ML101240946

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IR 05000361-10-002, 05000362-10-002; 01/01/2010 - 03/24/2010; San Onofre Nuclear Generating Station, Units 2 & 3; Integ Resid & Reg Report; Fire Prot, Maint Effect, Maint Risk & Em Work, Op Eval, Postmaint Test, Ref Outages, Id.& Res.Of Pro
ML101240946
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 05/04/2010
From: Ryan Lantz
NRC/RGN-IV/DRP/RPB-D
To: Ridenoure R
Southern California Edison Co
References
FOIA/PA-2011-0221, FOIA/PA-2011-0157 IR-10-002
Download: ML101240946 (77)


See also: IR 05000361/2010002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

R E GI ON I V

612 EAST LAMAR BLVD, SUITE 400

ARLINGTON, TEXAS 76011-4125

May 4, 2010

Mr. Ross T. Ridenoure

Senior Vice President and

Chief Nuclear Officer

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

SUBJECT:

SAN ONOFRE NUCLEAR GENERATING STATION - NRC INTEGRATED

INSPECTION REPORT 05000361/2010002 and 05000362/2010002

Dear Mr. Ridenoure:

On March 24, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at your San Onofre Nuclear Generating Station, Units 2 and 3 facility. The enclosed integrated

inspection report documents the inspection findings, which were discussed on March 23, 2010,

with you, and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents 12 NRC identified findings and two self-revealing findings of very low

safety significance (Green). All of these findings were determined to involve violations of NRC

requirements. Additionally, three licensee-identified violations, which were determined to be of

very low safety significance, are listed in this report. However, because of the very low safety

significance and because they are entered into your corrective action program, the NRC is

treating these findings as noncited violations, consistent with Section VI.A.1 of the NRC

Enforcement Policy. If you contest the violations or the significance of the noncited violations,

you should provide a response within 30 days of the date of this inspection report, with the basis

for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, D.C. 20555-0001, with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas,

76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,

Washington, D.C. 20555-0001; and the NRC Resident Inspector at the San Onofre Nuclear

Generating Station facility. In addition, if you disagree with the characterization of any finding in

this report, you should provide a response within 30 days of the date of this inspection report,

with the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC

Southern California Edison Company

- 2 -

Resident Inspector at San Onofre Nuclear Generating Station. The information you provide will

be considered in accordance with Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, and its

enclosure, will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records component of NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/ Donald B. Allen for

Ryan E. Lantz, Chief

Project Branch D

Division of Reactor Projects

Docket Nos.

50-361; 50-362

License Nos. NPF-10, NPF-15

Enclosure:

NRC Inspection Report 05000361/2010002 and 05000362/2010002

w/Attachment: Supplemental Information

cc w/Enclosure:

Chairman, Board of Supervisors

County of San Diego

1600 Pacific Highway, Room 335

San Diego, CA 92101

Gary L. Nolff

Assistant Director-Resources

City of Riverside

3900 Main Street

Riverside, CA 92522

Mark L. Parsons

Deputy City Attorney

City of Riverside

3900 Main Street

Riverside, CA 92522

Southern California Edison Company

- 3 -

Gary H. Yamamoto, P.E., Chief

Division of Drinking Water and

Environmental Management

1616 Capitol Avenue, MS 7400

P.O. Box 997377

Sacramento, CA 95899-7377

Michael L. DeMarco

San Onofre Liaison

San Diego Gas & Electric Company

8315 Century Park Ct. CP21C

San Diego, CA 92123-1548

Director, Radiological Health Branch

State Department of Health Services

P.O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414

The Mayor of the City of San Clemente

100 Avenida Presidio

San Clemente, CA 92672

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814

Douglas K. Porter, Esquire

Southern California Edison Company

2244 Walnut Grove Avenue

Rosemead, CA 91770

Albert R. Hochevar

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Steve Hsu

Department of Health Services

Radiologic Health Branch

MS 7610, P.O. Box 997414

Sacramento, CA 95899-7414

Southern California Edison Company

- 4 -

R. St. Onge

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Chief, Technological Hazards Branch

FEMA Region IX

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Southern California Edison Company

- 5 -

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Chuck.Casto@nrc.gov)

DRP Director (Dwight.Chamberlain@nrc.gov)

DRP Deputy Director (Anton.Vegel@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Deputy Director (Troy.Pruett@nrc.gov)

Senior Resident Inspector (Greg.Warnick@nrc.gov)

Resident Inspector (John.Reynoso@nrc.gov)

Branch Chief, DRP/D (Ryan.Lantz@nrc.gov)

Senior Project Engineer, DRP/D (Don.Allen@nrc.gov)

SONGS Administrative Assistant (Heather.Hutchinson@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Project Manager (Randy.Hall@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

ROP Reports

DRS/TSB STA (Dale.Powers@nrc.gov)

OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)

Regional State Liaison Officer (Bill.Maier@nrc.gov)

NSIR/DPR/EP (Eric.Schrader@nrc.gov)

File located: R:\\Reactors\\Songs\\2010\\SO2010-002-RP-GGW.doc

SUNSI Rev Compl.

Yes No

ADAMS

Yes No

Reviewer Initials

DBA

Publicly Avail

Yes No

Sensitive

Yes ; No

Sens. Type Initials

DBA

RI:DRP

RI:DRP

SRI:DRP

C:DRS/OB

C:DRS/EB1

JReynoso

JJosey

GWarnick

MHaire

TFarnholtz

/DAllen for E/ /DAllen for E/

/RA/

/DAllen for/

/RML for/

5/3 /10

5/3 /10

5/3/10

4/29/10

4/29/10

C:DRS/EB2

C:DRS/PSB1

C:DRS/PSB2

C:DRP

NO'Keefe

MShannon

GWerner

RLantz

/RA/

/JLarsen for/

/RA/

/DAllen for/

4/28/10

4/29/10

4/29/10

4/30/10

OFFICIAL RECORD COPY

T=Telephone

E=E-mail

F=Fax

- 1 -

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

50-361, 50-362

License:

NPF-10, NPF-15

Report:

05000361/2010002 and 05000362/2010002

Licensee:

Southern California Edison Co. (SCE)

Facility:

San Onofre Nuclear Generating Station, Units 2 and 3

Location:

5000 S. Pacific Coast Hwy

San Clemente, California

Dates:

January 1, 2010 through March 24, 2010

Inspectors:

D. Allen, Senior Project Engineer

P. Elkmann, Senior Emergency Preparedness Inspector

J. Josey, Resident Inspector

J. Reynoso, Resident Inspector

B. Rice, Reactor Engineer

W. Schaup, Project Engineer

G. Warnick, Senior Resident Inspector

Approved By:

Ryan E. Lantz

Chief, Project Branch D

Division of Reactor Projects

- 2 -

Enclosure

SUMMARY OF FINDINGS

IR 05000361/2010002, 05000362/2010002; 01/01/2010 - 03/24/2010; San Onofre Nuclear

Generating Station, Units 2 & 3; Integ Resid & Reg Report; Fire Prot, Maint Effect, Maint Risk &

Em Work, Op Eval, Postmaint Test, Ref Outages, Id.& Res.of Prob, Event F/U

The report covered a 3-month period of inspection by resident inspectors and an announced

baseline inspection by a regional based inspector. Fourteen Green noncited violations of

significance were identified. The significance of most findings is indicated by their color (Green,

White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination

Process. Findings for which the significance determination process does not apply may be

Green or be assigned a severity level after NRC management review. The NRC's program for

overseeing the safe operation of commercial nuclear power reactors is described in NUREG-

1649, Reactor Oversight Process, Revision 4, dated December 2006.

A.

NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The inspectors identified three examples of a noncited violation of

Technical Specification 5.5.1.1.d, for the failure of contractor and station

personnel to properly implement the requirements of a station fire protection

procedure for control of hot work activities. Specifically, between January 4 and

March 17, 2010, three examples were identified where contractor and station

personnel failed to properly implement the requirements of procedure

SO123-XV-1.41, Control of Ignition Sources, Revision 14, Steps 6.2.1

and 6.4.1.3. Specifically, contractor and station personnel failed to ensure that

combustible materials were covered or removed from the ignition source.

Following the inspectors identification of each example, the licensee immediately

stopped the hot work activities and restored compliance with the requirements of

procedure SO123-XV-1.41. This issue was entered into the licensees corrective

action program as Nuclear Notifications NNs 200729747, 200746059 and

200835830.

The finding is greater than minor because if left uncorrected, the practice of

conducting hot work in a manner that allows uncontrolled combustibles to be

within the procedurally specified exclusion area would have the potential to lead

to a more significant safety concern, in that, it could result in a fire in or near risk

important equipment. The finding is associated with the Initiating Events

Cornerstone. The inspectors determined that Manual Chapter 0609, Appendix F,

Fire Protection Significance Determination Process, does not address the

potential risk significance of shutdown fire protection findings, and Appendix G,

Shutdown Operations Significance Determination Process, does not address

fire protection findings, and therefore could not be applied to shutdown plant

conditions. Because of this, the inspectors used Manual Chapter 0609,

Appendix M, Significance Determination Process Using Qualitative Criteria.

The NRC management review was performed by using the Manual Chapter

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Enclosure

0609, Appendix F, Phase 1 Worksheet, to establish a bounding analysis. Using

the bounding analysis, the finding is determined to have very low safety

significance because the finding represented a low degradation rating, in that, it

did not have any significant effect on the likelihood that a fire might occur, or that

a fire which does occur might not be promptly suppressed. This finding had a

crosscutting aspect in the area of human performance associated with work

practices, in that, the licensee failed to define and effectively communicate

expectations regarding procedural compliance and personnel following

procedures H.4(b) (Section 1R05).

Green. The inspectors identified a noncited violation of 10 CFR 50.65(a)(4),

Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power

Plants, involving multiple instances where operations and work control

personnel failed to adequately assess and implement appropriate risk

management activities. Specifically, between February 18, and February 23,

2010, operations and work control personnel failed to adequately assess and

manage the increase in risk associated with maintenance activities in the

electrical switchyard. Following the inspectors identification of the findings, the

licensee adequately assessed and managed the increase in risk for the

maintenance activities. This issue was entered into the licensees corrective

action program as Nuclear Notifications NNs 200801929 and 200805635.

The finding is greater than minor since it was similar to both more than minor

Examples 7.e and 7.f in NRC Inspection Manual Chapter 0612, Appendix E,

Examples of Minor Issues, because when the activities were correctly assessed

plant procedures required risk management actions to be taken. The finding is

associated with the Initiating Events Cornerstone. The inspectors determined

that the licensee does not maintain a shutdown probabilistic risk analysis model,

and as such, an incremental core damage probability cannot be estimated for the

plant conditions that existed at the time of the performance deficiency. For this

reason, the inspectors determined that Manual Chapter 0609, Appendix K,

Maintenance Risk Assessment and Risk Management Significance

Determination Process, Flowchart 2, could not be used to determine the risk

significance the finding. Using the qualitative review process of Manual Chapter

0609, Appendix M, Significance Determination Process Using Qualitative

Criteria, the finding is determined to have very low safety significance because

the finding did not result in any additional loss of defense in depth systems. This

finding has a crosscutting aspect in the area of human performance associated

with the work practices because the licensee failed to define and effectively

communicate expectations regarding procedural compliance and that personnel

follow procedures H.4(b) (Section 1R13).

Cornerstone: Mitigating Systems

Green. The inspectors identified a noncited violation of 10 CFR 50.65(b)(2)(ii) for

the licensees failure to appropriately scope the steam driven auxiliary feedwater

pump trench eductor in the maintenance rule monitoring program. Specifically,

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Enclosure

from the inception of the facilities monitoring program through March 2010, the

licensee failed to properly scope the steam drive auxiliary feedwater pump trench

educator. The eductors prevent water from accumulating in the trench because

water in contact with the pumps steam supply piping would cause condensation

of the steam in the pipe. Condensation would cause the turbine to over speed,

which would render the pump incapable of performing its specified safety

function. This issue was entered into the licensees corrective action program as

Nuclear Notification NN 200765185.

The finding is greater than minor because it is associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and directly affected

the cornerstone objective of ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using the Manual Chapter 0609, Significance Determination Process, Phase 1

Worksheets, the finding is determined to have very low safety significance

because the finding: (1) is not a design or qualification issue confirmed not to

result in a loss of operability or functionality; (2) did not represent an actual loss

of safety function of the system or train; (3) did not result in the loss of one or

more trains of nontechnical specification equipment; and (4) did not screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating

event. The inspectors determined that since the scoping of the systems had

occurred more than 2 years in the past, and the opportunity to reevaluate system

scoping had not occurred recently, that the finding did not represent current plant

performance and therefore did not have a crosscutting aspect associated with it

(Section 1R12).

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the

licensees failure to properly implement procedure requirements to ensure that

applicable risk significant operating experience was entered into the corrective

action program for timely evaluation. Specifically, on December 17, 2009, the

operating experience review committee failed to properly implement the

requirements of procedure SO23-XV-40, Sharing Industry Information,

Revision 1. An industry operating experience report review determined the

operating experience was not applicable and was distributed as information only;

not requiring any action. The same industry operating experience was later

determined to be applicable by the probabilistic risk assessment group, and

interim compensatory measures were initiated on February 10, 2010, to address

the issues. This issue was entered into the licensees corrective action program

as Nuclear Notifications NN 200805879.

The finding is greater than minor because it is associated with the procedure

quality attribute of the Mitigating Systems Cornerstone and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Using the Manual Chapter 0609, Significance Determination Process, Phase 1

Worksheets, the finding is determined to have very low safety significance

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Enclosure

because the finding: (1) is not a design or qualification issue confirmed not to

result in a loss of operability or functionality; (2) did not represent an actual loss

of safety function of the system or train; (3) did not result in the loss of one or

more trains of nontechnical specification equipment; and (4) did not screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating

event. This finding has a crosscutting aspect in the area of human performance

associated with decision-making because the operating experience review

committee did not use a systematic process when making a safety significant

decision, to ensure safety is maintained and obtaining interdisciplinary inputs and

reviews on risk-significant decisions H.1(a) (Section 1R13).

Green. The inspectors identified two examples of a noncited violation of

10 CFR Part 50, Appendix B, Criterion V, Instruction, Procedures, and Drawing,

for the failure of operations personnel to follow procedures to approve and

document operability determinations using adequate or technically correct

information. Specifically, on January 15, and January 22, 2010, operations

personnel failed to follow procedure SO123-XV-52, Functionality Assessments

and Operability Determinations, Revision 14, in that, the documented bases for

operability for degraded conditions did not adequately support the basis for an

operability position taken by the licensee. Following the inspectors identification

of the issues, operations personnel performed new operability determinations to

provide adequate bases for operability. This issue was entered into the

licensees corrective action program as Nuclear Notifications NNs 200765208

and 200753880.

The finding is greater than minor because, if left uncorrected, inadequate

operability determinations would have the potential to lead to a more significant

safety concern. Specifically, the failure to recognize that risk significant

equipment is in a potentially inoperable condition and as such, may not be able

to perform its specified safety function would not be recognized and accounted

for by operators. The finding is associated with the Mitigating Systems

Cornerstone. Using the Manual Chapter 0609, Significance Determination

Process, Phase 1 Worksheets, the finding is determined to have very low safety

significance because the finding: (1) is not a design or qualification issue

confirmed not to result in a loss of operability or functionality; (2) did not

represent an actual loss of safety function of the system or train; (3) did not result

in the loss of one or more trains of nontechnical specification equipment; and (4)

did not screen as potentially risk significant due to a seismic, flooding, or severe

weather initiating event. This finding has a crosscutting aspect in the area of

problem identification and resolution associated with the corrective action

program because the licensee failed to thoroughly evaluate problems such that

the resolutions addressed causes and extent of conditions as necessary P.1(c)

(Section 1R15).

Green. A self-revealing Green noncited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, was identified for failure of

maintenance planning personnel to develop and specify an adequate

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Enclosure

postmaintenance test in the work instructions used to perform maintenance on

the backup nitrogen regulator for the component cooling water surge tank.

Specifically, on October, 25, 2009, Maintenance Order MO 800335873 did not

specify postmaintenance testing instructions that would verify that nitrogen

supply valve PCV 5403 would perform satisfactorily in service, following

calibration, and properly control surge tank pressure during changes in surge

tank levels. This issue was entered into the licensees corrective action program

as Nuclear Notifications NNs 200766430 and 200887764.

The finding is greater than minor because it is associated with the procedure

quality attribute of the Mitigating Systems Cornerstone and affects the associated

cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Furthermore, the finding is similar to more than minor example 3.i in NRC

Inspection Manual Chapter 0612, Appendix E, Examples of Minor Issues, in

that, an extensive engineering evaluation was required to verify that the

component cooling water system remained capable of performing its safety

function during a design basis earthquake. Using the Manual Chapter 0609,

Appendix G, Shutdown Operations Significance Determination Process,

Phase 1 guidance, the finding is determined to have very low safety significance

because the finding did not result in an increase in the likelihood of a loss of

reactor coolant system inventory, degrade the ability to add reactor coolant

system inventory, or degrade the ability to recover decay heat removal. This

finding has a crosscutting aspect in the area of human performance associated

with work practices because maintenance planning personnel failed to follow

procedures to develop adequate work instructions to perform maintenance on

safety-related equipment H.4(b) (Section 1R19).

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure

of licensee personnel to follow procedure SO123-XV-50.CAP-1, Writing Nuclear

Notifications for Problem Identification and Resolution, Revision 2, and enter

conditions adverse to quality into the corrective action program. Specifically,

between January 4 and March 14, 2010, the inspectors identified multiple

instances, including two programs, where licensee personnel were aware of the

existence of conditions adverse to quality, but failed to appropriately enter them

into the corrective action program without being prompted by the inspectors.

This issue was entered into the licensees corrective action program as Nuclear

Notifications NNs 200778816 and 200780926.

The finding is greater than minor because it was similar to more than minor

example 3.j in NRC Manual Chapter 0612, Appendix E, Examples of Minor

Issues, in that programmatic deficiencies were identified associated with this

issue that would have the potential to lead to more significant safety concerns if

left uncorrected. Specifically, contractor and licensee personnels failure to enter

conditions adverse to quality into the station corrective action program could

result in the licensees failure to recognize that risk significant equipment is in a

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Enclosure

degraded or nonconforming condition, and as such, may not be able to perform

its specified safety function. The finding is associated with the Mitigating

Systems Cornerstone. Using the Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheets, the finding is determined to have

very low safety significance because the finding: (1) is not a design or

qualification issue confirmed not to result in a loss of operability or functionality;

(2) did not represent an actual loss of safety function of the system or train; (3)

did not result in the loss of one or more trains of non-technical specification

equipment; and (4) did not screen as potentially risk significant due to a seismic,

flooding, or severe weather initiating event. This finding has a crosscutting

aspect in the area of problem identification and resolution associated with the

corrective action program because the licensee failed to implement a corrective

action program with a low threshold for identifying issues. This also includes

identifying such issues completely, accurately, and in a timely manner

commensurate with their safety significance P.1(a) (Section 4OA2).

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure

of maintenance personnel to follow Work Order 800195196 and provide

appropriate oversight to transmission and distribution personnel while performing

work in the electrical switchyard. Specifically, on February 26, 2010,

maintenance personnel failed to follow Work Order 800195196, and procedure

SO123-XV-15.3, Temporary System Alteration and Restoration, Revision 17, to

provide appropriate oversight of transmission and distribution personnel who

were performing work in the plant switchyard, which resulted in the over torquing

of nine bolts on the reserve auxiliary transformer circuit breakers. The licensee

corrected the over torqued bolt condition. This issue was entered into the

licensees corrective action program as Nuclear Notifications NNs 200803364

and 200811993.

The finding is greater than minor because circumventing procedural

requirements, if left uncorrected, would have the potential to lead to a more

significant safety concern, in that, more risk significant equipment could be

rendered inoperable without the knowledge and approval of appropriate

management or control room personnel. The finding is associated with the

Mitigating Systems Cornerstone. Using the Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheets, the finding is determined to have

a very low safety significance because the finding: (1) is not a design or

qualification issue confirmed not to result in a loss of operability or functionality;

(2) did not represent an actual loss of safety function of the system or train;

(3) did not result in the loss of one or more trains of nontechnical specification

equipment; and (4) did not screen as potentially risk significant due to a seismic,

flooding, or severe weather initiating event. This finding has a crosscutting

aspect in the area of human performance associated with work practices

because maintenance personnel failed to ensure supervisory and management

oversight of work activities, including contractors, such that nuclear safety was

supported H.4(c) (Section 4OA2).

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Enclosure

Green. A self-revealing noncited violation of Technical Specification 5.5.1.1 was

identified for the failure of operations personnel to follow procedures for operating

the component cooling water system. Specifically, on January 27, 2010,

operations personnel failed to follow the requirements of procedure SO123-2-17,

Component Cooling Water System Operation, Revision 31, while performing a

planned drain down of the component cooling water surge tanks. Operations

personnel failed to maintain the surge tank pressure, in accordance with

procedure SO23-2-17, such that, component cooling water surge tank pressure

was permitted to go low out of the expected operating range. As a result of this

low surge tank pressure, operators declared the component cooling water and

shutdown cooling train A systems inoperable. This issue was entered into the

licensees corrective action program as Nuclear Notification NN 200771367.

The finding is greater than minor because the continued failure to follow

procedures when operating safety-related plant equipment, if left uncorrected,

would have the potential to lead to a more significant safety concern. The finding

is associated with the Mitigating Systems Cornerstone. Using the Manual

Chapter 0609, Appendix G, Shutdown Operations Significance Determination

Process, Phase 1 guidance, the finding is determined to have very low safety

significance because the finding did not result in an increase in the likelihood of a

loss of reactor coolant system inventory, degrade the ability to add reactor

coolant system inventory, or degrade the ability to recover decay heat removal.

This finding has a crosscutting aspect in the area of human performance

associated with work practices because operations personnel failed to use

proper human error prevention techniques and proceeded in the face of

unexpected circumstances when operating the component cooling water system

H.4(a) (Section 4OA3).

Cornerstone: Barrier Integrity

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated

with the licensees failure to adequately implement procedures SO123-I-3.7,

Refueling Foreign Material Exclusion Control, Revision 6, and SO123-I-1.18,

Foreign Material Exclusion, Revision 14. Specifically, between January 12,

2010, and February 23, 2010, multiple occasions were identified during Refueling

Outage U2C16, where licensee personnel failed to implement appropriate foreign

material exclusion controls in areas designated as Zone 1 foreign material

exclusion areas. This issue was entered into the licensees corrective action

program as Nuclear Notifications NNs 200760484, 200742082, 200743834 and

200805961.

The finding is greater than minor because it is associated with the human

performance attribute of the Barrier Integrity Cornerstone and affects the

cornerstone objective of providing reasonable assurance that physical barriers

protect the public from radionuclide releases caused by accidents or events.

Furthermore, the programmatic deficiencies that were identified associated with

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Enclosure

this issue would have the potential to lead to a more significant safety concern, if

left uncorrected. Specifically, licensee personnels continued failure to implement

appropriate foreign material exclusion controls would result in degradation and

adverse impacts on materials and systems associated with the spent fuel pool or

the reactor cavity. Using the Manual Chapter 0609, Appendix G, Shutdown

Operations Significance Determination Process, Phase 1 guidance, the finding

is determined to have very low safety significance because the finding did not

result in an increase in the likelihood of a loss of reactor coolant system

inventory, degrade the ability to add reactor coolant system inventory, or degrade

the ability to recover decay heat removal. This finding had a crosscutting aspect

in the area of human performance associated with work practices because the

licensee failed to define and effectively communicate expectations regarding

procedural compliance which resulted in a failure to follow procedure by licensee

personnel H.4(b) (Section 1R20).

Cornerstone: Occupational Radiation Safety

Green. The inspectors identified a noncited violation of Technical Specification 5.8.3 for the failure of radiation protection personnel to appropriately barricade

and conspicuously post an area that was accessible to personnel that could have

resulted in radiation doses greater than 1.0 rem in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. Specifically, from

February 2004 through March 17, 2010, the radiation personnel failed to

appropriately barricade and conspicuously post the access ladder to the upper

refueling cavity when it was being used as the means to control access to an

individual high radiation area in the lower cavity where the maximum measured

radiation dose rate was 2.8 rem per hour. The inspectors determined that the

ladder was not appropriately barricaded and conspicuously posted, and as such

the controls the licensee had in place were easily circumvented. On March 17,

2010, radiation protection personnel appropriately barricaded and conspicuously

posted the access ladder to the upper refueling cavity. This issue was entered

into the licensees corrective action program as Nuclear Notifications

NNs 200793188 and 200837345.

The finding is greater than minor because it is associated with the program and

process attribute of the Radiation Safety Cornerstone and directly affected the

associated cornerstone objective of ensuring the adequate protection of the

worker health and safety from exposure to radiation from radioactive material

during routine civilian nuclear reactor operation. Using Manual Chapter 0609,

Appendix C, Occupational Radiation Safety Significance Determination

Process, this finding is determined to have very low safety significance because

it did not involve: (1) an ALARA planning or work control issue, (2) an

overexposure, (3) a substantial potential for overexposure, or (4) an impaired

ability to assess dose. The inspectors determined that since the licensee had not

recently re-evaluated the locked high radiation area controls associated with this

ladder; this finding did not represent current plant performance, and therefore,

did not have a crosscutting aspect associated with it (Section 1R20).

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Enclosure

Other Findings

SL-IV. The inspectors identified a noncited violation of 10 CFR 50.72,

Immediate Notification Requirements for Operating Nuclear Power Reactors,

for the licensees failure to notify the NRC Operations Center within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

following discovery of an event meeting the reportability criteria as specified.

Specifically, on December 23, 2009, the licensee failed to notify the NRC

Operations Center within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> after the discovery of an event or condition that

resulted in a condition where the spent fuel pool cooling system was prevented

from fulfilling its safety function of residual heat removal with the complete core

off loaded. This issue was entered into the licensees corrective action program

as Nuclear Notification NN 200733257.

The finding is greater than minor because the NRC relies on licensees to identify

and report conditions or events meeting the criteria specified in regulations in

order to perform its regulatory function, and when this is not done the regulatory

function is impacted. The inspectors reviewed this issue in accordance with

Inspection Manual Chapter 0612 and the NRC Enforcement Manual. Through

this review, the inspectors determined that traditional enforcement was

applicable to this issue because the NRC's regulatory ability was affected. The

inspectors determined that this finding was not suitable for evaluation using the

significance determination process, and as such, was evaluated in accordance

with the NRC Enforcement Policy. The finding was reviewed by NRC

management and because the violation was determined to be of very low safety

significance, was not repetitive or willful, and was entered into the corrective

action program, this violation is being treated as a Severity Level IV noncited

violation consistent with the NRC Enforcement Policy. This finding has a

crosscutting aspect in the area of problem identification and resolution

associated with the corrective action program because the licensee failed to

thoroughly evaluate problems such that the resolutions addressed causes and

extent of conditions as necessary. This includes properly classifying, prioritizing,

and evaluating for operability and reportability conditions adverse to quality

P.1(c) (Section 4OA2).

SL-IV. The inspectors identified a noncited violation of 10 CFR 50.73, Licensee

Event Report System, associated with the failure of nuclear regulatory affairs

personnel to submit a licensee event report within 60 days following discovery of

an event meeting the reportability criteria as specified. Specifically, nuclear

regulatory affairs personnel failed to submit a licensee event report within 60

days following discovery of a complete loss of spent fuel pool cooling event that

occurred on February 13, 2007. This issue was entered into the licensees

corrective action program as Nuclear Notifications NNs 200740135 and

200733257.

The finding is greater than minor because the NRC relies on licensees to identify

and report conditions or events meeting the criteria specified in regulations in

order to perform its regulatory function, and when this is not done the regulatory

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Enclosure

function is impacted. The inspectors reviewed this issue in accordance with

Inspection Manual Chapter 0612 and the NRC Enforcement Manual. Through

this review, the inspectors determined that traditional enforcement was

applicable to this issue because the NRC's regulatory ability was affected. The

inspectors determined that this finding was not suitable for evaluation using the

significance determination process, and as such, was evaluated in accordance

with the NRC Enforcement Policy. The finding was reviewed by NRC

management and because the violation was determined to be of very low safety

significance, was not repetitive or willful, and was entered into the corrective

action program, this violation is being treated as a Severity Level IV noncited

violation consistent with the NRC Enforcement Policy. Since the inadequate

reportability determination had been made in 2007, and the licensees

reportability program has undergone significant revision since this time, the

inspectors determined that this was not reflective of current licensee performance

and therefore did not have a crosscutting aspect associated with it (Section

4OA2).

SL-IV. The inspectors identified a noncited violation of 10 CFR 50.59, Changes,

Test, and Experiments, for the failure of licensing personnel to obtain a technical

specification license amendment for a change made to the technical specification

bases concerning the emergency chilled water system. Specifically, in 1996,

licensing personnel implemented a technical specification bases change for

Limiting Condition for Operation 3.7.10, Emergency Chilled Water, which

changed the intent and application of the technical specification, and added

wording which allowed a period of time for required support systems to be

inoperable without declaring the emergency chillers inoperable. This issue was

entered into the licensees corrective action program as Nuclear Notifications

NNs 200747320 and 200758329.

The finding is greater than minor because the failure to follow the requirements of

10 CFR 50.59 and receive prior NRC approval for changes in licensed actions

impacted the NRCs regulatory ability. The inspectors reviewed this issue in

accordance with Inspection Manual Chapter 0612 and the NRC Enforcement

Manual. Through this review, the inspectors determined that traditional

enforcement was applicable to this issue because the NRC's regulatory ability

was affected. The inspectors determined that this finding was not suitable for

evaluation using the significance determination process, and as such, was

evaluated in accordance with the NRC Enforcement Policy. The finding was

reviewed by NRC management and because the violation was determined to be

of very low safety significance, was not repetitive or willful, and was entered into

the corrective action program, this violation is being treated as a Severity

Level IV noncited violation consistent with the NRC Enforcement Policy. Since

the bases change was made in 1996, the inspectors determined that this was not

reflective of current licensee performance and therefore did not have a

crosscutting aspect associated with it (Section 4OA2).

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Enclosure

B.

Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee, have

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. These violations and

corrective action tracking numbers are listed in Section 4OA7.

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Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 2 began the inspection period shutdown for a scheduled refueling outage (U2C16) and

steam generator replacement, and remained there for the duration of the inspection period.

Unit 3 began the inspection period at full power. Between March 4 and March 10, 2010, the unit

reduced power to 50 percent for fuel conservation, and remained there for the duration of the

inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

Readiness for Impending Adverse Weather Conditions

a.

Inspection Scope

Since coastal flooding with potential tornados and high winds were forecast in the vicinity

of the facility for January 20 through January 22, 2010, the inspectors reviewed the

licensees overall preparations/protection for the expected weather conditions. On

January 20, 2010, the inspectors walked down the Unit 3 auxiliary feedwater structure

and the off site power distribution system because their safety-related functions could be

affected or required as a result of high winds or tornado-generated missiles or the loss of

offsite power. The inspectors evaluated the licensee staffs preparations against the

sites procedures and determined that the staffs actions were adequate. During the

inspection, the inspectors focused on plant-specific design features and the licensees

procedures used to respond to specified adverse weather conditions. The inspectors

also toured the plant grounds to look for any loose debris that could become missiles

during a tornado. The inspector's evaluated operator staffing and accessibility of

controls and indications for those systems required to control the plant. Additionally, the

inspectors reviewed the Updated Final Safety Analysis Report and performance

requirements for systems selected for inspection, and verified that operator actions were

appropriate as specified by plant-specific procedures. The inspectors also reviewed a

sample of corrective action program items to verify that the licensee identified adverse

weather issues at an appropriate threshold and dispositioned them through the

corrective action program in accordance with station corrective action procedures.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one readiness for impending adverse weather

condition sample as defined in IP 71111.01-05.

b.

Findings

No findings of significance were identified.

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Enclosure

1R04 Equipment Alignments (71111.04)

.1

Partial Walkdowns

a.

Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

February 23, 2009, Unit 2, containment alignment for integrated leakage rate test

March 10, 2010, Unit 3, auxiliary feedwater pump MP-141 alignment

March 11, 2010, Unit 2, emergency diesel generator train A

March 22, 2010, Unit 2, saltwater cooling train A

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Final Safety Analysis Report, technical specification

requirements, administrative technical specifications, outstanding work orders, corrective

action documents, and the impact of ongoing work activities on redundant trains of

equipment in order to identify conditions that could have rendered the systems incapable

of performing their intended functions. The inspectors also walked down accessible

portions of the systems to verify system components and support equipment were

aligned correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were

no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program with the appropriate significance characterization. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four partial system walkdown samples as

defined by IP 71111.04-05.

b.

Findings

No findings of significance were identified.

.2

Semi-Annual Complete Walkdown

a.

Inspection Scope

Between January 22, 2010, and March 24, 2010, the inspectors performed a complete

system alignment inspection of the Unit 2 safety injection system to verify the functional

capability of the system. The inspectors selected this system because it was considered

both safety-significant and risk-significant in the licensees probabilistic risk assessment.

The inspectors walked down the system to review mechanical and electrical equipment

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Enclosure

line ups, electrical power availability, system pressure and temperature indications, as

appropriate, component labeling, component lubrication, component and equipment

cooling, hangers and supports, operability of support systems, and to ensure that

ancillary equipment or debris did not interfere with equipment operation. The inspectors

reviewed a sample of past and outstanding work orders to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the corrective action program database to ensure that system equipment-

alignment problems were being identified and appropriately resolved. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one complete system walkdown sample as

defined by IP 71111.04-05.

b.

Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

Quarterly Fire Inspection Tours

a.

Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

January 4, 2010, Units 2 and 3, hot work activities in the saltwater cooling pipe

tunnel

January 14, 2010, Unit 2, auxiliary feedwater pump tunnel

February 9, 2010, Unit 2, safety equipment building rooms 2 through 5 and 15

February 10, 2010, Unit 3, penetration building

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to affect equipment that could initiate or mitigate a plant

transient, or their impact on the plants ability to respond to a security event. Using the

documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

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Enclosure

fire detectors and sprinklers were unobstructed, that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four quarterly fire-protection inspection samples

as defined by IP 71111.05-05.

b.

Findings

Introduction. The inspectors identified three examples of a Green noncited violation of

Technical Specification 5.5.1.1.d, for the failure of contractor and station personnel to

properly implement the requirements of a station fire protection procedure for control of

hot work activities.

Description. On January 4, 2010, while performing a fire protection walk down of the

Unit 2 salt water cooling tunnel the inspectors noted contract personnel, who were being

supervised by station personnel, performing what appeared to be hot work activities on

the salt water cooling piping. The inspectors noted that the activities were producing

sparks and the sparks were coming in contact with unprotected combustible materials.

The inspectors inquired about this activity and were informed that a portion of the work,

grinding activities, had been classified as hot work and as such a flame permit was

associated with it and a fire watch was present. The inspectors reviewed the flame

permit and noted that it required all combustible material within 35 feet of the activity to

removed or covered. When the inspectors pointed this out to the fire watch they were

informed by the station personnel that were present, including supervisors, that the

evolution that was producing the sparks that were coming in contact with the

unprotected combustibles was flapper wheeling activities and was not subject to hot

work controls. The inspectors pointed out that the grinding was a hot work activity that

was in progress and required all materials to be removed or covered within 35 feet.

The inspectors questioned this response concerning the flapper wheel activities and

reviewed station procedure SO123-XV-1.41, Control of Ignition Sources, Revision 14,

to validate what they had been told. During this review the inspectors noted that

Section 6.2.1 stated, in part, For sanding and flapper wheel activities, all

flammable/combustible material shall be removed from within the area where the field of

sparks would be expected to spread from this activity, and if relocation is impractical

then shield all combustibles. As such, the inspectors determined that the procedure

had not been appropriately followed for either activity. Also, the personnel who were

performing the work, supervising the work, and performing fire watch duties were not

familiar with the procedural requirements for the activities being performed. Nuclear

Notification NN 200729747 was initiated to document the inspectors concerns.

On January 14, 2010, the inspectors observed work activities in the Unit 2 auxiliary

feedwater tunnel, and noted that welders were conducting hot work activities with

unprotected combustibles within 35 feet of the work area. The inspectors noted that the

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Enclosure

flame permit for the activity identified that all combustible material within 35 feet of the

activity either had to be removed or covered. When the inspectors pointed this out to the

fire watch and welders, the activity was stopped. The licensee initiated Nuclear

Notification NN 200746059 to capture this concern, and conducted a human

performance error review board. During this review, the licensee determined that the fire

watch and the welders had failed to follow the requirements of procedure

SO123-XV-1.41.

On March 16, 2010, the inspectors passed through the turbine building and noted sparks

coming from the overhead. Upon further investigation, the inspectors noted that the

sparks were coming from work activities occurring on the level above and the sparks

were coming in contact with unprotected combustible materials. The inspectors noted

that a fire watch was posted in the area and inquired of the adequacy of the work site.

The fire watches initial response was that this area was more than 35 feet away from

the work area therefore it was not an issue. The inspectors were not satisfied with this

response and requested that a supervisor come to the area. During discussions with the

supervisor, the inspectors learned that the activities that were occurring above were

flapper wheeling activities, and that the work area was supposed to be completely

enclosed. The inspectors also determined that the work group was not familiar with the

procedural requirements associated with flapper wheel activities. As such, the

inspectors determined that the licensee had failed to follow procedure SO123-XV-1.41

for flapper wheel activities and remove or cover all flammable/combustible material from

within the area where the field of sparks would be expected to spread. The licensee

initiated Nuclear Notification NN 200835830 to capture this concern.

Analysis. The failure to follow the requirements of a station fire protection procedure for

control of hot work activities was a performance deficiency. The finding is greater than

minor because if left uncorrected, the practice of conducting hot work in a manner that

allows uncontrolled combustibles to be within the procedurally specified exclusion area

would have the potential to lead to a more significant safety concern, in that, it could

result in a fire in or near risk important equipment. The finding is associated with the

Initiating Events Cornerstone. The inspectors determined that Manual Chapter 0609,

Appendix F, Fire Protection Significance Determination Process, does not address the

potential risk significance of shutdown fire protection findings, and Appendix G,

Shutdown Operations Significance Determination Process, does not address fire

protection findings, and therefore could not be applied to shutdown plant conditions.

Because of this, the inspectors used Manual Chapter 0609, Appendix M, Significance

Determination Process Using Qualitative Criteria. The NRC management review was

performed by using the Manual Chapter 0609, Appendix F, Phase 1 Worksheet, to

establish a bounding analysis. Using the bounding analysis, the finding is determined to

have very low safety significance because the finding represented a low degradation

rating, in that, it did not have any significant effect on the likelihood that a fire might

occur, or that a fire which does occur might not be promptly suppressed. This finding

had a crosscutting aspect in the area of human performance associated with work

practices, in that, the licensee failed to define and effectively communicate expectations

regarding procedural compliance and personnel follow procedures H.4(b).

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Enclosure

Enforcement. Technical Specification 5.5.1.1.d requires, in part, that written procedures

be established, implemented, and maintained covering Fire Protection Program

implementation. The Fire Protection Program was implemented, in part, by procedure

SO123-XV-1.41, Control of Ignition Sources, Revision 14. Procedure SO123-XV-1.41,

Steps 6.2.1 and 6.4.1.3, required that combustible materials be covered or removed

from the ignition sources. Contrary to the above, between January 4 and March 17,

2010, three examples were identified where contractor and station personnel failed to

properly implement the requirements of procedure SO123-XV-1.41, Steps 6.2.1 and

6.4.1.3. Specifically, contractor and station personnel failed to ensure that combustible

materials were covered or removed from the ignition source. Following the inspectors

identification of each example, the licensee immediately stopped the hot work activities

and restored compliance with the requirements of procedure SO123-XV-1.41. Because

this finding is of very low safety significance and has been entered into the licensees

corrective action program as Nuclear Notifications NNs 200729747, 200746059 and

200835830, this violation is being treated as a noncited violation, consistent with Section

VI.A of the NRC Enforcement Policy: NCV 05000361/2010002-01, Failure to Implement

Fire Protection Plan Requirements Related to Hot Work Activities.

1R06 Flood Protection Measures (71111.06)

a.

Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, the flooding analysis,

and plant procedures to assess seasonal susceptibilities involving internal flooding;

reviewed the Updated Final Safety Analysis Report and corrective action program to

determine if licensee personnel identified and corrected flooding problems; inspected

underground bunkers/manholes to verify the adequacy of sump pumps, level alarm

circuits, cable splices subject to submergence, and drainage for bunkers/manholes;

verified that operator actions for coping with flooding can reasonably achieve the desired

outcomes; and walked down the one area listed below to verify the adequacy of

equipment seals located below the flood line, floor and wall penetration seals, watertight

door seals, common drain lines and sumps, sump pumps, level alarms, and control

circuits, and temporary or removable flood barriers. Specific documents reviewed during

this inspection are listed in the attachment.

March 15, 2010, Unit 3, auxiliary feedwater pump house

These activities constitute completion of one flood protection measures inspection

sample as defined by IP 71111.06-05.

b.

Findings

No findings of significance were identified.

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Enclosure

1R11 Licensed Operator Requalification Program (71111.11)

a.

Inspection Scope

On March 9, 2010, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems, and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

Licensed operator performance

Crews clarity and formality of communications

Crews ability to take timely actions in the conservative direction

Crews prioritization, interpretation, and verification of annunciator alarms

Crews correct use and implementation of abnormal and emergency procedures

Control board manipulations

Oversight and direction from supervisors

Crews ability to identify and implement appropriate technical specification

actions and emergency plan actions and notifications

The inspectors compared the crews performance in these areas to pre-established

operator action expectations and successful critical task completion requirements.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one quarterly licensed-operator requalification

program sample as defined in IP 71111.11.

b.

Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

March 4, 2010, Units 2 and 3, instrument air system

March 24, 2010, Unit 3, auxiliary feedwater system

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Enclosure

The inspectors reviewed events caused by ineffective equipment maintenance that

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

Implementing appropriate work practices

Identifying and addressing common cause failures

Scoping of systems in accordance with 10 CFR 50.65(b)

Characterizing system reliability issues for performance

Charging unavailability for performance

Trending key parameters for condition monitoring

Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or (a)(2)

Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of two quarterly maintenance effectiveness

samples as defined in IP 71111.12-05.

b.

Findings

Introduction. The inspectors identified a Green noncited violation of 10 CFR

50.65(b)(2)(ii) for the licensees failure to appropriately scope the steam driven auxiliary

feedwater pumps trench eductor in the maintenance rule monitoring program.

Description. On January 21, 2010, operations personnel observed that water had come

in contact with the steam line mud leg in the Unit 3 steam driven auxiliary feedwater

pump steam supply trench during heavy rains. Operations personnel declared the

auxiliary feedwater pump inoperable in accordance with procedure SO23-2-4, Auxiliary

Feedwater System Operation, Revision 27, until the piping could be blown down and

the pump run for 30 minutes to verify that the piping was dried out. The licensee entered

this issue into their corrective action program as Nuclear Notification NN 200758566.

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Enclosure

The inspectors reviewed the maintenance rule functional failure evaluation associated

with Nuclear Notification NN 200758566. The inspectors noted that the licensee had

concluded that this event was not a functional failure of the eductor. The licensees

evaluation focused on the performance criteria of the auxiliary feedwater pump, and did

not appear to consider appropriate criteria for the trench eductor. The basis for the

conclusion was a calculation that had been performed to demonstrate that water in

contact with the steam line mud leg did not make the auxiliary feedwater pump

inoperable.

The eductors were installed in 1986 and were used to remove water from the steam

supply trench to prevent adverse affects on the auxiliary feedwater pump. Trench water

in contact with the pumps steam supply piping would cause condensation of the steam

in the pipe causing the potential for the turbine to over speed, which would render the

pump incapable of performing it specified safety function.

The inspectors observed that the trench eductor was not connected to the auxiliary

feedwater system, but that it was a support system installed to facilitate the auxiliary

feedwater pump being able to perform its specified safety function. The inspectors

questioned the adequacy of evaluating a failure of the eductor to perform its function,

preventing water from accumulating in the trench, against the performance criteria of the

auxiliary feedwater system, which was to provide a reliable source of feedwater to steam

generators during normal and emergency conditions. Through discussions with the

licensees maintenance rule coordinator, the inspectors determined that the eductors

were not scoped in the stations maintenance rule monitoring program. The

maintenance rule coordinator informed the inspectors that the eductors were not scoped

in the maintenance rule monitoring program because their failure could not directly

cause the failure of the auxiliary feedwater pump, and the station was not required to

consider hypothetical failures that resulted from system interdependencies that have not

been previously seen. The inspectors determined that the licensee had developed a

narrow interpretation of what directly meant based on a narrow interpretation of some

examples from NUMARC 93-01, Industry Guideline for Monitoring the Effectiveness of

Maintenance at Nuclear Power Plants.

Through more reviews, the inspectors noted that the licensee determined that the

eductors had been installed to assist in removing any accumulated water in the trench,

to limit buildup of water to ensure that condensate does not accumulate in the steam

lines and cause an overspeed trip of the turbine. Furthermore, this had been done

based on past plant experience dealing with water causing condensation in the steam

piping. Therefore, the inspectors determined that the licensee had inappropriately

interpreted 10 CFR 50.65(b)(2)(ii), with regard to nonsafety-related structures, systems

and components whose failure could prevent safety-related structures, systems, and

components from fulfilling their safety-related function, and had failed to appropriately

scope the eductors for both Units 2 and 3 in the stations maintenance rule monitoring

program.

Analysis. The failure to properly scope the auxiliary feedwater trench eductors in the

maintenance rule monitoring program was a performance deficiency. The finding is

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Enclosure

greater than minor because it is associated with the equipment performance attribute of

the Mitigating Systems Cornerstone and directly affected the cornerstone objective of

ensuring the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Using the Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheets, the finding is determined to

have very low safety significance because the finding: (1) is not a design or qualification

issue confirmed not to result in a loss of operability or functionality; (2) did not represent

an actual loss of safety function of the system or train; (3) did not result in the loss of one

or more trains of nontechnical specification equipment; and (4) did not screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating event.

The inspectors determined that since the scoping of the systems had occurred more

than 2 years in the past, and the opportunity to reevaluate system scoping had not

occurred recently, that the finding did not represent current plant performance and

therefore did not have a crosscutting aspect associated with it.

Enforcement. Title 10 CFR 50.65(b)(2)(ii) requires, in part, that the scope of the

monitoring program specified in paragraph (a)(1) of this section shall include nonsafety

related structures, systems and components whose failure could prevent safety-related

structures, systems, and components from fulfilling their safety-related function.

Contrary to the above, from the inception of the facilities monitoring program through

March 2010, the licensee failed to properly scope the steam drive auxiliary feedwater

pump trench eductor into the maintenance rule monitoring program. Because this

violation is of very low safety significance and has been entered into the licensees

corrective action program as Nuclear Notification NN 200765185, this violation is being

treated as a noncited violation consistent with Section VI.A of the NRC Enforcement

Policy: NCV 05000361;05000362/2010002-02, Failure to Appropriately Scope Auxiliary

Feedwater Pump Trench Eductors in the Maintenance Rule Monitoring Program.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and safety-

related equipment listed below to verify that the appropriate risk assessments were

performed prior to removing equipment for work:

January 13-14, 2010, Units 2 and 3, use of non-conservative technical

specifications for new fuel movement related to proposed change number

PCN 593

January 20, 2010, Unit 2, proposed cavity drain down activities during inclement

weather

February 3, 2010, Unit 2, diving operations in the intake area

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Enclosure

February 10-12, 2009, Units 2 and 3, safety monitor model change interim

measures to address uncertainty associated with manual operation of motor

operated valves

February 17, 2010, Units 2 and 3, mobile crane use in the electrical switchyard

The inspectors selected these activities based on potential risk significance relative to

the reactor safety cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of six maintenance risk assessments and

emergent work control inspection samples as defined by IP 71111.13-05.

b.

Findings

1. Operating Experience Review

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees

failure to properly implement procedure requirements to ensure that applicable risk

significant operating experience was entered into the corrective action program for timely

evaluation.

Description. On December 17, 2009, an industry operating experience report was

reviewed by the operating experience review committee regarding lessons learned from

the industry related to the expected differential pressure across locally operated valves,

which must be considered when evaluating the ability of operators to change valve

position in accident conditions. The review determined the operating experience was

not applicable and was distributed as information only; not requiring any action. On

February 10, 2010, the probabilistic risk assessment group initiated interim

compensatory measures for the safety monitor model used to assess the risk associated

with on-line work activities. The interim actions were taken following the probabilistic risk

assessment groups recognition that the industry operating experience report had a

potential impact and were conservatively used to address uncertainty associated with

the manual operation of auxiliary feedwater motor operated valves under the differential

pressures expected during accident conditions.

On February 11, 2010, the inspectors questioned the timeliness of the risk significant

operating experience report evaluation that took several months to be properly assessed

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Enclosure

by the probabilistic risk assessment group. On February 23, 2010, based on prompting

by the inspectors, the licensee initiated Nuclear Notification NN 200805879 to

investigate the timeliness of their operating experience review of the event involving the

expected differential pressure across locally operated valves which could impact risk

significant components. The evaluation identified the initial industry operating

experience review failed to recognize the applicability of the operating experience or the

potential risk significant impact that needed further analysis. As such, this information

was not entered into the corrective action program, and therefore, not directed to

appropriate subject matter experts or communicated to the affected station groups in a

timely manner as required by procedure SO23-XV-40, Sharing Industry Information,

Revision 1. The evaluation also concluded the operating experience review committee

lacked a knowledge basis to recognize the potential implications, and instead of using a

systematic approach, depended upon distribution to other departments and personnel to

assess the need for entry into the corrective action program for evaluation of the impact

to risk-significant and safety-significant activities.

Analysis. The failure to properly implement procedure requirements to ensure adequate

review of applicable industry operating experience was a performance deficiency. The

finding is greater than minor because it is associated with the procedure quality attribute

of the Mitigating Systems Cornerstone and affects the associated cornerstone objective

to ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Using the Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheets, the finding is determined to

have very low safety significance because the finding: (1) is not a design or qualification

issue confirmed not to result in a loss of operability or functionality; (2) did not represent

an actual loss of safety function of the system or train; (3) did not result in the loss of one

or more trains of nontechnical specification equipment; and (4) did not screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating event.

This finding has a crosscutting aspect in the area of human performance associated with

decision-making because the operating experience review committee did not use a

systematic process when making a safety significant decision, to ensure safety is

maintained and obtaining interdisciplinary inputs and reviews on risk-significant

decisions H.1(a).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires that activities affecting quality shall be prescribed by

documented instructions, procedures or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with those instructions,

procedures, and drawings. Procedure SO23-XV-40, Sharing Industry Information,

Revision 1, required actions to ensure a review of industry operating experience for

applicability and the need for timely evaluation in the corrective action program.

Contrary to the above, on December 17, 2009, the operating experience review

committee failed to properly implement the requirements of procedure SO23-XV-40.

Specifically, an industry operating experience report review determined the operating

experience was not applicable and was distributed as information only; not requiring any

action. The same industry operating experience was later determined to be applicable

by the probabilistic risk assessment group, and interim compensatory measures were

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Enclosure

initiated on February 10, 2010, to address the issues. Because this finding is of very low

safety significance and has been entered into the licensees corrective action program

as Nuclear Notifications NN 200805879, this violation is being treated as a noncited

violation consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000361;05000362/2010002-03, Failure to Enter Operating Experience into Corrective Action

Program for Timely Evaluation.

2. Risk Assessment for Switchyard Activities

Introduction. The inspectors identified a Green noncited violation of 10 CFR 50.65(a)(4),

Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power

Plants, involving multiple instances where operations and work control personnel failed

to adequately assess and implement appropriate risk management activities for work in

the stations electrical switchyard.

Description. On February 17, 2010, the licensee determined that the station had failed

to perform an adequate risk assessment for proposed crane activities in the switchyard

with regard to Unit 3, which was operating at full power. Before allowing the activities to

commence the licensee performed the required risk assessment, and classified the work

as a high risk activity in the switchyard for Unit 3, and commenced the crane activity.

The inspectors subsequently reviewed the risk assessment on February 18, 2010.

During their review, the inspectors determined that this assessment had been performed

only for Unit 3, as identified under the additional requirements section, which stated;

maintain requirements per procedure SO23-5-1.8.1, Shutdown Nuclear Safety,

Revision 23, on Unit 2. Based on this, the inspectors questioned how the activities being

performed in the switchyard had been assessed with regard to Unit 2, which was

shutdown in Mode 5 at the time.

The inspectors reviewed procedure SO23-5-1.8.1, and noted that the following:

The stated objective of the procedure was to provide guidelines for controlling

evolutions and activities while in Mode 5 and 6 to ensure that Shutdown Safety

Functions are maintained Operable, Functional, or Available as required to

support the station philosophy of Defense in Depth

Section 6.1.1 defined electrical power availability as a Shutdown Safety Function

Attachment 1, Definitions, Section 1.8 defined a high risk evolution as; Outage

activities, plant configurations, or conditions during shutdown where the plant is

more susceptible to an event causing the loss of a shutdown safety function.

Section 6.11, Control of High Risk Evolutions, provided specific guidance on

evaluating these evolutions and establishing required risk management actions

As a result, the inspectors determined that; an adequate risk assessment had not been

performed for Unit 2, and the requirements of Section 6.11 of procedure SO23-5-1.8.1

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Enclosure

had not been implemented with respect to implementing required risk management

actions for the on-going crane activities in the switchyard.

The inspectors presented this information indicating a failure to adequately assess risk

associated with the crane activities and implement appropriate risk management actions,

relative to Unit 2 to the licensee. During discussions with station personnel, the

inspectors were informed that the station believed that the Defense in Depth planning

sheets were the stations risk assessment for Unit 2, and since they had not removed any

of the identified systems from service they were within their analysis. The inspectors

pointed out that procedure SO23-5-1.8.1, Section 6.1.1.3 stated, in part:

The selected safety function fulfillment plans are recorded in the Defense in

Depth planning sheets. These are tables which document the pre-planned safety

function fulfillment plan methods, safety function protection plan, or other

contingency plans for each safety function.

Accordingly, the inspectors identified that the crane activities had not been assessed

and incorporated into the stations defense in depth strategy, and as such, the Defense in

Depth planning sheets were not an appropriate risk assessment for this activity.

The licensee determined that an appropriate risk assessment had not been performed,

and when one was performed, risk management actions were identified as required by

procedure SO23-5-1.8.1. On February 19, 2010, the licensee initiated Nuclear

Notification NN 200801929 to document the issue and implement corrective actions.

Subsequently, on February 23, 2010, the inspectors questioned why operations

personnel were allowing work on a support system for a Unit 2 emergency diesel

generator while switchyard work was still in progress. While investigating this concern,

the licensee determined that the crane had been removed from the switchyard on

February 19, 2010. This resulted in the risk management actions for the Unit 2

emergency diesel generators being discontinued. However, there was a failure to

recognize and properly assess a man-lift that was staged for use in the switchyard. Use

of the man-lift would also require risk management actions for the Unit 2 emergency

diesel generators. Subsequently, the licensee was able to determine that the man-lift

had not been used from February 19 through 23, 2010. The licensee initiated Nuclear

Notification NN 200805635 to document this issue.

Analysis. The failure to perform an adequate risk assessment and implement

appropriate risk management actions was a performance deficiency. The finding is

greater than minor since it was similar to both more than minor examples 7.e and 7.f in

NRC Inspection Manual Chapter 0612, Appendix E, Examples of Minor Issues,

because when the activities were correctly assessed plant procedures required risk

management actions to be taken. The finding is associated with the Initiating Events

Cornerstone. The inspectors determined that the licensee does not maintain a

shutdown probabilistic risk analysis model, and as such, an incremental core damage

probability cannot be estimated for the plant conditions that existed at the time of the

performance deficiency. For this reason, the inspectors determined that Manual

Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management

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Enclosure

Significance Determination Process, Flowchart 2, could not be used to determine the

risk significance the finding. Using the qualitative review process of Manual

Chapter 0609, Appendix M, Significance Determination Process Using Qualitative

Criteria, the finding is determined to have very low safety significance because the

finding did not result in any additional loss of defense in depth systems. This finding has

a crosscutting aspect in the area of human performance associated with the work

practices because the licensee failed to define and effectively communicate expectations

regarding procedural compliance and that personnel follow procedures H.4(b).

Enforcement. Title 10 CFR 50.65(a)(4), states in part, that before performing

maintenance activities (including but not limited to surveillance, postmaintenance testing,

and corrective and preventive maintenance), the licensee shall assess and manage the

increase in risk that may result from the proposed maintenance activities. Contrary to

the above, between February 18, and February 23, 2010, operations and work control

personnel failed to adequately assess and manage the increase in risk associated with

maintenance activities in the electrical switchyard. Following the inspectors

identification of the findings, the licensee adequately assessed and managed the

increase in risk for the maintenance activities. Because this finding is of very low safety

significance and has been entered into the licensees corrective action program as

Nuclear Notifications NNs 200801929 and 200805635, this violation is being treated as a

noncited violation, consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000361/2010002-04, Failure to Assess and Manage Risk for Electrical Switchyard

Impacting Maintenance.

1R15 Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors reviewed the following issues:

January 3-5, 2010, Unit 2, inspectors identified various seismic issues associated

with the gap required between containment interior and exterior structures

requiring various evaluations and Unit 3 at power entry

January 13, 2010, Unit 2, operability impact of through wall piping flaws found on

emergency core cooling system Train A piping

January 19, 2010, Unit 3, operability impact of a through wall piping flaw on the

common emergency core cooling system mini-flow line

January 22, 2010, Unit 2, operability impact due to suspected growth of through

wall piping flaws previously identified on emergency core cooling system Train A

piping

February 2, 2010, Unit 3, intake structure integrity

February 4, 2010, Unit 3, through wall flaw indication on emergency core cooling

system piping

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Enclosure

February 9-10, 2009, Units 2 and 3, seat leak requirements for component

cooling water pump discharge valves

February 12-14, 2010, Unit 2, safety related battery 2B007 surveillance results

indicate battery at 85 percent of service life

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and Updated

Final Safety Analysis Report to the licensees evaluations, to determine whether the

components or systems were operable. Where compensatory measures were required

to maintain operability, the inspectors determined whether the measures in place would

function as intended and were properly controlled. The inspectors determined, where

appropriate, compliance with bounding limitations associated with the evaluations.

Additionally, the inspectors also reviewed a sampling of corrective action documents to

verify that the licensee was identifying and correcting any deficiencies associated with

operability evaluations. Specific documents reviewed during this inspection are listed in

the attachment.

These activities constitute completion of eight operability evaluations inspection samples

as defined in IP 71111.15-05.

b.

Findings

Introduction. The inspectors identified two examples of a Green noncited violation of

10 CFR Part 50, Appendix B, Criterion V, Instruction, Procedures, and Drawing, for the

failure of operations personnel to follow procedures to approve and document operability

determinations using adequate or technically correct information.

Description. The inspectors reviewed the operability determinations documented in

Nuclear Notifications NNs 200745284 and 200760570, to verify the evaluation adequacy

and compliance with procedure SO123-XV-52, Functionality Assessments and

Operability Determinations, Revision 14. Nuclear Notification NN 200745284 was

written on January 14, 2010, to document a through wall pipe leak on the Unit 3

emergency core cooling system miniflow common discharge line. During their review,

the inspectors noted that the licensee had classified the flaw as a pinhole leak, based on

the visible appearance of the flaw at the time of discovery, and had developed an

immediate operability determination based on this characterization. However, at 12

midnight on January 15, 2010, as part of their prompt operability determination data

gathering, the licensee had performed nondestructive examination testing and

discovered that the flaw was actually a 0.5 inch linear flaw, and this was reported to

operations personnel at 00:45 a.m. Operations personnel believed that this new

classification was bounded by the original immediate operability determination.

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Enclosure

However, the inspectors noted that NRC Inspection Manual Part 9900 guidance,

Operability Determinations, Paragraph 4.6, Timing of Operability Determinations,

states, in part, If, at any time, information is developed that negates a previous

determination that there is a reasonable expectation that the structures, systems and

components is operable, the licensee should declare the structures, systems and

components inoperable. As such the inspectors determined that this new information,

the characterization of the flaw as a linear indication versus a pinhole, should have

resulted in a new immediate operability determination being performed. The inspectors

communicated their concerns to operations personnel. The licensee performed a new

immediate operability determination, and initiated Nuclear Notification NN 200753880 to

capture this issue in their corrective action program.

Nuclear Notification NN 200760570 was initiated to document an increase in flaw size

for previously identified flaws on the Unit 3 train A emergency core cooling system

suction header, identified during augmented inspections on January 22, 2010. As a

result of this new condition being identified, the licensee performed an immediate

operability determination using; the calculated growth rates, the calculated maximum

allowed flaw size, and the systems mission time of 120 days.

The inspectors determined that the licensees operability determination was inadequate.

Specifically, their use of a 120 day mission time did not adequately address the flaw

growth rate in relation to the calculated maximum allowed flaw size. Specifically, the

calculated flaw growth rate would exceed the maximum allowed flaw size before the

systems 120 day mission time would be completed. The inspectors informed the

licensee of their concerns. The licensee performed a new operability determination to

provide adequate bases for operability, and initiated Nuclear Notification NN 200765208

to capture this issue in their corrective action program.

Analysis. The failure to follow procedures to approve an adequate basis for operability

was a performance deficiency. The finding is greater than minor because, if left

uncorrected, inadequate operability determinations would have the potential to lead to a

more significant safety concern. Specifically, the failure to recognize that risk significant

equipment is in a potentially inoperable condition and as such, may not be able to

perform its specified safety function would not be recognized and accounted for by

operators. The finding is associated with the Mitigating Systems Cornerstone. Using

the Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheets,

the finding is determined to have very low safety significance because the finding: (1) is

not a design or qualification issue confirmed not to result in a loss of operability or

functionality; (2) did not represent an actual loss of safety function of the system or train;

(3) did not result in the loss of one or more trains of nontechnical specification

equipment; and (4) did not screen as potentially risk significant due to a seismic,

flooding, or severe weather initiating event. This finding has a crosscutting aspect in the

area of problem identification and resolution associated with the corrective action

program because the licensee failed to thoroughly evaluate problems such that the

resolutions addressed causes and extent of conditions as necessary P.1(c).

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Enclosure

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions or drawings of a type appropriate to the circumstances and

shall be accomplished in accordance with these instructions and drawings.

Procedure SO123-XV-52, Functionality Assessments and Operability Determinations,

Revision 14, required that operations personnel make a definitive statement of

operability and the basis for the statement. Contrary to the above, on January 15, and

January 22, 2010, operations personnel failed to follow procedure SO123-XV-52, in that,

the documented bases for operability for degraded conditions did not adequately support

the basis for an operability position taken by the licensee. Because this finding is of very

low safety significance and has been entered into the licensees corrective action

program as Nuclear Notifications NNs 200765208 and 200753880, this violation is being

treated as a noncited violation consistent with Section VI.A of the NRC Enforcement

Policy: NCV 05000362/2010002-05, Failure to Follow Procedure Results in an

Inadequate Operability Determination.

1R19 Postmaintenance Testing (71111.19)

a.

Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

January 29, 2010, Unit 2, retest of 2PCV-5403, nitrogen pressure control valve

train A for component cooling water surge tank

February 5, 2010, Unit 2, functional testing of spliced resistance temperature

detectors to reactor coolant system loop 2 hot leg channel B narrow range

February 5, 2010, Unit 2, boration dilution controls system preoperational testing

March 3, 2010, Unit 2, containment integrated leak rate test

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the Updated

Final Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and

various NRC generic communications to ensure that the test results adequately ensured

that the equipment met the licensing basis and design requirements. In addition, the

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Enclosure

inspectors reviewed corrective action documents associated with postmaintenance tests

to determine whether the licensee was identifying problems and entering them in the

corrective action program and that the problems were being corrected commensurate

with their importance to safety. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of four postmaintenance testing inspection

samples as defined in IP 71111.19-05.

b.

Findings

Introduction. A self-revealing Green noncited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, was identified for failure of

maintenance planning personnel to develop and specify an adequate postmaintenance

test in the work instructions used to perform maintenance on the backup nitrogen

regulator for the component cooling water surge tank.

Description. On January 27, 2010, both component cooling water surge tank levels

were lowered, using procedure SO23-2-17, Component Cooling Water System

Operation, Revision 31. The component cooling water surge tanks were required to

have a nitrogen pressure between 33-40 psig to remain operable. Pressure in

component cooling water surge tanks trains A and B were maintained with nitrogen

supply valves PCV 5403 and PCV 5404, respectively. The valves were designed to

regulate pressure at 38 +/-1 psig when properly calibrated. During the evolution,

operations personnel failed to follow procedure SO23-2-17 to monitor nitrogen pressure

such that it could be maintained while lowering level, since they incorrectly assumed the

nitrogen supply valves were properly calibrated and would automatically maintain surge

tank nitrogen pressure in the required range. However, nitrogen supply valve PCV 5403

did not function as expected and failed to maintain nitrogen surge tank pressure in the

acceptable range for operability. The performance deficiencies associated with this

event are documented as NCV 05000361/2010002-14 of this report.

Nuclear Notification NN 200771367 was initiated to evaluate the event. The evaluation

determined that nitrogen supply valve PCV 5403 did not have the correct setpoints and

was improperly calibrated. Instrument and control maintenance technicians last

completed a maintenance calibration on the valve on October 25, 2009, using procedure

SO123-II-9.176, Pressure Reducing Regulators - Calibration, Revision 2. During this

maintenance, technicians failed to follow the requirements of procedure SO123-II-9.176

to properly calibrate the pressure control valve which resulted in the pressure control

valve not properly maintaining nitrogen pressure in the surge tank as the volume in the

surge tank was lowered on January 27, 2010.

The inspectors reviewed the maintenance history for nitrogen supply valve PCV 5403,

including Maintenance Order MO 800335873, which implemented maintenance

procedure SO123-II-9.176 to perform the calibration. The maintenance procedure

contained a section for restoration and return to service following the calibration. The

inspectors observed that the maintenance procedure SO123-II-9.176, Section 6.4,

Restoration and Return to Service, did not require any postmaintenance or functional

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Enclosure

test to ensure the nitrogen supply valve would properly maintain pressure following the

calibration when returned to service. The inspectors also observed that Maintenance

Order MO 800335873 did not specify any other test or verification that would ensure that

nitrogen supply valve PCV 5403 was capable of performing its design function following

the maintenance activity.

Procedure SO123-I-1.7, Work Order Preparation and Processing, Revision 30,

Attachment 5, Step 1.1, contained instructions for the determination of adequate

postmaintenance test requirements for maintenance activities. Procedure SO123-I-1.7,

Step 1.1.1 stated, in part, that if the maintenance procedure did not list any test

requirements, then refer to procedure SO23-I-1.25, Post Maintenance Testing,

Revision 0, for guidelines in determining adequate testing requirements. Procedure

SO23-I-1.25, Attachment 4, described a functional test as a test or verification to ensure

that the component, equipment, or subsystem that was affected by the maintenance

activity was completely capable of performing its design function. Further, it stated that

functional tests or checks, such as verification that calibrations have been satisfactorily

completed, should be considered where specific test guides have not been provided.

Following this review, the inspectors concluded that Maintenance Order MO 800335873

did not specify adequate postmaintenance testing as required by procedures

SO123-I-1.7 and SO23-I-1.25.

The inspectors communicated their observations to licensee personnel, and verified that

their concerns were captured in Nuclear Notifications NNs 200766430 and 200887764.

An engineering analysis was required to demonstrate that the component cooling water

system train A remained operable during the period from October 25, 2009, to

January 27, 2010. The engineering evaluation determined that the system would have

been able to fulfill all its intended safety functions as defined in the Updated Final Safety

Analysis Report, Section 9.2.2.2. Following the improper calibration determination, on

January 28, 2010, nitrogen supply valve PCV 5403 was re-calibrated and an adequate

postmaintenance test was performed.

Analysis. The failure to establish work instructions to include adequate postmaintenance

test requirements to verify equipment operability following maintenance was a

performance deficiency. The finding is greater than minor because it is associated with

the procedure quality attribute of the Mitigating Systems Cornerstone and affects the

associated cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Furthermore, the finding is similar to more than minor example 3.i in NRC Inspection

Manual Chapter 0612, Appendix E, Examples of Minor Issues, in that, an extensive

engineering evaluation was required to verify that the component cooling water system

remained capable of performing its safety function during a design basis earthquake.

Using the Manual Chapter 0609, Appendix G, Shutdown Operations Significance

Determination Process, Phase 1 guidance, the finding is determined to have very low

safety significance because the finding did not result in an increase in the likelihood of a

loss of reactor coolant system inventory, degrade the ability to add reactor coolant

system inventory, or degrade the ability to recover decay heat removal. This finding has

a crosscutting aspect in the area of human performance associated with work practices

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Enclosure

because maintenance planning personnel failed to follow procedures to develop

adequate work instructions to perform maintenance on safety-related equipment

H.4(b).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Maintenance Order MO 800335873 established the

instructions to perform a calibration for a safety-related pressure reducing regulator.

Contrary to the above, on October, 25, 2009, Maintenance Order MO 800335873 did not

include adequate testing required to demonstrate that the component cooling water

system remained operable following maintenance. Specifically, Maintenance Order

MO 800335873 did not specify postmaintenance testing instructions that would verify

that nitrogen supply valve PCV 5403 would perform satisfactorily in service, following

calibration, and properly control surge tank pressure during changes in surge tank

levels. Because this finding is of very low safety significance and has been entered into

the licensees corrective action program as Nuclear Notifications NNs 200766430 and

200887764, this violation is being treated as a noncited violation consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000361/2010002-06, Failure to

Perform an Adequate Postmaintenance Test.

1R20 Refueling and Other Outage Activities (71111.20)

a.

Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the Unit 2

refueling outage (U2C16) and steam generator replacement, including activities

associated with a stuck reactor vessel head alignment pin, conducted January 26-28,

2010, to confirm that licensee personnel had appropriately considered risk, industry

experience, and previous site-specific problems in developing and implementing a plan

that assured maintenance of defense-in-depth. During the refueling outage, the

inspectors observed portions of the shutdown and cooldown processes and monitored

licensee controls over the outage activities listed below.

Configuration management, including maintenance of defense-in-depth, is

commensurate with the outage safety plan for key safety functions and

compliance with the applicable technical specifications when taking equipment

out of service

Clearance activities, including confirmation that tags were properly hung and

equipment appropriately configured to safely support the work or testing

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error

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Enclosure

Status and configuration of electrical systems to ensure that technical

specifications and outage safety-plan requirements were met, and controls over

switchyard activities

Monitoring of decay heat removal processes, systems, and components

Verification that outage work was not impacting the ability of the operators to

operate the spent fuel pool cooling system

Reactor water inventory controls, including flow paths, configurations, and

alternative means for inventory addition, and controls to prevent inventory loss

Controls over activities that could affect reactivity

Maintenance of secondary containment as required by the technical

specifications

Refueling activities, including fuel handling and sipping to detect fuel assembly

leakage

Licensee identification and resolution of problems related to refueling outage

activities

Specific documents reviewed during this inspection are listed in the attachment.

Refueling Outage U2C16 was still in progress at the end of this inspection period.

Consequently, these activities constitute only a partial completion of one refueling outage

and other outage inspection sample as defined in IP 71111.20-05.

b.

Findings

1. Foreign Material Exclusion Area Controls

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure of

licensee personnel to follow procedures associated with foreign material exclusion

controls in areas designated as Zone 1 foreign material exclusion areas, on multiple

occasions, during Refueling Outage U2C16.

Description. On January 13, 2010, while performing core reload operations, station

personnel identified foreign material in the bottom of the reactor cavity. Refueling

personnel decided that since this material was not in the way of the current assemblies

being loaded that the reload could continue and the material recovered at a more

convenient time in the future. Refueling personnel generated Nuclear Notification

NN 200743228 to capture this issue in the corrective action program.

The inspectors reviewed this nuclear notification as well as procedure SO123-I-1.18,

Foreign Material Exclusion Control, Revision 14. During this review the inspectors

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Enclosure

noted that Attachment 5, Foreign Material Exclusion Controls, Section 13, Recovery

from Loss of FME Control, required, in part, to promptly stop all work in the immediate

area, not take any action that could cause further migration of the foreign material,

recover the foreign material if it can be easily retrieved, or generate a Notification which

should evaluate whether the associated work can resume before recovering the foreign

material. The inspectors determined that the actions of refueling personnel following the

identification of foreign material in the reactor cavity were contrary to the requirements of

procedure SO123-I-1.18. The inspectors informed the licensee of their observations,

and the licensee entered this issue into their corrective action program as Nuclear

Notification NN 200743834. Subsequently, the licensee determined that refueling

personnel had failed to reference procedure SO123-I-1.18 when foreign material had

been discovered on January 13, 2010.

During subsequent observations of the licensees activities in and around other Zone 1

foreign material exclusion areas (areas which required the highest level of foreign

material exclusion controls) the inspectors identified four additional instances where

licensee personnel failed to appropriately implement procedural requirements associated

with Zone 1 foreign material exclusion controls. Specifically:

January 12, 2010, station personnel were instructed to enter the Zone 1 foreign

material exclusion area around the spent fuel pool wearing anti-contamination

clothing, booties and gloves, and then remove the clothing and place it in the

trash bag in the area without entering it in the foreign material exclusion log so

that it could be tracked

January 22, 2010, the inspectors identified an instance where the foreign

material exclusion area watch logged material being brought out of the Zone 1

foreign material exclusion area around the reactor refueling cavity that had not

been logged into the area, which represented a loss of foreign material exclusion

controls

January 22, 2010, the inspectors identified a nylon rope in the Zone 1 foreign

material exclusion area around the reactor refueling cavity being used to restrain

material that had frayed ends that were not adequately covered

February 23, 2010, the inspectors identified that the Zone 1 foreign material

exclusion area around the Unit 3 spent fuel pool had material in it that was not

being tracked and controlled as required

The inspectors concluded that not all of these examples of the licensees failure to follow

procedure SO123-I-3.7, Refueling Foreign Material Exclusion Control, directly resulted

in the introduction of foreign material into a critical system. They were, however,

indicative of a programmatic issue associated with the licensees proper implementation

of the foreign material exclusion control program. The inspectors informed the licensee

of their observations, and the licensee entered this issue into their corrective action

program as Nuclear Notifications NNs 200742082, 200760484, and 200805961.

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Enclosure

Analysis. The failure of licensee personnel to follow procedures for the control of foreign

material was a performance deficiency. The finding is greater than minor because it is

associated with the human performance attribute of the Barrier Integrity Cornerstone and

affects the cornerstone objective of providing reasonable assurance that physical

barriers protect the public from radionuclide releases caused by accidents or events.

Furthermore, the programmatic deficiencies that were identified associated with this

issue would have the potential to lead to a more significant safety concern, if left

uncorrected. Specifically, licensee personnels continued failure to implement

appropriate foreign material exclusion controls would result in degradation and adverse

impacts on materials and systems associated with the spent fuel pool or the reactor

cavity. Using the Manual Chapter 0609, Appendix G, Shutdown Operations

Significance Determination Process, Phase 1 guidance, the finding is determined to

have very low safety significance because the finding did not result in an increase in the

likelihood of a loss of reactor coolant system inventory, degrade the ability to add reactor

coolant system inventory, or degrade the ability to recover decay heat removal. This

finding had a crosscutting aspect in the area of human performance associated with

work practices because the licensee failed to define and effectively communicate

expectations regarding procedural compliance which resulted in a failure to follow

procedure by licensee personnel H.4(b).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Contrary to the above, between January 12, 2010, and

February 23, 2010, the inspectors identified several examples where the licensee failed

to adequately implement foreign material exclusion controls as required by procedure

SO123-I-1.18. Because this finding is of very low safety significance and has been

entered into the licensees corrective action program as Nuclear Notifications

NNs 200760484, 200742082, 200743834 and 200805961, this violation is being treated

as a noncited violation consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000361/2010002-07, Failure to Adequately Implement Foreign Material

Exclusion Controls.

2. Controls for Locked High Radiation Area

Introduction. The inspectors identified a Green noncited violation of Technical

Specification 5.8.3 for the failure of radiation protection personnel to appropriately

barricade and conspicuously post an area that was accessible to personnel that could

have resulted in radiation doses greater than 1.0 rem in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

Description. On February 12, 2010, while touring the Unit 2 containment building, the

inspectors noted that the ladder that provided access to the upper refueling cavity was

being used to control access to a locked high radiation area in the lower refueling cavity.

The inspectors noted that the ladder had a safety cage around it, a swing door to restrict

access inside of the safety cage, and the locked high radiation sign was attached to the

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Enclosure

swing door of the safety cage. However, there was nothing on the back side of the

ladder to either restrict access or denote it as a locked high radiation area.

The inspectors questioned the adequacy of the posting and access control method being

used by the licensee. Specifically, the placement of the sign on the swing door was such

that it was not clearly visible if the ladder was approached from the back side, and the

inspectors concluded that its placement was confusing as to where the locked high

radiation area actually was. The inspectors also questioned whether the back side of

the ladder was appropriately barricaded and conspicuously posted in a way to prevent

access. The inspectors informed the licensee of their concerns. The licensee initiated

Nuclear Notification NN 200793188 to capture this concern in the corrective action

program.

The licensees initial determination was that the posting was adequate and the back side

of the ladder was sufficiently controlled. The inspectors questioned this determination

and initiated discussions with the NRC Office of Nuclear Reactor Regulation.

The inspectors determined that the posting and method of barricading the ladder was

inadequate. Specifically, the controls the licensee had in place were easily

circumvented, and as such, the inspectors determined that the licensee had failed to

appropriately control access to the lower refueling cavity where there was an area where

the maximum measured radiation dose rate was 2.8 rem per hour. On March 17, 2010,

radiation protection personnel appropriately barricaded and conspicuously posted the

access ladder to the upper refueling cavity.

Analysis. The failure to appropriately barricade and conspicuously post areas that are

accessible to personnel that could result in radiation doses greater than 1.0 rem in 1

hour was a performance deficiency. The finding is greater than minor because it is

associated with the program and process attribute of the Radiation Safety Cornerstone

and directly affected the associated cornerstone objective of ensuring the adequate

protection of the worker health and safety from exposure to radiation from radioactive

material during routine civilian nuclear reactor operation. Using Manual Chapter 0609,

Appendix C, Occupational Radiation Safety Significance Determination Process, this

finding is determined to have very low safety significance because it did not involve:

(1) an ALARA planning or work control issue, (2) an overexposure, (3) a substantial

potential for overexposure, or (4) an impaired ability to assess dose. The inspectors

determined that since the licensee had not recently re-evaluated the locked high

radiation area controls associated with this ladder; this finding did not represent current

plant performance, and therefore, did not have a crosscutting aspect associated with it.

Enforcement. Technical Specifications 5.8.3 states, in part, that individual high radiation

areas that are accessible to personnel that could result in radiation doses greater than

1.0 rem in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, and that are within large areas where no enclosure exists to enable

locking and where no enclosure can be reasonably constructed, the individual area shall

be barricaded and conspicuously posted. Contrary to the above, from February 2004

through March 17, 2010, the radiation personnel failed to appropriately barricade and

conspicuously post the access ladder to the upper refueling cavity when it was being

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Enclosure

used as the means to control access to an individual high radiation area in the lower

cavity where the maximum measured radiation dose rate was 2.8 rem per hour.

Because this violation is of very low safety significance and it was entered into the

licensees corrective action program as Nuclear Notifications NNs 200793188 and

200837345, this violation is being treated as a noncited violation consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000361/2010002-08, Failure to

Appropriately Control Access to a Locked High Radiation Area.

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedure

requirements, and technical specifications to ensure that the seven surveillance activities

listed below demonstrated that the systems, structures, and/or components tested were

capable of performing their intended safety functions. The inspectors also verified that

licensee personnel identified and implemented any needed corrective actions associated

with the surveillance testing.

January 22, 2010, Unit 2, high pressure and low pressure safety injection open

check valve inservice test results review

February 11, 2010, Unit 3, salt water cooling pump P113 comprehensive full flow

test

March 3, 2010, Unit 2, local leak rate test penetration 19

March 9, 2010, Unit 2, inservice valve test of pressurizer spray valve MU976

March 10, 2010, Unit 3, reactor power calibration surveillance

March 16, 2010, Unit 3, containment spray pump in-service and valve test

March 22, 2010, Unit 2, low pressure safety injection pump MP016

The inspectors witnessed test performance and/or reviewed test performance

documentation to verify that the significant surveillance test attributes were adequate to

address the following:

Prevention of preconditioning

Evaluation of testing impact on the plant

Clear acceptance criteria and procedure guidance

Adequacy of test equipment

Adequacy of documentation of test results and data

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Enclosure

Adequacy of jumper/lifted lead controls

Testing frequency and method demonstrated technical specification operability

Test equipment removal

Restoration of plant systems

Fulfillment of ASME Code requirements

Updating of performance indicator data

Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

Reference setting data

Annunciators and alarms setpoints.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of seven surveillance testing inspection samples

as defined in IP 71111.22-05.

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a.

Inspection Scope

The inspectors performed an in-office review of the San Onofre Nuclear Generating

Station Emergency Plan, Revision 28, submitted by the licensee December 17, 2009.

This revision updated letters of agreement with offsite authorities, updated the letter of

agreement with the Institute of Nuclear Power Operations, and updated the site policy

regarding the responsibilities of the shift manager.

This revision was compared to its previous revision, to the criteria of NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1, and to the standards in

10 CFR 50.47(b) to determine if the revision adequately implemented the requirements

of 10 CFR 50.54(q). This review was not documented in a safety evaluation report and

did not constitute approval of licensee-generated changes; therefore, this revision is

subject to future inspection.

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Enclosure

These activities constitute completion of one sample as defined in Inspection Procedure

71114.04-05.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1

Data Submission Issue

a.

Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the Fourth

Quarter 2009 performance indicators for any obvious inconsistencies prior to its public

release in accordance with Inspection Manual Chapter 0608, Performance Indicator

Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b.

Findings

No findings of significance were identified.

.2

Unplanned Scrams per 7000 Critical Hours (IE01)

a.

Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical

Hours performance indicator for Units 2 and 3 for the period from the first quarter 2009

through the fourth quarter 2009. To determine the accuracy of the performance indicator

data reported during those periods, performance indicator definitions and guidance

contained in NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, was used. The inspectors reviewed the licensees operator

narrative logs, issue reports, event reports and NRC Inspection reports for the period of

January 1, 2009, through December 31, 2009, to validate the accuracy of the submittals.

The inspectors also reviewed the licensees issue report database to determine if any

problems had been identified with the performance indicator data collected or

transmitted for this indicator and none were identified. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of two unplanned scrams per 7000 critical hours

samples as defined in Inspection Procedure 71151-05.

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Enclosure

b.

Findings

No findings of significance were identified.

.3

Unplanned Scrams with Complications (IE02)

a.

Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams with

Complications performance indicator for Units 2 and 3 for the period from the first

quarter 2009 through the fourth quarter 2009. To determine the accuracy of the

performance indicator data reported during those periods, performance indicator

definitions and guidance contained in NEI Document 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, was used. The inspectors reviewed the

licensees operator narrative logs, issue reports, event reports and NRC integrated

inspection reports for the period of January 1, 2009, through December 31, 2009, to

validate the accuracy of the submittals. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the

performance indicator data collected or transmitted for this indicator and none were

identified. Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of two unplanned scrams with complications

samples as defined in Inspection Procedure 71151-05.

b.

Findings

No findings of significance were identified.

.4

Unplanned Power Changes per 7000 Critical Hours (IE03)

a.

Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Transients per 7000

Critical Hours performance indicator Units 2 and 3 for the period from the first quarter

2009 through the fourth quarter 2009. To determine the accuracy of the performance

indicator data reported during those periods, performance indicator definitions and

guidance contained in NEI Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6, was used. The inspectors reviewed the licensees

operator narrative logs, issue reports, event reports and NRC integrated inspection

reports for the period of January 1, 2009, through December 31, 2009, to validate the

accuracy of the submittals. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the performance

indicator data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of two unplanned transients per 7000 critical hours

samples as defined in Inspection Procedure 71151-05.

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Enclosure

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical

Protection

.1

Routine Review of Identification and Resolution of Problems

a.

Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included: the complete and

accurate identification of the problem; the timely correction, commensurate with the

safety significance; the evaluation and disposition of performance issues, generic

implications, common causes, contributing factors, root causes, extent of condition

reviews, and previous occurrences reviews; and the classification, prioritization, focus,

and timeliness of corrective. Minor issues entered into the licensees corrective action

program because of the inspectors observations are included in the attached list of

documents reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b.

Findings

No findings of significance were identified.

.2

Daily Corrective Action Program Reviews

a.

Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

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Enclosure

b.

Findings

No findings of significance were identified.

.3

Selected Issue Follow-up Inspection

a.

Inspection Scope

During a review of items entered in the licensees corrective action program, the

inspectors recognized a corrective action item documenting the issues listed below. The

inspectors considered the following during the review of the licensees actions: (1)

complete and accurate identification of the problem in a timely manner; (2) evaluation

and disposition of operability/reportability issues; (3) consideration of extent of condition,

generic implications, common cause, and previous occurrences; (4) classification and

prioritization of the resolution of the problem; (5) identification of root and contributing

causes of the problem; (6) identification of corrective actions; and (7) completion of

corrective actions in a timely manner.

January 5, 2010, Unit 2, reportability review associated with the loss of spent fuel

pool cooling event that occurred on December 23, 2009

February 14, 2010, Unit 2, main transformer and unit auxiliary transformer

breaker trips following attempted start of reactor coolant pump motor M004 as

documented in Nuclear Notification NN 200794912

February 26, 2010, Unit 2, inadequate oversight of transmission and distribution

personnel who were performing work in the plant switchyard per Work Order 800195196

These activities constitute completion of three in-depth problem identification and

resolution samples as defined in IP 71152-05.

b.

Findings

1. Missed Eight Hour Report

Introduction. The inspectors identified a Severity Level IV noncited violation of

10 CFR 50.72, Immediate Notification Requirements for Operating Nuclear Power

Reactors, for the licensees failure to notify the NRC Operations Center within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

following discovery of an event meeting the reportability criteria as specified.

Description. On December 23, 2009, Unit 2 was in refueling outage U2C16 with; all fuel

off-loaded to the spent fuel pool, train A of saltwater cooling in service, train B was out of

service and drained for maintenance, spent fuel pool cooling was in service and

providing residual heat removal, and component cooling water was in service providing

cooling to spent fuel pool cooling. At approximately 10:00 a.m., operations personnel

received the saltwater cooling train A low flow and component cooling water heat

exchanger differential pressure high alarms. They noted flow rapidly lowering and heat

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Enclosure

exchanger differential pressure rising. Based on the observed plant conditions,

operations personnel entered abnormal operating instruction SO23-13-7, Loss of

Component Cooling Water/Saltwater Cooling, Revision 14. This procedure directed

operations personnel to secure both the saltwater cooling and the component cooling

water pumps, and line up for reverse flow of the saltwater cooling heat exchanger, based

on the observed indications. Due to this action, operations personnel entered Licensee

Controlled Specification 3.7.106, Spent Fuel Pool Operation, Condition B, and initiated

procedure SO23-3-2.11, Spent Fuel Pool Operations, Revision 26, Attachment 17, to

monitor spent fuel pool temperature due to the loss of spent fuel pool cooling.

Approximately one and one half hours later, reverse flow of the heat exchanger was

initiated and verified to be satisfactory and the abnormal operating instruction was

exited.

On January 5, 2010, the resident inspectors reviewed the licensees followup of this

event. During their review, the inspectors noted that the licensee had concluded the

event was caused by debris entering the system through a failed pump suction screen.

The licensee had also concluded that this event was not reportable to the NRC. This

decision had been made based on the licensees determination that the Technical

Specifications for component cooling water, 3.7.7, and salt water cooling, 3.7.8, were

only applicable in Modes 1-4, and when in Modes 5 and 6, the operability requirements

are determined by the systems they support, and Unit 2 was defueled and, therefore,

outside of all defined Modes. Therefore component cooling water and salt water

cooling were not required to be OPERABLE by any Technical Specification, and as such

not reportable.

The inspectors questioned the licensees reportability conclusion. The inspectors noted

that the applicability of Licensee Controlled Specification 3.7.106 was At all times with

irradiated fuel in the spent fuel pool, and as such, this specification was not mode

dependant. The inspectors also determined that this required the component cooling

water and salt water cooling systems be in operation as support systems for the spent

fuel pool cooling system to be operable. Furthermore, the inspectors noted that

procedure S023-5-1.8.1, Shutdown Nuclear Safety, Revision 23, classified the spent

fuel pool cooling system as providing the safety function fulfillment plan by providing

residual heat removal with the core off loaded to the spent fuel pool. As such, this event

prevented the fulfillment of the safety function of structures or systems that are needed

to remove residual heat when the salt water cooling and component cooling water

pumps were secured, and should have been reported to the NRC as such.

The inspectors informed the licensee of their concerns. The licensee initiated Nuclear

Notification NN 200733257 to address this concern. Subsequently, the licensee

determined that this event did represent an event that prevented the fulfillment of the

safety function of structures or systems that are needed to remove residual heat, and

submitted a late 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> report and Licensee Event Report 05000361/2009-004-00, Both

Trains of Spent Fuel Pool Cooling Inoperable Results in a Loss of Safety Function.

Analysis. The failure to make an applicable non-emergency 8-hour event notification

report within the required time frame was a performance deficiency. The finding is

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Enclosure

greater than minor because the NRC relies on licensees to identify and report conditions

or events meeting the criteria specified in regulations in order to perform its regulatory

function, and when this is not done the regulatory function is impacted. The inspectors

reviewed this issue in accordance with Inspection Manual Chapter 0612 and the NRC

Enforcement Manual. Through this review, the inspectors determined that traditional

enforcement was applicable to this issue because the NRC's regulatory ability was

affected. The inspectors determined that this finding was not suitable for evaluation

using the significance determination process, and as such, was evaluated in accordance

with the NRC Enforcement Policy. The finding was reviewed by NRC management and

because the violation was determined to be of very low safety significance, was not

repetitive or willful, and was entered into the corrective action program, this violation is

being treated as a Severity Level IV noncited violation consistent with the NRC

Enforcement Policy. This finding has a crosscutting aspect in the area of problem

identification and resolution associated with the corrective action program because the

licensee failed to thoroughly evaluate problems such that the resolutions addressed

causes and extent of conditions as necessary. This includes properly classifying,

prioritizing, and evaluating for operability and reportability conditions adverse to quality

P.1(c).

Enforcement. Title 10 CFR 50.72, Immediate Notification Requirements for Operating

Nuclear Power Reactors, requires, in part, that the licensee shall notify the NRC

Operations Center within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> after discovery of a nonemergency event described in

paragraph (b)(3)(v). Title 10 CFR 50.72(b)(3)(v)(B) requires, in part, any event or

condition that at the time of discovery could have prevented the fulfillment of the safety

function of structures or systems that are needed to remove residual heat shall be

reported within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> of discovery. Contrary to the above, on December 23, 2009, the

licensee failed to notify the NRC Operations Center within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> after the discovery of

an event or condition that resulted in a condition where the spent fuel pool cooling

system was prevented from fulfilling its safety function of residual heat removal with the

complete core off loaded. This finding was determined to be applicable to traditional

enforcement because the failure to report conditions or events meeting the criteria

specified in regulations affects the NRCs regulatory ability. The finding was evaluated in

accordance with the NRC's Enforcement Policy. The finding was reviewed by NRC

management and because the violation was of very low safety significance, was not

repetitive or willful, and was entered into the corrective action program as Nuclear

Notification NN 200733257, this violation is being treated as a Severity Level IV noncited

violation, consistent with the NRC Enforcement Policy: NCV 05000361/2010002-09,

Failure to Notify the NRC Within Eight Hours of a Non-Emergency Event.

2. Missed Licensee Event Report

Introduction. The inspectors identified a Severity Level IV noncited violation of

10 CFR 50.73, Licensee Event Report System, associated with the failure of nuclear

regulatory affairs personnel to submit a licensee event report within 60 days following

discovery of an event meeting the reportability criteria as specified.

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Enclosure

Description. During their review of a recent issue involving the loss of spent fuel pool

cooling, documented as NCV 05000361/2010002-09 in this report, the inspectors

became aware of another instance where spent fuel pool cooling had been lost.

Specifically, on February 13, 2007, Unit 2 was operating at 100 percent, with train A

spent fuel pool cooling pump 2P009 out of service for maintenance, and train B pump

2P010 in service providing cooling. At approximately 12:49 p.m., pump 2P010 tripped

on over current, which resulted in a complete loss of spent fuel pool cooling. Based on

this plant condition, operations personnel entered abnormal operating instruction SO23-

13-23, Loss of Spent Fuel Pool Cooling, Revision 10, and entered Licensee Controlled

Specification 3.7.106, Spent Fuel Pool Operation. Approximately 78 minutes later

operators restored pump 2P010 to service, which restored spent fuel pool cooling.

The licensee entered this issue into their corrective action program as Action Request

AR 070200583, and performed a reportability evaluation. Through this evaluation,

regulatory affairs personnel concluded this event was not reportable because the

conditions of Licensee Controlled Specification 3.7.106 were satisfied. Specifically,

spent fuel pool cooling had been lost for 78 minutes and specification 3.7.106 had a 6

hour action statement.

The inspectors questioned the licensees reportability conclusion. Specifically, the

inspectors noted that the Updated Final Safety Analysis Report, Section 3.1.6.2,

Criterion 61 - Fuel Storage and Handling and Radioactivity Control, identified that the

spent fuel pool cooling system provides cooling to remove residual heat from the spent

fuel pool, and Section 9.1.3, Spent Fuel Pool Cooling and Cleanup System, stated that

the system was designed to provide continuous cooling for the spent fuel pool. As such,

the inspectors determined that this event represented a condition that alone prevented

the fulfillment of the safety function of the spent fuel pool cooling system that was

needed to remove residual heat.

The inspectors informed the licensee of their concerns. The licensee initiated Nuclear

Notification NN 200740135 to address this concern. Subsequently, the licensee

determined that this event did represent a condition that alone prevented the fulfillment

of the safety function of the spent fuel pool cooling system that was needed to remove

residual heat, and submitted a Licensee Event Report 05000361/2007-007-00,

Inoperable SFP Cooling Pumps Results in Loss of Safety Function.

Analysis. The failure to submit a required licensee event report within 60 days following

an event requiring a report to the NRC was a performance deficiency. The finding is

greater than minor because the NRC relies on licensees to identify and report conditions

or events meeting the criteria specified in regulations in order to perform its regulatory

function, and when this is not done the regulatory function is impacted. The inspectors

reviewed this issue in accordance with Inspection Manual Chapter 0612 and the NRC

Enforcement Manual. Through this review, the inspectors determined that traditional

enforcement was applicable to this issue because the NRC's regulatory ability was

affected. The inspectors determined that this finding was not suitable for evaluation

using the significance determination process, and as such, was evaluated in accordance

with the NRC Enforcement Policy. The finding was reviewed by NRC management and

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Enclosure

because the violation was determined to be of very low safety significance, was not

repetitive or willful, and was entered into the corrective action program, this violation is

being treated as a Severity Level IV noncited violation consistent with the NRC

Enforcement Policy. Since the inadequate reportability determination had been made in

2007, and the licensees reportability program has undergone significant revision since

this time, the inspectors determined that this was not reflective of current licensee

performance and therefore did not have a crosscutting aspect associated with it.

Enforcement. Title 10 CFR 50.73, Licensee Event Report System, requires, in part,

that a licensee shall submit a licensee event report for any event of the type described in

paragraph (a)(1) within 60 days after the discovery of the event.

Title 10 CFR 50.73(a)(2)(v)(B) requires, in part, that licensees report any event or

condition that alone could have prevented the fulfillment of the safety function of

structures or systems that are needed to remove residual heat. Contrary to the above,

nuclear regulatory affairs personnel failed to submit a licensee event report within 60

days following discovery of a complete loss of spent fuel pool cooling event that

occurred on February 13, 2007. This finding was determined to be applicable to

traditional enforcement because the failure to report conditions or events meeting the

criteria specified in regulations affects the NRCs regulatory ability. The finding was

evaluated in accordance with the NRC's Enforcement Policy. The finding was reviewed

by NRC management and because the violation was of very low safety significance, was

not repetitive or willful, and was entered into the corrective action program as Nuclear

Notification NN 200740135, this violation is being treated as a Severity Level IV noncited

violation, consistent with the NRC Enforcement Policy: NCV 05000361/2010006-10,

Failure to Report a Safety System Functional Failure.

3. Technical Specification Bases Change

Introduction. The inspectors identified a Severity Level IV noncited violation of

10 CFR 50.59, Changes, Test, and Experiments, for the failure of licensing personnel

to obtain a technical specification license amendment for a change made to the technical

specification bases concerning the emergency chilled water system.

Description. While performing a review of an event on Unit 2 involving the loss of spent

fuel pool cooling, documented as NCV 05000361/2010002-09 in this report, the

inspectors noted a concern associated with Units 2 and 3 emergency chillers. The

inspectors noted that Units 2 and 3 share two emergency chillers, ME-335 and ME-336,

between the two units, and one chiller would normally be lined up to be operated from

the Unit 2 component cooling water system and one chiller would be lined up to be

operated from the Unit 3 component cooling water system. On December 23, 2009,

emergency chiller ME-336 was lined up to Unit 2 and emergency chiller ME-335 was

lined up to Unit 3, when Unit 2 experienced a clogging event of the only operable train of

salt water cooling system which resulted in a loss of component cooling water. The

inspectors questioned why operations personnel for Unit 3 failed to enter Technical

Specification 3.7.10, Emergency Chilled Water, in response to this event. Specifically,

the inspectors noted that the units technical specifications defined operability as:

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A system, subsystem, train, component or device shall be OPERABLE or have

OPERABILITY when it is capable of performing its specified function(s). Implicit

in this definition shall be the assumption that all necessary attendant

instrumentation, controls, normal and emergency electrical power sources,

cooling or seal water, lubrication or other auxiliary equipment that are required for

the system, subsystem, train, component or device to perform its function(s) are

also capable of performing their related support function(s).

As such, the inspectors determined that the loss of the only operable train of salt water

cooling which resulted in the loss of component cooling water represented the loss of

required support systems for the emergency chiller, which were required for the chiller to

be considered operable.

The inspectors informed operations personnel of their concern. Operations personnel

subsequently informed the inspectors that they had 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to transfer the emergency

chiller before it had to be considered inoperable, and referred the inspectors to the

bases of Technical Specification 3.7.10, which stated, in part:

An emergency chiller is considered OPERABLE when it is or can be aligned to

either Unit's operating or standby OPERABLE Component Cooling Water (CCW)

critical loop, provided that the OPERABLE CCW critical loop can be placed in

operation within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after a design basis event is detected in the Control

Room. Thus, an emergency chiller, under normal circumstances, remains

OPERABLE during a transfer operation between OPERABLE CCW critical loops

completed in less than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

The inspectors questioned whether this language constituted a change to the intent of

the technical specification. The licensee initiated Nuclear Notification NN 200747320 to

evaluate the inspectors concern.

The inspectors determined that the licensee had changed the bases for Technical

Specification 3.7.10 to add the 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> allowance in 1997 under bases change B96-001.

The inspectors reviewed this bases change package and determined that the

10 CFR 50.59 review that licensing personnel performed had not appropriately

evaluated this allowance. Furthermore, the inspectors determined that the only

documentation the licensee had to support the 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> allowance was a memorandum

from Engineering to Operations, V. Barone to T. Vogt, dated December 22, 1994,

Component Cooling Water System/Emergency Chilled Water System Interaction,

SONGS, Units 2 and 3, which the inspectors determined was not adequate to support

the bases change.

Following consultation with the NRC Technical Specification Branch regarding the intent

of Technical Specification 3.7.10, the inspectors determined that the intent of the

specification was that the emergency chiller could not be considered operable if a

required support system was inoperable. Consequently, the inspectors determined that

the licensees bases change had, in effect, changed the intent of Technical

Specification 3.7.10, and this had been done without a license amendment. As such,

the inspectors determined that on December 23, 2009, operations personnel failed to

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Enclosure

enter Limiting Condition of Operation 3.7.10 when a required support system for the

emergency chillers was inoperable, which rendered emergency chiller ME-336

inoperable.

The inspectors informed the licensee of their determination. The licensee initiated

Nuclear Notification NN 200758329 to address this issue. Subsequently, the licensee

determined that the bases change did constitute a change to the technical specifications.

Analysis. The failure to adequately implement the requirements of 10 CFR 50.59 for a

change made to the bases of Technical Specification 3.7.10, which changed the intent of

the specification, was a performance deficiency. The finding is greater than minor

because the failure to follow the requirements of 10 CFR 50.59 and receive prior NRC

approval for changes in licensed actions impacted the NRCs regulatory ability. The

inspectors reviewed this issue in accordance with Inspection Manual Chapter 0612 and

the NRC Enforcement Manual. Through this review, the inspectors determined that

traditional enforcement was applicable to this issue because the NRC's regulatory ability

was affected. The inspectors determined that this finding was not suitable for evaluation

using the significance determination process, and as such, was evaluated in accordance

with the NRC Enforcement Policy. The finding was reviewed by NRC management and

because the violation was determined to be of very low safety significance, was not

repetitive or willful, and was entered into the corrective action program, this violation is

being treated as a Severity Level IV noncited violation consistent with the NRC

Enforcement Policy. Since the bases change was made in 1996, the inspectors

determined that this was not reflective of current licensee performance and therefore did

not have a crosscutting aspect associated with it.

Enforcement. Title 10 CFR 50.59 (c)(1)(i) states, in part, that a licensee may make

changes in the facility as described in the final safety analysis report (as updated)

without obtaining a license amendment pursuant to 10 CFR 50.90 only if a change to the

technical specifications incorporated in the license is not required. Contrary to the

above, in 1997, licensing personnel implemented a technical specification bases change

for Limiting Condition for Operation 3.7.10, Emergency Chilled Water, which changed

the intent and application of the technical specification. Specifically, licensing personnel

added wording which allowed a period of time for required support systems to be

inoperable without declaring the emergency chillers inoperable. This finding was

determined to be applicable to traditional enforcement because the failure to follow the

requirements of 10 CFR 50.59 and receive prior NRC approval for changes in licensed

actions impacted the NRCs regulatory ability. The finding was evaluated in accordance

with the NRC's Enforcement Policy. The finding was reviewed by NRC management

and because the violation was of very low safety significance, was not repetitive or

willful, and was entered into the corrective action program as Nuclear Notifications NNs

200747320 and 200758329, this violation is being treated as a Severity Level IV

noncited violation, consistent with the NRC Enforcement Policy: NCV 05000361;05000362/2010002-11, Failure to Obtain a License Amendment for a Technical

Specification Bases Change.

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Enclosure

4. Threshold for Problem Identification

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure of

licensee personnel to follow procedures to enter conditions adverse to quality into the

corrective action program.

Description. The inspectors reviewed Nuclear Notification NN 200794912 which had

been initiated following operations personnel attempted start of reactor coolant pump

motor M004, following work being performed on its control panel under engineering

change package 800074306. The attempted start resulted in the main transformer

breakers and the unit auxiliary transformer breakers tripping. The inspectors noted that

the licensee had determined that maintenance personnel had encountered an issue with

the installation of new components causing interference with existing terminal boards in

the panels. This resulted in the maintenance personnel deviating from the approved

engineering change package 800074306 and relocating a terminal block within the

panel. The inspectors determined that this deviation was inappropriate because it

resulted in a change in the scope of the work, and as such, should have required a

revision to the engineering change package.

Subsequently, the inspectors attended the human performance error review board which

reviewed the sequence of events and relevant facts associated with this issue. During

this review, licensee personnel confirmed that maintenance personnel had deviated from

the engineering change package when relocating the terminal blocks. They also pointed

out that this had been done under verbal approval from station engineering in response

to Nuclear Notification NN 200247324, Task 31.

At the completion of the review board, the inspectors expressed concerns to the licensee

about how this work had been accomplished and the fact that a nuclear notification had

not been written to capture this issue in the corrective action program. The licensee

informed the inspectors that this work had been done using the modification problem

reporting process detailed in procedure SO123-XXIX-2.16, Modification Problem

Reports, Revision 7, and that another nuclear notification was not necessary since their

process had been followed.

The inspectors reviewed the modification problem reporting process and noted that for

systems that were out of service with modifications being performed, maintenance

personnel were directed to generate a principle notification, and then add tasks to this

nuclear notification as issues were encountered. The inspectors questioned this process

since it appeared to conflict with corrective action program procedure

SO123-XV-50.CAP-1, Writing Nuclear Notifications for Problem Identification and

Resolution, Revision 2. Specifically, Section 6.1.3 required that, All SONGS

employees and supplemental personnel are responsible for promptly identifying,

reporting and documenting problems by writing a nuclear notification.

During subsequent review, the inspectors determined that the modification problem

reporting process was being used for modification activities on safety-related equipment

as well. Specifically, Nuclear Notifications NN 200457233 and 200718733 had been

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Enclosure

initiated as principle notifications for issues discovered while performing modifications to

the turbine of the steam driven auxiliary feedwater pump and the train B emergency

diesel generator. As such, the inspectors determined that this represented a program

operating outside of the corrective action program. The licensee initiated Nuclear

Notification NN 200770377 to capture the inspectors concern. Subsequently, the

licensee determined that this program was being implemented in a manner inconsistent

with the corrective action program.

As the inspectors continued to monitor the licensees activities during the refueling

outage they became aware that contractor personnel were being allowed to implement

their own problem identification process, field change requests, instead of entering all

conditions adverse to quality into the licensees corrective action program as required.

The inspectors determined that this contractor process was being used for issues that

were identified with safety-related and non-safety-related plant equipment. The

inspectors questioned this program because it appeared to be another example of a

program operating outside of the corrective action program.

The inspectors informed the licensee of their concern. The licensee informed the

inspectors that they had opted to allow the contractor to use their process during the

refueling outage, and that licensee staff was reviewing all field change requests to

determine if they warranted generation of a nuclear notification. The licensee informed

the inspectors that this contractor process was being implemented in accordance with

procedure 25221-000-GPP-GCP-00018, Field Change Request/Notices, Revision 0.

When the inspectors asked about the procedure controlling the licensees staff reviews

of the field change requests they were informed that there was none.

The inspector reviewed procedure GPP-GCP-00018 and noted that its purpose was for

systems that were out of service with modifications being performed under engineering

change packages. It directed contractor personnel to initiate a field change request

when issues were identified, which would be reviewed by contractor personnel for

disposition using contractor procedures. The inspectors concluded that this was an

additional process that did not meet the requirements of procedure

SO123-XV-50.CAP-1, Section 6.1.3. The licensee initiated Nuclear Notification

NN 200827841 to document the inspectors concern. Subsequently, the licensee

determined that this program was being implemented in a manner inconsistent with the

corrective action program.

The inspectors concluded that these examples of licensee personnels failure to enter

conditions adverse to quality into the licensees corrective action program, individually

and collectively, did not impact the licensees overall ability to monitor the condition of

station equipment. However, multiple departments, which included supervisors, were

responsible for not entering conditions adverse to quality into the corrective action

program even when these issues clearly resulted in degraded and nonconforming

conditions. Therefore, these instances were indicative of a systemic programmatic issue

with proper implementation of the corrective action program, with respect to

communicating and reinforcing the requirements for nuclear notification initiation.

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Enclosure

Analysis. The failure to follow procedures for entering conditions adverse to quality into

the corrective action program was a performance deficiency. The finding is greater than

minor because it was similar to more than minor example 3.j in NRC Manual Chapter 0612, Appendix E, Examples of Minor Issues, in that programmatic deficiencies were

identified associated with this issue that would have the potential to lead to more

significant safety concerns if left uncorrected. Specifically, contractor and licensee

personnels failure to enter conditions adverse to quality into the station corrective action

program could result in the licensees failure to recognize that risk significant equipment

is in a degraded or nonconforming condition, and as such, may not be able to perform its

specified safety function. This finding is associated with the Mitigating Systems

Cornerstone. Using the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheets, the finding is determined to have very low safety significance

because the finding: (1) is not a design or qualification issue confirmed not to result in a

loss of operability or functionality; (2) did not represent an actual loss of safety function

of the system or train; (3) did not result in the loss of one or more trains of nontechnical

specification equipment; and (4) did not screen as potentially risk significant due to a

seismic, flooding, or severe weather initiating event. This finding has a crosscutting

aspect in the area of problem identification and resolution associated with the corrective

action program because the licensee failed to implement a corrective action program

with a low threshold for identifying issues. This also includes identifying such issues

completely, accurately, and in a timely manner commensurate with their safety

significance P.1(a).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Procedure SO123-XV-50.CAP-1, Writing Nuclear

Notifications for Problem Identification and Resolution, Revision 2, required, in part, All

SONGS employees and supplemental personnel are responsible for promptly

identifying, reporting and documenting problems by writing a Nuclear Notification.

Contrary to the above, between January 4 and March 14, 2010, the inspectors identified

multiple examples where licensee and contractor personnel failed to appropriately enter

identified conditions adverse to quality into the corrective action program, without being

prompted by the inspectors. Because this finding is of very low safety significance and

has been entered into the licensees corrective action program as Nuclear Notifications

NNs 200778816 and 200780926, this violation is being treated as a noncited violation,

consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000361;05000362/2010002-12, Failure to Enter Conditions Adverse to Quality into the

Corrective Action Program.

5. Oversight of Switchyard Work Activities

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure of

maintenance personnel to follow Work Order 800195196 and provide appropriate

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Enclosure

oversight to transmission and distribution personnel while performing work in the

electrical switchyard.

Description. In accordance with work order 800195196 and procedure SO123-XV-15.3,

Temporary System Alteration and Restoration, Revision 17, maintenance personnel

were required to provide transmission and distribution personnel with a calibrated torque

wrench, followed by oversight and concurrent verification, to complete steps associated

with torquing bolts on the reserve auxiliary transformer circuit breakers, since these bolts

were designated as critical components. Further, the work order also required

maintenance personnel to perform independent torque verifications on the bolted

connections of the reserve auxiliary transformer circuit breakers.

On February 22, 2010, maintenance personnel were preparing to implement Work Order 800195196 steps for performing the independent torque verification on the reserve

auxiliary transformer circuit breakers. During their preparation, maintenance personnel

determined that transmission and distribution personnel had not been provided with a

calibrated torque wrench, and there had not been oversight and concurrent verification

of the bolt torquing on the reserve auxiliary transformer circuit breakers as required by

the work order. Maintenance personnel subsequently generated Nuclear Notification

NN 200803364 to request engineering input for performing the torque verifications, and

to identify the possibility of rework.

The inspectors reviewed Nuclear Notification NN 200803364 and Work Order 800195196. During their review the inspectors questioned the wording of the nuclear

notification, in that it stated that the work order had not been followed, however, no

actions were identified to correct this condition. Also, the section of the work order that

directed the bolt torquing did not allow the independent verification to be performed

without the concurrent verification having already been performed.

The inspectors questioned licensee personnel as to the purpose of the nuclear

notification, and learned that it had been written to have engineering personnel provide

acceptable torque values since it was possible that the bolts had been torqued to values

that exceeded the values specified in the work order. During these discussions, the

inspectors determined that the licensee intended to continue to use this work order to

perform the independent verification. The inspectors determined that this was

inappropriate since the work order could no longer be performed as written, and as it

was intended.

The inspectors informed the licensee of their concerns, and the licensee entered this

issue into their corrective action program as Nuclear Notification NN 200811993.

Subsequently, the licensee determined that nine of the bolted connections had been

torqued to values that exceeded the values specified in the work order. The licensee

corrected the over torqued bolt condition.

Analysis. The failure to follow work order instructions and provide proper oversight and

concurrent verification to transmission and distribution personnel performing work in the

switchyard was a performance deficiency. The finding is greater than minor because

circumventing procedural requirements, if left uncorrected, would have the potential to

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Enclosure

lead to a more significant safety concern, in that, more risk significant equipment could

be rendered inoperable without the knowledge and approval of appropriate management

or control room personnel. This finding is associated with the Mitigating Systems

Cornerstone. Using the Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheets, the finding is determined to have a very low safety significance

because the finding: (1) is not a design or qualification issue confirmed not to result in a

loss of operability or functionality; (2) did not represent an actual loss of safety function

of the system or train; (3) did not result in the loss of one or more trains of nontechnical

specification equipment; and (4) did not screen as potentially risk significant due to a

seismic, flooding, or severe weather initiating event. This finding has a crosscutting

aspect in the area of human performance associated with work practices because

maintenance personnel failed to ensure supervisory and management oversight of work

activities, including contractors, such that nuclear safety was supported H.4(c).

Enforcement. Title 10 of the CFR, Part 50, Appendix B, Criterion V, Instructions,

Procedures, and Drawings, requires, in part, that activities affecting quality shall be

prescribed by documented instructions, procedures or drawings, of a type appropriate to

the circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Work Order 800195196, and procedure SO123-XV-15.3,

Temporary System Alteration and Restoration, Revision 17, provided instructions for

performing maintenance on critical components associated with the reserve auxiliary

transformers. Contrary to the above, on February 26, 2010, maintenance personnel

failed to follow work order 800195196, and procedure SO123-XV-15.3, to provide

appropriate oversight of transmission and distribution personnel who were performing

work in the plant switchyard, which resulted in the over torquing of nine bolts on the

reserve auxiliary transformer circuit breakers. Because this finding is of very low safety

significance and has been entered into the licensees corrective action program as

Nuclear Notifications NNs 200803364 and 200811993, this violation is being treated as a

noncited violation consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000361/2010002-13, Failure to Adequately Implement Station Work Order.

4OA3 Event Follow-up (71153)

.1

Event Follow Up

a.

Inspection Scope

The inspectors reviewed the below listed events for plant status and mitigating actions

to: (1) provide input in determining the appropriate agency response in accordance with

Management Directive 8.3, NRC Incident Investigation Program; (2) evaluate

performance of mitigating systems and licensee actions; and (3) confirm that the

licensee properly classified the event in accordance with emergency action level

procedures and made timely notifications to NRC and state/governments, as required.

January 27, 2010, Unit 2, component cooling water surge tank drain down

evolution

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Enclosure

March 17, 2010, Units 2 and 3, review extent of condition inspections for

identification of leaks in schedule 10 piping

Documents reviewed by the inspectors are listed in the attachment.

These activities constitute completion of two inspection samples as defined in Inspection

Procedure 71153-05.

b.

Findings

Introduction. A self-revealing Green noncited violation of Technical Specification 5.5.1.1

was identified for the failure of operations personnel to follow procedures for operating

the component cooling water system.

Description. Prior to the event, both component cooling water surge tank levels were

rising due to intersystem leakage. The problem with intersystem leakage was being

investigated and was eventually discovered to be from a cross tie valve which was not

adequately closed. On January 27, 2010, operations personnel planned to use

procedure SO23-2-17, Component Cooling Water System Operation, Revision 31, to

drain down the component cooling water surge tank. Prior to the drain down evolution,

operations personnel failed to perform an adequate pre-job brief or properly review of

the procedure regarding maintaining pressure since the surge tank draining had become

a routine evolution to compensate for the intersystem leakage. Furthermore, operations

personnel performing the evolution failed to use the proper human error prevention

techniques regarding the change in plant conditions and proceeded with the evolution

without asking for help. Due to time pressures and complacency, operations personnel

proceeded with the assumption that the nitrogen supply valves would maintain the

nitrogen pressure within the required limits during the drain down evolution.

Procedure SO23-2-17 required operations personnel to perform the following steps:

.1 THROTTLE OPEN S2(3)1203MU117, CCW Train A HX E001 CCW (Shell

Side) Drain Valve.

.2 While maintaining CCW surge tank pressure 33-40 psig, LOWER CCW

Surge Tank to the desired level, then CLOSE S2(3)1203MU117, CCW Train A

HX E001 CCW (Shell Side) Drain Valve.

An equipment operator commenced the drain down evolution and opened the

appropriate component cooling water heat exchanger shell drain valves and observed

levels dropped to 60 percent in the surge tanks. The plant was in a refueling outage and

changes to radiological control boundaries prevented the operator from having

immediate access to the surge tank pressure gauge, which was in the next room. The

equipment operator rationalized that the pressure regulator would properly function to

maintain the required pressure band, and decided to continue with the rest of his rounds

before checking pressure. About two hours later, the equipment operator observed

component cooling water train A surge tank pressure was at 30 psig, which was below

the minimum pressure for operability per procedure SO23-2-17. Control room personnel

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Enclosure

were notified and declared the component cooling water train A and associated

shutdown cooling loop inoperable. This required an unplanned entry into Technical

Specification 3.9.5.A, and immediate actions to restore the shutdown cooling loop.

Operations personnel raised the level in the component cooling water train A surge tank

to 65 percent, which increased the surge tank pressure to 34 psig, which was within the

acceptable range. Operations personnel also initiated an immediate investigation and

discovered the nitrogen pressure regulator was not maintaining the proper pressure in

component cooling water surge tank train A.

Analysis. The failure to follow procedures for operating plant equipment was a

performance deficiency. The finding is greater than minor because the continued failure

to follow procedures when operating safety-related plant equipment, if left uncorrected,

would have the potential to lead to a more significant safety concern. The finding is

associated with the Mitigating Systems Cornerstone. Using the Manual Chapter 0609,

Appendix G, Shutdown Operations Significance Determination Process, Phase 1

guidance, the finding is determined to have very low safety significance because the

finding did not result in an increase in the likelihood of a loss of reactor coolant system

inventory, degrade the ability to add reactor coolant system inventory, or degrade the

ability to recover decay heat removal. This finding has a crosscutting aspect in the area

of human performance associated with work practices because operations personnel

failed to use proper human error prevention techniques and proceeded in the face of

unexpected circumstances when operating the component cooling water system

H.4(a).

Enforcement. Technical Specification 5.5.1.1 requires, in part, that procedures be

established, implemented, and maintained covering the activities specified in Appendix

A, Typical Procedures for Pressurized Water Reactors and Boiling Water Reactors, of

Regulatory Guide 1.33, Quality Assurance Program Requirements (Operations), Dated

February 1978. Appendix A, Item 3.e, requires procedures for operating the component

cooling water system. Procedure SO23-2-17, Component Cooling Water System

Operation, Revision 31, provided instructions for operating the component cooling water

system. Contrary to the above, on January 27, 2010, operations personnel failed to

follow the requirements of procedure SO123-2-17, while performing a planned drain

down of the component cooling water surge tanks. Specifically, operations personnel,

while draining the component cooling water surge tank, failed to maintain the surge tank

pressure, in accordance with procedure SO23-2-17, such that, component cooling water

surge tank pressure was permitted to go low out of the expected operating range. As a

result of this low surge tank pressure, operators declared the component cooling water

and shutdown cooling train A systems inoperable. Because this finding is of very low

safety significance and has been entered into the licensees corrective action program

as Nuclear Notification NN 200771367, this violation is being treated as a noncited

violation consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000361/2010002-14, Failure to Follow Operations Procedure to Monitor Component

Cooling Water Surge Tank Pressure.

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Enclosure

4OA6 Meetings

Exit Meeting Summary

On January 6, 2010, the inspector conducted a telephonic exit meeting to present the results of

the in-office inspection of changes to the licensees emergency plan to Mr. B. Ashbrook,

Manager, Onsite Emergency Preparedness. The licensee acknowledged the issues presented.

On March 23, 2010, the inspectors presented the results of the resident inspections to Mr. R.

Ridenoure, Senior Vice President and Chief Nuclear Officer, and other members of the licensee

staff. The licensee acknowledged the issues presented.

The inspectors asked the licensee whether any materials examined during the inspections

should be considered proprietary or sensitive. The inspectors returned or destroyed all

proprietary information reviewed during the inspections and all identified sensitive information

has been returned to the appropriate licensee custodian.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as noncited violations.

.1

Title 10 CFR 50.65(a)(4), states in part, that before performing maintenance activities

(including but not limited to surveillance, post maintenance testing, and corrective and

preventive maintenance), the licensee shall assess and manage the increase in risk that

may result from the proposed maintenance activities. Contrary to the above, on

February 17, 2010, the licensee failed to adequately assess and manage the increase in

risk associated with maintenance activities in the electrical switchyard. Specifically, the

licensee determined that the station had failed to perform an adequate risk assessment

for proposed crane activities in the switchyard with regard to Unit 3, which was operating

at full power. Before allowing the activities to commence the licensee performed the

required risk assessment, and classified the work as a high risk activity in the switchyard

for Unit 3, and commenced the crane activity. This was licensee identified because the

failure to perform a risk assessment was identified by licensee personnel during an

additional final review prior to commencing work. Using Inspection Manual Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance

Determination Process flowchart 1, Assessment of Risk Deficit, the finding is

determined to be of very low safety significance because it only involved risk

management actions. The issue was entered into the licensee's corrective action

program as Nuclear Notification NN 200767351.

.2

Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

requires, in part, that activities affecting quality shall be prescribed by documented

instructions, procedures or drawings, of a type appropriate to the circumstances and

shall be accomplished in accordance with these instructions, procedures, or drawings.

Contrary to the above, on December 20, 2009, licensee personnel failed to follow

procedure SO123-XV-50.CAP-1, Writing Nuclear Notifications for Problem Identification

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Enclosure

and Resolution, Revision 2, and enter conditions adverse to quality into the corrective

action program. Specifically, when engineering inspections identified what appeared to

be indications on emergency core cooling system suction piping train A on Unit 3,

operations personnel were not informed, and an operability assessment was not

performed. Subsequently, on January 13, 2010, while performing inspections on the

Unit 3 emergency core cooling system suction piping, engineering personnel again

identified indications and informed operations personnel, which resulted in the piping

being declared inoperable until the ASME code case evaluations could be performed.

This was licensee identified because licensee personnel identified the failure to follow

procedures during follow up investigations. Using the Manual Chapter 0609,

Significance Determination Process, Phase 1 Worksheets, this finding is determined to

have a very low safety significance because the finding: (1) is not a design or

qualification issue confirmed not to result in a loss of operability or functionality; (2) did

not represent an actual loss of safety function of the system or train; (3) did not result in

the loss of one or more trains of non-technical specification equipment; and (4) did not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. The issue was entered into the licensee's corrective action program as

Nuclear Notification NN 200756139.

.3

Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part,

measures to be established to assure that applicable regulatory requirements and the

design basis, as defined in 10 CFR 50.2 and as specified in the license application, for

those components to which this appendix applies are correctly translated into

specifications, drawings, procedures, and instructions. Contrary to the above, on

February 3, 2010, the licensee failed to appropriately classify a section of emergency

core cooling system mini-flow piping as ASME code class II as specified in the Updated

Final Safety Analysis Report. This was licensee identified because licensee personnel

identified this issue during their reviews. Using the Manual Chapter 0609, Significance

Determination Process, Phase 1 Worksheets, this finding is determined to have a very

low safety significance because the finding: (1) is not a design or qualification issue

confirmed not to result in a loss of operability or functionality; (2) did not represent an

actual loss of safety function of the system or train; (3) did not result in the loss of one or

more trains of non-technical specification equipment; and (4) did not screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating event.

The issue was entered into the licensee's corrective action program as Nuclear

Notification NN 200778570.

ATTACHMENT: SUPPLEMENTAL INFORMATION

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Adler, Manager, Maintenance/Systems Engineering

B. Arbour, Operator Continuing Training Supervisor

J. Armas, Supervisor, Maintenance Engineering Fluid Process

B. Ashbrook, Manager, Emergency Preparedness

D. Axline, Technical Specialist, Nuclear Regulatory Affairs

D. Bauder, Plant Manager

B. Corbett, Manger, Performance Improvement

G. Cook, Manager, Compliance, Nuclear Regulatory Affairs

R. Elsasser, Manger, Training

J. Fee, Manager, Site Emergency Preparedness

S. Gardner, Electrical/System Engineering Manager

M. Graham, Manager, Plant Operations

A. Hochevar, Station Manager, Plant Operations

E. Hubley, Director, Maintenance/Construction

G. Johnson, Jr., Senior Nuclear Engineer, Maintenance/Systems Engineering

K. Johnson, Manager, Design Engineering

L. Kelly, Engineer, Nuclear Regulatory Affairs

D. Spires, Director, Work Control

J. Madigan, Manager, Health Physics

A. Meichler, Mechanical/System Engineering Supervisor

B. MacKissock, Director, Plant Operations

N. Quigley, Manager, Maintenance/System Engineering

R. Richter, Engineering Supervisor, Fire Protection

C. Ryan, Manager, Maintenance & Construction Services

R. St. Onge, Director Nuclear Regulatory Affairs

J. Todd, Manager, Security

D. Wilcockson, Manager of Operations Training

NRC Personnel

D. Loveless, Senior Reactor Analyst

M. Runyan, Senior Reactor Analyst

A-1

Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed 05000361/2010002-01

NCV

Failure to Implement Fire Protection Plan Requirements

Related to Hot Work Activities (Section 1R05)05000361/2010002-02

05000362/2010002-02

NCV

Failure to Appropriately Scope Auxiliary Feedwater Pump

Trench Eductors in the Maintenance Rule Monitoring Program

(Section 1R12)05000361/2010002-03

05000362/2010002-03

NCV

Failure to Enter Operating Experience into Corrective Action

Program for Timely Evaluation (Section 1R13)05000361/2010002-04

NCV

Failure to Assess and Manage Risk for Electrical Switchyard

Impacting Maintenance (Section 1R13)05000362/2010002-05

NCV

Failure to Follow Procedure Results in an Inadequate

Operability Determination (Section 1R15)05000361/2010002-06

NCV

Failure to Perform an Adequate Postmaintenance Test

(Section 1R19)05000361/2010002-07

NCV

Failure to Adequately Implement Foreign Material Exclusion

Controls (Section 1R20)05000361/2010002-08

NCV

Failure to Appropriately Control Access to a Locked High

Radiation Area (Section 1R20)05000361/2010002-09

NCV

Failure to Notify the NRC Within Eight Hours of a

Nonemergency Event (Section 4OA2)05000361/2010002-10

05000362/2010002-10

NCV

Failure to Report a Safety System Functional Failure (Section

4OA2)05000361/2010002-11

05000362/2010002-11

NCV

Failure to Obtain a License Amendment for a Technical

Specification Basis Change (Section 4OA2)

A-2

Attachment 05000361/2010002-12

05000362/2010002-12

NCV

Failure to Enter Conditions Adverse to Quality into the

Corrective Action Program (Section 4OA2)05000361/2010002-13

NCV

Failure to Adequately Implement Station Work Order (Section

4OA2)05000361/2010002-14

NCV

Failure to Follow Operations Procedure to Monitor

Component Cooling Water Surge Tank Pressure (Section

4OA3)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

PROCEDURES

NUMBER

TITLE

REVISION

SO23-13-8

Severe Weather

7

NUCLEAR NOTIFICATIONS

NUMBER

200498067

200755444

Section 1R04: Equipment Alignment

PROCEDURES

NUMBER

TITLE

REVISION

SO23-3-2.7.2

Safety Injection System Removal/Return to Service

Operation

22

SO2-V-3.12

Attachment 5; Containment Integrated Leakage Rate Test

8

SO23-2-4

Auxiliary Feedwater System Operation

27

A-3

Attachment

SO23-2-13.1

Diesel Generator Alignment

6

SO23-2-8.1

Saltwater cooling System Return to Service Evolution

9

NUCLEAR NOTIFICATIONS

NUMBER

200806892

MAINTENANCE ORDERS

NUMBER

800466402

DRAWINGS

NUMBER

TITLE

REVISION

40112 A and C

P&I Diagram Safety Injection System

23

MISCELLANEOUS

NUMBER

WCD 30005922

Section 1R05: Fire Protection

PROCEDURES

NUMBER

TITLE

REVISION

SO123-XV-1.41

Control of Ignition Sources

14

SO23-XV-4.13

Control of Work and Storage Areas Within the Protected

Area

5

SO123-XIII-

4.600

Fire Protection Impairment

10

A-4

Attachment

SO123-XV-1.41

Control of Ignition Sources

14

NUCLEAR NOTIFICATIONS

NUMBER

200729747

200746059

DRAWINGS

NUMBER

TITLE

REVISION

2-006

SONGS pre-fire plans

6

Section 1R06: Flood Protection Measures

NUCLEAR NOTIFICATIONS

NUMBER

200758566

200409164

200765185

200001761

200760572

200318922

200758652

CALCULATIONS

NUMBER

TITLE

REVISION

M-0120-015

Plant Flood Analysis Review

8

N-4090-009

Units 2&3 Auxiliary Feedwater Pump Room and Doghouse

Pressure Temperature Analysis

0

Section 1R11: Licensed Operator Requalification Program

PROCEDURES

NUMBER

TITLE

REVISION

SO23-15-56

Alarm Response Instruction 56A

8

A-5

Attachment

SO23-13-18

Reactor Protection System Failure

30

SO23-12.1

Standard Post Trip Actions

22

SO23-12-10

Safety Function Status Checks

4

SO123-VIII-10

Emergency Coordinator Duties

26

SO123-VIII-1

Loss of RCS Inventory

29

Section 1R12: Maintenance Effectiveness

PROCEDURES

NUMBER

TITLE

REVISION

SO123-XV-5.3

Maintenance Rule Program

11

NUCLEAR NOTIFICATIONS

NUMBER

200815548

200409164

200760572

200765185

200318922

200758652

200758566

200001761

200819522

200804181

200815848

MAINTENANCE ORDERS

NUMBER

800078277

MISCELLANEOUS

NUMBER

TITLE

REVISION /

DATE

SONGS System Health Report AFWS 4th Quarter-2009

DBD-SO23-780

Auxiliary Feedwater System

9

A-6

Attachment

STS-SO123-

2001

Maintenance Rule Scoping Matrix

February

23, 2000

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

PROCEDURES

NUMBER

TITLE

REVISION

SO23-XX-8

Integrated Risk Management

3

SO123-I-1.37

Diver Safety During Intake and Forebay Structure Diving

Operations

4

SO23-XX-8

Integrated Risk Management

4

SO23-5-1.8.1

Shutdown Nuclear Safety

23

SO23-12-11

EOI Supporting Attachments

7

SO23-12-8

Station Blackout

21

NUCLEAR NOTIFICATIONS

NUMBER

200155657

200741690

200755444

200789579

200787617

200810952

200818599

200819462

200797351

200402733

200805635

200801929

MAINTENANCE ORDERS

NUMBER

800436397

800074316

A-7

Attachment

CALCULATIONS

NUMBER

TITLE

REVISION

PRACP-10-

0001

PRA Change Package

0

E4C-088

Emergency Diesel Generator Loading

2

E4C-017

125V Battery & DC System Sizing

20

MISCELLANEOUS

NUMBER

TITLE

REVISION /

DATE

NRC

Administrative

Letter 89-10

Dispositioning of Technical Specifications that are

Insufficient to assure Plant Safety

December

28,1998

IPE-HC-075

Operator Action Summary Data Sheet Post-Initiator Human

Error Probability Calculation Worksheet

August 28,

2006

DCP-2&3-

7048.00SE

10 CFR 50.54(x) Unit to Unit Diesel Generator Crosstie

0

Section 1R15: Operability Evaluations

PROCEDURES

NUMBER

TITLE

REVISION

SO23-3-3.31.3

Component Cooling Water Valve Testing - Offline

15

SO123-XV-52

Functionality Assessments and Operability Determinations

14

NUCLEAR NOTIFICATIONS

NUMBER

200791845

200792682

200769743

200745284

200744216

A-8

Attachment

200714391

200744216

200743712

200760570

MAINTENANCE ORDERS

NUMBER

800451952

CALCULATIONS

NUMBER

M-DSC-443

M-DSC-441

MISCELLANEOUS

NUMBER

TITLE

DATE

AR 000201278

Operability Assessment

February

25, 2000

Section 1R19: Postmaintenance Testing

PROCEDURES

NUMBER

TITLE

REVISION

SO123-XX-5

Work Clearance Application/Work Clearance

Document/Work Authorization Record

28

SO123-II-9.174

Resistance Temperature Detector or thermistor functional

Verification

1

SO2-XXVI-

9.8001.62890.1

Unit 2 boration dilution control system preoperational test

2

SO123-XXVI-

2.5

Preparation, Revision and Approval of Preoperational,

Acceptance and Special Test Procedures

4

SO23-II-20

Ovation Distributed Control System (DCS)

2

A-9

Attachment

NUCLEAR NOTIFICATIONS

NUMBER

NMO800449052

200766430

NMO 800356395

800250944

20683701

200681431

200651946

200651922

200806892

DRAWINGS

NUMBER

TITLE

REVISION

35149

Area 2C6 conduit and tray 30-45 foot elevation

25

MAINTENANCE ORDERS

NUMBER

ECP 800162890

ECP 800390458

MISCELLANEOUS

NUMBER

TITLE

REVISION /

DATE

M37629

Environment qualification Data Sheets

0

N14856B4

Data Sheet 2TE0921X2

January 28,

2009

Section 1R20: Refueling and Other Outage Activities

PROCEDURES

NUMBER

TITLE

REVISION

SO23-XV-2

Troubleshooting Plant Equipment and Systems

5

NUCLEAR NOTIFICATIONS

NUMBER

NMO800448825

200765286

200766808

200796087

200769743

A-10

Attachment

200709732

200765286

200800403

200791630

MISCELLANEOUS

NUMBER

TITLE

REVISION /

DATE

07050054-01

Fire Protection Impairment Form

May 17,

2007

Bechtel QA

Policy No. Q-12

Codes, Standards, and Regulatory Requirements

3

Sample Id

129939

Release of Liquid, Sludge, Slurry, or Sand

February

23, 2010

Section 1R22: Surveillance Testing

PROCEDURES

NUMBER

TITLE

REVISION

SO23-3-3.31.9

RCS Pressure Isolation Valve Testing Hydro Pump Method-

offline

13

SO23-3-3.31.2

ECCS Valve Testing - Offline

11

SO23-XVII-

8.1.1

Visual Inspection of High Pressure Safety Injection System

5

SO23-3-3.60.4

Saltwater Cooling Pump and Valve Testing

11

SO23-3-3.2

Excore Nuclear Instrumentation Calibration

15

SO23-3-3.25

Once a Shift Surveillance Modes 1-4

31

SO23-3-3.30

Inservice Valve Testing Program

20

SO23-5-1.5

Plant Shutdown for Hot Standby to Cold Shut Down

31

A-11

Attachment

SO23-2-13

Diesel Generator Operation

43

SO23-3-3.60.2

LPSI Surveillance Operating Instruction

9

SO23-3-3.60.7

Containment Spray Pump and Valve Testing

12

NUCLEAR NOTIFICATIONS

NUMBER

200791243

200794544

200823123

200827929

200581670

200829333

200835386

200835812

DRAWINGS

NUMBER

TITLE

REVISION

SO23-507-2-1-

623-X2

8 inch Type 9211 Valve Assembly

1

MISCELLANEOUS

NUMBER

TITLE

DATE

Fisher Anomaly

Notice

FAN 88-2

October 11,

1988

S21204MP016

CPT

Inservice Pump Test Record

March 21,

2010

Section 4OA3: Event Follow-Up

PROCEDURES

NUMBER

TITLE

REVISION

SY-SO023-G-2

Systems Engineering guideline

3

A-12

Attachment

DRAWINGS

NUMBER

TITLE

REVISION

S2-1204-ML-

001

From Refueling Water Tank T-005 to Line 108 @ VA. 001

10

S2-1204-ML-

002

From Control Valve 2HV-9301 to Line 109

9

S2-1204-ML-

003

Containment Spray Pump P-013 Suction from Containment

Emergency Sump

20

S2-1204-ML-

004

Containment Spray Pump P-013 Suction from Containment

Emergency Sump

20

S2-1204-ML-

008

From Line 004 Containment Emergency Sump to High

Pressure Safety injection Pump P-019

20

S2-1204-ML-

032

From Line 003 Refuel water tank T-006 to Low Pressure

Safety injection Pump P-015

24

S2-1204-ML-

080

From Line 079 Valve 046 to Refueling Water Tank T-005

8

S2-1204-ML-

151

From 2HV-9306 on Line 052 to Line 080 to Refuel Tank T-

006

2

S2-1219-ML-

068

From Refuel water tank T-005 to Refueling Water Tank T-

006

1

S2-1219-ML-

072

From Refuel water tank T-006 to Drain

0

S2-1219-ML-

073

From Refuel water tank T-005 to Drain

0

S2-1219-ML-

107

From Line 080 Safety Injection to Refuel water tank T-005

8

S2-1204-ML-

033

From Line 031 Refuel Water Tank T006 Sys 1204 to LP

Safety Injection Pump

20

S2-1204-ML-

007

HPSI Pump P-017 Suction from Refueling Tank T-005

15

A-13

Attachment

A-14

Attachment

S2-1204-ML-

009

HPSI Pump P-018 Suction from Refueling Tank T-005

16