ML17056C227

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Insp Repts 50-220/92-25 & 50-410/92-29 on 921101-1212. Violations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maint,Surveillance,Emergency Planning, Security & Safety Assessment/Quality Verification
ML17056C227
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 01/05/1993
From: Larry Nicholson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17056C225 List:
References
50-220-92-25, 50-410-92-29, NUDOCS 9301190052
Download: ML17056C227 (44)


See also: IR 05000220/1992025

Text

Report Nos.:

Docket Nos.:

License Nos.:

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

92-25; 92-29

50-220; 50-410

DPR-63; NPF-69

Licensee:

Niagara Mohawk Power Corporation

301 Plainfield Road

Syracuse,

New York

13212

Facility:

Location:

Dates:

Nine Mile Point, Units

1 and 2

Scriba, New York

November

1 through December

12, 1992

Inspectors:

W. L. Schmidt, Senior Resident Inspector

W. F. Mattingly, Resident Inspector (in training)

. S. A. Greenlee, Reactor Engineer

P. D.

rysdale, Sen'

tor Engineer

Approved by:

Larry

. Nicholson, Chief

React r Projects Section No. 1A

Division of Reactor Projects

ate

In

ection Summar:

This inspection report documents routine and reactive inspections of

plant operations, radiological controls, maintenance,

surveillance, emergency planning,

security, and safety assessment/quality

verification activities.

Results:

See Executive Summary.

930ii900S2 930ii2

PDR

ADOCK 05000220

8

PDR

0

Executive Summary (Continued)

EXECUTIVE SUMMARY

Nine Mile Point Units 1 and 2

NRC Region I Inspection Report Nos. 50-220/92-25 I 50-410/92-29

11/01/92 - 12/12/92

Plant 0 erations

Both of the units were operated safely over the period.

Operators at Unit 2 did an excellent

job in response

to a failed reactor protection relay and in response

to the subsequent

reactor

scram.

Radiolo ical Controls

The implementation of the radiological control program was observed to be satisfactory over

the period.

Maintenance and Surveillance

Maintenance and surveillance activities conducted at both units were observed to be generally

well conducted.

The maintenance

organization responded well when a maintenance

technician removed the wrong drain plug from an emergency

diesel generator heat exchanger

causing a small contained spill of chromated coolant.

At Unit 2, a gauge with the wrong

range was installed on the 1B standby liquid control pump suction during surveillance testing.

This issue was not technically significant, since the gauge was digital and should have had

sufficient accuracy.

However, the persons verifying calibration, installing and using the

gauge did not identify and correct the problem, or did not notify the inservice testing

department and complete a procedure change as required by the surveillanc'e test. For this

reason,

and because of previous problems with the use of improperly ranged gauges during

surveillance testing, a violation was issued.

Emer enc

Plannin

During the period, the 1992 partial-participation emergency drill was conducted.

The drill

had to be suspended

for several hours to allow the site staff to respond to the reactor scram

at Unit 2.

0

Executive Summary (Continued)

En ineerin

and Technical

u

ort

Review of a 10 CFR 2.206 petition to shutdown Unit 1 was conducted with respect to a

provided list of primary containment and reactor coolant system isolation valves.

The

inspector found that the valves specified on the list were properly addressed

as not needing

testing or were being tested according to the IST plan, the technical specifications,

and the

UFSAR.

The inspectors observed that the security force properly implemented the observed portions

of the security plan.

afet

Assessment/

ualit Verification

The post-trip review process functioned well following the November 4 reactor scram.

Plant

management

used good safety perspective and ensured that problems were addressed

prior to

plant restart.

A Safety Review and Audit Board meeting was attended and found to provide

good review and oversight of site activities.

A review of the 1992 Licensee Event Reports

(LERs) indicated that the failure to properly assess

plant impact was a common contributor to

nine separate

events.

~-

TABLEOF CONTENTS

1.0

SUMMARY OF FACILITYACTIVITIES

1.1

Niagara Mohawk Power Corporation Activities ........

1.2

NRC Activities .. ~......................

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1.2.1

NRC Receipt of Petition for Emergency Enforcement

and Request for Public Hearing on Unit 1 ~......

Action

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2.0

PLANT OPERATIONS (71707,93702)

2.1

Plant Operations Review - Unit 1

2.2

Plant Operations Review - Unit 2

2.2.1

Review of November 4 Reactor Scram....,

.

~ ..

2.2.2 Partial Loss of Offsite Power

2

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3.0

RADIOLOGICALAND CHEMISTRY CONTROLS (71707).............

5

3.1

Routine Observations - Unit 1 and Unit 2 ............ ~.......

5

4.0

MAINTENANCE(62703)

4.1

Observation of Maintenance Activities - Unit 1

4.1.1

Liquid Poison Loop 12 Pressure Tap Installation.........

4.1.2

Emergency Diesel Generator Cooling Heat Exchanger

D'isassembly

4.2

Observation of Maintenance Activities - Unit 2

4.2.1

Division II Emergency Diesel Generator Local Annunciator

Failure Troubleshooting ........................

4.2.2

Division I Emergency Diesel Generator Speed Control Failure

4.2.3

Division II Emergency Diesel Generator High Vibration Trip

.

4.2.4

High Pressure

Core Spray Valve Breaker Assembly Inspection

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5.0

SURVEILLANCE(61726)

5.1

Observation of Surveillance Activities - Unit 1

5.1.1

Average Power Range Monitor (APRM) Weekly Instrument

Channel Test.............................

5.1.2

Feedwater High Pressure

Coolant Injection Testing

5.1.3

Reactor Building Emergency Ventilation Testing ~......

5.2

Observation of Surveillance Activities - Unit 2

5.2.1

Standby Liquid Control System Surveillance Testing

9

9

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10

11

11

Table of Contents (Continued)

6.0

ENGINEERING AND TECHNICALSUPPORT

6..1

Unit 1

6.1.1

Preliminary Review of Primary Containment/Reactor

Coolant

System Isolation Valve Administrative Deficiencies

6..2

Unit 2

6.2.1

Temporary Modification of the Unit 2 B-Loop Recirculation

Flow Controller................. ~...........

12

12

12

13

13

7.0

SAFETY ASSESSMENT AND QUALITYVERIFICATION(40500, 71707,

92700)

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7.1

Review of Licensee Event Reports - Unit 1

7.2

Safety Review and Audit Board Meetings.... ~.............

7.3

(Open) Unresolved Item 50-220/92-24-04 and 50-410/92-28-04:

Adequacy of Corrective Actions

~ .

14

14

14

14

8.0

MANAGEMENTMEETINGS........ ~......................

17

  • The NRC inspection manual procedure or temporary instruction that was used as inspection

guidance is listed for each applicable report section.

DETAI

1.0

SUMMARYOF FACILITYACTIVITIES

1.1

Nia ara Mohawk P wer

o

oration Activitie

The Niagara Mohawk Power Corporation (NMPC) operated Nine Mile Point Unit 1 (Unit 1)

safely, essentially at full power over the period.

NMPC operated Nine Mile Point Unit 2 (Unit 2) safely, essentially at full power, until a

November 4 reactor scram.

The scram resulted from the failure of a normally energized

relay in the reactor protective system (RPS).

NMPC completed their review of this event on

November 6 and restarted the unit on November 7.

Operators increased

reactor power to

100% and safely operated

the unit through the remainder of the period.

On November 15,

one of the two offsite power lines was de-energized

due to an equipment failure in its supply

breaker, located in the Scriba switchyard.

1.2

NRC Activities

Resident inspectors conducted inspection activities during normal, backshift and weekend

hours over this period.

There were 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> of backshift (evening shift) and 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> of deep

backshift (weekend, holiday, and midnight shift) inspection during this period.

During the week of December 7 a routine inspection of the environmental monitoring

program was conducted.

The findings of this inspection willbe documented in Combined

Inspection Report 92-28/33.

From November 3-5 the routine partial participation emergency preparedness

inspection was

conducted.

Combined Inspection Report 92-27/31 documents the observations

and findings

during the November 4 drill.

On December

1, a meeting was held with NMPC senior management

in NRC Region I to

discuss recent performance at both units.

Attachment

1 to this report provides the list of

attendees

and the presentation

material provided by NMPC.

1.2.1

NR

Recei

t of Petition for Emer enc

Enforcemen

Action and R

ue t for Public

Hearin

on Unit

1

On October 27, 1992, a petition was filed under 10 CFR 2.206, requesting that the NRC

order NMPC to immediately cease power operation at Unit 1 and place the unit in a cold

shutdown condition.

The petition further requested

that the NRC hold a public hearing

before authorizing resumption of power operation.

The basis for such an order and hearing

included concerns

that:

(1) the Unit 1 feedwater system operating in its high pressure

coolant injection (HPCI) mode does not meet NRC requirements for an engineered

safety

feature systems (ESF) grade HPCI system; and (2) 45 percent of containment isolation valves

have administrative deficiencies.

The NRC staff's initial review of this petition, documented in NRC letter dated

December 4, 1992, to the petitioner, did not identify any need for an immediate order to

shutdown Unit 1. With respect to the HPCI concern, initial staff review determined that the

emergency systems met the NRC requirements for core cooling in accordance with 10 CFR 50.46.

The feedwater system operating in its HPCI mode is not taken credit for in the 10 CFR 50, Appendix K analysis; but rather the automatic depressurization

(ADS) and core

spray (CS) systems are relied upon to depressurize

the reactor and cool the core,

respectively.

While this mode of feedwater system operation is not an ESF grade system, it

is required to be operable by technical specifications.

The inspectors reviewed and observed

portions of the quarterly surveillance testing on this system and found, as documented in

section 5.1.2 below, that it adequately

demonstrated

the operability of the system.

With

respect to the concerns on administrative deficiencies on primary containment isolation

valves, the staff found, based on the initial inspection documented in section 6.1.1 below,

that minor deficiencies exist, but that valves were being properly tested to ensure proper

operation of the isolation function.

2.0

PLANT OPERATIONS (71707,93702)

2.1

Plant 0 erations Review - Unit

1

The inspectors observed good control of plant operations by the Unit 1 operations staff.

Control room operators operated the plant safely.

NMPC took a good initiative to increase

the ability of the station shift supervisor (SSS) and the assistant

station shift supervisor

(ASSS) to supervise

the other member of the operations crews by removing walls and

rearranging their office space within the control room.

2.2

Plant 0 erations Review - Unit 2

The inspector observed good control of plant operations by the Unit 2 operations staff.

Control room operators operated the unit safely and took appropriate actions to address

problems such as the failed RPS relay discussed

below.

Operators were always aware of the

reasons for annunciated

alarms on control room panels.

2.2.1

Review f November 4 Reactor

cram

The inspector observed that the operating crew performed excellently during their response

to

the November 4 reactor scram.

The ASSS performed very well as he carried out the

emergency operating procedures

anddirected the activities of the crew.

The SSS was also

very effective at maintaining an overall assessment

of plant conditions and provided proper

oversight of the ASSS and the crew.

The reactor operators and non-licensed operators

performed well with respect to monitoring and controlling reactor vessel level and pressure

using the feedwater, reactor core isolation cooling (RCIC), safety relief valve (SRV), and

residual heat removal (RHR) systems.

While operating at 100% power, following half scram testing on the A RPS channel,

operators detected

smoke coming from one of the B RPS channel cabinets, in the back of the

control room.

The SSS opened the cabinet and observed smoke coming from what he

thought was a normally energized B RPS relay, because of its location and lack of

component identification tag.

The SSS prudently ordered that the B RPS relays be de-

energized by inserting a manual half scram of the B RPS logic. After the B RPS channel

was de-energized

the SSS determined,

through discussion with operators and instrument and

control (I&C) technicians,

that the subject relay was actually powered from A RPS (although

located in a B RPS cabinet), and thus had not been de-energized

by placing the manual scram

on the B RPS channel.

Before the SSS could order that the manual half scram be cleared from the B RPS channel

and inserted on the A RPS channel, the power supply fuse to the affected relay failed.

The

blown fuse together with the B RPS half scram caused one-quarter of the control rods to be

inserted,

as designed.

The insertion of these control rods caused reactor power to decrease

from 100% to 14%, and reactor water level decreased

due to the power transient to the low

level scram setpoint within about ten seconds.

At that point an automatic full scram occurred

and all control rods were inserted.

Operators took effective actions to control reactor vessel water level and pressure.

To limit

the plant cooldown the main steam isolation valves were shut.

Operators

used RCIC,

recirculating to the condensate

storage tank and manual opening of SRVs to control reactor

pressure,

while the steam condensing

mode of RHR was readied for operation.

Communication between the SRV operator and the other operators controlling reactor vessel

level with the feedwater system and the RCIC system was very good.

The SRV operator

noticed that one valve gave both an open and closed indication on the control panel when it

was signaled to open.

This valve was then shut and not used in the following SRV cycling

sequence.

During the SRV cycling, reactor water level changed up to 60 inches, with level

swelling as the valve was open and shrinking when the valve was closed.

These level

changes

caused

several isolations of RCIC on high level and a second low level reactor

scram.

The operations staff and plant management

exhibited very good questioning attitudes during

the post-scram review process and functioned well to ensure that issues needing resolution

were completed prior to unit restart.

The critique conducted by the reactor analyst

supervisor was very good as operators were given the opportunity to discuss their

observations

and actions.

This process

lead to the identification and resolution of several

issues that included the failure of the RPS relay, the SRV position indication problem, and

reactor water level changes during the SRV operation.

The inspector attended the pre-restart

Site Operations Review Committee (SORC) meeting and found that all the issues necessary

for restart were either dispositioned or tracked to allow disposition prior to restart.

NMPC

could not determine the cause for the RPS relay failure prior to startup, but did take

thermographic pictures of the other similar relays and planned to incorporate this into a

preventive maintenance (PM) schedule.

The failed relay was replaced with an equivalent

replacement relay.

The inspector interviewed procurement personnel and reviewed the

vendor's product quality certificate, NMPC's spare parts equivalency review and the quality

control inspection reports for the replacement relay.

Alldocumentation for the replacement

relay was satisfactory.

Good discussion was observed during the review of the repair for the SRV acoustic monitor

SRV that did not have positive indication of position.

Plant management

took the necessary

actions to ensure that the monitor was operable prior to startup.

This included de-inerting

the drywell and replacing a broken acoustic pickup.

The reactor water level swings observed during SRV operation were analyzed and

determined to have been caused by actual fluctuation in the reactor level as the pressure of

the coolant was changed,

not due to gasses

coming out of solution in the reference legs of the

instruments.

The inspector reviewed the response of the RPS system to this event and found that it was

according to the design.

The reason for having RPS relays of the other division (A RPS

relays in B RPS cabinets) was for 10 CFR 50, Appendix R fire considerations,

to allow a

backup scram to occur iffire damage to one RPS channel precluded its normally energized

scram relays from opening.

NMPC submitted licensee event report (LER) 92-22, on December 4.

This LER adequately

discussed

the event and the corrective actions taken.

The LER stated that GE had provided

the industry with information on potential failures of the type of relay that failed, but that the

failure of this relay did not relate to GE's information.

The inspector considered

this LER

open pending review of the GE information and PM program on these relays.

2.2.2

Partial Loss of

ffsite Power

On November 15, with the unit operating at 100% power, offsite power line 5 was lost to

Unit 2 because its offsite supply breaker (R50) inadvertently opened.

The control room had

no knowledge of problems with the offsite breaker before it opened.

The Division I and III

emergency diesel generators

(EDG) started to supply power to their busses.

Operators took

appropriate actions by parallelling the EDGs with the remaining offsite power supply and

then securing the EDGs.

Initiallyoperators could not parallel the Division I EDG with line 6

because

the operators did not have speed control of the EDG when preparing to parallel.

Operators identified a broken connector on the speed sensing probe and were able to parallel

and secure the EDG (further corrective actions on this problem are discussed

in section 4.2.2

below).

NMPC review of the R50 breaker indicated that it had tripped open on low nitrogen

accumulator pressure in its operating mechanism.

This nitrogen accumulator pressurizes

the

hydraulic operator for this breaker and is designed to trip open at a given low pressure

setpoint.

NMPC offsite maintenance determined that the shaft on the hydraulic pump, used

to keep the pressure in the nitrogen accumulator and thus the hydraulic system, had failed.

This caused the motor to run without the pressure being restored to normal.

Preventive

maintenance

on this breaker and on the other offsite power breaker (R60) had been

conducted within several weeks of this breaker failure.

This failure was similar to a previous

event that occurred when R60 opened due to low nitrogen pressure.

In that case, control

room operators

had been previously told by the offsite maintenance crew that the breaker

would not open ifnitrogen pressure

decreased.

The inspector toured the offsite switchgear and discussed

the failures of the breakers with the

offsite maintenance

personnel.

NMPC site management

directed that the independent safety

engineering group (ISEG) review the recent loss of offsite power and determine what action

needed

to be taken to limit these occurrences.

This instance was the sixth time in several

years that either a partial or complete loss of offsite power has occurred.

NMPC submitted

LER 92-23 documenting this incident on December

14, 1992.

This LER remained open

pending further inspection review of the corrective actions.

3.0

RADIOLOGICALAND CHEMISTRY CONTROLS (71707)

3.1

Routine Ob ervations -

nit 1 and Unit 2

The inspectors observed good use of radiological protection practices, proper use of

procedures,

and adherence

to postings during routine plant tours.

e

4.0

MAINTENANCE(62703)

Inspectors observed and reviewed selected activities to verify that safety-related

maintenance

was conducted in accordance with approved procedures,

technical specifications,

and

appropriate industrial codes and standards.

Observations

and reviews included verification of

the proper use of: administrative authorizations and tag outs (including lifted leads), certified

parts and materials, calibrated test equipment, proper radiological requirements,

controlled

drawings, and correctly established quality control hold points.

4.1

bservation of Maintenance Activitie -

nit 1

4.1.1

Li uid P i on

12 Pre

ure T

In

llation

The inspector observed portions of the installation of a pressure

tap between the liquid poison

pump 12 and its discharge check valve, to assist in quarterly system reverse flow testing.

Both the mechanics

and QA inspectors demonstrated

proper quality control throughout the

implementation of this simple design change.

The welding technic and post-weld inspections

were satisfactory.

The mechanics performing the maintenance

were very knowledgeable and

performed the procedure properly, using good radiological work practices and proper

cleanliness controls.

4.1.2

Emer enc

Die

1

enerator

lin

Heat Exchan er Di

sem

1

Chemistry and maintenance

technicians performed a routine quarterly inspection of EDG-102

cooling water heat exchanger 79-03.

Partial disassembly of the cooler required draining the

tube (raw water) side and removing the "floating head" at one end to gain visual access

to

the internal tubing.

The maintenance procedure directed the technicians to drain residual

water from the cooler head area by removing the drain plug on the underside of the assembly

prior to unbolting the head flange.

The procedure contained a diagram showing drain plugs

on the underside of the cooler, but did not identify the specific internal areas that could be

drained by each plug.

The technician mistakenly removed a plug on the shell side of the

cooler, draining approximately

15 gallons of potassium chromated jacket cooling water onto

surrounding equipment and floor spaces before the drain plug was reinserted.

The inspector

observed other maintenance

technicians in the diesel room respond quickly to contain the

spilled water and to prevent a release of the liquid from the building.

Environmental

protection, fire department,

operations,

and other site organizations immediately responded

to

the diesel room to assess

the potential consequences

of this spill. All maintenance work in

the diesel room was suspended

until the cause of the incident was determined and corrective

actions were taken to prevent a recurrence.

The inspector considered

the critique conducted by maintenance

to have fully addressed

the

incident and adequately identified the needed corrective actions, prior to resuming work.

The primary corrective action was to revise the maintenance procedure by clearly labelling

the different drain plugs on the heat exchanger housing.

Maintenance supervisors considered

0

that close supervisory monitoring, additional training, and detailed pre-job briefings were not

warranted for this task because of its relative simplicity. However, supervisors did advise

other personnel of the procedure change and emphasized

the specific locations of the

different cooler drain plugs.

The inspector discussed

with the system engineer potential operability consequences

related

to possible water intrusion on electrical components

near the diesel coolers.

A thorough

inspection of the diesel fuel transfer pump, the lube oil pump, and the lube oil emersion

heater was made by the system engineer and electrical maintenance

technicians.

No water

had apparently entered

these components.

Also, no additional makeup to the jacket cooling

water system was required since the expansion tank level was still in its normal band.

No

other diesel operability concerns were identified. Alladjacent surfaces on the diesel

equipment pallet were wiped to remove spilled liquid and all surrounding floor areas were

thoroughly cleaned.

The inspector considered

that the licensee's overall response

to this

event was timely and appropriate.

When heat exchanger disassembly

resumed,

the inspector observed direct supervisory

oversight in the work area.

When the cooler internals were exposed,

a site chemistry

technician performed a visual inspection of and took samples for laboratory analysis from the

internal head and tube areas.

The inspector reviewed the inspection criteria contained in the

procedure and independently verified that internal heat exchanger

surfaces on the raw water

side were in generally good condition, free from excessive corrosion and flow blockage, and

that muscle shells or fragments were not present.

Relatively small amounts of

microbiologically-induced corrosion were present on the internal surface of the cooler head,

but most of this material was removed when samples were taken.

The inspector discussed

the inspection methodology with the chemistry technician and found him to be very

knowledgeable and experienced

in this type of heat exchanger inspection.

The technician

made appropriate entries in the procedure to reflect his visual inspection.

Samples for

subsequent

laboratory analysis were properly labeled.

Overall, mechanical maintenance

technicians were knowledgeable of diesel heat exchanger

construction and disassembly/reassembly

requirements.

They demonstrated

adequate skill

and attention to procedure requirements during reassembly of the heat exchanger.

The

inspector discussed with the maintenance

supervisor the deficiency event report (DER)

written to evaluate the cooling jacket water spill and considered

that all factors associated

with the event were properly identified and documented.

4.2

ervati

n f Mainten n

Ac ivi ie -

nit 2

4.2.1

Division II Emer enc

Diesel

enerator Local Annunciator Failure Trouble hootin

The operations department and I&C technicians took conservative, timely and effective

actions to evaluate and correct a loss of power to the local Division II EDG annunciators.

During routine rounds on November 5, an operator found the local panel annunciators

0

inoperable.

Further investigation revealed that the isolation breaker upstream of the three

annunciator power supplies had tripped and would not reset.

The operating crew

conservatively declared the EDG inoperable and took appropriate actions in accordance with

the technical specifications (TS).

The inspector observed the annunciator troubleshooting and return to service conducted by

I&C technicians.

The technicians identified a short circuit on the output of one power supply

and properly questioned why the fuse upstream of that supply did not blow prior to the

tripping of the upstream breaker.

Further investigation identified that the three power

supplies for the annunciators

have a common output; vice supplying separate

rows of

annunciators

as previously thought.

Thus, with all three power supplies feeding the fault, the

limiton the individual fuses was not exceeded,

but the combined current was enough to trip

the breaker.

The failed power supply was replaced and the Division II EDG was returned to

operable status.

NMPC initiated a DER to evaluate the adequacy of this design.

4.2.2

Divisi n I Emer enc

Diesel

enerator

S

ntr

1 Failure

The inspector determined that the operations and I&C departments

aggressively pursued

returning the Division I EDG to service following failure of the speed sensor discussed

in

section 2.2.2 above.

The inspector reviewed the work conducted and discussed

the

troubleshooting effort with the system engineer and the SSS.

A broken connector on the

speed sensor caused

the lack of control.

The connector was replaced,

the EDG was then run

to verify speed control and returned to service.

NMPC determined that the connector

apparently broke due to vibration of the wiring conduit and wrote a DER for engineering to

evaluate the mounting of the conduit.

Since the Division II EDG configuration is the same

as Division I, the evaluation willinclude the Division II EDG conduit mounting.

4.2.3

Division II Emer enc

Diesel Generator Hi h Vibration Tri

The operations and I&C departments

and the system engineer did an excellent job

troubleshooting and repairing a condition that caused

a non-emergency trip following a post-

maintenance

test of the Division II EDG.

On November 13 the EDG tripped, during its 5

minute unloaded cooldown run, on an annunciated

high vibration condition.

Troubleshooting revealed that a true high vibration condition did not cause the trip, since the

vibration trip unit was not in a tripped condition (the unit must be manually reset ifit does

trip). This trip is pneumatically actuated, with the vibration trip unit bleeding air from its

associated

pneumatic lines, lowering pressure

enough to actuate a pressure switch that

initiates an engine trip (unless an emergency signal is present).

A check valve upstream of

the vibration trip unit will normally hold sufficient pressure in the trip unit pneumatic lines to

prevent an engine trip; however, this time, it appears

that the check valve leaked enough air

to activate the vibration trip unit pressure switch.

9

I&C technicians removed, inspected,

cleaned,

and conducted a satisfactory air drop test on

the vibration trip unit pneumatic lines.

Subsequent

operation and cooldown of the diesel was

successful.

4.2.4

Hi h Pre

r

re

ra

Valve Breaker Assem

l

In

ection

The inspector observed portions of the periodic preventive maintenance

and testing on the

high pressure core spray (HPCS) suppression

pool test bypass valve, 2CSH*MOV111,

breaker assembly at the motor control center located in the Division IIIsafety-related

switchgear room.

The activity was properly performed per electrical preventive maintenance

procedure N2-EPM-GEN-V520.

Activities specifically observed included:

clean, inspect,

and test the valve open and close relays, breaker overload contacts, control power

transformer, breaker auxiliary contacts, breaker, and cubicle; and installation of the breaker

assembly into the motor control center.

Proper primary containment integrity was

maintained while 2CSH*MOV111, a primary containment isolation valve, was inoperable.

The electricians were experienced with the procedure,

knowledgeable of the breaker

assembly operation, and used proper electrical maintenance

techniques.

Electrical

maintenance supervisory involvement was good.

Based on the above observations

the

inspector concluded that the breaker assembly was in satisfactory condition.

5.0

SURVEILLANCE (61726)

The inspectors reviewed safety-related

surveillance activities by observation of testing in

progress,

interviews, and review of records and verified that:

required administrative

approval was obtained, procedural precautions

and limitations were observed,

review of test

data was accurate and timely, surveillances conformed to TS, calibrated test equipment was

used, radiological controls were observed,

and required surveillance frequencies

were met.

5.1

Observation

f urveillance Activities - Unit 1

5.1.1

Avera e Power Ran

e Monitor APRM Weekl

In trument

hannel T t

The inspector observed the weekly channel functional test on APRM 12 required by TS and

noted the following:

1) communications and coordination between the I&C technicians and

the control room operators were satisfactory;

2) the I&C technicians had an excellent

working knowledge of the procedure;

3) all required log entries were made and proper

authorization to perform the procedure was obtained; and 4) the surveillance was conducted

properly and resulted in a determination that the instrument was functioning properly.

10

5.1.2

Feedwater Hi h Pr

sure

lant In'ecti n Te tin

Operations personnel satisfactorily performed the quarterly feedwater HPCI pump and check

valve operability test following procedure N1-ST-Q3, which satisfied the periodic pump and

valve operability test required by the TS.

The test involved a reactor power reduction to

1800 MW, in order to test with two condensate

pumps in operation.

It demonstrated

that

each HPCI pump provided flow above the minimum specified at the pump differential

pressure conditions delineated by specification MDC-11, "Pump Curves and Acceptance

Criteria." The test also verified that each HPCI pump discharge check valve adequately

seated

to prevent reverse flow through an idle pump and it obtained vibration measurements

from each pump and motor as part of the plant's equipment performance trending program.

The inspector accompanied

the system engineer during the test of HPCI train 11 and

observed technicians recording flow and differential pressure

data.

The inspector

independently verified that the test data taken was as recorded and then confirmed that the

data met the acceptance

criteria specified by the procedure.

The calculations required by the

procedure using recorded test data were also verified to be correct and met specified

acceptance

criteria. All measuring and test equipment (M&TE) installed for this test was

verified to have an appropriate range for the test and was in its current calibration period.

The inspector determined that this test adequately

demonstrated

the operability of HPCI

pump 11.

The test was properly performed, and was reviewed and accepted by operations

management.

The test of HPCI train 11 was also used to provide post-maintenance

test acceptability of a

repair that was made on a pinhole leak in the 2" recirculation line from the pump to the main

condenser.

The inspector reviewed the inspection document for this repair and confirmed

that the acceptance

criteria were satisfied.

After the test of train 11, the inspector reviewed the official test results conducted the prior

week for train 12 and verified that the recorded data was acceptable for pump and check

valve operability.

5.1.3

Reactor Buildin

Emer enc

Ventilation Testin

Operators satisfactorily performed the monthly secondary containment and reactor building

emergency ventilation system operability test required by TS, over a period of several days,

according to surveillance test procedure N1-ST-M8.

One ventilation train was removed from

service for testing, while the other was kept in a standby condition.

The test involved running each emergency

fan for a minimum of ten hours, with the in-line

heaters on, while flow and d/p data was obtained to verify proper performance of the

charcoal and HEPA filters. The ability of the system to maintain a minimum -0.25 inches of

water differential pressure between the reactor building and the outside atmosphere

was also

confirmed by this test.

The inspector observed the system operating indications on the

0

0

11

control room instruments used by operators for the test.

Minor inconsistencies

in the

recorded data were noted by the inspector, but were promptly corrected by operations

personnel performing the test.

The final recorded data used for system operability were

reviewed by the inspector and were properly reviewed by site operations and technical

support personnel.

5.2

Observati

n f urveillance Activi ie -

nit 2

5.2.1

Standb

Li uid Control S stem Surveillance Testin

The inspector found that the operability and inservice testing (IST) procedure for the standby

liquid control system (SLC), adequately

met the requirements of the TS, the updated final

safety analysis report (UFSAR), and Section XI of the ASME Code.

During testing

communications between the personnel were excellent.

However, the inspector identified

that a pump suction test equipment gauge,

needed for IST data, did not meet the procedure

requirements.

Further, problems were observed with the understanding of I&C technicians

using ultrasonic flow meters and vibration instrumentation.

While observing the test, the inspector found that the M&TEpump suction pressure

gauge

had a range of 0-200 inches of water; while the procedure required the installation of a gauge

with a range of 0-100 inches of water.

Once this was identified to testing personnel the test

was secured

and declared invalid.

Review of the test procedure showed that 0-100 inch

water gauge was specified in the test equipment list, in the test equipment calibration list,

and at the installation verification step.

Further, the procedure required that ifany test

equipment was to be used that was different from that specified in the procedure the IST

department needed to be contacted and the procedure changed.

The technical significance of using the wrong pump suction pressure gauge range was low

since the gauge was digital and, therefore, should have been sufficiently accurate and

readable through most of its range; however, the inspector was concerned

that licensee

personnel failed to follow their procedures

and then subsequently

failed to note the error

themselves.

Additionally, as noted in LER 91-03, NMPC personnel have used improper

gage ranges during IST on several occasions in the past; however, the changes to the

surveillance test procedure initiated as a result of these past problems were very evident, and

should have been sufficient to prevent recurrence.

Thus, the failure by NMPC personnel to

follow the surveillance test procedure was seen as violation of TS 6.8.1 (vice ineffective

corrective actions), which requires that written procedures

be implemented for surveillance

testing (50-410/92-29-01).

Following the identification of the installation of the wrong gauge,

a 0-100 inch of water

gauge was installed and the test reperformed.

NMPC initiated a DER to resolve the gauge

installation issue.

12

During both performances of this test the inspector noted that the flow indication given by

the ultrasonic flow device increased

as the test was performed, without a change in the

system flow characteristic.

NMPC determined that the most probable cause was a drift in

the instrument's zero point, due to high background sonic energy in the pipe where the flow

was being measured

or due to an increase in the temperature of the fluid as it was circulated

to the test tank.

Following the second performance,

the flow rate was in the high alert

range.

However, once the pump was stopped (i.e., system flow was actually zero) the

ultrasonic instrument indicated some flow. NMPC initiated a DER to analyze the zero

reference drift problem.

The inspector asked the I&C technicians involved in the test about the effects on the

vibration instrument frequency response

when using the nine inch extension on the probe.

The technicians replied that the frequency response

was not changed and, thus, the probe

could be used when necessary

to get to out-of-the-way locations.

This indicated a lack of

understanding of the vibration test equipment since the use of the probe significantly effects

the frequency response.

Additionally, as indicated in LER 92-04, NMPC previously failed

to meet TS requirements

because of improper use and understanding of the nine inch probe

extension. Ifthe nine inch probe extension is used to obtain ASME Code required data on

the SLC pumps, the frequency response of the vibration instrument will not meet the

requirements.

The inspector did note that ifthe surveillance procedure was followed

correctly, the nine inch probe extension would not be used for gathering ASME Code data

and that it had not been used for this purpose during this test.

NMPC IST supervision were aware of the I&C technicians'ack of knowledge on the use of

ultrasonic flow and vibration test equipment.

They were working to reduce the number of

personnel who operate this equipment, and to increase the training for this smaller group.

The inspector had no additional questions or concerns.

6.0

ENGINEERING AND TECHNICALSUPPORT (71707, 37700)

6.i

((nit i

6.1.1

Preliminar

Review f Primar

ontainment/Reactor

oolant

tern Isolation Valve

Administrative Deficiencies

As discussed

in section 1.2.1 above, a 10 CFR 2.206 petition was received which dealt in

part with administrative deficiencies on primary containment and reactor coolant system

isolation valves.

Attachment 5 to the petition provided a list of 84 valves, and 17 associated

notes describing these deficiencies.

To ascertain ifthere were any current operability

concerns with the listed valves the inspector reviewed:

IST program plan issued on

November 2, 1992, the UFSAR, the current TS, a proposed TS amendment

dated February

7, 1992, and the numerous surveillance tests used to demonstrate operability of primary

containment and reactor coolant system isolation valves.

13

Preliminarily, the inspector found that of these 84 valves, 76 were currently in the IST

program, with appropriate testing listed including; exercise,

stroke timing, and leakage rate

testing.

Four valves were associated

with the non-safety related HPCI mode of the feedwater

system and therefore, were not in the IST plan.

Two other valves were not in the IST plan

since blank flanges had been installed upstream of the valves.

The final two valves were not

included in the IST plan since the valves did not need

10 CFR 50, Appendix J testing due to

a water seal.

With respect to differences between the TS tables and the UFSAR tables for

these valves, the inspector found that the proposed TS amendment addressed

the concerns for

valves currently considered

by NMPC to be isolation valves.

The proposed TS amendment

also clarifies the leakage rate testing requirements for valves which currently are exempted

from the requirement of 10 CFR 50, Appendix J.

Review of surveillance testing showed that

applicable testing criteria for stroke timing were being implemented. Ifa valve was

currently not in the TS tables it was being tested as appropriate with the IST plan, with

stroke times that were more conservative than those specified in the proposed TS

amendment.

The inspector also verified that valves which receive automatic closure signals

on a loss of coolant accident were properly functionally tested during the performance of the

refueling cycle loss of coolant/loss of offsite power function test.

This preliminary review did not identify any condition that would indicate that the identified

valves were not being tested to ensure their operability.

NMPC stated that this amendment

corrects all the noted problems and that once it is issued'he UFSAR will be updated.

However, the proposed TS amendment

has not been issued and is still under review by the

NRR staff.

6.2

6.2.1

Tem orar

Modification of the Unit 2 B-Loo

Recirculati

n Flow Controller

During power ascension,

following the scram on November 4, the plant experienced

significant flow oscillations on the B recirculation loop, caused by problems with the valve

stem velocity sensor for the B flow control valve.

NMPC implemented a temporary

modification to the recirculation flow controller rather than enter the drywell and repair the

sensor.

The modification, recommended

by GE, was installed and tested with a GE technical

representative

present at the site.

The most significant part of the modification consisted of

removing the velocity sensor input from the control circuit and replacing it with a signal of

constant value.

The inspector reviewed the engineering design change package and the associated

10 CFR 50.59 safety evaluation, and observed portions of the modification testing.

The inspector

found that the modification was technically sound and would allow proper operation of the

recirculation flow control valve.

Further, the safety evaluation adequately

demonstrated

that

an unreviewed safety question did not exist as a result of the modification and that TS

requirements

were not affected.

14

7.0

SAFETY ASSESSMENT AND QUALITYVERIFICATION (40500, 71707,

92700)

7.1

Review of Licensee Event Re orts - Unit I

LER 91-07, dated July 23, 1991, discussed

a reactor building emergency ventilation system

isolation due to a damaged

cable in a radiation monitor trip unit. NMPC initiallycommitted

to replace the damaged

cable during the next refuel outage; however, subsequent

engineering

evaluation determined that a permanent repair to the existing cable would be satisfactory.

The inspector agreed that the repair would be satisfactory following discussions with NMPC

personnel.

A supplement to the LER will not be issued.

7.2

Safet

Review and Audit Board Meetin

The inspector observed portions of the Safety Review and Audit Board (SRAB) meeting on

December 2, 1992, and reviewed the October 7-8, 1992, SRAB meeting minutes.

The

SRAB, composed of senior managers,

engineers,

and consultants,

technically competent in

various fields of nuclear energy, functions to provide an independent review and audit of

designated plant activities per TS 6.5.3.

Proper committee composition was present and

presentations

by various members and subcommittees

were clear and well prepared.

In-depth

discussions

were held on various safety-related

matters including:

entry into limiting

conditions for operation for planned maintenance while operating, the frequency of loss of

offsite power events at Unit 2, and engineering implementation of the software QA program.

The inspector concluded that both SRAB meetings satisfied the objectives of TS 6.5.3.

7.3

0 en

nres lved Item SO-220

2-24-04 and

0-41

2-28-04: Ad

uac

of

orrective Action

As part of the effort to assess

the adequacy of recent corrective actions, the inspectors

reviewed all of the 1992 LERs for both units.

The most common similarity between the

events was the failure of NMPC personnel to assess

adequately

the plant impact associated

with various conditions and actions.

During 1992, nine reportable events were caused,

at

least in part, by improper assessment of the potential affects of operations and maintenance

activities.

A brief summary of each event is listed below.

Any violations of regulatory

requirements

have been addressed

in previous inspection reports.

Unit 1

~Januar

10 and 22

I

2 LER

2-01

- Operators failed to take actions required by the

Unit 1 TS when portions of the turbine stop valve closure scram and the generator load reject

scram were bypassed

at greater than 45% power.

The bypass conditions occurred because of

an equipment malfunction together with an improper valve lineup.

The operators were aware

of the problem because of an annunciator indicating that the main turbine first stage pressure

was low.

0

15

The most significant cause of the operator's failure to follow the TS was that they apparently

did not fully understand

the implications of the turbine first stage pressure instrument sensing

a low pressure condition.

Further, the abnormal alarm was not logged by the operating crew

and a DER was not written.

~ Februa

21

1

2 LER

2-

- The plant was isolated from its ultimate heat sink (Lake

Ontario) for approximately five minutes.

This was a result of closing the screenhouse

forebay, with the plant in a reverse flow condition, and the subsequent inability to reopen

Gate D immediately.

Gate D was closed to test its control circuit following modification.

A contributing cause of this event was that operators

and maintenance

supervision failed to

assess

adequately

the potential impact of closing Gate D on the plant.

~

Se tember 4-5

1

2

LER

2-10

- Several instances occurred where the minimum

number of operable reactor trip system channels was less than required.

This resulted

from bypassing two intermediate range neutron monitors because of anticipated

"spiking," then subsequently placing average power range neutron monitors in bypass

for various operational and maintenance

reasons.

The most significant cause of this event was that the control room operators did not

correctly assess

the effect of concurrently placing various neutron monitors in a

bypass condition.

Unit 2

~Janua

1

1

2 LER 92-03

- An unexpected

secondary containment isolation signal was

received when workers de-energized

a reactor building ventilation system radiation monitor

(the above refuel floor monitor).

The system responded correctly to the loss of power.

The cause of this event was a failure to perform an adequate job/plant impact assessment

prior to commencing work on the radiation monitor.

~

March 2

1

2 LER

2-06

- The plant lost both 115 kV offsite power sources,

lines 5 and 6.

Line 5 was lost when technicians accidentally actuated

an over-current

relay during maintenance.

Line 6 was subsequently

lost when operators attempted to

cross-tie it to the line 5 loads.

Line 6 was isolated from the plant, by design, because

of interlocks (associated

with the over-current relay trip) that were affected when the

cross-tie was attempted.

16

The cause of this event was a failure to perform an adequate job/plant impact

assessment

prior to commencing work on the over-current relay.

Additionally,

operators compounded

the event by improperly assessing

the impact of the relay trip

on the ability of line 6 to supply line 5 loads.

~

Jul

28

1

2 LER 92-18

- The plant lost 115 kV offsite power line 6 due to failure

of its associated

offsite supply breaker; however, NMPC personnel were aware that

the breaker was experiencing problems more than thirteen hours before the trip; but

they improperly assessed

that the malfunction would not cause the breaker to trip.

A significant contributing cause of this event was a failure to perform an adequate

plant impact assessment

of the breaker malfunction.

~

Au u t 22

1

2

LER 92-17

- The reactor scrammed

on low reactor vessel water

level during an attempt by the control room operators to switch feed pumps.

The cause of this event was improper operation of the feedwater and condensate

systems.

The operators did not understand

the consequences

of some of their

manipulations of these systems.

Se tember 16

1

2 LER

2-1

- The plant experienced

an automatic isolation of

the reactor water cleanup system (an engineered

safety feature) due to a high

temperature condition in the reactor water cleanup system pump room.

The high

temperature condition was caused by an improper ventilation system configuration.

The improper configuration was established during maintenance

on the emergency

recirculation unit coolers.

The cause of this event was a failure to perform an adequate plant impact assessment

of the maintenance

on the emergency recirculation unit coolers.

e tember 2

1 92

LER

2-20

- The plant lost 115 kV offsite supply line 5 when a

crane boom, being used to place concrete,

came close to the line, and the resulting

arc through the crane to the ground caused

the line to trip.

A possible contributing cause of this event was a failure to perform a plant impact

assessment

of the work. Ifthe work had been assessed

for plant impact, and had

been coordinated with the control room, the incident might have been prevented.

The corrective actions for each event listed above have generally been good when

considering the individual event and possibly one or two past events.

The corrective actions

tended to focus on fixing or creating procedures,

letting other personnel know about the

event (via a Lessons Learned Transmittal), and conducting some specific event related

17

training.

The corrective actions have not, however, focused on the broad scope of failures to

assess

adequately

the impact of various operations and maintenance activities.

NMPC was

conducting their own analysis of past LERs for the adequacy of corrective actions.

This

unresolved item remains open pending further inspector review.

8.0

MANAGEMENTMEETINGS

At periodic intervals and at the conclusion of the inspection, meetings were held with senior

station management

to discuss the scope and findings of this inspection.

Based on the NRC

Region I review of this report and discussions

held with Niagara Mohawk representatives,

it

was determined that this report does not contain safeguards

or proprietary information.

0