maintenance Issues (92700, 92902)
M8.1
Administrative Closure of Escalated Enforcement Items
The escalated
enforcement items (EEls) listed below are being administratively
closed, due to the issuance of the indicated enforcement action (EA) letter and
associated
determination.
EEI 50-220/96-12-01:
EEI 50-220/96-12-05:
EEI 50-220/96-1 2-06:
EEI 50-220/96-12-07:
closed by EA 97-007, withdrawn
closed by EA 97-007, withdrawn
III. ENGINEERING
E1
Conduct of Engineering (37551)
E1.1
General Comments
Using NRC Inspection Procedure 37551, the resident inspectors frequently reviewed
design and system engineering activities, including justifications for operability
determinations,
and the support by the engineering organizations to plant activities.
E2
Engineering Support of Facilities and Equipment
(37551)
E2.1
Maintenance on Unit 1 Service Water Valve Violated Secondar
Containment
~lnte rit
a.
Ins ection Sco
e
During preparation for maintenance
on a service water valve in the Unit 1 reactor
building, NMPC identified that the maintenance
had the potential to jeopardize
secondary containment integrity. The inspectors discussed the issue with the SSS
and the system engineer, reviewed the event notification and the revised WO, and
observed the rescheduled
maintenance activities on the service water valve.
b.
Observations
and Findin s
On January 27, 1998, during preparations for routine maintenance
on the Unit 1
reactor building service water drag valve (TCV-72-146), the system engineer for
the service water system questioned whether the planned maintena'nce
could
jeopardize secondary containment (reactor building) integrity. On January 29,
NMPC determined that the maintenance
did provide a possible pathway to violate
secondary containment, and placed the planned maintenance
on hold.
In addition,
because this evolution was routinely performed, most recently on December 11,
15
1997, an event notification to the NRC was initiated in accordance with 10 CFR 50.72.
F
The planned maintenance was the routine replacement of the internal strainer in the
drag valve; to perform this, the valve bonnet must be removed.
Since there is no
downstream valve,'the drag valve cannot be isolated.
Unit 1 TS, Section 3.4.1,,
limits the reactor building leakage rate to 1600 cubic feet per minute (cfm). If
service water was lost during the maintenance,
a pathway from the reactor building
to the outside atmosphere would exist,'xceeding the TS limitfor reactor building
leakage.
Previously, the maintenance was performed without entering the
associated
LCO. The LCO allowed four hours to return the leakage rate to within
allowable limits, or initiate a shutdown and be in cold shutdown within the next ten
hours.
Normally, the valve bonnet was removed for greater than four hours, thus
exceeding the allowable LCO time frame.
The failure to initiate an orderly shutdown
after the bonnet was removed for greater than four hours was a violation of the
Unit 1 TS, Section 3 4.1. This non-repetitive, licensee identified and corrected
violation is being treated as a Non-Cited Violation, consistent with Section VII.B.1
of the NRC Enforcement Policy.
(NCV 50-220/98-01-04)
The inspectors reviewed the associated
work order (WO 98-00509-02), the
mechanical maintenance
procedure (N1-MMP-072-247), the markup (1-98-87), the
service water system piping and instrumentation drawing (C-19022-C), and other
related documentation.
The inspectors observed performance of the drag valve
strainer replacement on February 7.
The WO was appropriately revised to include a
statement of plant impact:
"breaching of service water pressure boundary is a
breach of secondary containment."
Because of difficulties encountered
in the past
when removing the valve bonnet from the valve body, a jacking device was
manufactured to aid in this portion of the task.
In addition, to ensure that the
bonnet would be removed for no more that four hours, the maintenance technicians
conducted
a "dry-run" of the evolution prior to'performing the actual work. The
inspectors noted several maintenance
supervisors and managers present at the job-
site observing the work, The inspectors considered the preplanning of the work and
the dry-run to be significant contributors in being able to complete the work in less
than two hours.
The inspectors identified that the attached permit for the scaffold being used for the
maintenance
indicated that the expected load was 600 pounds and that the scaffold
was erected for an indefinite period of time. The inspectors discussed with one of
the maintenance
supervisors
in the area the fact that the maintenance
personnel
and tools on the scaffold platform exceeded the expected load.
The supervisor
stated that this had been identified the day before, and that the actual capacity was
1050 pounds.
The inspectors then questioned whether the scaffold had been
analyzed for permanent installation.
Review by NMPC identified that the scaffold
had not been appropriately processed for permanent installation in accordance with
Procedure N1-MAP-MAI-0301,"Scaffold Control," Revision 8; specifically,
paragraph 1.2.2 requires that scaffolding used as a permanent platform be
processed
as a design change.
DER 1-98-325 was initiated to document the
problem and initiate corrective action.
The failure to perform a design change for
16
the permanently installed scaffold constitutes
a violation of minor significance and is
being treated as a Non-Cited Violation, consistent with Section IV of the'NRC
(NCV 50-220/98-01-05)
Conclusion
As a result of a good questioning attitude by a system engineer,
NMPC identified
that maintenance
on the Unit 1 service water drag valve in the reactor building
violated secondary containment integrity. Past maintenance
on the valve exceeded
the allowable limiting condition for operation outage time, and a reactor shutdow'n
had not been initiated in accordance with the technical specification requirements.
(NCV) The inspectors identified that NMPC failed to perform a design change for
permanently installed scaffolding.
(NCV)
Lon standin
Holdout on Tem erature Control Valve for Unit 1 Control Room
Emer enc
Ventilation S stem
Ins ection Sco
e
The inspectors identified a yellow holdout on the control room emergency
ventilation system (CREVS) temperature control valve (TCV) dating from 1992. The
inspectors questioned the SSS and determined that the valve was inoperable.
The
inspectors reviewed the holdout log, the WO, the DER, the UFSAR, and the
associated
procedures.
Observations
and Findin s
During a tour of the Unit 1 control room, the inspectors identified a yellow holdout
(YHO 1-92-10045) on the temperature control valve (TCV 210.1-56) for the
CREVS. The YHO was dated January 16, 1992.
Discussions with the SSS
revealed that the TCV had been inoperable since the early 1980s.
The TCV is a three-way control valve for the chilled water to the control room
ventilation area coolers.
The TCV controller failed as a result of aging, and a one-
for-one replacement was not available.
In 1983, a bypass valve around
TCV 210.1-56 was installed per modification N1-83-61. The bypass was to ensure
maximum cooling and maintain the control room temperature below 75 degrees
Fahrenheit,
as stated in the UFSAR, for protection of vital equipment and personnel
comfort. This portion of the ventilation system was also part of the control room
emergency ventilation system (CREVS). The CREVS would be initiated if the
radiation monitors in the ventilation intake from outside detected
a high radiation
level, such as the result of a main steam line break outside containment.
101-01 was initiated in 1994 to replace the TCV controller.
In May 1996, DER 1-
96-1223 was initiated to document the longstanding YHO, and to note that the
system drawing failed to include the bypass valve or indicate that the TCV was
failed open.
The disposition for the DER was to retire the TCV in place; the DER
also noted that a safety evaluation would be required since the TCV was shown on
an UFSAR drawing. The scheduled completion date was December 18, 1997. The
17
DER further stated that the control room temperature could be regulated by
positioning the ventilation dampers.
The DER stated that engineering had evaluated
that the current system operation would not impact the intent of the system design.
The TCV was added to the "Plant Equipment Retirement List" per Technical
Department Instruction N1-TDI-18, "Equipment Retirement."
The Plant Equipment
Retirement List was a tracking mechanism for out-of-service equipment, but the TDI
still required documentation to be completed before the equipment was formally
retired-in-place.
As of the date of the inspection, no action had been taken to
complete this documentation.
Subsequent to the end of the inspection period,
NMPC management decided to attempt to repair the valve or find a replacement
"
controller, if possible.
NMPC Procedure GAP-DES-03, "Control of Temporary Modifications," defines
temporarily lifted leads that modify the electrical circuit design or configuration as
an example of a temporary modification. The procedure further states that
temporary alterations identified and controlled by other administrative processes
are
exempt from the requirements of the procedure.
However, GAP-DES-03, Section
1.2, specifically states that, even though excluded from the temporary modification
procedure requirements, the exemptions are not excluded from the requirements of
NMPC Procedure NIP-SEV-01, "ApplicabilityReviews and Safety Evaluations."
As
of the date of the inspection, NMPC had not performed either an applicability review
or a safety evaluation.
This is a violation of the Unit 1 TS, Section 6.8.1, which
requires procedures to be implemented, as written. (VIO 50-220/98-01-06)
C.
Conclusion
The inspectors identified that the temperature control valve for the Unit 1 control
room emergency ventilation system had been inoperable since 1983. The
administrative controls to disposition the failed valve had not been properly
implemented; i.e., the controlled drawings did not indicate the inoperable valve, nor
was an engineering evaluation performed, as required by procedures, to determine if
continued operation with the degraded condition was acceptable.
(VIO)
E8
Miscellaneous Engineering Issues (90712, 92700, 92903)
E8.1
Closed
LER 50-410 97-05-01: Hi h Pressure
Core S
ra
S stem Ino erable Due
to Failed Unit Cooler
The technical issues associated with this LER were described in NRC Inspection
Report (IR) 50-410/97-04, Section 02.2.
The inspectors completed an in-office
review of the additional information provided in LER 50-410/97-05, Supplement
1,
and found it acceptable.
This LER is closed.
18
E8.2
Closed
LER 50-220 97-10-01:TS Re uired Shutdown Due to Emer enc
Coolin
Condenser Tube Leak
The technical issues associated with this LER were described in NRC IR 50-220/
97-07, Section 01.2; NRC IR 50-220/97-11, Section M1.2; and NRC IR 50-220/
97-12, Section E8.7.
Subsequent to the original LER, the licensee identified
additional information pertinent to the event and included that information in
Supplement
1 to the LER. The inspectors performed an in-office review of the
LER supplement.
NMPC concluded that the EC condenser tube failures resulted from a combination of
thermal fatigue and intergranular stress corrosion cracking due to the upper tubes of
the EC condenser tube bundles being in a continuous steam condensing mode.
The
licensee determined the root cause of the failed tubes resulted from an original
design deficiency, in that the EC condenser return isolation valve leakage limitations
were not specified.
NMPC also stated that an opportunity was missed to identify
this condition during a 1977 modification, in which an originally installed
temperature
alarm system was modified without a thorough understanding of the
system design basis.
This modification resulted in masking the normal operating
water level in the EC condenser steam inlet piping.
The LER supplement further detailed isotopic analysis reviews by the Unit 1
chemistry department,
and NMPC concluded that small EC condenser tube leaks
likely existed since March 1996.
NMPC also included in the LER supplement that:
(1) dose calculations for the quarter ending September were well below TS offsite
dose limits, (2) the EC system decay heat removal function was not significantly
affected by the EC condenser tube degradation,
and (3) the EC system station
blackout and 10 CFR 50 Appendix R functions could have still been performed.
The inspectors verified that the LER supplement was completed in accordance with
the requirements of 10 CFR 50.73. Specifically, the description and analysis of the
event, as contained in the LER supplement, were consistent with the
inspectors'nderstanding
of the event.
The inspectors considered the root cause and
corrective and preventive actions as described
in the supplement were reasonable.
This LER supplement
is closed.
E8.3
Closed
LER 50-410 97-13: Prior to 1992
Emer enc
Switch ear Not Seismicall
Qualified With Breakers Racked Out
a.
Ins ection Sco
e
The inspectors reviewed the details associated with the LER and the applicable DER
and procedures.
In addition, the inspectors reviewed the LER to verify completion
in accordance with 10 CFR 50.73.
'I
E
19
Observations
and Findin s
On October 29, 1997, NMPC determined that prior to April 30, 1992, Unit 2 had
racked out circuit breakers from 4160-volt switchgear such that the switchgear no
longer met seismic requirements.
The licensee identified this issue during a review
of NRC Information Notice (IN) 97-53, "Circuit Breakers Left Racked Out in Non-
Seismically Qualified Positions."
A member of the Unit 2 operations support staff
noted that other licensees
had reported similar conditions, but no report could be
located for Unit 2.
~On March 27, 1992, while Unit 2 was shutdown for refueling, NMPC initiated DER
2-92-Q-1144to address the seismic qualification of circuit breakers
in the racked
out condition. The initial SSS review of the DER concluded that operability and
reportability determinations were not applicable.
During the DER disposition, NMPC
design engineering determined that the switchgear were only seismically qualified
with the breakers racked in. Therefore, the switchgea'r would have been inoperable
during situations with breakers racked out,
Prior to April 30, 1992, the practice at
Unit 2 was to rack out circuit breakers for an extended period, although the practice
was limited to only one safety division at a time.
In 1997, NMPC concluded that prior to April 30, 1992, they had probably racked
out breakers in excess of eight hours.
When a division of AC (alternating current]
was energized, Unit 2 TS 3.8.3.1 required the division to be reenergized within
eight hours or be in at least HoT sHuTDowN within the next twelve hours.
Based on
DER 2-92-Q-1144, NMPC revised the applicable procedures to halt the practice of
leaving circuit breakers in the racked out position.
The inspectors considered the
actions taken to prevent recurrence to be appropriate and effective, based on
current observations during plant tours.
However, the failure to meet the
requirements of TS 3.8.3.1, prior to April 30, 1992, was a violation. This non-
repetitive, licensee-identified and corrected violation is being treated as a Non-Cited
Violation, consistent with Section VII.B.1 of the NRC Enforcement Policy.
(NCV.50-41 0/98-01-07)
Although NMPC took adequate
actions in 1992 to discontinue the practice of
racking out breakers, they failed to recognize during their review that the practice
had placed them in an unanalyzed condition, and that the condition was reportable.
The failure to report an unanalyzed condition to the NRC is a violation of 10 CFR 50.72 and 50.73. This failure constitutes
a violation of minor significance and
is'eing
treated as a Non-Cited Violation, consistent with Section IV of the NRC
(NCV 50-410/98-01-08) As described
in the LER, the reason
for not recognizing reportability could not be determined, but a contributing factor
was that the DER process
in 1992 was not clear relative to the reporting
requirements.
Since 1992, improvements have been made to the DER procedure,
and plant personnel were trained on the reporting requirements.
The inspectors
have reviewed the DER procedure and,considered
the reportability guidance to be
acceptable.
20
The inspectors verified that the LER was completed in accordance with the
requirements of 10 CFR 50.73.
Specifically, the description and analysis of the
event, as contained in the LER, were consistent with the inspectors'nderstanding
of the event.
The root cause and corrective and preventive actions as described
in
'he
LER were reasonable.
This LER is closed.
C.
Conclusion
Prior to April 30, 1992, Unit 2 operated with circuit breakers in the racked out
position, and failed to recognize the adverse impact on switchgear seismic
qualification and, therefore, switchgear operability.
appropriate actions in 1992 to preclude future operations with breakers in the
racked out position, they failed to recognize that they were in an unanalyzed
condition, and that the condition was reportable.
(NCV)
E8.4
Closed
LER 50-410 97-16: Missed TSSR 4.3.4.1.2 for ATWS-RPT Tri of LFMG
Ins ection Sco
e
The inspectors reviewed the details associated with the LER and the applicable
DERs, TSs and UFSAR sections.
The inspectors reviewed surveillance test
procedures
and applicable plant drawings, and discussed with members of the
NMPC engineering and licensing staffs the ATWS-related testing performed at
Unit 2.
In addition, the inspectors reviewed the LER to verify completion in
accordance with 10 CFR 50.73.
b.
Observations
and Findin s
While drafting the LCOs for the ATWS-RPT [anticipated transient without scram-
recirculation pump trip] section of the Unit 2 improved technical specifications (ITS),
NMPC noted that the current logic system functional testing (LSFT) for the ATWS-
RPT did not include the trip of the low frequency motor generator (LFMG) on high
reactor pressure,
as described in the basis for the ITS.
DER 2-97-3105 was
initiated to document the concern, which was identified on November 7, 1997,
while Unit 2 was shutdown for repair to a recirculation flow control valve. Although
NMPC was evaluating whether testing was required by their current TSs, they
made a one-time revision to the applicable surveillance test procedure and, on
November 9, satisfactorily tested the trip of the LFMG on high reactor pressure.
Subsequently,
on December 3, 1997, NMPC determined that the LSFT of the
ATWS-RPT of the LFMG trip for high reactor pressure was required by technical
specification surveillance requirement (TSSR) 4.3.4.1.2.
The inspectors reviewed the applicable UFSAR and TS sections, and DERs.
The
inspectors determined that the failure to previously complete LSFT of the ATWS-
RPT LFMG trip on high reactor pressure was a violation of TSSR 4.3.4.1.2.
This
failure constitutes
a violation of minor significance and is being treated as a Non-
Cited Violation, consistent with Section IV of the NRC Enforcement Policy.
(NCV 50-41 0/98-01-09)
21
NMPC stated in the LER that the same issue had been previously reviewed through
DER 2-96-3268, initiated in December 1996.
During that review, NMPC had
determined that testing of the ATWS-RPT LFMG trip on high reactor pressure was
not necessary to satisfy TSSR 4.3 4.1.2. The basis, as stated in the LER, was that
the LFMG trip on high reactor pressure did not affect the transients, since during the
ATWS the peak reactor pressure
and peak cladding temperature would have
occurred before the 25-second time delay would have caused the LFMG to trip.
The inspectors discussed the testing requirements
and UFSAR description with
members of NMPC's engineering, technical support, and licensing groups.
The
discussions
also focused on how the licensee reached their incorrect conclusion in
1996 that the testing was not required.
The inspectors determined that the
conclusion was based on a non-conservative
interpretation of the UFSAR.
The inspectors, with members of the Unit 2 system engineering staff, reviewed the
applicable procedures
and plant drawings and verified that the revised surveillance
test adequately tested the time delay and the LFMG trip. The inspectors noted that
although the licensee recorded the actual time delay observed during the test, they
did not provide an acceptable
range of values.
Through discussions with the
Engineering Manager, the inspectors ascertained that, based on an engineering
determination, the times obtained were acceptable.
The inspectors also discussed
with the Maintenance and Engineering Managers, the failure to specify an
acceptable
range.
They agreed that the failure to specify acceptable values was a
poor practice; a DER was written to review this further. The inspectors considered
the failure to specify an acceptability range for the LFMG time delay as a weakness
in the procedure and in the review of the associated
procedure change.
The inspectors verified that the LER was corn'pleted in accordance with the
requirements of 10 CFR 50.73.
Specifically, the description and analysis of the
event, as contained in the LER, were consistent with the inspectors'nderstanding
of the event.
The root cause and corrective and preventive actions as described
in
the LER were reasonable.
This LER is closed.
Conclusion
NMPC identified that a portion of the Unit 2 testing for the recirculation pump trip in
response to an anticipated transient without scram was not completed in
accordance with the technical specifications.
(NCV) Specifically, the logic system
functional testing failed to include the high reactor pressure trip of the low
frequency motor generator.
In addition, the failure to specify an acceptability range
for the LFMG time delay in the subsequent
procedure change procedure indicated
weaknesses
in the procedure and in the review of the associated
procedure change.
Furthermore, in December 1996, NMPC missed an opportunity to identify the
inadequate
surveillance test due to a non-conservative interpretation of the UFSAR.
0
22
Closed
VIO 50-220 96-07-03: UFSAR Drawin
Chan
ed Without Performin
a
10 CFR 50.59 Safet
Evaluation
The inspectors performed an in-office review of the licensee response to an
inadequate
10 CFR 50.59 safety evaluation for a proposed revision to the Unit 1
UFSAR service water system drawing.
The preliminary safety evaluation incorrectly
concluded that the UFSAR was unaffected.
Therefore, no safety evaluation was
performed.
The licensee's root cause and corrective actions for the violation, as
stated in their November 1996 response to the NRC, were appropriate.
conducted
a random sample review of preliminary safety evaluations generated
between 1990 and 1994 to determine the potential scope of the issue.
The
inspectors determined that the licensee's review was thorough.
The inspectors
considered the actions to prevent recurrence to be adequate.
Based upon the
inspectors'eview,
the violation is closed.
Closed
10 CFR 21 Notification: Potentiall
Defective Diesel Generator Air Start
Ins ection Sco
e
The inspectors reviewed the details associated with the 10 CFR 21 (Part 21)
notification regarding potentially defective Graham-White air start solenoid valves
for EMD EDGs, and NMPC's evaluation for applicability to both units.
The
inspectors reviewed the applicable DER for each unit and discussed the related
issues with members of NMPC's engineering staff.
Observations
and Findin s
On January 22, 1998, Engine Systems, Inc. (ESI) issued
a Part 21 notification (SC
97-04Property "GE part 21" (as page type) with input value "SC</br></br>97-04" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.) pertaining to possibly defective air start solenoid valves used with EMD
EDGs.
Specifically, in 1990 the valves were modified with a larger internal spring
to reduce air leakage past the valves.
However, ESI recently determined that with
the increased spring size, the valves may not operate satisfactorily with a combined
low air system pressure ((200 pounds per square inch gage (psig)) and low
solenoid coil voltage ((105 volts direct current (Vdc)).
ESI recommended that (1) if
the minimum coil terminal voltage could not be maintained, then the internal spring
should be replaced with an appropriately-sized
spring, and (2) if the valve springs
were not replaced, then the licensee should test an installed or spare solenoid valve
to verify proper operation at the site specific minimum air pressure
and voltage.
NMPC reviewed the Part 21 and identified that both Unit 1 EDGs and the Unit 2
Division III (high pressure core injection system) EDG contained the suspect valves.
At Unit 1, the licensee determined that the worst-case condition would be a system
air pressure of 191 psig combined with a solenoid coil terminal voltage of 100.2
Vdc. This worst case voltage was based on end-of-life battery conditions.
determined that for a minimum system air pressure of 191 psig, a coil voltage of
107 Vdc would be sufficient to ensure proper valve operation.
Since both Unit 1
23
station batteries were replaced in the Spring 1997, NMPC recalculated coil terminal
voltage using an appropriate aging factor for the current condition of the installed
batteries,
and concluded that coil terminal voltages were adequate to ensure valve
operability.
However, this evaluation only provided a short-term justification, and
based on discussion with the EDG system engineer, NMPC intends to replace the
valves in the near future.
At Unit 2, the worst case condition would be 215 psig system air pressure
combined with approximately 109 Vdc at the solenoid coil. Therefore, system air
pressure
and voltage were adequate to ensure operability of the installed valves.
'owever,
based on discussions with the EDG system engineer, NMPC was
evaluating whether to replace the valves in May 1998, during the refueling outage,
or complete the testing as recommended
by ESI in the Part 21.
The inspectors reviewed the Part 21, and considered the licensee's actions to
address the concern at each unit to be timely and technically sound.
Therefore, this
Part 21 is closed.
Conclusion
The licensee's actions at both units to address
an industry concern with potentially
defective emergency diesel generator air start solenoid valves was timely and
technically sound."
0 ened
10 CFR 21 Notification: Potentiall
Defective GE SBM-T
e Switches
Unit 1
Ins ection Sco
e
NMPC initiated a DER as a result of a General Electric Nuclear Energy (GENE) issued
Part 21 notification of a possible adverse condition related to the spring-return
function of some GE-provided control switches that could damage the associated
control circuits.
The inspectors reviewed the Part 21, the DER, and the related
operating procedures,
and discussed the issue with control room personnel.
Observations
and Findin s
On January 27, 1998, GENE issued
a Part 21 notification informing licensees of a
possible failure of certain GE SBM-ty'pe control switches having a spring-return
feature and which were manufactured after March 1996. The switches were
manufactured
as a commercial grade item by another division of GE; GENE then
dedicated the switches and supplied them to nuclear power plants as a basic
component for safety-related applications.
In early January 1998, GENE was
notified by another licensee of a failure of one of the switches to automatically
spring return to the normal position; subsequently,
GENE was notified of several
other failures.
GENE determined that the most probable failure mode was
mechanical binding internal to the switch. The Part 21 listed two safety concerns:
(1) possible damage to the control circuitry, and (2) the possibility that the control
~
~
circuits would not be able to perform the safety function due to the failure to reset
to the normal position.
NMPC identified that seven GE SBM-type switches manufactured after March 1996
were installed in safety-related functions in Unit 1: control switches for the EC
condenser vent-to-torus blocking valves; containment spray bypass-to-torus
blocking valves; and the containment spray test-to-torus flow control valve.
engineering initiated DER 1-98-0202to resolve this concern.
The inspectors reviewed the DER and Part 21 notification, and discussed the issue
with the maintenance engineer responsible for the disposition.
In addition, the
inspectors discussed the potential failure mechanism with Unit 1 control room
operators; all operators interviewed were knowledgeable of the need to ensure that
the switches were returned to the normal position.
The inspectors also reviewed
the affected procedures.
Neither Procedure N1-OP-13, "Emergency Cooling
System" or Procedure N1-OP-14, "Containment Spray System" contained
a
precautionary note about the possible failure of the spring return switches.
This
was discussed with the ASSS, who stated that he would discuss the development
of a temporary procedure change with his management.
The NRC willreview the
DER disposition upon completion.
This will be tracked as an open Part 21 item.
Conclusion
NMPC responded quickly and appropriately to a vendor notification related to a
possible failure of spring-return switches used in the emergency cooling and
containment spray systems at Unit 1. Control room operators were aware of the
potential failure mode; however, the associated
operating procedures
had not been
revised to include a precautionary note related to the concern.
Closed
URI 50-220 96-05-03: Lack of 10CFR50.59 Safet
Evaluation for the
Modification to Restore the Unit 1 Blowout Panels to Com liance with UFSAR
During the NRC Special Inspection 50-220/96-05regarding
the Unit 1 reactor and
turbine building blowout panels being outside the design basis, an apparent violation
was identified regarding the lack of 10 CFR 50.59 safety evaluation for the March
1995 modification to restore the blowout panel relief pressures to compliance with
the UFSAR. Following the enforcement conference, the NRC reclassified this issue
as an unresolved item pending additional NRC review, as documented
in the letter
from the NRC to NMPC dated June 18, 1996.
Prior to March 1995, the reactor and turbine building blowout panels were fastened
with shear bolts larger than those specified on plant drawings causing the relief
pressure to be greater than that described in the UFSAR.
In March 1995, NMPC
modified the blowout panels by removing every other shear bolt, which was
intended to restore the relief pressure to that stated within the UFSAR. The
particular concern described in NRC IR,.50-220/96-05 was that, although the UFSAR
did not explicitly describe the size or spacing of the blowout panel bolting, the
change did alter the blowout panel design.
Therefore, it should have required a
25
10 CFR 50.59 safety evaluation.
Following discussions with NRR, it was concluded that this modification did not
change the system design as described
in the UFSAR, nor did it involve a change to
the TS; therefore, the modification to'restore the blowout panels to the pressure
stated in the UFSAR did not need a 10 CFR 50.59 safety evaluation.
The
inspectors had no further questions,
and this item is closed.
E8.9
Closed
Unit 2 S ecial Re ort: Division I Standb
EDG Non-valid Test and Non-
valid Failure
On January 8, 1998, the Division I EDG tripped on overspeed
during a monthly
surveillance test.
Subsequently, the licensee verified that an actual overspeed
condition did not occur, and that a fault in the test mode circuitry caused the trip.
Particularly, the optical isolator transmitter board and associated
receiver board in
the secondary start circuitry failed due to thermal aging.
The failed circuitry
provided a repeater signal to trip the EDG in an overspeed condition; however, this
signal was only utilized in the test mode and is bypassed
during the emergency
mode.
The isolator was replaced and the EDG was re-tested successfully.
The
isolator failure was documented
in DER 2-98-0033, and NMPC began evaluating the
need to replace additional isolators, as part of the DER review.
As required by TS 4.8.1.1.3, NMPC documented the EDG failure in a special report
to the NRC (NMPC letter NMP2L 1749 dated February 5, 1998).
As documented
in that report, NMPC determined that the test was non-valid based on the guidance
provided in NRC Regulatory Guide (RG) 1.108, "Periodic Testing of Diesel Generator
Units Used as Onsite Electric Power Systems at Nuclear Power Plants," because the
trip was initiated from a portion of circuitry bypassed
in the emergency mode.
The
inspectors reviewed the applicable plant drawings and confirmed that the trip would
not have occurred in the emergency mode.
The inspectors'eview of the failure,
and the guidance provided in RG 1.108, indicates that NMPC appropriately
determined that the failure and test were non-valid.
E8.10 Administrative Closure of Escalated Enforcement Items
The escalated
enforcement items (EEls) listed below are being administratively
closed, due to the issuance of the indicated enforcement action (EA) letter and
.
associated
determination:
EEI 50-410/96-15-02:
EEI 50-410/96-16-01:
EEI 50-410/96-16-02:
EEI 50-410/96-16-03:
EEI 50-410/96-16-04:
EEI 50-410/96-16-05:
EEI 50-410/96-1 6-06:
EEI 50-410/96-1 6-10:
closed by EA
closed by EA
closed by EA
closed by EA
closed by EA
closed by EA
closed by EA
closed by EA
96-475, VIO 3013
96-494, VIO 3043
96-494, VIO 3043
96-494, VIO 2023
96-494, VIO 2013
96-494, VIO 3023
96-494, withdrawn
96-494, VIO 3033
26
In addition, two of the EEls were classified as non-cited violations (NCVs) in the EA
letter; as such, these NCVs are being assigned tracking numbers in this inspection
report:
EEI 50-410/96-16-07:
EEI 50-41 0/96-1 6-08:
closed by EA 96-494, NCV 50-410/98-01-10
closed by EA 96-494, NCV 50-410/98-01-11
IV. PLANT SUPPORT
Using NRC Inspection Procedure 71750, the resident inspectors routinely monitored
the performance of activities related to the areas of radiological controls, chemistry,
security, and fire protection.
Minor deficiencies were
discussed with the responsible management,
and significant observations
are
detailed below.
R1
Radiological Protection and Chemistry Controls (71750)
R1.1
Potentiall
Contaminated Truck Released from Unit 1
On February 9, 1998, NMPC was notified that radiation levels on an empty flat-bed
trailer, released from Unit 1 on February 7, 1998, may have exceeded
levels
specified in 49 CFR, Part 173.443(c).
The trailer was placed in a secure area on
Babcock and Wilcox's property in Parks Township, Pennsylvania to await further
surveys and evaluation.
This is characterized
as an unresolved item pending
further surveys and review of the results by NRC.
(URI 50-220/98-01-12)
R8
Miscellaneous RP&C Issues (71750)
R8.1
Administrative Closure of Escalated Enforcement Items
The escalated
enforcement items (EEls) listed below are being administratively
closed, due to the issuance of the indicated enforcement action (EA) letter and
associated
determination:
EEI 50-220/97-07-07:
EEI 50-220/97-07-09:
closed by EA 97-530, VIOs 1033 & 1034
EEI 50-220 & 50-410/97-07-10:
EEI 50-220 & 50-410/97-07-12:
closed by EA 97-530, withdrawn
In addition, two of the EEls were classified as non-cited violations (NCVs) in the EA
letter; as such, these NCVs are being assigned tracking numbers in this inspection
report:
EEI 50-220 & 50-410/97-07-06:
closed by EA 97-530,
NCV 50-220 & 50-410/98-01-13
EEI 50-220 & 50-410/97-07-11:
closed by EA 97-530,
NCV 50-220 & 50-410/98-01-14
~
~
27
F2
Status of Fire Protection Facilities and Equipment (71750)
F2.1
Unit 1 Un lanned Fire Alarms and Preaction
S rinkler S stem Actuation
Ins ection Sco
e
The inspectors reviewed the circumstances
surrounding unplanned fire alarms and
preaction sprinkler system actuation at Unit 1. The inspectors evaluated control
room and fire brigade response to the event, and discussed the issue with fire
protection supervision,
b.
Observations
and Findin s
On January 8, 1997, multiple fire alarms were indicated in the Unit 1 control room
originating from local fire panels (LFPs) 3, 4, and 5 in the Unit 1'turbine building
(TB). Control room staff announced the alarms and investigation by the fire brigade
identified that a LFP-3 detection zone was in an alarm condition and that a preaction
sprinkler system had initiated on TB 261'261-foot] elevation.
Subsequently, wet
pipe sprinkler system water flow alarms were received on LFPs 3, 4 and 5 for the
offgas building, TB 291',elevation,
and TB 351'levation, respectively.
The inspectors observed licensee actions from both the Unit 1 control room and in
the TB. The fire brigade confirmed that no fire existed, and that no water had
actually been discharged to the TB. Due to inclement weather (rain and high
winds), numerous roof leaks had been detected during the day, and the licensee
identified water in an area adjacent to a fire detector located in TB 261'.
Subsequent
licensee investigation concluded that water intrusion into this detector
resulted in the initial preaction sprinkler system alarm on LFP-3. Additionally, the
licensee presumed that the false indication of the wet pipe system water flow
alarms was caused by a backup of the sprinkler system drain header, since water
had overflowed the air gap funnel drain cups associated with the wet pipe sprinkler
system on TB 261'nd TB 277'. The inspectors observed that both control "room
and fire brigade personnel responded
appropriately to the event and the
investigation effort was adequately coordinated.
Through discussions with the fire protection supervisor, previous similar
occurrences
were attributed to limited drainage on the wet pipe system common
drain header,
and that the water overflow on TB 277'as likely a result of system
backpressure.
The system had design features, including retard chambers and
check valves, to minimize the impact of system backpressure
perturbations,
producing erroneous alarms.
However, the fire protection supervisor stated that
erroneous
alarms sometimes occurred, even during routine surveillance testing.
System backpressure,
concurrent with check valve leakage, could result in pressure
switch actuations and provide false indications of wet pipe system flow on TB
261'nd
TB 291'levations.
The inspectors considered that the failure to fully
investigate and resolve previous similar, occurrences was a weakness
and likely
contributed to the recent event.
28
The licensee issued
a DER 1-98-0040 to document the issue, and several Problem
Identification (PID) entries were made to address
1) the potential poor system
drainage,
2) the roof leakage,
and 3) check valve seat leakage.
The inspectors
walked down the affected fire protection systems with the fire protection
supervisor.
The system configuration appeared to support the licensee's conclusion
for actuation of the wet pipe system flow indications.
The licensee replaced
a
check valve located on TB 261', and the inspectors observed that the check valve
body and seat revealed significant wear and corrosion, and the valve disc was
degraded.
Subsequent
discussion witlithe supervisor indicated that further
corrective action included replacement of similar-type ch'eck valves within the wet
pipe system to preclude the backpressure
spikes.
The inspectors considered
licensee corrective actions to be appropriate.
Although the inspectors did not
consider fire protection system operability to be affected by the degraded
components, the impact of the deficiencies could hinder plant personnel responding
to an in-plant fire due to potential multiple false alarms.
c.
Conclusions
Control room and fire brigade personnel appropriately responded to numerous Unit 1
fire alarm actuations,
and the investigation effort appeared
adequately coordinated.
The failure to fully investigate and resolve previous similar false fire protection
system actuations was a weakness
and likely contributed to the recent event.
Although Unit 1 fire suppression
system operability did not appear to be affected by
degraded components, the impact of the deficiencies could hinder plant personnel
responding to an in-plant fire due to potential multiple false alarms.
V. IVIANAGENENTMEETINGS
X1
Exit Meeting Summary
At periodic intervals, and at the conclusion of the inspection period, meetings were
held with senior station management to discuss the scope and findings of this
inspection.
The final exit meeting occurred on March 6, 1998.
During this meeting, the
resident inspector findings were presented.
NMPC did not dispute any of the
findings or conclusions.
Based on the NRC Region
I review of this report, and
discussions with NMPC representatives,
it was determined that this report does not
contain safeguards
or proprietary information.
ATTACHMENT1
PARTIALLIST OF PERSONS CONTACTED
Nia ara Mohawk Power Cor oration
R. Abbott
D. Barcomb
D. Bosnic
J. Burton
H. Christensen
J ~ Conway
G. Correll
R. Dean
A. DeGracia
S. Doty
K. Dahlberg
G. Helker
A. Julka
P. Mazzafero
L. Pisano
R. Randall
V. Schuman
R. Smith
R. Tessier
C. Terry
C. Ware
K. Ward
D. Wolniak
Plant Manager, Unit 1 (Acting)
Manager, Unit 2 Radiation Protection
Manager, Unit 2 Operations
Manager, Quality Assurance
Manager, Security
Vice President, Nuclear Engineering
Manager, Unit 1 Chemistry
Manager, Unit 2 Engineering
Manager, Unit 1 Work Control
Manager, Unit 1 Maintenance
Plant Manager, Unit 2 (Acting)
Manager, Unit 2 Work Control
Director, ISEG
Manager, Unit 1 Technical Support
Manager, Unit 2 Maintenance
Manager, Unit 1 Engineering
Manager, Unit 1 Radiation Protection
Manager, Unit 1 Operations
Manager, Training
Vice President,
Nuclear Safety Assess
Manager, Unit 2 Chemistry
Manager, Unit 2 Technical Support,
Manager, Licensing
ment 5. Support
INSPECTION PROCEDURES USED
IP 37551
IP 62707
IP 71714
IP 71750
IP 92700
IP 92902
IP 92904
10 CFR Part 21 Inspections at Nuclear Power Plants
On-Site Engineering
Surveillance Observations
Maintenance Observations
Plant Operations
Cold Weather Preparations
Sustained Control Room and Plant Observation
Plant Support
In-Office Review of Written Reports of Nonroutine Events at Power
Reactor Facilities
Onsite Followup of Written Reports of Nonroutine Events at Power
Reactor Facilities
Followup -, Plant Operations
Followup - Maintenance
Followup - Engineering
Followup - Plant Support,
A-1
I
Attachment
1
ITEMS OPENED, CLOSED, AND UPDATED
OPENED
50-41 0/98-01-01
50-220/98-01-02
50-220/98-01-03
50-220/98-01-04
50-220/98-01-05
50-220/98-01-06
50-41 0/98-01-07
50-410/98-01-08
50-41 0/98-01-09
50-41 0/98-01-1 0
50-41 0/98-01-1
1
50-220/98-01-1 2
50-220 &
50-41 0/98-01-1 3
NCV
NCV
NCV
NCV
Inadequate Separation Between Conduits for Safety-
Related Temperature
Elements
Failure to Perform Required Engineering Evaluations on
Longstanding Catch Containments
Liquid Poison System Surveillance Testing Inadequacy
Service Water Valve Maintenance Violated Secondary
Containment
Failure to Perform a Design Change for a Permanently
Installed Scaffold
Failure to Perform an Engineering Safety Analysis for
Inoperable CREVS TCV Failed Since 1992
Switchgear Inoperable due to Racked Out Circuit
Breakers
Failure to Report an Unanalyzed Condition
Failure to Perform LSFT of the ATWS-RPT LFMG Trip on
High Pressure
Administrative Closure of EEI 50-410/96-16-07
Administrative Closure of EEI 50-410/96-16-08
Potentially Contaminated Truck Released Offsite
Administrative Closure of EEI 50-220 & 50-410/97-07-
06
50-220 &
50-41 0/98-01-14
~
Administrative Closure of EEI 50-220 & 50-410/97-07-
11
Part 21
GE SBM-Type Switches
CLOSED
50-220/96-1 2-01
50-220/96-1 2-05
Failure to Include Six SSCs in the Scope of the
Maintenance
Rule
Ineffective Goals and Monitoring for (a)(1) SSCs
50-410/96-1 5-02
50-410/96-1 6-01
50-410/96-1 6-02
Failure to Check MOV Pressure
Locking Calculations
Control Room Chiller Deficiencies for SW Setpoints
Control Room Chillers Inoperable due to SW Setpoints
A-2
Attachment
1
50-410/96-1 6-03
50-410/96-1 6-04
50-410/96-1 6-05
50-410/96-1 6-07
50-410/96-1 6-08
Failure to Repair Control Room Chillers After Previous
TI'Ips
RCIC Lube Oil PCV Failed Open Since 1991
RCIC Design Calculations Incorrect and No Independent
Review
No Safety Evaluation Performed for RCIC PCV Failed
Open
UFSAR Not Updated When New Design for RCIC PCV
=
Installed
50-410/96-1 6-10
50-220 &.
50-410/97-07-06
50-220/97-07-07
50-220/97-07-09
50-220 5,
50-41 0/97-07-1 0
50-220 5
50-41 0/97-07-1
1
50-410/98-01-01
50-41 0/98-01-02
50-220/98-01-04
50-220/98-01-05
50-41 0/98-01-07
50-41 0/98-01-08
50-410/98-01-09
50-410/98-01-1 0
50-41 0/98-01-1
1
50-220 5
50-41 0/98-01-1 3
50-220 6
50-41 0/98-01-1 4
EEI
EEI
EEI
NCV
NCV
NCV
NCV
.NCV
NCV
Design Errors Related to RCIC
Failure to Update PCPs
Radwaste Shipment Exceeded 49 CFR Limits
Radwaste Shipments to Wrong Address
Radwaste Shipment of Wrong Liner
Failure to Identify and Correct Problems with PCPs
Inadequate
Separation Between Conduits for Safety-
Related Temperature Elements
Failure to Perform Required Engineering Evaluations on
Longstanding Catch Containments
'
Service Water Valve Maintenance Violated Secondary
Containment
Failure to Perform a Design Change for a Permanently
Installed Scaffold
Violation of TSs Switchgear Inoperable due to Racked
Out Circuit Breakers
Failure to Report an Unanalyzed Condition
Violation of TSs Failure to Perform LSFT of the ATWS-
RPT LFMG Trip on High Pressure
Administrative closure of EEI 50-410/96-16-07
Administrative closure of EEI 50-410/96-16-08
Administrative closure of EEI 50-220 5. 50-410/97-07-'06
Administrative closure of EEI 50-220 5 50-410/97-07-11
A-3
0
Attachment
1
50-410/97-05-01
50-220/97-10-01
50-410/97-1 3
50-41 0/97-1 6
50-410/98-01
50-410/98-02
50-220/96-07-03
50-220/96-05-03
Part 21
LER
LER
LER
LER
LER
LER
Potentially Defective Diesel Generator Air Start Solenoid
Valves
HPCS System Inoperable Due to Failed Unit Cooler
TS Required Shutdown Due to EC Condenser Tube Leak
Prior to 1992, Emergency Switchgear Not Seismically
Qualified with Breakers Racked Out
Missed TSSR 4.3.4.1.2 for ATWS-RPT Trip of LFMG
Entry Into TS 3.0.3 Due to Containment Atmospheric
Gaseous/Particulate
Radiation Monitors Inoperable
Violation of TS 6.2.2.b - No Licensed Operator At-the-
Controls
UFSAR Drawing Changed Without Performing a
10CFR50.59 Safety Evaluation
Lack of 10 CFR 50.59 Safety Evaluation for the
Modification to Restore the Unit 1 Blowout Panels to
Compliance with UFSAR
WITHDRAWN
50-220/96-1 2-06
50-220/96-1 2-07
50-410/96-1 6-06
50-220 5
50-41 0/97-07-1 2
Unacceptable
Performance Criteria to Verify Preventive
Maintenance was Effective
Ineffective Monitoring and Untimely Evaluation of (a)(2)
RCIC Inoperable Since 1991
Failure to Conduct Audits of Vendors Supplying
Shipping Casks
UPDATED
None
LIST OF ACRONYMS USED
ASSS
ATWS-RPT
cfm
CFR
CSO
DER
Alternating Current
Assistant Station Shift Supervisor
Anticipated Transient Without Scram - Reactor Pump Trip
cubic feet per. minute
Code of Federal Regulations
Containment Monitoring System
Control Room Emergency Ventilation System
Chief Station Operator
Deviation/Event Report
A-4
Attachment
1
EC
FRI
IN
IR
I<V
LCO
LER
LFMG
pCI/sec
NRC
Part 21
pslg
'FO
'SE
SORC
Enforcement Action
Emergency Cooling
Escalated Enforcement Item
Engineering Supporting Analysis
Engineered Safeguards
Feature
Engine Systems, Inc.
Fuel Reliability-Index
High Pressure
Information Notice
Inspection Report
Inservice Testing
Improved Technical Specifications
kiloVolt
Limiting Condition for Operation
Licensee Event Report
Low Frequency Motor Generator
Logic System Functional Testing
microCuries per second
Motor-Operated Valve
Non-Cited Violation
Niagara Mohawk Power Corporation
Notice of Enforcement Discretion
Nuclear Regulatory Commission
Title 10 of the Code of Federal Regulations Part 21
Pressure
Control Valve
Public Document Room
pounds per square inch gage
Reactor Building Closed Loop Cooling
Reactor Core Isolation Cooling
Refueling Outage
Regulatory Guide
Reactor Operator
Safety Evaluation
Station Operating Review Committee
Senior Reactor Operator
Structure, System, and Component
Station Shift Supervisor
Turbine Building
Turbine Building Closed Loop Cooling
Temperature Control Valve
A-5
'l
Attachment
1
TS
TSSR
Unit 1
Unit 2
Vdc
YHO
Technical Specification
Technical Specification Surveillance Requirement
Updated Final Safety Analysis Report
Nine Mile Point Unit 1
Nine Mile Point Unit 2
Unresolved Item
volts direct current
Violation
Work Order
Yellow Holdout
A-6