ML111930432

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Appeal of Final Significance Determination of a Red Finding and Reply to a Notice of Violation; EA-11-018
ML111930432
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 06/08/2011
From: Swafford P
Tennessee Valley Authority
To: Mccree V
Document Control Desk, Region 2 Administrator
References
EA-11-018, IR-11-008
Download: ML111930432 (51)


Text

Tennessee Valley Authority, 1101 Market Street, LP 3R, Chattanooga, Tennessee 37402 Preston D. Swafford Executive Vice President and Chief Nuclear Officer June 8,2011 10 CFR 2.201 Mr. Victor M. McCree Regional Administrator, Region II U.S. Nuclear Regulatory Commission Marquis One Tower 245 Peachtree Center Avenue, NE, Suite 1200 Atlanta, Georgia 30303-1 257 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001 Browns Ferry Nuclear Plant, Unit 1 Facility Operating License No. DPR-33 NRC Docket No. 50-259

Subject:

Appeal of Final Significance Determination of a Red Finding and Reply to a Notice of Violation; EA-11-018

References:

1) Letter from NRC to WA, Final Significance Determination of a Red Finding, Notice of Violation, and Assessment Follow-up Letter (NRC Inspection Report No. 05000259/2011008) Browns Ferry Nuclear Plant, dated May 9, 2011
2) Letter from NRC to WA, NRC Report 05000259/2010005, 05000260/2010005, and 05000296/2010005; Preliminary Greater Than Green Finding Browns Ferry Nuclear Plant, dated March 2, 2011
3) Letter from WA to NRC, Request for Regulatory Conference or Public Management Meeting, dated June 2, 2011
4) Letter from NRC to WA, Response to Request for Regulatory Conference or Public Management Meeting, dated June 7, 2011 printed on recycled paper

U.S. Nuclear Regulatory Commission June 8,2011 Page 2 Reference 1 provided the Nuclear Regulatory Commission (NRC) Final Significance Determination (FSD) and a Notice of Violation (NOV) related to the degraded condition of the Browns Ferry Nuclear Plant (BFN), Unit 1, low pressure coolant injection (LPCI)/residual heat removal (RHR) outboard injection valve 1-FCV-74-66. The valve failed to open on October 23, 2010, when operators attempted to place RHR Shutdown Cooling loop II in service to support Unit I refueling outage activities. The valve disc was subsequently found to be separated from the disc skirt/stem assembly and lodged in the seat. The NRCs finding was that the licensees failure to establish adequate design control and perform adequate maintenance on valve 1-FCV-74-66, which resulted in the valve being left in a significantly degraded condition and RHR loop II unable to fulfill its safety function, was the originally identified performance deficiency. The NRC had provided a preliminary greater than Green significance determination in Reference 2. The NRC concluded in its letter of May 9, 2011 that the FSD for the valve failure was Red due primarily to fire risk. In its May 9, 2011 letter, the NRC also acknowledged that inadequate design control may not have been a primary contributor to the valve failure and that it was unlikely that the valve failure was caused by unthreading of the valve internals due to undersized welds.

The Tennessee Valley Authority (WA) acknowledges the safety significance of this event and continues to implement extensive corrective actions to reduce fire risk as quickly as possible at BFN. As an example, BFN has just completed implementing changes to certain of the Safe Shutdown Instructions that can be used in the event of an Appendix R type fire to provide guidance to operators on the use of alternate means to provide water to the reactor core should the primary means not be available. WA is continuing to implement the changes discussed at the April 4, 2011 Regulatory Conference and illustrated by the graph provided in Enclosure 1.

While WA does not agree with the performance deficiency identified in the May 9, 2011 NRC letter regarding the non-compliance of BFNs Inservice Testing (1ST) Program with the American Society of Mechanical Engineers (ASME) Operation and Maintenance Code (CM Code), 1995 Edition, 1996 Addendum, Section ISTC 4.1, WA has initiated a number of actions to enhance the 1ST program related to the issues raised in Reference 1. Most significantly, WA has assembled a team of industry-recognized 1ST experts including the principal author of NUREG 1482, Guidelines for Inservice Testing at Nuclear Power Plants, Revision 1. This team is conducting a review of BFNs 1ST Program and its implementation for compliance and performance issues. The 1ST programs for TVAs other nuclear plants will likely be included in this review process. Other corrective actions may be identified once the root cause analysis is completed and approved.

WA has also been in contact with other licensees of similar plants and pressurized water reactor plants regarding their implementation of CM Code Section ISTC 4.1 and found that their understanding and implementation of this code requirement is the same as WAs. Accordingly, TVA has engaged the Nuclear Energy Institute (NEI) on the need to assemble an industry perspective with regard to this issue and consider the generic implications of implementing the requirements of the CM Code as described in the May 9, 2011 NRC letter and whether any appropriate industry actions are warranted.

U. S. Nuclear Regulatory Commission June 8,2011 Page 3 As demonstrated during the Regulatory Conference on April 4, 2011, WA thoroughly analyzed the safety significance, root cause, and extent of cause and condition of the failure of valve 1-FCV-74-66. When disassembled following its failure, valve 1-FCV-74-66 was found to have several non-conformances relative to applicable design documents, including lack of an anti-rotation key, undersized tack welds between the disc and disc skirt/stem assembly, and lack of a thrust washer. These non-conformances were the basis for the original performance deficiency identified by the NRC in Reference 2, because they were assumed to be the cause of the disc separation from the disc skirt/stem assembly. However, the actual cause of the failure was found to be a manufacturing deficiency, i.e., undersized threads in the disc skirt, which resulted in axial separation of the disc from the disc skirt/stem assembly. The originally identified deficiencies were found to not be contributors to the valve failure as acknowledged in the NRCs May 9, 2011 letter. Because WA could not have reasonably identified the manufacturing deficiency, no licensee performance deficiency existed. Corrective actions have been taken to assure operability of valve 1-FCV-74-66 and identical valves at BFN.

Subsequent to the Regulatory Conference, the NRC identified an inadequate 1ST program at BEN as the performance deficiency in Reference 1, where the NRC stated that the required 1ST program provided TVA with an opportunity to preclude and/or identify the LPCI valve failure sooner, and concluded that certain aspects of BENs 1ST Program were inadequate. WA considers that BFNs 1ST Program and its implementation are in compliance with Section ISTC 4.1 of the CM Code as it is understood by WA and many others in the industry, and that no licensee performance deficiency related to 1ST was related to the valve failure. This issue was not addressed by WA at the Regulatory Conference since the NRC did not, prior to the conference, identify the 1ST program as an issue. The NRCs position in the FSD regarding the 1ST program is not based on a complete understanding of the issues since WA did not have an opportunity to address the matter during the Regulatory Conference. As a result, WAs June 2, 2011 letter requested another Regulatory Conference or public management meeting to present information that was not provided at the Regulatory Conference nor in answer to NRC questions before and after the Regulatory Conference (Reference 3). As stated in our June 2, 2011 letter, TVA has assembled new information provided in Enclosure 2 regarding BFN and industry implemented 1ST programs that are pertinent to the performance deficiency identified in the NRCs FSD. As a result, WA has concluded as detailed in Enclosure 2, that there were no methods other than the ones implemented by WA to comply with the CM Code to detect the failure of valve 1-FCV-74-66. The NRC responded to our letter on June 7, 2011 (Reference 4),

and denied WAs request for a forum to discuss the performance deficiency identified as BFNs 1ST Program. The NRCs June 7, 2011 letter also denied WAs request to delay the date by when an appeal of the FSD must be submitted.

Accordingly, WA has carefully reviewed the FSD and NOV and provides this response. WA respectfully appeals the FSD in accordance with the process established in NRC Inspection Manual Chapter 0609, Attachment 0609.2, Process for Appealing NRC Characterization of Inspection Findings. Additionally, in accordance with NRC Manual Chapter 0305, Section 12.06, WA requests that NRC approve a deviation from the Action Matrix with respect to this finding. The detailed bases for the FSD appeal and Action Matrix deviation are provided in the . This deviation would be related to the scope of the NRC inspection that will be

U.S. Nuclear Regulatory Commission June 8,2011 Page 4 conducted in accordance with NRC Inspection Procedure 95003, and would be the subject of a meeting between the NRC and TVA as noted in the NRCs June 7, 2011 letter. Also, TVAs reply to the NOV is provided in Enclosure 3.

This appeal has sufficient merit for review since it falls into the category of new information that was not available at the time of the Regulatory Conference. As explained above, this information was not available at the time of the Regulatory Conference because TVA did not know at that time that an inadequate 1ST program would be identified as the performance deficiency. TVA informed the NRC in its June 2, 2011 letter, within the 30-day appeal period, that new information had been assembled. Furthermore, this performance deficiency raises significant generic issues because BENs 1ST Program for Section 4.1 of the OM Code is consistent with the 1ST programs for this provision of the code at other nuclear plants based on a preliminary survey of 17 other nuclear plants. As a result, NEI is now looking into the generic implications of implementing the OM Code as described in the NRCs May 9, 2011 FSD letter.

There are no new regulatory commitments in this FSD appeal. Should you have any questions, please contact Rod M. Krich at (423) 751-3628.

Respectfully, Preston D. Swafford

Enclosures:

1) Fire SDP Risk Reduction Curve
2) Final Significance Determination Appeal, Cornerstone: Mitigating Systems
3) Reply to a Notice of Violation; EA-1 1-018 cc (Enclosures):

NRC Deputy Executive Director for Reactor and Preparedness Programs NRC Deputy Executive Director for Materials, Waste, Research, State Tribal and Compliance Programs NRC Director, Office of Enforcement NRC Director, Office of Nuclear Reactor Regulation NRC Senior Resident Inspector, Browns Ferry Nuclear Plant

ENCLOSURE I Browns Ferry Nuclear Plant, Unit I Docket No. 50-259 Fire SDP Risk Reduction Curve

Fire SDP Risk Reduction Curve (Current Schedule) 2.50E-05 (1 .OE-5,1 .OE-4) 2.OOE-05 1 .50E05 L.

(U a,

>- m I- z a, C.)

m I U 0 1 .OOE-05 (j) 0 0 C

- (I, ii C)

(1.OE-6, 1.OE-5) 5.00E-06 (CDF< 1.OE-6) 0.00 E÷00 Pull- SSI With Forward Incipient Provide SSI SSI N FPA Alternate 805 SDP As Fire Divisional Revision Revision Safe Based Original Currently Detection Tray (Phase 1, (Phase 2, Shutdown SS I Value Scoped SDB Protection FA25, FAs CDF Path (Q2 > IL-6) (2012)

(Oct (Q1 2011) (Qi 2011) 26) 2011) 2010)

[_._ Extrapolated SDP Risk for Unit 1 2.29E-05 1 .85E-05 1 .67E-05 1 .26E-05 6.30E-06 5.68E-06 2.89E-06 I .OOE-06

-Extrapolated SDP Risk for Unit 2 2.13E-05 1 .85E-05 1 .70E-05 I .38E-05 6.88E-06 6.49E-06 3.76E-06 1 .OOE-06 IExtrapolated SDP Risk for Unit 3 1.66E-05 1 .35E-05 1.33E-05 1.12E-05 5.58E-06 5.15E-06 1.16E-06 1.OOE-06

ENCLOSURE 2 Browns Ferry Nuclear Plant, Unit I Docket No. 50-259 Final Significance Determination Appeal Cornerstone: Mitigating Systems

ENCLOSURE 2 Browns Ferry Nuclear Plant, Unit I Docket No. 50-259 Final Significance Determination Appeal Cornerstone: Mitigating Systems Introduction The NRCs Final Significance Determination (FSD) (Reference 1) characterized a performance deficiency associated with the Browns Ferry Nuclear Plant (BFN), Unit 1, low pressure coolant injection (LPCI)/residual heat removal (RHR) outboard inspection valve, 1-FCV-74-66, as a Red finding. The NRC considered the valve to be inoperable from March 13, 2009, to October 23, 2010, when the valve failed to open when operators attempted to place RHR Shutdown Cooling loop II in service to support Unit I refueling outage activities. As a result, the RHR loop II subsystem was inoperable while Unit I was operating in Mode 1.

Initially, in the NRCs preliminary greater than Green significance determination (Reference 2),

the NRC described the performance deficiency associated with the valve as a failure to establish adequate design control and perform adequate maintenance on the valve. The preliminary determination stated that visual inspections had identified that the valve disc was stuck in the valve seat, blocking RHR loop II flow. The disc was separated from the valve disc skirt/stem assembly. Two fillet welds between the disc skirt and the disc were fractured. The original statement of the performance deficiency was based upon an assessment that the welds were undersized, a disc skirt locking key was missing, and a thrust washer between the stem and the disc was missing. The performance deficiency also focused on maintenance in 2006 in which 1-FCV-74-66 was refurbished and the valve stem was replaced.

At a Regulatory Conference on April 4, 2011, Tennessee Valley Authority (WA) presented the results of its root cause evaluation based on comprehensive forensics performed on the valve.

WA determined that the disk separation from the disc skirt/stem assembly resulted from an original manufacturing defect undersized threads in the disc/skirt assembly. The valve was purchased from a vendor as an assembly in 1968 under the vendors 10 CFR Part 50, Appendix B Quality Assurance program. The valve was not taken apart to perform receipt inspections, since the manufacturer provided the required certifications and no reasonable basis existed thereafter to measure the threads and identify the undersized thread condition. The evaluation determined that undersized welds and the missing thrust washer and locking key were not the root cause or contributing causes of the valve failure. Accordingly, the root cause analysis determined that no licensee performance deficiency existed. The degraded condition was not the result of a failure to establish adequate design control or perform adequate maintenance as suggested in the NRC Report (Reference 2).

WA also presented at the Regulatory Conference the results of detailed analyses and laboratory testing by Performance Improvement International (PIt) to determine the valves capability to function in its as-found condition (i.e., separation of disc from disc skirt/steam assembly). Based on an energy balance approach to determine the energy that would be supplied to the valve body and associated deflection from each stem stroke, and the vibration E2-I of 21

effect and unseating force on the valve disc, P11 determined that the disk would have released from the seat and provided proper flow within seven minutes. This was supported by evidence that the disc separated in November 2008, but nonetheless the valve loosened and operated as a check valve capable of allowing flow in March 2009. Flow within at most seven minutes would render the valve functional for the limiting Appendix R fire event in the significance determination risk assessment. P11 stated that it had very high confidence in its findings.

In the FSD the NRC acknowledged that the weld configuration on 1-FCV-74-66 reasonably achieved its design function to prevent unthreading of the disc to skirt joint. Therefore, the NRC acknowledged the design aspects originally considered as part of the performance deficiency associated with the preliminary finding may not have been a primary contributor to the valve failure.

Nonetheless, the NRC in the FSD re-defined the performance deficiency related to design control and maintenance of the valve. The NRC stated that the required BFNs Inservice Test (1ST) Program provided TVA with an opportunity to preclude and/or identify the LPCI valve failure sooner. Based on certain specific information requested by NRC and provided by TVA after the regulatory conference, the NRC concluded that certain aspects of the WA 1ST program were deficient. In summary, the NRC FSD stated:

Based on our review, the NRC has determined that certain aspects of TVAs 1ST program were inadequate. Namely, the NRC determined that TVAs failure to implement an 1ST program in accordance with the American Society of Mechanical Engineers (ASME), Code for Operation and Maintenance of Nuclear Power Plants (CM Code), 1995 Edition, 1996 Addenda, Section ISTC 4.1, precluded the timely identification that the RHR loop II subsystem was unable to fulfill its safety function due to a failure of LPCI Outboard Injection Valve 1-FCV-74-66. The NRC has concluded that WAs 1ST program inadequacy was well within its purview, and represents a performance deficiency.

WAs appeal with respect to the FSD is based upon TVAs position that BENs 1ST Program was not inadequate as detailed in this enclosure and that no licensee performance deficiency related to 1ST was involved in the valve failure. This issue was not addressed at the Regulatory Conference by WA because NRC did not, prior to the conference, identify the 1ST program as an issue. The NRCs position in the FSD regarding BFNs 1ST Program is not based on a complete understanding of the issues since WA did not have an opportunity to address the matter during the Regulatory Conference, and raises significant generic issues.

In accordance with Manual Chapter 0609, Attachment 0609.02, WA maintains that an appeal of the FSD is appropriate because:

  • new information is available to address the revised performance deficiency related to the adequacy of BENs 1ST Program. The information was not presented at the regulatory conference only because BENs 1ST Program had not been raised by the NRC as a performance deficiency and was not discussed.

E2-2 of 21

1ST Program Adeciuacy The valve in question, Unit I RHR loop (system) II 1-FCV-74-66, serves primarHy to throttle RHR flow during shutdown cooling operations. During normal operation, this valve is in the fully open position. Its safety function is to remain in the fully open position in the event of an accident so that the LPCI pump can inject water into the reactor core. While the operators may use this valve to throttle LPCI flow post-accident, its primary safety function is to remain open. Furthermore, neither ultrasonic or radiographic testing can be used to determine the obturator position due to the valve configuration and construction materials.

TVA considers that BFNs 1ST Program is in full compliance with the American Society of Mechanical Engineers (ASME) Operation and Maintenance of Nuclear Power Plants Code (CM Code), 1995 Edition, 1996 Addenda, paragraphs ISTC 4.1 and ISTC 4.2.3, as mandated by NRC via 10 CFR 50.55a. The program as applied to this and similar valves is consistent with NUREG-1482, Guidelines for lnservice Testing at Nuclear Power Plants, Revision 1. In addition, benchmarking determined that BENs 1ST Program approach for implementing ISTC 4.1 and ISTC 4.2.3 is consistent with industry practices. These conclusions are in agreement with the professional opinion of industry-recognized experts as attested to in the attached affidavit (Attachment 2). The following discussion also supports this conclusion.

ISTC 4.1 covers testing performed on a 2-year basis. The first sentence of ISTC 4.1 states:

Valves with remote position indicators shall be observed locally at least once every 2 years to verify that valve operation is accurately indicated.

ISTC 4.1 is thus very specific in that it:

a. Provides the scope valves with remote position indicators
b. Mandates the method shall be observed locally
c. Specifies frequency at least once every 2 years
d. Defines a purpose verify that valve operation is accurately indicated This requirement must be taken in its entirety. It is improper to focus on the purpose without also focusing on the scope, method, and frequency. The following table shows how TVA complies with each aspect of this requirement through BFNs 1ST Program procedure 1-SR-3.3.3.1.4 (H II).

E2-3 of 21

ISTC 4.1 - First Sentence TVA BFN Procedure 1-SR-3.3.3.1.4(H II)

Provides scope valves with remote position

- Section 1.2 states that the scope indicators encompasses inservice testing of remote position indicators of RHR System II valves (including I -FCV-74-66)

Mandates the method shall be observed

- Section 7.2, steps [4] through [9] verifies, locally control room lights and visually (locally) checks valve position Specifies frequency at least once every 2

- Section 1.3 requires test performance every 2 years years per ASME CM Code Defines a purpose verify that valve operation

- Section 1.1 states this procedure verifies that is accurately indicated valve positions are accurately indicated The remaining sentences of ISTC 4.1 are not requirements applicable to 1-FCV-74-66 as shown in the table below.

ISTC 4.1 - Remaining Sentences Comments Where practicable, this local observation should While it is known that the NRC does not be supplemented by other indications such as recognize official Code Interpretations, WA use of flowmeters or other suitable considers that it is important to point out that instrumentation to verify obturator position. ASME CM Code Interpretation 99-9 and Code Interpretation Question I of Inquiry Tracking Number 11-913 (Attachment 1) clarify that use of supplemental indications is not a requirement of the ASME CM Code. While WA does not document use of supplemental indications to verify obturator position of 1-FCV-74-66, normal operating evolutions and 1ST full flow testing of the downstream check valve provide supplemental indication of 1-FCV-74-66 obturator position, although not specifically documented as such in the 1ST Program.

A similar valve at BFN experienced disc-to-stem separation in 1974. The root cause was determined to be unthreading of the disc from the skirt/stem due to flow induced vibration.

The design was changed for all similar valves at BFN following the 1974 event to eliminate the flow induced vibration failure mechanism.

This corrective action was fully effective in that separation due to flow induced vibration did not recur over the subsequent 36 years.

In 2008, degradation of various residual heat removal heat exchanger service water (RHR E2-4 of 21

HX SW) outlet flow control valves was found, including disc to stem separation (see NRC Special Inspection Report 05000259, 260, and 296/2008007). This was due to flow-induced vibration from throttling, a different failure mechanism than the one associated with valve 1-FCV-74-66 in 2010.

There was no other BFN or industry operating experience which indicated the current design of valve I -FCV-74-66 was susceptible to disc-to-skirt/stem separation caused by a manufacturing defect of undersized threads leading to a pull-out.

Therefore, there was no reason to consider formal documented use of supplemental methods of remote position indication.

The 2010 stem-to-disc separation event was detected by normal outage operating evolution of placing RHR System II in shutdown cooling mode. Once the separation was detected, WA took corrective action to disassemble and examine all similar valves across the three units for common cause as soon as conditions permitted. No other instances of incipient disc-to-skirt/stem failure were detected.

These observations need not be concurrent. For the reasons just noted, 1ST remote position verification (local observation) is not performed concurrent with other supplemental indication of 1-FCV-74-66 obturator position which occurs during the course of system operating evolution and 1ST full flow testing of the downstream check valve. Supplemental indication of obturator position is not specifically documented as such in the 1ST program.

Where local observation is not possible, other Local observation of 1-FCV-74-66 is possible indications shall be used for verification of valve and performed in accordance with procedure operation. 1-SR-3.3.3.1.4(H II). Therefore, this requirement is not applicable.

ISTC 4.2.3, which is also discussed in the FSD, covers testing that is performed on a quarterly frequency. It states:

The necessary valve obturator movement shall be determined by exercising the valve while obseiving an appropriate indicator, such as indicating lights that signal the required change of obturator position, or by obseiving other evidence, E2-5 of 21

such as changes in system pressure, flow rate, level, or temperature, that reflects change of obturator position.

Again, this provision is very specific in that it:

a. Provides the test scope the necessary valve obturator movement shall be determined
b. Mandates the method by exercising the valve while observing an appropriate indicator
c. Provides examples of appropriate indicators, such as indicator lights that signal the required change of obturator position, or by observing other evidence, such as changes in system pressure, flow rate, level, or temperature, that reflects change of obturator position.

This requirement must be taken in its entirety. It is improper to focus on the scope without also focusing on the method and examples. The table below shows how WA complies with each aspect of this requirement.

ISTC 4.2.3 TVA BFN Procedure 1-SI-3.6.1.3.5 (RHR II)

Provides test scope the necessary valve

- Section 1.1 states the purpose is to verify the obturator movement shall be determined opening time of 1-FCV-74-66. In addition, Section 1.2 states the valve will be operated through at least one complete cycle and will measure the time to stroke the valve to the position required to perform its safety function.

Mandates the method by exercising the

- Section 7.2, steps [1] through [4] exercises and valve while observing an appropriate indicator measures the valve stroke time while observing indicating lights Provides examples of appropriate indicators, such as:

. indicator lights that signal the required Section 3.OB defines the stroke time as the change of obturator position, period from initial switch movement to panel indication of completed valve travel. Section 7.2, steps [1] through [4] exercises and measures the valve stroke time using indicating lights.

Indicating lights are specifically cited as an example of an appropriate indicator to determine necessary obturator movement.

. or by, observing other evidence, such This option was not used because the other as changes in system pressure, flow example cited as an appropriate indicator rate, level, or temperature, that (indicating lights) is used. The use of the or by reflects change of obturator position. in the Code language indicates that only one method is required.

E2-6 of 21

In addition, CM Code Interpretation Question 2 of Inquiry Tracking Number 11-913 (Attachment 1) clarifies that when indicator lights are used, it is not a Code requirement to also observe other evidence that reflects change of obturator position. Furthermore, Section 1.3 states the test frequency as once per 92 days. Exercise testing is typically performed when the portion of the system, in which the valve is located is in static conditions. Specifically, valve 1-FCV-74-66 is located in a standby system so there is no possibility of a change in flow, pressure, temperature, etc., during the quarterly (i.e., 92 day) exercise test performed to satisfy ISTC 4.2.3.

NUREG-1482, Revision 1, Section 4.2.7 provides NRC guidance and recommendations regarding remote position indication verification of valves. Revision 1 of NUREG-1482 is the version applicable to BFN. NUREG-1482, Revision 1, specifically states that Revision 0(1995) is only valid for licensees who have not updated their 1ST programs to the 1995 Edition/i 996 Addenda or a later edition of the Code. BFNs 1ST Program complies with the 1995 Edition/i 996 Addenda as required by 10 CFR 50.55a(b)(3) and 10 CFR 50.55a(f)(4)(ii).

NUREG-1482, Revision 1, specifically states that it is applicable to the 1995 Edition/i 996 Addenda and later editions and addenda of the Code. The following table compares this guidance with TVAs implementation through testing of valve i-FCV-74-66.

NUREG-1482, Revision 1, Section 42.7, Comments Verification of Remote Position Indication for Valves by Methods Other Than Direct Observation

Introduction:

The purpose of Section 4.2.7 is to address those valves which cannot be observed locally. BFN CM Subsection ISTC 3700 [4.1] requires that valve i-FCV-74-66 can be observed locally.

valves with remote position indicators must be observed at least once every 2 years to verify that valve position is accurately indicated.

. Many valves (such as sealed solenoid valves and valves with enclosed stems) have no provision for verifying the position by direct observation.

  • To verify the position by observation, licensees can disassemble the valve, which could introduce additional valve failure mechanisms.
  • Cther methods (such as nonintrusive techniques, causing the flow to begin or cease, leak testing, and pressure E2-7 of 21

testing) can yield a positive indication of position.

NRC Recommendation: This recommendation is not applicable to BFN valve I -FCV-74-66 because it can be observed If licensees cannot verify remote valve locally.

position by local observation at the valve, an acceptable approach is for the licensee to observe operational parameters (such as leakage, pressure, and flow) that give a positive indication of the valves actual position(s).

  • This is consistent with Subsection ISTC 3700 [4.1].
  • The staff determined that the use of this portion of the OM Code would not require relief if the licensee implements all requirements of Subsection ISTC 3700 [4.1].
  • No other related requirements apply.

However, Commission approval is still required pursuant to 10 CFR 50.55a(f)(4)(iv).

For certain types of valves that can be The use of should in this recommendation is in observed locally, but for which valve stem agreement with ISTC 4.1, as further clarified by travel does not ensure that the stem is ASME Code Interpretation 99-9 and Code attached to the disk, the local observation Interpretation Question 1 of Inquiry Tracking should be supplemented by observing an Number 11-913 (Attachment 1) which state that operating parameter as required by use of supplemental indications is not a Subsections ISTC 3700 and 3520 [4.1, 4.2, requirement of the ASME OM Code.

and 4.5].

As noted in comments to ISTC 4.1 above, WA did not have information or reason to suspect the current design valve 1-FCV-74-66 was susceptible to disc-to-skirt/stem separation, and so there was no compelling reason to consider use of supplemental methods of remote position indication verification.

Basis for Recommendation:

Accurate position indication for safety-related No Comment valves is important for reactor operation under all plant conditions.

The Code requires licensees to verify the No Comment accuracy of the remote position indication for all valves in the 1ST Program that have remote position indication.

E2-8 of 21

Subsection ISTC 3700 [4.1] states that where This is not applicable to BFN valve 1-FCV-74-66 local observation is not possible, licensees because local observation is possible.

shall use other indications to verify operation.

Such indications are also useful to ensure No Comment that a valve disk is connected to the stem.

Licensees are not able to verify the accuracy This is not applicable to BFN valve 1-FCV-74-66 of remote position indication by local because local observation is possible.

observation of many valves, such as those with enclosed stems or sealed solenoid valves, where the valves do not have position indicators, such as pointers, on the valve actuators.

Many positive means are available to verify WA does not document use of supplemental the indication that a valve is open or closed. indications to verify obturator position of 1-FCV-For example, leak rate testing may yield 74-66. Normal operating evolutions and 1ST of positive indication that the disk is in the downstream check valve provide supplemental closed position. In addition, an in-line flow indication of 1-FCV-74-66 position indication.

rate instrument can indicate system flow or flow stoppage. System pressures or The 2010 stem-to-disc separation was detected differential pressure across a valve seat may by normal outage operating evolution of placing also give a positive indication of actual valve RHR System II in shutdown cooling mode. Once position. the separation was detected, WA took immediate action to disassemble and examine all similar valves across the three units for common cause. No other instances of disc-to-skirt/stem degradation were detected.

Based on the above analysis, TVA considers that the BFN 1ST program complies with the applicable requirements of the CM Code and is consistent with NRC guidance in NUREG-1482, Revision 1. This conclusion is consistent with the professional opinion of industry experts as attested to in the attached affidavit (Attachment 2). In this regard, some of the conclusions noted in the FSD letter appear to be based on an incomplete understanding of BFNs 1ST Program details. These points are addressed in the following table. (References are to of the FSD letter.)

Enclosure 2, page 3, first full paragraph Comments The NRC identified that the required 1ST 1ST-related remote position indication testing is program provided WA with an opportunity to performed on a 2-year frequency. The actual preclude and/or identify the LPCI valve failure detection method for the 1-FCV-74-66 sooner. degraded condition was a normal system operation evolution. This evolution occurred before there would have been an opportunity to perform 1ST remote position indication test using supplemental methods such as use of E2-9 of 21

flowmeters, etc. The system must be placed in service before an 1ST test can be performed using flowmeters. Note that the previous supplemental test (full flow check valve test) was successfully performed two years earlier.

In this regard, the post-conference WA stated, in the post-conference supplemental information provided by WA supplemental information provided to NRC, that highlighted that certain aspects of its 1ST BFNs 1ST Program is in compliance with the program were deficient OM Code and the guidance provided in NUREG-1 482, Revision 1. WA further clarified that although it is not a Code requirement to use supplemental methods such as flowmeters in addition to local observation for remote position indication verification, WA performs an 1ST-related full flow check valve test which can be credited as a supplemental method. In this case, the full flow check valve test is performed on a cold shutdown frequency, but does not specifically take credit for remote position indication verification testing of I -FCV-74-66.

Namely, TVAs failure to implement an 1ST TVA fully complies with ISTC 4.1 as shown in Program in accordance with the requirements Item 2 above.

of ASME 1995 Edition, 1996 Addenda, Section ISTC 4.1, precluded the timely identification 1ST-related remote position indication that the RHR loop II subsystem was unable to verification testing is required to be performed fulfill its safety function due to a failure of LPCI at least once every 2 years in accordance with Outboard Injection Valve 1-FCV-74-66 OM Code paragraph ISTC 4.1.

BFN procedure 1-Sl-3.2.21(ll), Cold Shutdown Testing of 1 -CKV-74-68, exercises check valve 1-CKV-74-68 to the full open position by verifying it is capable of passing at least 9,000 gpm Shutdown Cooling flow. This procedure uses valve 1-FCV-74-66 to throttle Shutdown Cooling flow as needed to achieve a flow rate of at least 9,000 gpm. The November 14, 2008 performance of this procedure shows that Section 7.2, Step [1.3] recorded an initial Shutdown Cooling flow of 7,000 gpm as indicated on 1-Fl-74-64. Then, Section 7.0, Step [1.3] throttled 1-FCV-74-66 to obtain a minimum flow rate of 9,000 gpm as indicated on 1-Fl-74-64. This step demonstrates that 1-FCV-74-66 was capable of throttling Shutdown Cooling flow and that 1-FCV-74-66 as well as 1 -CKV-74-68 were both capable of passing the required flow rate of at least 9,000 gpm. This procedure does not specifically take credit for verifying obturator position of 1-FCV-74-66, but the actions are performed just the same as if 1ST credit was beinq taken.

E2-1O of 21

Degradation of 1-FCV-74-66 was detected when Shutdown Cooling was being placed in service in October 2010. This occurred before the opportunity to perform the next scheduled 1 -Sl-3.2.21 (II).

Enclosure 2, page 3, second full paragraph Comments The in-service testing (1ST) program BFNs 1ST Program complies with the CM implemented by WA at Browns Ferry to meet Code Sections 4.1 and 4.2.3.

the requirements of 10 CFR 50.55a,

[incorporates by reference, with conditions, the The CM Code is designed to provide American Society of Mechanical Engineers reasonable assurance of valve operational (ASME), Code for Operation and Maintenance readiness.

of Nuclear Power Plants (CM Code), 1995 Edition, 1996 Addenda], was inadequate to The Code requirements do not provide identify the inability of LPCI Valve 1- FCV absolute assurance of valve operability. It is 66 to perform its intended safety function. possible that some types of valve degradation may go undetected by inservice testing which fully complies with all Code requirements and recommendations. This was the case with valve 1 -FCV-74-66.

Despite the operating experience with LPCI As explained above, a similar valve at BFN Valve 1-FCV-74-66 and other similar valves at experienced disc-to-stem separation in 1974.

Browns Ferry, Units 1, 2, and 3, the WA The root cause was determined to be program at Browns Ferry implemented in unthreading of the disc from the skirt/stem due response to 10 CFR 50.55a(b)(3)(ii) did not to flow induced vibration. The design was ensure that LPCI Valve 1-FCV-74-66 continued changed to eliminate the flow induced vibration to be capable of performing its design-basis failure mechanism for all similar valves at BEN safety function. following the 1974 event. This corrective action was fully effective in that separation due to flow induced vibration has not recurred over the next 36 years.

In 2008, degradation of various residual heat removal heat exchanger service water (RHR HX SW) outlet flow control valves was found, including disc to stem separation. This was due to flow-induced vibration from throttling, a different failure mechanism than the one associated with valve I -FCV-74-66 in 2010.

There was no other BFN or industry operating experience which indicated the current design of valve 1 -FCV-74-66 was susceptible to disc-to-skirt/stem separation caused by a manufacturing defect of undersized threads leadinci to disc-to-skirt/stem pull-out.

E2-11 of 21

Enclosure 2, page 3, last paragraph Comments In NUREG-1482 (April 1995), Guidelines for This is an incorrect reference. NUREG-1 482, lnservice Testing at Nuclear Power Plants, the Revision 0 (April 1995) does not apply to BEN.

NRC staff discussed its interpretation of the NUREG 1482, Revision 1 specifically states ASME CM Code requirement for verification of Revision 0 is only valid for licensees who have remote position indication. not updated their 1ST programs to 1995 Edition/I 996 Addenda or a later edition of the Code. BENs 1ST Program complies with the 1995 Edition/i 996 Addenda as required by 10 CFR 50.55a(b)(3) and 10 CFR 50.55a(f)(4)(ii).

NUREG-i482, Revision 1, specifically states it is applicable to 1995 Edition/i 996 Addenda and later editions and addenda. , page 4, first full paragraph Comments In Revision 1 to NUREG-i482, the NRC staff in NUREG-i482, Revision I revised the NUREG Section 4.2.7 discussed its interpretation of the 1482, Rev. 0, Section 4.2.5 (equivalent to ASME CM Code for position indication 4.2.7) language from must to should.

verification. The staff continued to specify that the first sentence in ISTC 4.1 provides the The term must is used numerous times in requirement for verification of the accuracy of NUREG-1482, Revision I to denote the remote position indication for all valves in requirements. Therefore, it seems clear the the 1ST program with remote position change from must to should in indication. The staff noted that when a Section 4.2.7 was for a reason other than to licensee cannot verify remote valve position by reflect that the NUREG provides guidance for local observation, an acceptable approach is to licensee 1ST Programs. The reasonable observe operational parameters (such as explanation for the change was because there leakage, pressure, and flow) that give a is no Code language or other regulatory positive indication of the valves actual requirement which supports the use of must.

position(s). The staff modified the discussion regarding supplementing local observations (i.e., must to should) to reflect that the NUREG provided guidance for licensee 1ST proq rams.

Enclosure 2, page 4, second full paragraph Comments The acceptance criteria requires that valve Procedure 1-SR-3.3.3.1 .4(H II), Section 6.OB position be visually checked in the correct states, position.

Visual verification of valve position (open/closed) is accurately indicated by its remote position indicators (red, green lights) at the Main Control Room panels. Local valve position verification can make use of limit switches, position indicators on the valve, valve E2-12 of 21

stem travel, etc., to determine valve position.

Section 7.2, steps [4] through [9] check the control room indicating lights and visually check valve position locally.

This method of verification does not ensure that There is an error in the enclosure where it the disc is attached to the disc and therefore is states, .. .disc is attached to the disc. . . It unable to adequately verify valve internal should state, . . .disc is attached to the operations, as described in the ASME code as stem.

obturator position.

This statement incorrectly implies it is a requirement of ISTC 4.1 that local observation of valve operation be supplement by other indications to verify obturator position. CM Code Interpretation 99-9 and Code Interpretation Question 1 of Inquiry Tracking Number 11-913 (Attachment 1) clarify this is not a requirement of the Code.

In addition, WA had knowledge that this valve WA does not agree with this statement. A design is susceptible to stem and disc similar valve at BFN experienced disc-to-stem separation based on its design configuration. separation in 1974. The root cause was determined to be unthreading of the disc from the skirt/stem due to flow induced vibration.

The design was changed to eliminate the flow induced vibration failure mechanism for all similar valves at BEN following the 1974 event.

This corrective action was fully effective in that separation due to flow induced vibration did not recur over the subsequent 36 years.

In 2008, degradation of various residual heat removal heat exchanger service water (RHR HX SW) outlet flow control valves was found, including disc-to-stem separation (see NRC Special Inspection Report 05000259, 260, and 296/208007). This was due to flow-induced vibration from throttling, a different failure mechanism than the one associated with valve 1-FCV-74-66 in 2010.

There was no other BFN or industry operating experience which indicated the current design of valve 1 -FCV-74-66 was susceptible to disc to-skirt/stem separation caused by a manufacturing defect of undersized threads leading to a pull-out.

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Enclosure 2, page 4, last paragraph Comments WA testing acceptance criteria for As explained above, procedure 1-SR-3.6.5 implementing procedure, 1-SR 3.6.1.3.5, (RHR II) complies with ISTC 4.2.3. Use of intended to meet the ASME code requirements indicating lights is specifically cited in ISTC via verification of the open/shut indicating lights 4.2.3 as an example of an appropriate indicator during valve stroke and time testing. to determine necessary obturator movement.

This surveillance was also unable to Procedure 1-SR-3.6.5 (RHR II) performs adequately verify obturator movement, and did exercising and stroke time measurement of 1-not identify the stem and disc separation. FCV-74-66 on a quarterly frequency. The use of indicating lights is the only practical and appropriate indicator to determine obturator movement during plant modes of operation present during quarterly testing. Specifically, valve 1 -FCV-74-66 is located in a standby system so there is no possibility of a change in flow, pressure, temperature, etc., during the quarterly (92 day) exercise test performed to satisfy ISTC 4.2.3. This approach is consistent with industry practices as attested to in the attached affidavit (Attachment 2).

Enclosure 2, page 5, first paragraph Comments The staff concluded that the opportunity existed As discussed above, the 1ST program complies for the testing program to discover the failure with Code requirements, as mandated by NRC had the testing program met the code via 10 CFR 50.55a, which are written to provide requirements to verify that valve operation is reasonable assurance of valve operational accurately indicated, readiness.

The 10 CFR 50.55a regulation and the Code requirements do not provide absolute assurance of valve operability. It is possible that some types of valve degradation may go undetected by inservice testing which fully complies with all Code requirements and recommendations. This was the case with valve 1 -FCV-74-66.

Enclosure 2, page 5, second paragraph, Comments first_bullet The staff questioned the licensee specifically As discussed above, BFNs 1ST Program on other actions beyond using the indication complies with ISTC 4.1 and ISTC 4.2.3.

lights to verify obturator movement. The Furthermore, the BFN methods are supported licensee responded that they use lights and by OM Code Interpretation 99-9 and Code local position indication (stem movement), Interpretation Question I of Inquiry Tracking because that meets the code requirements and Number 11-913 (attached) which have been E2-14 of 21

is consistent with industry practices. The staff approved through ASME which is the only has concluded that this was an improper organization authorized to interpret the OM interpretation and implementation of the code Code.

requirements.

Enclosure 2, page 5, second paragraph, Comments second_bullet The staff additionaNy verified, with the licensee, As performed in November 2008, procedure 1-that flow testing or flow parameter verification is Sl-3.2.21(ll) demonstrated full flow (9,000 gpm) not used to verify stem to disc separation. The was passed through check valve 1-CKV-74-68.

staff did not find that the other licensees This check valve is located downstream of procedures and actions provided a means to valve 1-FCV-74-66. Therefore, 1-FCV-74-66 identify stem to disc separation. Specifically passed at least 9,000 gpm in order to meet the the staff considered flow testing on the 1-FCV- acceptance criteria for the full flow test of 1-74-68 in the RHR loop Il system. This CKV-74-68. Specifically, performance of this procedure was not designed in any way for procedure used 1-FCV-74-66 to throttle verification of 1-FCV-74-66 proper obturator shutdown cooling flow through 1-CKV-74-68 movement and therefore was not able to meet from 7,000 gpm to 9,000 gpm. Although, ASME code requirements and continued ability procedure 1-Sl-3.3.21(ll) does not specifically of 1-FCV-74-66 to fulfill its safety function. address position indication verification of 1-FCV-74-66, it is incorrect to conclude that this procedure would not have verified proper obturator movement. This procedure was not able to be performed in October 2010 because it requires RHR System loop II to be in service in shutdown cooling mode of operation.

Degradation of 1 -FCV-74-66 was detected when placing RHR System II into service for shutdown cooling.

Enclosure 2, page 5, third paragraph Comments Furthermore, WA had operating experience A similar valve at BFN experienced disc-to-that indicated this valve design is susceptible to stem separation in 1974. The root cause was separation failures, determined to be unthreading of the disc from the skirt/stem due to flow induced vibration.

The design was changed to eliminate the flow induced vibration failure mechanism for all similar valves at BFN following the 1974 event.

This corrective action was fully effective in that separation due to flow induced vibration did not recur over the subsequent 36 years.

Previous issues experienced on multiple valves In 2008, degradation of various residual heat (including 1-FCV-74-66) at Browns Ferry removal heat exchanger service water (RHR established that this valve was susceptible to HX SW) outlet flow control valves was found, stem and disc separation. One similar instance including disc to stem separation. This was E2-15 of 21

resulted in a valve disc separating from the due to flow-induced vibration from throttling, a stem and becoming stuck in its seat. The different failure mechanism than the one previous failure was identified following a associated with valve 1-FCV-74-66 in 2010.

failure of the system to operate when being placed in service. Other valves at the Browns There was no other BEN or industry operating Ferry site also have experienced stem and disc experience which indicated the current design separation issues (see NRC Special Inspection of valve I -FCV-74-66 was susceptible to disc-Report 05000259, 260, and 296/2008007, to-skirt/stem separation caused by a Section 4OA2.f). manufacturing defect of undersized threads leading to a pull-out.

Review of NRC Information Notices, inspection reports, and other communications did not identify any instances where deficiencies in implementation of ASME OM Code 1ST Programs were cited in relation to disc-to-stem failures. Therefore, no precedent existed which would have warranted TVA corrective action.

Enclosure 2, page 5, fourth paragraph Comments Based on our review, the NRC has determined As discussed above, the 1ST program complies that certain aspects of TVAs 1ST Program with Code requirements, as mandated by NRC were inadequate. Namely, the NRC via 10 CFR 50.55a. TVAs 1ST Program was determined that TVAs failure to implement an submitted to the NRC in 2002 as required by 1ST Program in accordance with the American OM Code ISTA 1.4(c). Benchmarking Society of Mechanical Engineers (ASME), determined that BFNs 1ST Program approach Code for Operation and Maintenance of for implementing ISTC 4.1 and ISTC 4.2.3 is Nuclear Power Plants (OM Code), 1995 consistent with industry practices as attested to Edition, 1996 Addenda, Section ISTC 4.1, in the attached affidavit (Attachment 2).

precluded the timely identification that the RHR loop II subsystem was unable to fulfill its safety In addition, the following facts demonstrate that function due to a failure of LPCI Outboard 1ST would not have provided a more timely Injection Valve 1-FCV-74-66. identification of the 1-FCV-74-66 degradation.

. 1ST-related remote position indication testing is performed on a 2-year frequency.

. The actual detection method for the 1-FCV-74-66 degraded condition was a normal system operation evolution.

. This evolution occurred before there would have been an opportunity to perform 1ST remote position indication test using supplemental methods such as use of flowmeters, etc.

. The system must be placed in service before an 1ST test can be performed using_flowmeters.

E2-16 of 21

Review of NRC Information Notices, inspection reports, and other communications did not identify any instances where deficiencies in implementation of ASME CM Code 1ST Programs were cited in relation to disc-to-stem failures. Therefore, no precedent existed which would have warranted WA taking corrective action.

The NRC has concluded that TVAs 1ST WA has shown BFNs 1ST Program to be in Program inadequacy was well within its accordance with Code requirements and purview, and represents a performance industry practices. Therefore, it is not deficiency reasonable to consider this a performance deficiency simply because valve degradation was detected by a means other than the 1ST program.

Summary BFNs 1ST Program meets applicable requirements and guidance documents and, therefore, testing of valve 1 -FCV-74-66 does not represent a performance deficiency. It is in full compliance with the American Society of Mechanical Engineers (ASME), Code for Operation and Maintenance of Nuclear Power Plants (CM Code), 1995 Edition, 1996 Addenda, paragraphs ISTC 4.1 and ISTC 4.2.3, as mandated by NRC via 10 CFR 50.55a.

Benchmarking determined that BFNs 1ST Program approach for implementing ISTC 4.1 and ISTC 4.2.3 is consistent with industry practices. For example, BFNs sister plants have the same valves in the same application, and implement the requirements of ISTC 4.1 and 4.2.3 in the same manner as BFN.

Review of NRC Information Notices, inspection reports, and other communications did not identify any instances where deficiencies in implementation of ASME CM Code 1ST Programs were cited in relation to disc-to-stem failures. Therefore, no precedent existed which would have warranted WA taking corrective action.

The ASME CM Code language and its predecessor requirements related to remote position indication verification and valve exercising (ISTC 4.1 and ISTC 4.2.3) have remained unchanged from 1987 through the CM Code edition/addenda currently endorsed by NRC.

Current Code 1ST requirements are not designed such that they are capable of detecting degradation of the disc-to-stem connection. They are only capable of detecting failure after it has occurred. The NRC interpretation of the applicable CM Code requirements reflected in the FSD letter would have a significant impact on valve testing at BEN and other plants throughout the industry.

BENs 1ST Program would not have provided a more timely identification of the 1-ECV-74-66 degraded condition for the following reasons.

. 1ST-related remote position indication testing is performed on a 2-year frequency.

E2-17 of 21

  • The actual detection method for the 1-FCV-74-66 degraded condition was a normal system operation evolution.
  • This evolution occurred before there would have been an opportunity to perform 1ST remote position indication test using supplemental methods such as use of flowmeters, etc.
  • The system must be placed in service before an 1ST test can be performed using flowmeters.

Previous valve disc to stem separations at BFN were due to flow-induced vibration and were adequately addressed. Therefore, TVA did not have reason to consider use of supplemental methods in addition to local observation for 1ST remote position indication verification.

It is possible to detect degradation of a valve through normal plant operating evolutions.

Therefore, detection of valve degradation by a means other than the 1ST program does not necessarily represent an 1ST program inadequacy.

BENs 1ST Program does not represent a performance deficiency. Rather BFNs 1ST Program is in compliance with CM Code, ISTC 4.1 and ISTC 4.2.3 and industry practices as attested to in the affidavits from industry-recognized experts provided in Attachment 2 to this enclosure.

No Performance Deficiency NRC Manual Chapter 0609, Significance Determination Process, Section 0609-08, paragraph 08.01, addresses the development of inspection findings to be considered in the Reactor Oversight Program and states (emphasis in original): Findings must represent a deficiency in a licensees performance. TVA has previously demonstrated that the root cause of the inoperable valve I -FCV-74-66 was an original manufacturing defect that occurred prior to initial operation of BFN. The original manufacturers design requirements were not met, resulting in undersized disc skirt threads at the disc skirt/stem assembly connection. No receipt inspection of the thread size of this nature and classification was required. The manufacturer applied an Appendix B QA program and provided certification documentation.

WA also reviewed the maintenance history for the valve and determined that the disc skirt/stem assembly of the original assembly was not replaced prior to the failure and no work was performed that required measuring/confirming the disc skirt thread size. Moreover, as discussed above, the 1ST program at BFN complied with the applicable requirements of Section ISTC 4.1 of the CM Code. Based on industry benchmarking and expert assessments, the 1ST program at BFN was consistent with NRC requirements and industry practices, and did not reasonably provide an opportunity to identify the disc separation. Furthermore, based on the information provided in the previous section, fl/A has concluded that there were no methods other than the ones implemented by BFNs 1ST Program to detect the disc and disc skirt/stem assembly separation experienced by valve 1-FCV-74-66. Given that it was not reasonably within WAs ability to foresee, identify, or prevent the valve failure, there was no licensee performance deficiency to support a Red Finding or to warrant the related regulatory response based on the Reactor Oversight Process Action Matrix.

E2-18 of 21

This conclusion is also consistent with the NRCs Enforcement Policy. WA recognizes that licensees are ordinarily responsible for the acts of their vendors and contractors. However, Section 3.5 of the Policy provides that the NRC may refrain from issuing enforcement actions for violations resulting from matters not within a licensees control, such as equipment failures that were not avoidable by reasonable licensee QA measures or management controls. This policy is also reflected in NRC Enforcement Manual, Section 5.1.4.C, which allows NRC discretion not to issue enforcement actions where the licensees root cause analysis demonstrates that the equipment failure could not have been avoided or detected. NRC Manual Chapter 06112, page 18, also covers enforcement discretion where there is no performance deficiency.

WA is aware of several cases in which the NRC has previously exercised this discretion under the Reactor Oversight Program even for matters that may have involved regulatory violations and greater than Green findings. These examples are:

equipment failure could not have been avoided or detected by quality assurance program or other related control measures because Type 316 stainless steel heater sleeve material was not known to be susceptible to cracking.

  • Indian Point Nuclear Generating Station, Unit 3, NRC Integrated Inspection Report 05000286/2008005 and Exercise of Enforcement Discretion, dated February 5, 2009: safety injection pump breaker did not close during routine operation, but (although a violation) the breaker subcomponent problem that resulted in the inoperability was not within the licensees ability to foresee and correct and, as a result, the NRC did not identify a performance deficiency.
  • Three Mile Island Station, Unit 1, NRC Integrated Inspection Report 5000289/2009002, Exercise of Enforcement Discretion, dated May 13, 2009: a failed electrical relay caused a decay heat river water pump to be inoperable in excess of allowed outage time, but (although a violation) was not the result of a performance deficiency.

A similar outcome is particularly warranted in this case. The root cause for the equipment failure relates to manufacturing by a vendor prior to initial BEN Unit I start up. This does not reflect current licensee performance and thus should not trigger a current, enhanced regulatory response through the Reactor Oversight Process. Also, while TVA does not agree that BFNs 1ST Program was insufficient, the specific issues related to testing of valves of this type are being addressed through a review of BENs 1ST Program by a team of industryrecognized 1ST experts, including the principal author of NUREG-1482, Revision 1, for compliance or implementation issues. Any generic issues related coming out of this review related to BFNs 1ST Program will be addressed prospectively on a generic basis, following appropriate industry interactions.

E2-19 of 21

Action Matrix Deviation If, notwithstanding the lack of any TVA performance deficiency, the NRC chooses to uphold the FSD, TVA requests that the NRC approve a deviation from the Action Matrix in accordance with Manual Chapter 0305, Section 12.06. Deviations are to be utilized in rare instances, such as the present one, in which the regulatory actions dictated by the Action Matrix are not appropriate. The FSD, when entered into the Action Matrix, would lead to an inappropriate level of regulatory attention and diversion of licensee resources and management focus. There are several bases for the conclusion that a deviation is appropriate.

First, as discussed above, the FSD does not reflect on current WA performance. The valve failure was caused by an original manufacturing defect. And, even if the NRC maintains that BENs 1ST Program was a missed opportunity to identify disc separation in the valve, that conclusion would be based on new regulatory expectations for 1ST programs derived from this operating experience. These expectations were not anticipated in the industry or by WA, and therefore cannot be reasonably considered to reflect on TVAs overall, current performance.

Second, as discussed at the Regulatory Conference, the risk significance for the FSD is driven by a limiting Appendix R fire event. WA has previously initiated actions to address fire safe shutdown strategies at BFN and reduce plant risk due to serious fire events, including by transition to a NFPA 805 fire protection methodology (see the Fire SDP Reduction Curve in ). Specifically, the Safe Shutdown Instructions (SSIs) that would be used in the event of an Appendix R fire have been revised as described during the Regulatory Conference.

This revision provides the operators with guidance to use systems other than the ones specified in the SSIs to provide cooling water to the reactor should the systems specified in the SSls not function as expected. All of these actions will address the fire risk issues that would be addressed in a regulatory response under the Action Matrix.

Similarly, fire risk issues at BFN were addressed in connection with previous Yellow and White Findings under the Reactor Oversight Process issued on April 19, 2010 (EA-09-307). The NRC conducted inspections in accordance with Inspection Procedure 95002, and the greater than Green findings have since been closed. However, the present finding with risk dominated by the same fire risk considerations would drive a second assessment potentially including many of the same issues. NRC Manual Chapter 0308, Attachment 3, page 9, provides that there will be multiple inputs to the Action Matrix for conditions that overlap in time only if the findings are separate and independent of each other. In the present circumstances, the risk involved in each of the past and current findings is driven by the same current fire safe shutdown strategies at BEN, which are already in the process of being revised. The findings are, therefore, not separate and independent and should not be double-counted in the Action Matrix.

For all of these reasons, WA considers that a deviation from the Action Matrix would be appropriate if the FSD is upheld.

Clarifications The following clarifications are provided to address statement in the NRCs May 9, 2011 FSD letter.

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  • Cover letter, ninth paragraph, states that the discussion of BFNs 1ST Program issue during the April 29, 2011 conference call between the NRC and WA staffs included.

an exchange of information regarding the implementation of the CM Code requirements at Brown Ferry. . . In fact, the WA staff on that conference call was only able to state that they would investigate the issue, and ensure that it was entered into the Corrective Action Program since that was the first time this issue was identified to them.

  • Enclosure 2, Section 2, Valve Functionality, NRC Response, states in part that TVAs determination of the maximum time it takes for a disc to be freed from its seat was based on the. . . results of a single test. . . This same statement is made later regarding testing to determine the minimum time it takes for a disc to be freed from its seat. In fact there were five tests performed to determine the range of times it would take, from minimum to maximum, for a disc to be freed from its seat. This information was provided to the NRC in response to Round 2 Question No. 3 on April 13, 2011.
  • Enclosure 2, Section 2, Valve Functionality, NRC Response, states in part that. .

uncertainties in the testing methodology which challenged the level of confidence that the testing was representative of actual system conditions. . . . In fact, testing uncertainties and the confidence level that the results reflected actual valve performance were also discussed in response to Round 2 Question No. 3 on April 13, 2011. The confidence level was specified in that answer as 99.7%.

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ATTACHMENT I Three PDTI Avenue tel .21 2.591 .8500 Ne York, NY 1.212.591.8501 SFrr,A,E THE STANØARD 10016-5990 U.S.A. www.asme.org CODES & STANDARDS June 7,2011 Mark Gowin Tennessee Valley Authority Program Manager Appendix J and 1ST 1101 Market Street, LP 4J-C Chattanooga, TN 37402-280 1 Tele: (423) 751 -3669 Fax: (423) 751 -8247 Email: magowin(tva.gov

Subject:

ISTC-4.1 (ASME OM Code -1995 through OMa -1996 Addenda) and ISTC-3700 (ASME OM Code-1998 through 2004 Edition with 2006 Addenda); and ISTC-4.2.3 (ASME OM Code -1995 through OMa 1996 Addenda) and ISTC-3530 (ASME OM Code- 1998 through 2004 Edition with 2006 Addenda).

Reference:

Your Email Dated May 24, 2011 Item: Inquiry Tracking Number 11-913 Question (1): If it is practicable, is it a requirement of ISTC-4. 1 (ISTC-3700) that local observation of valve operation be supplemented by other indications to verify obturator position?

Reply (1): No Question (2): If remote indicating lights provide confirmation of changes in obturator position, is it a requirement of ISTC-4.2.3 (ISTC-3530) to also observe other evidence, such as changes in system pressure, flow rate, level, or temperature, that reflects change of obturator position?

Reply (2): No Sincerely, Robert Horvath Secretary, O&M Standards Committee Phone: 212-591-8514 Fax: 212-591-8501 E-Mail: horvathr(asme.org Attachment I - Page 1 of I

ATTACHMENT 2 Browns Ferry Nuclear Plant, Unit I Docket No. 50-259 Final Significance Determination Appeal Cornerstone: Mitigating Systems JOINT AFFIDAVIT OF STEVEN UNIKEWICZ, WESLEY ROWLEY, AND MARK GOWIN IN SUPPORT OF FSD APPEAL Steven M. Unikewicz

[SMU] My name is Steven M. Unikewicz. I am currently employed as Principal Engineer, Program Manager, for Alion Science and Technology in Vienna, Virginia. In my position at Alion Science and Technology I am responsible for providing component and plant system evaluations and analysis to the nuclear industry.

2. [SMU] Prior to joining Alion Science and Technology, I was a Senior Mechanical Engineer, Mechanical Branch, Office of Nuclear Reactor Regulation, at the U.S.

Nuclear Regulatory Commission involved in the review and development of codes, standards and regulations regarding the inservice testing of components at nuclear power generating stations.

3. [SMU] While at the NRC, I prepared NUREG-1482, Revision 1, Guidelines for Inservice Testing at Nuclear Power Plants. NUREG-1482, Revision 1, provides licensees guidelines and recommendations for developing and implementing programs for the inservice testing of pumps and valves at commercial nuclear power plants.
4. [SMU] This affidavit is prepared to support Enclosure 2 to the Final Significance Determination Appeal Cornerstone: Mitigating Systems for Browns Ferry Attachment 2 Page 1 of 6

ATTACHMENT 2 Nuclear Plant, Unit 1 (FSD Appeal). A statement of my professional qualifications is attached to this affidavit as Attachment A.

5. [SMU] With respect to this joint affidavit, I have included my initials within brackets (i.e., [SMU]) immediately preceding those sections I prepared.

C. Wesley Rowley

6. [CWR] My name is Wesley Rowley. I am currently a Fellow at the ASME. This affidavit is prepared to support Enclosure 2 to the FSD Appeal. A statement of my professional qualifications is attached to this affidavit as Attachment B.
7. [CWRJ Since 1989, I have been a member of the ASME Board on Nuclear Codes

& Standards, which is jointly responsible for guiding the 1000 technical volunteers on eight standards committees, including the Committee on Operations & Maintenance of Nuclear Power Plants. I have been a member of the Operations & Maintenance Main Committee since 1984 and a member of the Subgroup ISTE since 2000. The O&M Committee develops the ASME OM Code and the ASME CM Standards/Guides.

8. [CWR] With respect to this joint affidavit, I have included my initials within brackets (i.e., [CWR]) immediately preceding those sections I prepared.

Mark A. Gowin

9. [MAG] My name is Mark Gowin. I am currently employed as the Corporate Codes Program Manager for Tennessee Valley Authority. This affidavit is Attachment 2 -Page 2 of 6

ATTACHMENT 2 prepared to support Enclosure 2 to the FSD Appeal. A statement of my professional qualifications is attached to this affidavit as Attachment C.

10. [MAG] I have thirty-one years experience in design, construction, modification, and testing of BWR and PWR systems. The last twenty-five years have been primarily focused on development and implementation of engineering programs to meet the requirements of ASME CM Code, ASME Section Xl, and 10 CFR Part 50, Appendix J. In my current position at WA I provide governance and oversight of ASME CM Code Inservice Testing (1ST) Programs for all WA nuclear units. I am responsible for ensuring that the 1ST Programs meet Code and regulatory requirements and industry best practices.
11. [MAG] With respect to this joint affidavit, I have included my initials within brackets (i.e., [MAG]) immediately preceding those sections I prepared.

Statement of Expert Opinion

12. [All] The purpose of this affidavit is to demonstrate that the technical and factual information within my area of expertise and relied upon by WA in the FSD Appeal is consistent with my professional judgment and expert conclusions.
13. [All] I have reviewed the Letter from NRC to TVA, Final Significance Determination of a Red Finding, Notice of Violation, and Assessment Follow-up Letter (NRC Inspection Report 05000259/2011008) Browns Ferry Nuclear Plant, dated May 9, 2011. I have also reviewed the American Society of Mechanical Engineers (ASME), Code for Operation and Maintenance of Nuclear Power Plants (CM Code), 1995 Edition, 1996 Addenda, Sections ISTC 4.1 and ISTC Attachment 2- Page 3 of 6

ATTACHMENT 2 4.2.3. I am also familiar with the 1ST program at Browns Ferry Nuclear Plant, Unit 1.

14. [SMU, CWR] Based on my review of the BFN 1ST program and my professional judgment, I conclude that the BFN 1ST Program is in compliance with the American Society of Mechanical Engineers (ASME) Operation and Maintenance of Nuclear Power Plants Code (CM Code), 1995 Edition, 1996 Addenda, Paragraphs ISTC-4.1 and ISTC-4.2.3. The BFN 1ST methods are also supported by ASME Code Interpretation 99-9, which clarifies that supplemental indications are not a requirement of the ASME CM Code to verify valve obturator position.
15. [SMU] Based on my review of the BEN 1ST program and my expertise as author of NUREG-1482, Revision 1, I further conclude that the BEN 1ST program is consistent with NUREG-1482, Guidelines for Inservice Testing at Nuclear Power Plants, Revision 1.
16. [MAG] I have determined through benchmarking with other plants that BENs 1ST Program approach for implementing ISTC-4.1 and ISTC-4.2.3 is consistent with industry practices, including the 1ST program at its sister plant.
17. [SMU] I actively participated in the drafting of the ESD Appeal for WA. I provided technical input related to 1ST program adequacy, including compliance with the applicable ASME OM Code requirements for 1ST Programs and NUREG-1482, Revision 1. I have reviewed those sections of the appeal addressing 1ST program adequacy and compliance with ASME Code requirements and NUREG-1482 and fully support the discussion provided therein.

Attachment 2 Page 4 of 6

ATTACHMENT 2

18. [CWR] I actively participated in the drafting of the FSD Appeal for WA. I provided technical input related to 1ST program adequacy, including compliance with the applicable ASME OM Code requirements for 1ST Programs. I have reviewed those sections of the appeal addressing 1ST program adequacy and compliance with ASME Code requirements and fully support the discussion provided therein.
19. [MAG] I actively participated in the drafting of the FSD Appeal for WA. I provided technical input related to 1ST program adequacy, including benchmarking of the BFN 1ST program. I have reviewed those sections of the appeal addressing 1ST program adequacy and benchmarking and fully support the discussion provided therein.
20. [All] I hereby certify under penalty of perjury that the foregoing is true and complete to the best of my knowledge, information, and belief. Executed on June 8,2011.

Executed in accord with 10 C.F.R. § 2.304(d),

Is! Steven Unikewicz Steven Unikewicz Principal Engineer Alion Science & Technology 1577 Spring Hill Rd, Suite 450 Vienna, Va 22182 (703) 439-7133 sunikewiczalionscience.com Attachment 2 - Page 5 of 6

ATTACHMENT 2 Executed in accord with 10 C.F.R. § 2.304(d),

Is! C. Wesley Rowley C. Wesley Rowley, PE Vice President The Wesley Corporation P.O. Box 747 Green Valley, AZ 85622 (520) 777-8941 cwrowley@aoi corn Executed in accord with 10 C.F.R. § 2.304(d),

Is/Mark A. Gowin Mark A. Gowin Corporate Codes Program Manager Tennessee Valley Authority 3159 Vista Dr.

Cleveland, TN 37312 (423) 503-5931 gpwin(isi-ist.com - Page 6 of 6

Attachment A STEVEN M UNIKEWICZ 43177 Glenelder Terrace Ashburn, VA 20147 (703) 439-7133 E: unikewiczsasme.orci OBJECTIVE: To apply my formal education and practical experience in an Engineering, Licensing or Engineering Management capacity to enhance the production and use of water and energy.

Particular interest in new nuclear plant development design, construction and operation.

SUMMARY

Work experience shows extensive experience in the field of Nuclear Power and Process Plant Regulation, Engineering, Design, Construction, Operation and project management. Performed multi-million dollar, multi-discipline projects on time and within budget. Performed complex regulatory and design issues in a complete, efficient manner. History of increasing leadership roles with employers, the technical community and the local community.

AWARDS:

USNRC Special Achievement Award, Palo Verde Inspection, April 3, 2006 USNRC Performance Awards, December 2003, 2004 and 2005 USNRC Special Act Award, Support of NRC Regional Offices, August 24, 2005 USNRC Special Act Award, GSI 191 Safety Evaluation Report, March 29, 2005 USNRC Region Ill Special Act Award, Kewaunee Special Inspection, August 4, 2004 USNRC Special Act Award, TMI Special Inspection, September 16, 2003 USNRC Special Act Award, September 9, 2003 American Society of Mechanical Engineers (ASME) 2002 Dedicated Service Award Northeast Utilities/ASME Distinguished Engineer of the Year 2000 WORK EXPERIENCE January 2008 Alion Science and Technology, Vienna, Va To Present Principal Engineer, Program Manager Responsible for component and plant system evaluations and analysis. Technical areas include NPSH, gas entrainment in fluid systems, pump minimum flow protection, Plant Operability assessments, in-service testing of pumps and valves and Regulatory Review and support on all aspects of plant design and operation. Responsible for providing expert consulting services in the areas of GSI-191 Ex and In-Downstream Effects and Chemical Effects to the nuclear power industry.

Specifically, wrote the MHI(Mitsubishi Heavy Industries) Downstream Effects (ex-vessel) report for the US-APWR new reactor submittal to the USNRC including their white paper on NPSH. Provided training and consultation to the Korean Electric Power Research Institute on the development and Implementation of their AOV and Fire Protection programs. Provided research and technical support to St. Lucie Nuclear station on their response to NRC GL 08-01 and on Instrument Air issues. Provide NRC and NEI interface for MHI and other US Nuclear Utilities Since June 2008 working with (badged) Calvert Cliffs Nuclear Station (CCNPP) and Nine Mile Point (NMP) containment walkdowns, Chemical Effects Issues and Downstream Effects evaluations.

Supported CCNPP during the Spring 2009, 2010 and 2011 refueling outages. Trained in various Constellation programs and have written design changes and engineering packages.

Have consulted with numerous other nuclear plants and utilities on air entrainment, system flow balancing and other plant design and operational issues.

Act as Alion interlace with NRC as needed.

Attachment A I of 5

Attachment A S M Unikewicz Page 2 July 2002 US Nuclear Regulatory Commission, Washington DC To January 2008 Senior Mechanical Engineer, Office of Nuclear Reactor Regulation, Mechanical Branch Member, USNRC Headquarters Incident Response Team, Reactor Safety Team counterpart to Protective Measure Team Lead reviewer of USNRC GSI-191, Containment Sumps downstream effects. This includes systems, components and reactor vessel reviews. Mechanical Engineer involved in the review and development of Codes, Standards and Regulations regarding the In-Service Testing of Components at Nuclear Power Generating Stations. Author of NUREG-1482, rev 1 Guidelines for Inservice Testing at Nuclear Power Plants. Principal reviewer and writer of the Davis Besse High Pressure Injection System and Pump modifications USNRC Safety Evaluation. NRC lead on Emergency Diesel Generator, air operated valve and pump issues. Branch lead on pump, valve and EDG design, operation, and testing issues. Provide technical leadership and guidance to NRC Headquarters Staff, and Regional and Site Inspectors and to the power industry. Member of two ASME Code for Operation and Maintenance of Nuclear Power Plants (CM Code) Code Committees; OM16 Diesel Drive Working Group and OM19 Air Operated Valves.

NRC/NRR contact and technical representative to OM ISTB, Committee on Pumps. NRC representative to three industry users groups; Air Operated Valve Users Group (AUG), Emergency Diesel Generator Users Group, and the Inservice Test Owners Group (ISTOG) and frequently interact with the Nuclear Energy Institute (NEI) on various technical and policy issues. Routinely write technical and safety evaluations for ASME Code relief requests and proposed license amendments to site Technical Specifications. Lead NRR Division of Engineering mechanical reviewer for issues pertaining to Emergency Diesel Generators and heat exchangers (non-steam generator). Writer of numerous USNRC generic communications. Technical reviewer for Westinghouse AP1000 DCD. Involved with review of the other new reactor designs submitted to USNRC.

NRRJDCI representative to the Operating Experience (OpE) program. Routinely involved in special inspections of critical systems at US commercial sites. Developed and presented formal classroom training, as an instructor to NRC Region Offices and Inspectors on Inservice Testing and on the design, operation and testing of air operated valves. Act as Division Branch Chief as needed.

Nov 2007 Fru-con Construction, Woodbridge, Va.

to May 2009 Part-time Start-up Engineer Responsible for preparing and implementing plan to start-up and commission the Broad Run Waste Reclamation Facility and Kent Narrows Waste Facility and supporting start up and testing at the Arlington, Va. and New Design Road, Fredrick Md. facilities.

February 2002 Modern Continental South, Griffith Water Treatment Plant, Lorton Va.

To October 2006 Chief Engineer/Start-up Engineer Lead Engineer for the construction of the 128 MGD, $120m water treatment facility. Supervised a 6 person multi-discipline engineering and design staff. Supported field construction, resolved design conflicts, specified and purchased mechanical and chemical systems equipment.

Mechanical Field / Start-up Engineer for the construction of the 128 MGD, $120m water treatment facility.

Author and principal developer of the start-up plan. Wrote test plans, test procedures and supervised the testing of mechanical and fluid systems. Supported field construction and resolved design conflicts.

Part-time Start-up Engineer July 2002 to commissioning in Oct 2006.

Attachment A -2 of 5

Attachment A S M Unikewicz Page 3 Author of the Start-up Plan and operations guidelines for the 11 Chemical Feed Systems, Flocculation I Sedimentation and Filtration System and the Finished Water Pumping System. Supervised final submittal preparation, O&M Manual preparation and final closeout and beneficial use documentation. Acted as pump installation, test and commissioning specialist.

April 2001 Energy Education lnc, Wichita Falls, TX To January 2002 Consulting Engineer Provided technical advice and guidance on the use and conservation of energy and utilities resources including proper specification, design and operation of boiler and HVAC systems for School Districts.

Trained clients in the interpersonal and technical aspects of the EEl program. Guided clients in the management of people and the operation of complex systems.

May 1992 Northeast Utilities, Waterford, CT To April 2001 Position: Senior Engineer Millstone Unit 2 Design Engineering Accident Management Team Mechanical Engineer, Station Emergency Response Organization.

Member, Nuclear Safety Assessment Board, Engineering Sub-Committee.

6/99 to 4/01 Technical and Project lead for mechanical and fluid system design and technical issues at Millstone Unit 2. Specifically, prepared and implemented design changes, including cost benefit analysis, budget management, schedule development, and coordination of all project aspects relating to projects and design changes. Lead Engineer for station evaluations and modifications.

Projects included Millstone 3, Turbine Long Shank Buckets, ASME VIII Vessel erosion/corrosion repairs in Millstone 2 Secondary Systems. Peer mentor for junior engineering and design personnel. Discipline Engineer for mechanical systems and component modifications. Wrote Safety Evaluations, Technical Specification Changes, FSAR Changes and detailed reviews and analysis of systems and components.

Chair of the Millstone Station Design Control Manual (DCM) Working Group. The DCM guides the engineering and design processes at the station.

4/98 to 6/99 Acting Supervisor MP2 MEPL Program Group (Material, Equipment & Parts Q list).

Responsible for the maintenance, technical evaluation, and implementation of the MEPL Program and Q-list at Millstone 2.

9/97 to 4/98 Acting Supervisor, Plant Engineering Group. The group was comprised of 25 Engineers and designers responsible for the field implementation of all plant modifications to Millstone Unit 2. The group was multi-discipline (mechanical, civil, l&C, and elect). We implemented in excess of 80 large scale modifications in 8 months.

5/97 to 9/97 Projects Lead for Task Managed Mechanical Design and Modifications for Millstone 2.

Responsible for the design of over 30 large scale design modifications with an engineering budget of $6.5 million. Projects managed were performed by Raytheon Engineers, Stone and Webster, Proto-Power Corporation, and Duke Engineering.

Attachment A 3 of 5

Attachment A S M Unikewicz Page 4 11/96 to 5/97 Acting Supervisor, System Design Engineering. Responsible for the design, evaluation, and modification of all mechanical plant systems including the responsibility of the 10CFR5O Appendix R Program.

5/92 to 11/96 Senior Engineer, Millstone Unit 2 Design Engineering. Technical lead for all RBCCW issues, GL 96-06 concerns and all other issues associated with Millstone 2. Senior Project and Mechanical Systems Engineer for projects at Millstone 2. Specifically prepared and implemented design changes, cost benefit analysis, budget and schedule.

Managed and coordinated all aspect relating to projects, their evaluation and their implementation. Large projects included the redesign of the containment sump Recirculation System; Unit Station and Instrument Air Upgrades; Spent Fuel Storage Capacity Increase; Demonstration of NFBC Compaction; a new Nitrogen Storage and Feed Facility for the Condensate Storage Tank and House Loads; CRAC System Modifications, redesign of the RCP Motor Lube Oil Collection System.

Lead and Mechanical Engineer for mechanical systems and component and station evaluations and modifications. Performed detailed reviews and analysis of systems and components. Performed Safety Evaluations and made changes to Technical Specifications, FSAR, etc.

Aug 1989 Northeast Utilities, Berlin CT To May 1992 Position: Engineer, Fossil Plant Programs, Fossil Hydro Engineering and Construction Life Extension! Non Destructive Evaluation coordinator for NEUs nine (9) reheat power plants.

Developed and implemented NDE Programs to evaluate and monitor all high energy, thick-walled, boiler and piping components.

Developed and implemented NDE programs to assess the condition of power plant heat exchangers.

Mechanical discipline engineer for mechanical systems and components analysis, evaluation and modification.

July 1985 Northeast Utilities, Berlin CT to Aug 1989 Position: Engineer, Balance of Plant Systems, Generation Mechanical Engineering Responsible for the engineering, design, analysis, procurement and installation of modifications to NEU Nuclear Power Stations (Connecticut Yankee and Millstone Units I, II, and Ill). Major Projects included the analysis of the CY Service Water System to ensure compliance with design and operational requirements; the redesign, procurement and installation of the Millstone II Condenser (900 MWe unit).

June 1982 Connecticut Yankee Atomic Power Co. Haddam Neck CT To July 1985 Position: Engineering Technician Assistant to Engineering Manager providing research and support of special projects. Developed the Stops/Seals installation and inspection program. Performed evaluations and design changes to plant systems and components. Performed performance monitoring of reactor fuel burn-up and reactor core performance. Certified lSl Level II Examiner. Performed vibration monitoring of critical plant equipment.

AttachmentA-4of 5

Attachment A S M Unikewicz Page 5 PUBLICATIONS (sample)

ASME Energy Talking Point (ETP) 1, Three Signs the End of Oil Exports is Coming, Feb 03, 2011 ASME Position Paper PSi 1-04, Expanding Nuclear Power in the United States, January 2011 Technical Reviewer, Nuclear Engineering Handbook, K.D. Kok CRC Press 2009 NUREG 1482, Guidelines for Inservice Testing at Nuclear Power Plants, Rev. 1, January 2005 Speaker/Moderator ASME Climate Change Workshop, Washington DC, July 15, 1999 Fluid Transients in a Voided System, co-author, ASME Fluids Division, Nov 1998 Implementation of Spent Fuel Storage options A Utility Project Engineers Perspective, ANS/ASCE High Level Radioactive Waste Management Conference LV, NV 5/22/94 Guest Lecturer, George Washington University, School of Graduate Studies, Nov 2009, Nov 2010 th 9

Speaker/Moderator NRC/ASME Pump and Valve Symposium, Washington DC, July 18, 2006 Speaker NRC/NEI Joint Workshop NRC Generic Letter 96-06 Thermal Overpressurization of Piping, Gaithersburg, MD, Dec 4, 1997 Speaker, Institute of Nuclear Materials Management, Spent Fuel Pool Storage Options, Washington DC, Jan 27, 1994 Panelist NRC Generic Letter 96-06 Thermal Overpressurization of Piping, ASME International Joint Power Conference, Nov 4, 1997 PROFESSIONAL SOCIETIES Member, American Society of Mechanical Engineers Chair, ASME Energy Committee Member, ASME 0M19 Code Committee, Air Operated Valves Member, ASME OM Code, New Reactors Sub-Group Member, ASME Plant Operations and Design Committee Former Member, ASME 0M16 Code Committee, Diesel Drive Working Group Former Member, Board on Pre-College Education, Council on Education Former Chair, Systems & Power Generation Facilities Design Committee, Power Division EDUCATION: University of Hartford, West Hartford CT Bachelor of Science Mechanical Engineering TRAINING USNRC Incident Investigation Team, qualified 2/14/03 ASME Leadership Development Intern, Council on Engineering, 1995 1996 ASME Short Course Interpretation and Evaluation of Weld Defects, March 1990 Formerly Certified ASME Level II Visual Examiner VT I, II, III, IV Formerly Certified Asbestos Supervisor, Certification # 421 P & P/S PUBLIC SERVICE Colchester CT, Board of Education Member, Secretary 19982001 Colchester CT, Water and Sewer Commission, Member 1992 1998 -

REFERENCES Available upon request AttachmentA-5of5

Attachment B ASME Professional Resume of C. Wesley Rowley, PE Education:

BS in General Engineering, University of Illinois, 1965 MS in Nuclear Engineering, University of Illinois, 1967 MA in Strategic Studies, Naval War College, 1986 Current Experience:

1 976-pres ASME International, Fellow (since 1998) 1 989-pres Member, Board on Nuclear Codes & Standards Jointly responsible for guiding the 1000 technical volunteers on six standards committees and three Boiler & Pressure Vessel subcommittees:

  • Committee on Nuclear Air & Gas
  • B&PV Subcommittee on Nuclear Design Treatment
  • B&PV Subcommittee on Inservice
  • Committee on Operations & Maintenance Inspection of NPPs
  • B&PV Subcommittee on Nuclear
  • Committee on Cranes for Nuclear Facilities Accrediation
  • Committee on Nuclear Quality Assurance
  • Committee on Qualification of Mechanical Equipment
  • Committee on Nuclear Risk Management 1 976-pres Member of Operations & Maintenance Main Committee (since 1984);

member of the Subgroup ISTE (since 2000). The O&M Committee develops the ASME OM Code and the ASME OM Standards / Guides.

2001 -pres Member of the Post Construction Main Committee (since 2002); also member of the PCC Subcommittee on Repair & Testing (since 2001);

member of the Non-metallic Repair Project Team (since 2001); chairman of the Non-metallic Repair Project Team (since 2002). The PCC develops PCC- 1, PCC-2, and PCC-3 standards.

2003-pres Chairman of BPV / Subcommittee II, Materials / Special Working Group, Non-Metallic Materials. The SWG-NMM is responsible for BPV Section II / Part E, Non-metallic Materials.

2006-pres Member of BPV / Subcommittee III, Nuclear Power / Special Working Group Polyethylene Pipe. The SWG-PP is responsible for Code Case N755.

Attachment B - I of 2

Attachment B 200 6-pres Member of Nominating Committee (chairman since 2007) 2006-pres Co-chairman of the Nuclear Risk Management Coordinating Committee.

Responsible for coordinating risk management issues between the technical societies (e.g., ASME, ANS, and IEEE).

Past Experience:

1989-pres Past chairman of BNC&S (2002-2005); past member of Committee on Board Operations (2000-2002); past member of Committee on Honors and Awards (1997-2002); past chairman of Board Risk Mgmt Task Group 1999-2002); past chairman of Board Strategic Planning for Facilities 1990-1993.

1 976-pres Previous member of the O&M Executive Committee (1987-2002);

previous chairman and member of O&M Special Committee on Standards Planning (1990-2002); previous chairman and member of the Electrical Subgroup (1982-1984); previous member of the O&M Subcommittee on Performance Testing (1976-89); previous member of the O&M Closed Cooling Water Systems Project Team (published OM 1982).

2003 -2006 Past chairman of Joint BPV III-XI Project Team on Plastic Pipe 2002-2005 Past member, Council on Codes & Standards; past member of CC&S-TF on Performance-Based Standards Attachment B -2 of 2

Attachment C Mark A. Gowin 3159 Vista Dr.

Cleveland, TN 37312 Phone: 423-503-5931 Email: mgowin@isi-ist.com

SUMMARY

OF WORK EXPERIENCE Thirty one years experience in design, construction, modification, and testing of BWR and PWR systems. The last twenty five years have been primarily focused on development and implementation of engineering programs to meet the requirements of ASME OM Code, ASME Section XI, and 10CFR5O, Appendix J.

ASME OMCode Inservice Testing Programs

  • Provide governance, oversight, and technical support of ASME OM Code Inservice Testing (1ST) Programs for all WA nuclear units to ensure the 1ST Programs meet Code, regulatory, and industry best practices.
  • Develop and implement ten-year updates of numerous Inservice Testing Programs (Pumps and Valves) to incorporate the latest edition and addenda of OM Code endorsed by NRC. This included preparation of program documents, relief requests, and implementation procedures.
  • Conduct multi-day training classes for Inservice Testing Program Owners including development of training materials
  • Perform pump and valve tests
  • Provide technical support for resolution of Inservice Testing Program and component related issues.
  • Audit/Assessment of Inservice Testing Programs
  • Regular attendance of OM Code Committee meetings Appendix J Containment Leak Rate Testing Programs
  • Provide governance, oversight, and technical support of 10CFR5O.55a, Appendix J, Containment Leak Rate Testing Programs for all WA nuclear units to ensure the 1ST Programs meet Code, regulatory, and industry best practices.
  • Develop and implement Appendix J Leak Rate Programs including program documents and implementation procedures.
  • Perform Type B and C containment local leak rate tests
  • Develop and implement ASME Section XI IWE Containment Inservice Inspection Programs including program documents, relief requests, and drawings
  • Develop and implement ASME Section Xi Pressure Test Programs including program document, relief requests, and drawings
  • Development of a Repair/Replacement Work Order/NIS-2 tracking database for Browns Ferry Unit 1 Recovery.
  • Assist in development and implementation of ASME Section XI Inservice Inspection Programs including drawings, component counts, and database update.

Check Valve andRelief Valve Testing Programs

  • Develop and implement plant wide check valve and relief valve programs with scope which include and extend beyond the ASME Inservice Testing Program requirements.

Engineering and Design

  • Project engineering for plant modifications including preparation of design changes, 10CFR5O.59 review, development of implementation procedure work order, resolution of field installation problems, and post-modification testing.

Attachment C I of 6

Attachment C SUM11ARY OF WORK EXPERIENCE (Continued)

Engineering and Consulting Business Owner (Prior to employment at TVA)

Founder and owner of Program Engineering and Consulting, Inc. (PEC, Inc.) which specializes in development, implementation, and auditJassessment of engineering programs such as, Inservice Inspection, Inservice Testing, and Appendix J. PEC, Inc. has been in business since February 2002 and provided services to Bruce Power (Canada), Eskom (South Affica), Florida Power and Light, Nuclear Management Company, Progress Energy, and Tennessee Valley Authority. PEC, Inc. has engaged in short term and long term fixed-price contracts and staff augmentation contracts with peak annual revenue of one million dollars. Responsibilities include: marketing and business development; preparation of bid proposals; execution and maintenance of contracts; customer relations; invoicing/billing; payroll; compliance with State and Federal regulations and taxes (unemployment, excise, income, FICA, Medicare, etc.); Project management (budget, schedule, manpower) of simultaneous projects involving up to 6 full-time and 3 part-time personnel.

INDUSTRY PARTICIPATION

  • Attend and participate in ASME OM Code meetings since 2002. Current member of Subgroup ISTB
  • Member of Inservice Testing Owners Group. Attend meetings and participate in working group activities.
  • Attend and participate in NRC/ASME Symposiums on Pump and Valve Testing
  • Attend ANSIJANS 56.8, Containment System Leakage Testing requirements, committee meetings and participate in working group activities
  • Member of Appendix J Owners Group. Host of 2010 annual meeting and participate in group activities EDUCATION / CERTWLCATION
  • Cleveland State Conununity College 1976 1977
  • University of Tennessee Knoxville 1977 1978 (completed engineering courses such as calculus, statics, dynamics, etc.; degree not completed)
  • Various utility sponsored training courses such as: BWR Systems; Root Cause Analysis; 10CFR5O.59 Evaluation; Independent Qualified Review; Design Change/Modifications
  • Experience level and training required to obtain TVA Qualification Cards for Inservice Testing Program, Appendix J Program, Pressure Test Program, and Containment Inservice Inspection Program.

DETAILED WORK EXPERIENCE 1/08 to Corporate Codes Program Manager Tennessee Valley Authority Present Corporate Office Chattanooga, TN

  • Provide governance and oversight of ASME OM Code Inservice Testing (1ST) Programs for all TVA nuclear units. Responsibility to ensure the 1ST Programs meet Code, regulatory, and industry best practices.
  • Provide governance and oversight of 10CFR5O, Appendix J, Containment Leak Rate Test Programs for all TVA nuclear units. Responsibility to ensure the Appendix J Programs meet Code, regulatory, and industry best practices.
  • Provide technical authority for to all TVA nuclear units in matters related to 1ST and Appendix J.

Attachment C -2 of 6

Attachment C 3/02 to Sr Program Engineer, Program Engineering and Consulting, Inc.

1/08 Browns Ferry Nuclear Plant Appendix J Program Engineer responsible for development and implementation of Unit 1 Appendix 3 Containment Leak Rate Testing Program. This includes preparation of the Appendix 3 program plan, review of associated design change notices and work orders, review of implementing test procedure revisions and review of completed test data.

  • IWE Program Engineer responsible for development and implementation of Unit 1 IWE program.

This includes preparation of the IWE program plan, relief requests, scan plan, review of associated design change notices and work orders, coordination/scheduling of inspection activities and resolution of program related issues.

Shearon Harris Nuclear Plant

  • Prepared ten year update of Inservice Testing (1ST) Program to 2001 Edition/2003 Addenda of ASME OM Code.
  • Determined 1ST Program scope and test requirements.
  • Prepared implementing test procedure mark-ups.

Koeberg Nuclear Power Station

  • Prepared ten year update of Inservice Testing (1ST) Program to 2001 EditionJ2003 Addenda of ASME OM Code.
  • Determined 1ST Program scope and test requirements.

Bruce Nuclear Development Plant

  • Developed Check Valve Condition Monitoring Program for Units I 4 similar to Units 5 8 below.

7/01 to 1ST Engineer, BCP Technical Services 3/02 H. B. Robinson Nuclear Plant

  • Prepared ten year update of Inservice Testing (1ST) Program to 1995 Edition/i 996 Addenda of ASME OM Code.
  • Determined 1ST Program scope and test requirements.
  • Wrote/revised all associated 1ST Program administrative procedures including safety/relief valve testing program and check valve condition monitoring program.
  • Reviewed all surveillance test procedure revisions to ensure compliance with OM Code test requirements and ensure all 1ST Program required tests captured.

2/00 to 1ST Technician, Onsite Engineering Services 7/01 Bruce Nuclear Development Plant

  • Develop a Check Valve Condition Monitoring Program for Units 5 8. -
  • Participate in Expert Panel to recommend preventive maintenance activities for check valves.
  • Develop Microsoft Access database for the Check Valve Program and Basis Document.

Attachment C -3 of 6

Attachment C 7/99 to 1ST Engineer, BCP Technical Services 2/00 D.C Cook Nuclear Plant

  • Performed duties as Safety and Relief Valve Testing Program Manager such as:
  • Developed a Safety and Relief Valve Testing Program.
  • Scheduled and coordinate onsite testing of safety and relief valves.

St. Lucie Nuclear Plant

  • Resolved NRC request for additional information for the 1ST Program update.
  • Prepared 1ST Program revision (including new relief request and refueling outage justifications) to incorporate plant modifications and NRC request for additional information.

8/98 to IST/ISI Engineer, Enertech Servus 7/99 Various Nuclear Plants

  • Developed comprehensive pump tests in accordance with ASME Section XI, 1995 Edition.
  • Performed independent ISI /IST assessment.

10/97 to 1ST Engineer, Enertech Servus 8/98 Shearon Harris Nuclear Plant

  • Performed duties as 1ST Coordinator on temporary basis until permanent position filled.
  • Reviewed all 1ST related test performance packages for acceptability and test data trending.
  • Reviewed design change packages and procedure revisions for 1ST compliance.
  • Resolved day-to-day 1ST related technical issues.
  • Reviewed work orders and assigned post-maintenance testing requirements.
  • Prepared ten year update of the Inservice Testing Program.
  • Determined 1ST Program scope and test requirements.
  • Prepared 1ST Program Plan, administrative procedures and 10CFR5O.59 safety evaluations.
  • Developed 1ST Basis Document to justify component inclusion/exclusion in 1ST Program.
  • Developed Microsoft Access database for the 1ST Program and 1ST Basis Document.

6/97 to 1ST /151 Engineer, Enertech Servus 10/97 Unit 3 Millstone Nuclear Plant

  • Developed ASME Section XI Pressure Test Program for the second ten-year interval.
  • Developed individual pressure test boundaries that optimize the use of normal plant operating conditions and surveillance tests.
  • Developed Microsoft Access database to correlate individual test boundaries with specific code requirements and relief requests (e.g., test pressure, hold time, VT-2 boundary).
  • Wrote generic surveillance procedure to perform all periodic pressure tests.

Attachment C -4 of 6

Attachment C 1/96 to 1ST Program Coordinator, System Engineering Department 6/97 Vermont Yankee Nuclear Plant

  • Performed activities associated with the ASME Section XI Inservice Testing Program including development and maintenance of program document, oversight of program implementation and maintaining awareness of industry/regulatory issues.
  • Provided day-to-day assistance and technical input to Operations, Design Engineering and Maintenance personnel related to 1ST activities.
  • Reviewed surveillance procedures, design changes and LCO maintenance plans.
  • Prepared Event Reports including investigation, root cause analysis and corrective action.

Sr. Engineer, System Engineering Department

  • Performed major revision to 1ST Program to incorporate changes identified during development of the basis document. This revision included program scope changes, test type and frequency changes, new/revised cold shutdown and refueling outage justifications and new relief requests.
  • Designed Microsoft Access database for the 1ST Program and Basis Document.

4/95 to Sr. Engineer, Contracted to Tennessee Valley Authority, Technical Support Section, NSSS Systems 12/95 Sequoyah Nuclear Plant

  • Wrote/revised surveillance testing procedures for ten year update of ASME Section XI Inservice Testing Program (1989 Edition, OMa-1988, Parts 1, 6 and 10).

8/94 to Sr. Engineer, Contracted to Mechanical Engineering and Construction Department 4/95 Vermont Yankee Nuclear Plant

  • Project Engineer for containment modification project. These duties included:
  • Prepared design change package, installation and testing procedure, 10CFR5O.59 evaluations, labor/material cost estimates, project budget and project schedule.
  • Coordinated modification implementation with other plant activities.
  • Ensured modification completion within budget and schedule requirements.
  • Trained as Root Cause Evaluator.

1/93 to Sr. Mechanical Technologist, Contracted to Tennessee Valley Authority 4/94 Watts Bar Nuclear Plant

  • Wrote/revised surveillance testing procedures for ten year update of ASME Section XI Inservice Testing Program (1989 Edition, OMa-1988, Parts 1, 6 and 10).

9/92 to Mechanical Engineer, Contracted to Carolina Power and Light, Nuclear Engineering 1/93 Brunswick Nuclear Plant

  • Prepared installation and testing portions of design change packages.
  • Prepared procedures for installation and acceptance testing of modifications.
  • Certified as Design Verifier and Qualified Safety Reviewer (10CFR5O.59).

2/92 to Mechanical Engineer, Contracted to Gulf States Utilities, NSSS Design Engineering 9/92 River Bend Station

  • Prepared design change packages and 1 OCFR 50.59 safety evaluations.
  • Performed field engineering for implementation of modifications.
  • Closure of design change packages and various other outstanding items.

Attachment C -5 of 6

Attachment C 8/86 to Mechanical Engineer, Contracted to Tennessee Valley Authority, Systems Engineering 2/92 Sequoyah Nuclear Plant Prepared procedures to satisfy Technical Specification surveillance requirements such as:

5/84 to System Engineer, Bechtel Corp, Georgia Power Company 8/86 Plant Vogtle

  • Conducted NSSS and BOP systems walk downs, initiated work authorizations and expedited design and field activities to ensure systems completion and start-up per project schedules.
  • Performed deviation report (non conformance item) evaluation and closure.

12/81 to Field Engineer, Bechtel Corp., Mechanical Engineering Group 5/84 Enrico Fermi II

  • Developed and implemented ASME Section XI repair/replacement and testing packages.
  • Performed troubleshooting and maintenance engineering for pumps and valves.
  • Prepared design change packages for modifications and upgrades.
  • Conducted functional tests and hydrostatic/pneumatic pressure tests.

2/81 to Field Engineer, Mercury Co., Louisiana Power and Light 12/81 Waterford III

1/80 to Designer, Contracted to Tennessee Valley Authority, Division of Engineering and Design 2/81 Bellefonte Nuclear Plant

  • Generated instrumentation loop schematics, flow diagrams, installation details, control panel layouts and other I & C related drawings.

Attachment C -6 of 6

ENCLOSURE 3 Browns Ferry Nuclear Plant, Unit I Docket No. 50-259 Reply to a Notice of Violation, EA-1I-018

ENCLOSURE 3 Browns Ferry Nuclear Plant, Unit I Docket No. 50-259 Reply to a Notice of Violation, EA-1 1-018 Restatement of Violation During an NRC inspection completed on December 31, 2010, a violation of NRC requirements was identified. In accordance with the NRC Enforcement Policy, the violation is listed below:

Browns Ferry Nuclear Plant Unit I Technical Specification (TS) LCO 3.5.1, Emergency Core Cooling System (ECCS) Operating, requires, in part, that each ECCS injection/spray subsystem shall be operable in Modes 1, 2, and 3.

Action statement Condition A states that with one low pressure ECCS injection/spray subsystem inoperable, restore the low pressure ECCS injection/spray subsystem to operable status within seven days. Action statement Condition B states that with the required action and associated completion time of Condition A not met, be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in Mode 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Contrary to the above, from March 13, 2009 to October 23, 2010, a Unit 1 low pressure ECCS injection/spray subsystem was inoperable while in Modes 1, 2, and 3, and the licensee failed to restore the subsystem to operable status within seven days, or complete Action statement Condition A and B within the required time. Specifically, the Unit I Residual Heat Removal Loop II subsystem was inoperable, because the licensee failed to maintain the Unit outboard Low Pressure Coolant Injection (LPCI) valve 1-FCV-74-66 in an operable condition, which rendered a low pressure ECCS injection/spray subsystem (the RHR loop II subsystem) inoperable while Unit I was operating in Mode 1.

This violation is associated with a Red significance determination process finding for Unit I in the Mitigating Systems cornerstone.

Admission or Denial TVA admits the Technical Specification operability violation.

Reasons for the Violation WA determined that the root cause of the valve failure was an original manufacturing deficiency. Separation of the valve disc from the disc skirt/stem assembly was due to E3-1 of 2

undersized skirt threads. Backpressure on the disc exceeded the strength of the threaded connection when the valve was cycled open, causing axial thread pull-out.

Corrective Steps Taken and Results Achieved

  • WA repaired valve 1-FCV-74-66 by reworking the skirt threads to their original design configuration to preclude disc separation. The RHR loop II subsystem was restored to operability.
  • WA verified that the valve discs were intact in all like valves, but was unable to unscrew the discs from the skirt/stems to verify proper thread size. WA added welded gussets to the disc to skirt/stem interface on all like valves to preclude disc separation.
  • TVA implemented controls limiting back-pressure on the valves.

Date of Full Compliance Valve 1-FCV-74-66 was repaired and restored to operable status during the Unit 1 refueling outage that ended November 23, 2010. Other like valves were examined and modified during shutdowns of all three units that ended as follows: Unit 1 on May 26, 2011; Unit 2 on April 2, 2011; and Unit 3 on May 31, 2011.

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