ML100330574
ML100330574 | |
Person / Time | |
---|---|
Site: | Wolf Creek |
Issue date: | 02/02/2010 |
From: | Chamberlain D NRC/RGN-IV/DRP |
To: | Matthew Sunseri Wolf Creek |
References | |
IR-09-007 | |
Download: ML100330574 (55) | |
See also: IR 05000482/2009007
Text
UNITED STATES
NUCLEAR RE GULATO RY COM M I SSI ON
R EGI ON I V
612 EAST LAMAR BLVD, SUI TE 400
ARLIN GTON, TEXAS 76011-4125
February 2, 2010
Matthew W. Sunseri, President and
Chief Executive Officer
Wolf Creek Nuclear Operating Corporation
P. O. Box 411
Burlington, KS 66839
Subject: WOLF CREEK GENERATING STATION - NRC SPECIAL INSPECTION
REPORT 05000482/2009007
Dear Mr. Sunseri:
On December 4, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a special
inspection at your Wolf Creek Generating Station. This inspection examined activities
associated with the stations performance during a loss of offsite power on August 19, 2009.
The NRCs initial evaluation of this issue, using the criteria in NRC Management Directive 8.3,
NRC Incident Investigation Program, determined that the estimated Incremental Conditional
Core Damage Probability was 6.1 x 10-6. This guided the NRC to charter and conduct a special
inspection.
The enclosed report documents the inspection results, which were discussed at the exit meeting
on December 22, 2009, with you and other members of your staff. The inspection examined
activities conducted under your license as they relate to safety and compliance with the
Commissions rules and regulations and with the conditions of your license. The inspection
team reviewed selected procedures and records, observed activities, and interviewed
personnel.
This report documents seven NRC-identified and self-revealing findings of very low safety
significance (Green). Six of these findings were determined to involve violations of NRC
requirements. Additionally, one licensee-identified violation, which was determined to be of very
low safety significance, is listed in this report. However, because of their very low safety
significance and because they are entered into your corrective action program, the NRC is
treating these findings as noncited violations, consistent with Section VI.A.1 of the NRC
Enforcement Policy. If you contest the noncited violations in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your denial, to
the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, D.C. 20555-0001, with copies to the Regional Administrator, U.S. Nuclear
Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington,
Texas, 76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,
Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Wolf Creek Generating
Station. In addition, if you disagree with the characterization of any finding in this report, you
should provide a response within 30 days of the date of this inspection report, with the basis for
your disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector
Wolf Creek Nuclear Operating Corp. -2-
at the Wolf Creek Generating Station. The information you provide will be considered in
accordance with Inspection Manual Chapter 0305.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its
enclosure, will be available electronically for public inspection in the NRC Public Document
Room or from the Publicly Available Records component of NRCs document system (ADAMS).
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the
Public Electronic Reading Room).
Sincerely,
/RA/ A. Vegel for
Dwight D. Chamberlain, Director
Division of Reactor Projects
Docket: 50-482
Licenses: NPF-42
Enclosure: NRC Inspection Report 05000482/2009007
w/Attachments: Supplemental Information
Charter
NRC Technical Review of the August 19, 2009, Self-Revealing Flaw in
Essential Service Water System Piping
cc w/Enclosure:
Vice President Operations/Plant Manager
Wolf Creek Nuclear Operating Corporation
P.O. Box 411
Burlington, KS 66839
Jay Silberg, Esq.
Pillsbury Winthrop Shaw Pittman LLP
2300 N Street, NW
Washington, DC 20037
Supervisor Licensing
Wolf Creek Nuclear Operating Corporation
P.O. Box 411
Burlington, KS 66839
Chief Engineer
Utilities Division
Kansas Corporation Commission
1500 SW Arrowhead Road
Topeka, KS 66604-4027
Office of the Governor
State of Kansas
Topeka, KS 66612-1590
Wolf Creek Nuclear Operating Corp. -3-
Attorney General
120 S.W. 10th Avenue, 2nd Floor
Topeka, KS 66612-1597
County Clerk
Coffey County Courthouse
110 South 6th Street
Burlington, KS 66839
Chief, Radiation and Asbestos
Control Section
Bureau of Air and Radiation
Kansas Department of Health and
Environment
1000 SW Jackson, Suite 310
Topeka, KS 66612-1366
Chief, Technological Hazards
Branch
FEMA, Region VII
9221 Ward Parkway
Suite 300
Kansas City, MO 64114-3372
Wolf Creek Nuclear Operating Corp. -4-
Electronic distribution by RIV:
Regional Administrator (Elmo.Collins@nrc.gov)
Deputy Regional Administrator (Chuck.Casto@nrc.gov)
DRP Director (Dwight.Chamberlain@nrc.gov)
DRP Deputy Director (Anton.Vegel@nrc.gov)
DRS Director (Roy.Caniano@nrc.gov)
DRS Deputy Director (Troy.Pruett@nrc.gov)
Senior Resident Inspector (Chris.Long@nrc.gov)
Resident Inspector (Charles.Peabody@nrc.gov)
Site Secretary (Shirley.Allen@nrc.gov)
Branch Chief, DRP/B (Geoffrey.Miller@nrc.gov)
Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)
Senior Public Affairs Officer (Victor.Dricks@nrc.gov)
Public Affairs Officer (Lara.Uselding@nrc.gov)
Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
Regional Counsel (Karla.Fuller@nrc.gov)
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
OEMail Resource
ROPreports
DRS/TSB STA (Dale.Powers@nrc.gov)
OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)
File located: R:\_REACTORS\_WC\2009\WC 2009007RWD.doc ML#100330574
ADAMS: No : Yes SUNSI Review Complete Reviewer Initials: RWD
- Publicly Available : Non-Sensitive
Category A. Non-Publicly Available Sensitive
KEYWORD:
C:DRP/B SPE:DRP/B SRI:DRP/B RI:DRP:/B
GMiller RDeese DDumbacher GTutak
/RA/ /RA/ /RA/ via e-mail /RA/ via e-mail
1/31/10 1/28/10 1/26/10 1/26/10
SME/HQ RI:DRP/B
JMedoff CLong
/RA/ via e-mail /RA/
1/19/10 1/26/10
OFFICIAL RECORD COPY T= Telephone E= E-mail F = Fax
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket: 50-482
License: NPF-42
Report: 05000482/2009007
Licensee: Wolf Creek Nuclear Operating Corporation
Facility: Wolf Creek Generating Station
Location: 1550 Oxen Lane SE
Burlington, Kansas
Dates: September 21 through December 4, 2009
Inspectors: R. Deese, Senior Project Engineer
D. Dumbacher, Senior Resident Inspector, Callaway Plant
G. Tutak, Reactor Inspector
J. Medoff, Senior Mechanical Engineer
M. Runyan, Senior Reactor Analyst
C. Long, Senior Resident Inspector, Wolf Creek Generating Station
C. Peabody, Resident Inspector, Wolf Creek Generating Station
Approved By: G. Miller, Chief, Project Branch B, Division of Reactor Projects
1 Enclosure
SUMMARY OF FINDINGS
IR 05000482/2009007; 09/21/09 through 12/4/09; Wolf Creek Generating Station, Special
Inspection in response to the loss of offsite power and essential service water leak on
August 19, 2009.
This report covered a 5-day period (September 21-25, 2009) of onsite inspection, with in office
review through December 4, 2009. This special inspection was conducted by a senior project
engineer, a senior resident inspector, a reactor inspector, a headquarters specialist, and a
senior reactor analyst assisted by a senior resident inspector and a resident inspector. Six
Green noncited violations and one Green finding of significance were identified. The
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using
NRC Inspection Manual Chapter 0609, "Significance Determination Process." Findings for
which the significance determination process does not apply may be Green or be assigned a
severity level after NRC management review. The NRC's program for overseeing the safe
operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor
Oversight Process," Revision 4, dated December 2006.
A. NRC-Identified Findings and Self-Revealing Findings
Cornerstone: Initiating Events
- Green. The team identified a finding associated with the licensees failure to
recognize the adverse conditions related to their offsite power system as
prescribed by Procedure AP 28A-100, Condition Reports. Specifically, the
licensee failed to enter pertinent switchyard operating experience and six
occurrences of offsite power line losses as adverse conditions in their corrective
action program as of August 2009. The licensee entered these deficiencies in
their corrective action program as Wolf Creek Condition Reports 00022242
and 00022241.
This finding is greater than minor because, if left uncorrected, the failure to fully
utilize the corrective action program could become a more significant safety
concern. The inspectors determined that this finding impacted the Initiating
Events Cornerstone equipment maintenance attribute and affected the
cornerstone objective to limit the likelihood of those events that upset plant
stability and challenge critical safety functions during shutdown as well as power
operations. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and
Characterization of Findings, the issue screened as having very low safety
significance because it did not contribute to both the likelihood of a reactor trip
and the likelihood that mitigation equipment or functions would not be available
(Section 1R2).
- Green. The team reviewed a self-revealing noncited violation of Technical
Specification 5.4.1.a, Procedures, after operators failure to monitor and
maintain steam generator water levels resulted in an unanticipated turbine trip
signal and feedwater isolation. On August 21, 2009, while in Mode 3, Wolf Creek
operators, using an intermittent method of feeding steam generators over shift
turnover, lost control of the level in steam generator A. This resulted in increased
levels above the P-14 feedwater isolation actuation setpoint. Contributing to the
loss of level control was the disabling of a previously established operator
2 Enclosure
selectable alarm for the steam generator level. The licensee entered this
deficiency in their corrective action program as Wolf Creek Condition
Report 00019295.
This finding is greater than minor because it impacted the Initiating Events
Cornerstone human performance attribute and affected the cornerstone objective
to limit the likelihood of those events that upset plant stability and challenge
critical safety functions during shutdown as well as power operations. Using
Manual Chapter 0609.04, Phase 1 - Initial Screening and Characterization of
Findings, the issue screened as having very low safety significance because it
did not contribute to both the likelihood of a reactor trip and the likelihood that
mitigation equipment or functions would not be available and it did not increase
the likelihood of a fire or internal/external flooding. This finding has a
crosscutting aspect in the area of human performance associated with the
decision making component because licensee personnel failed to make safety-
significant or risk-significant decisions using a systematic process especially
when faced with uncertain or unexpected plant conditions to ensure that safety is
maintained H.1(a) (Section 1R7).
Cornerstone: Mitigating Systems
- Green. The team identified a noncited violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, regarding the licensees
failure to follow the requirements of Procedure AP 26C-004, Technical
Specification Operability. Specifically, licensee personnel failed to perform an
operability evaluation for the impact of the 2009 pressure transient and internal
corrosion on the essential service water system. The Wolf Creek essential
service water system was degraded by a system pressure transient on August
19, 2009. Also in 2009, widespread internal corrosion resulted in at least three
through wall leaks. Discovery of these conditions had been documented in the
corrective action program but had not resulted in performance of an operability
evaluation of the current and potentially future impact on the system as a whole.
The licensee entered this deficiency in their corrective action program as Wolf
Creek Condition Report 00022240.
This finding is greater than minor because it is associated with the Mitigating
Systems Cornerstone attribute of equipment performance and adversely affected
the objective to ensure equipment availability and reliability. Using Manual
Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,
the issue screened as having very low safety significance because it was not a
design or qualification deficiency that resulted in a loss of operability or
functionality, did not create a loss of system safety function of a single train for
greater than the technical specification allowed outage times, and did not affect
seismic, flooding, or severe weather initiating events. This finding has a
crosscutting aspect in the area of problem identification and resolution
associated with the corrective action program because licensee personnel failed
to thoroughly evaluate problems such that the resolutions address causes and
extent of conditions P.1(c) (Section 1R2).
- Green. The team identified a noncited violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, regarding the licensees
3 Enclosure
failure to follow the requirements of Procedure AI 28A-010, Screening Condition
Reports. Specifically, licensee personnel failed to properly screen condition
reports for the essential service water system adverse conditions of internal
corrosion and loss of offsite power induced system pressure transient since
April 2008. The adverse conditions met the procedures definitions to require a
root cause analysis prior to September 2009, but none was performed. The
licensee entered this deficiency in their corrective action program as Wolf Creek
Condition Report 00022239.
This finding is greater than minor because, if left uncorrected, the failure to fully
utilize the corrective action program could become a more significant safety
concern. The inspectors determined that this finding impacted the Mitigating
Systems Cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial
Screening and Characterization of Findings, the issue screened as having very
low safety significance because it was not a design or qualification deficiency that
resulted in a loss of operability or functionality, did not create a loss of system
safety function of a single train for greater than the technical specification allowed
outage times, and did not affect seismic, flooding, or severe weather initiating
events. This finding has a crosscutting aspect in the area of problem
identification and resolution associated with the corrective action program
because licensee personnel failed to thoroughly evaluate problems such that the
resolutions address causes and extent of conditions P.1(c) (Section 1R2).
- Green. The team identified a noncited violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, regarding the licensees
failure to provide adequate guidance to identify and address pitting, corrosion,
and surface indications in the essential service water system. A 2007 licensee
self-assessment on lake water corrosion issues recommended improvements in
lake water chemistry control procedures to establish a pit monitoring program. In
September 2009 NRC inspectors noted that the lake water monitoring and
chemistry control procedures did not contain quality standards or acceptance
criteria for newly discovered flaws or abnormal gross degradation due to erosion,
pitting, or corrosion. This resulted in delaying repairs until such degradations
(pitting) had become through-wall leaks. Several instances of internally identified
corrosion were not entered into the corrective action program until essential
service water piping had thinned to below the minimum ASME code allowed wall
thickness. The licensee entered this deficiency in their corrective action program
as Wolf Creek Condition Report 00022243.
This finding is greater than minor because it is associated with the Mitigating
Systems Cornerstone attribute of procedure quality and adversely affected the
objective to ensure equipment availability and reliability. Using Manual
Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,
the issue screened as having very low safety significance because it was not a
design or qualification deficiency that resulted in a loss of operability or
functionality, did not create a loss of system safety function of a single train for
greater than the technical specification allowed outage times, and did not affect
seismic, flooding, or severe weather initiating events. This finding has a
crosscutting aspect in the area of problem identification and resolution
associated with the corrective action program because licensee personnel failed
4 Enclosure
to take appropriate corrective actions to address safety issues and adverse
trends in a timely manner P.1(d) (Section 1R4).
- Green. The team identified a noncited violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, regarding the licensees
failure to provide adequate guidance to address the impact of a loss of offsite
power event on the essential service water system. On August 19, 2009, seven
hours following a loss of offsite power, the NRC senior resident identified leakage
from the piping on the 1988 elevation of the auxiliary building. Wolf Creek
Procedure STN PE-040G, Transient Event Walkdown, required that systems
subject to expected transient dynamic forces following a reactor trip to have a
post-trip walkdown to identify any structural damage. This procedure did not
include the essential service water system as a vulnerable system. The
procedure only specifically identified portions of systems inside containment. As
a result, no walkdown was performed for the essential service water system on
August 19, 2009. The licensee entered this deficiency in their corrective action
program as Wolf Creek Condition Report 00022265.
This finding is greater than minor because it is associated with the Mitigating
Systems Cornerstone attribute of procedure quality and adversely affected the
objective to ensure equipment availability and reliability. Using Manual
Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings,
the issue screened as having very low safety significance because it was not a
design or qualification deficiency that resulted in a loss of operability or
functionality, did not create a loss of system safety function of a single train for
greater than the technical specification allowed outage times, and did not affect
seismic, flooding, or severe weather initiating events. This finding has a
crosscutting aspect in the area of problem identification and resolution
associated with the operating experience component because the licensee failed
to institutionalize lessons learned through changes to station walkdown
procedures P.2(b) (Section 1R5).
- Green. The team identified a noncited violation of License Condition 2.C.(5),
Fire Protection, for the failure to establish a compensatory fire watch in a timely
manner per the station fire protection program. On August 19, 2009, a complete
loss of offsite power resulted in fire protection trouble alarms on fire protection
panel KC-008. The control room supervisor acknowledged the alarms.
Procedure ALR KC-888, Fire Protection Panel KC-008 Alarm Response,
required an impairment and compensatory measures for the affected smoke
detectors. The following day, NRC inspectors noted that impairments and fire
watches for the 13 affected fire zones on KC-008 had not been initiated. The
licensee entered this deficiency in their corrective action program as Wolf Creek
Condition Report 00019320.
This finding was more than minor since it was associated with the protection
against external factors attribute of the Mitigating Systems Cornerstone and
adversely affected the cornerstone objective to ensure the availability, reliability,
and capability of systems that respond to initiating events to prevent undesirable
consequences. Using Manual Chapter 0609, Appendix F, Fire Protection
Significance Determination Process, the inspectors determined that the finding
had an adverse affect on the fixed fire protection systems element of fixed fire
5 Enclosure
detection systems. This finding was determined by a senior reactor analyst to be
of very low safety significance because of a low exposure time of the
uncompensated deficiency. This finding has a crosscutting aspect in the area of
human performance associated with the work practices component because the
licensee failed to ensure supervisory oversight of work activities such that
nuclear safety is supported H.4(c) (Section 1R5).
B. Licensee-Identified Violations
One violation of very low safety significance, which was identified by the licensee, was
reviewed by the inspectors. Corrective actions taken or planned by the licensee have
been entered into the licensees corrective action program. This violation and its
condition report number are listed in Section 4OA7.
6 Enclosure
REPORT DETAILS
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency
Preparedness
1R0 Introduction
On August 19, 2009, the NRC determined that a special inspection was warranted, in
part, based on the potential safety significance of a complete loss of offsite power and
because of potential generic issues associated with essential service water design and
internal corrosion.
The inspection charter required the team to: (1) review the circumstances related to the
discovery of the degraded conditions, (2) assess the licensees determination of cause
and effectiveness of actions taken to resolve and prevent recurrence of these problems,
and (3) assess the effectiveness of licensee programs to maintain the physical condition
of the offsite power systems and the essential service water system. The team
evaluated the licensee actions to address these issues including extent of condition,
extent of cause, and common cause questions. Specific focus was on licensee
response to prior instances of loss of the offsite power lines and assessment of
implementation of general design criteria requirements for independence of the offsite
power lines. The inspectors reviewed the licensees Generic Letter 89-13, Service
Water System Problems Affecting Safety-Related Equipment, program to ensure
appropriate testing was being performed that would demonstrate essential service water
system ability to function under design-basis conditions.
The team conducted their reviews in accordance with NRC Inspection Procedure 93812,
Special Inspection Procedure. The special inspection team reviewed procedures,
corrective action documents, as well as design and maintenance records for the
equipment of concern. The team interviewed key station personnel regarding the
events, reviewed the root cause analysis, and assessed the adequacy of corrective
actions. The team walked down and inspected the equipment in the field. A list of
specific documents reviewed is provided as Attachment 1. The charter for the special
inspection is provided as Attachment 2.
1R1 Sequence of Events Related to the Event
On August 19, 2009, Wolf Creek Generating Station experienced a complete loss of
offsite power to the two essential 4 kV bus transformers, XNB01 and XNB02, for about
49 seconds. This condition resulted from a lightning strike causing a fault four miles to
the east of the plant on the tie-line to La Cygne 345 kV substation. Wave trap and
tuning circuitry damage caused carrier system signal failures which prevented the feeder
breakers from two other substations, Rose Hill and Benton, from getting block signals.
Thus, these substation feeds were also rendered unavailable to Wolf Creek. The Wolf
Creek main generator experienced a load change from approximately 1220 MW to
100 MW. This resulted in a turbine trip - reactor trip. All reactor coolant pump motors
tripped on underfrequency. The main generator protection lockout relay 386-2G
actuated, opening the main generator output breakers. At 49.6 seconds after the
initiating event, the feeder breakers to 4 kV busses NB01 and NB02 were tripped open
7 Enclosure
by loss of voltage relays. At 55.2 seconds after the initiating event, the transmission
system operator closed the Wolf Creek - Rose Hill transmission network line
breaker 345-50. This restored one transmission line, supporting offsite power to Wolf
Creeks essential 4 kV bus transformers. At 56.5 seconds, the emergency diesel
generator output breakers NE001 and NE002 closed onto safety related 4 kV busses
NB01 and NB02. At 12 minutes, the Wolf Creek - Benton 345 kV network line
breaker 345-120 was closed by the transmission operator, restoring a second
transmission line supporting offsite power. At 13 minutes and 6 seconds, the
transmission system operator restored the third transmission line. One hour and
50 minutes after the event, offsite power was restored to safety related bus NB02.
Two hours and 54 minutes after the event, offsite power was restored to safety related
bus NB01.
This was the second loss of offsite power event at Wolf Creek in less than 18 months.
The first occurred on April 7, 2008, during a refueling outage. For both of the loss of
offsite power events, damage requiring repairs occurred within the essential service
water system. In this event, a 3/8-inch hole developed in the licensees service water
system.
1R2 Review of Problem Identification and Resolution Aspects of the Event
.1 Review of Operating Experience
a. Licensee Review of Operating Experience
Responsibility for most of the switchyard work rested with Westar Energy. As a result,
Wolf Creek typically did not enter switchyard-related maintenance and industry operating
experience into the corrective action program. Wolf Creek only entered external
operating experience evaluations into the corrective action program. Wolf Creek
received external operating experience, but did not effectively communicate the grid and
switchyard recommendations to Westar Energy.
Wolf Creek completed Self-Assessment 05-001, Transformer and Switchyard Self-
Assessment, in March 2005, to evaluate the interface of the nuclear power plant and
the switchyard in terms of maintenance, operation, design, and performance monitoring
relative to large power transformers and switchyard equipment. Wolf Creek also
evaluated Westars control of the grid as it affects the nuclear plant in terms of stability of
offsite power. Wolf Creek also reviewed transmission line design and grid voltage
control.
The licensees incident investigation team reviewed over 30 condition reports that were
generated from self-assessments and other industry operating experience. Based on
their review, the licensee team concluded that the performance improvement programs,
such as the Corrective Action Program, were not being used or implemented effectively.
Improper screening of condition reports had not allowed Wolf Creek to adequately
describe and evaluate problems.
b. Inspection Scope
The team reviewed internal operating experience by obtaining a list of plant corrective
action documents related to the offsite power and essential service water system. The
8 Enclosure
team further examined the licensees review of industry operating experience which
included inspection of the licensees operating experience program and specific review
of related condition reports for the August 19, 2009, event.
For external operating experience, the NRC Operating Experience Branch provided the
results of keyword searches related to offsite power and essential service water issues
and findings associated with essential service water leaks. The NRC Operating
Experience Branch also provided a list of licensee event reports, NRC Information
Notices, NUREG documents, and other operating experience information. The team
selected operating experience information that was applicable to this inspection and
reviewed how the licensee had addressed the items in their root cause analyses related
to these events or had processed the information through their operating experience
program. As part of their review, the inspectors performed an essential service water
system walkdown to determine if applicable industry operating experience had been
incorporated into system design and maintenance practices.
c. Findings
No findings of significance were identified.
.2 Review of Root Cause Analysis
a. Licensee Review
Incident Investigation Team
On August 20, 2009, the licensee established an incident investigation team to perform a
root cause analysis to investigate the facts and identify the causes of the loss of offsite
power and subsequent plant trip on August 19, 2009. The licensees final root cause
analysis was completed on October 1, 2009. The team consisted of site personnel,
Westar staff, and industry experts. The team conducted their review in accordance with
Procedure AI 28A-001, Level 1 CR Evaluation (IIT). The incident investigation teams
objectives were to:
- Determine the sequence of events
- Assess the risk and safety-significance of the event
- Identify and validate root and contributing causes
- Conduct an extent of condition review
- Determine extent of cause
- Develop corrective actions to limit likelihood of recurrence
- Evaluate existing procedures and processes
- Determine why prior corrective actions and applicable operating experience were
not effective in preventing the event.
9 Enclosure
Licensee Root Cause Methodology
The licensee performed their analysis utilizing a structured root cause analysis method
in accordance with Procedures AI 28A-001, Level 1 CR Evaluation (IIT), and
AI 28A-016, Cause Analysis Methods and Techniques. The licensee interviewed plant
personnel and reviewed condition reports, procedures, and other important documents
to perform the root cause analysis. The licensee created a detailed event and causal
factors chart to establish the sequence of events and provide a complete view of the
causes and contributors to the incident. The licensee used fault tree analysis, change
analysis, common cause analysis, hardware failure analysis, and hazard-barrier-target
analysis to supplement the investigation. The licensee also completed a management
oversight and risk tree analysis and an event cause and effect diagram to complete the
investigation.
Licensee Root Cause Analysis
The licensee determined that the root cause of the event was that Wolf Creek and the
transmission and distribution organization have not sufficiently ensured a mutually
desired level of reliable service for substation and transmission interfacing equipment
with Wolf Creek.
The licensee determined that the following issues contributed to the event:
- Westar Energys transmission line and substation design/maintenance had not
always applied updated electric utility industry practices to ensure the desired
level of reliable service for the applicable substations and transmission systems.
- A reliability-centered maintenance program was in progress for Wolf Creek
Generating Station, but not fully implemented for the Wolf Creek Substation.
Reliability-centered maintenance for the remote substation terminals and
transmission preventive maintenance, inspection, and testing had not been
effectively developed or implemented to the point equipment reliability meets
expectations.
- Relevant operating experience for substation and transmission systems had not
been effectively reviewed or utilized by Wolf Creek and shared with the
transmission and distribution organization.
- A process did not exist between Wolf Creek and the transmission and distribution
organization to effectively coordinate corrective action evaluations, action
tracking, and priorities.
b. Inspection Scope
The team reviewed the licensees root cause analysis prepared for the loss of offsite
power event. The team membership, team charter, report methodology, root and
contributing causes, recommended corrective actions, and supporting documentation
were reviewed. The team interviewed personnel who participated in the root cause
determination as well as personnel who were charged to implement corrective actions of
the report.
10 Enclosure
c. Findings
No findings of significance were identified.
.3 Review of Licensee Corrective Actions
a. Licensee Review
Licensee Review of Extent of Condition
The licensee determined the extent of condition to be the area of owner-controlled
equipment that was not previously fully considered to be within the scope of equipment
needing life cycle management and maintenance strategies in response to prior industry
operating experience. This equipment includes transformers or other communications
equipment in the carrier system, including wave traps, lightning arrestors, cabling, relays
and protection schemes, switches, disconnects, breakers, tuners, and surge arrestors.
The entire 345 kV switchyard and transmission system were included in the extent of
condition review. This equipment has the potential to adversely impact Wolf Creek and
offsite power source operation and reliability. The licensee factored the extent of
condition into all of the corrective actions planned in response to the loss of offsite power
event.
Licensee Corrective Actions
The existing equipment vulnerability was resolved by actions taken to replace all three
Rose Hill substation coupling capacitor voltage transformers, walk down the Rose Hill
and Wolf Creek substations, and test the carrier system for the three transmission lines
providing offsite power to Wolf Creek.
b. Inspection Scope
The team reviewed the licensees root cause analysis to determine if it was conducted to
a level of detail commensurate with the significance of the problem. As part of their
review, the inspectors interviewed key station personnel from operations, design and
system engineering, maintenance, and the corrective action program. Additionally, the
team interviewed incident investigation team members and members of the licensees
Corrective Action Review Board.
The team reviewed the licensees corrective actions to ensure they addressed the extent
of condition and whether they were adequate to prevent recurrence. In particular, the
team reviewed station procedures and processes to determine if any other issues exist
within Wolf Creeks offsite power system or essential service water system.
c. Findings and Observations
Root Cause Analysis
The inspectors determined that the licensees analysis accurately captured the root
cause of the offsite power event. Since the event was determined to be caused by
improper oversight of the switchyard between Wolf Creek and Westar, the inspectors
noted that the licensee appropriately identified a need to implement several corrective
actions related to improving the understanding of the importance of a reliable offsite
11 Enclosure
power system. The inspectors concluded the corrective actions were appropriate. The
inspectors noted that there was not a similar corresponding analysis or effort by the
licensee regarding leakage from the essential service water system following the loss of
offsite power event.
1. Entry of Conditions into the Corrective Action Program
Introduction. The team identified a Green finding regarding the licensees failure to
follow the requirements of Procedure AP 28A-100, Condition Reports, associated with
failure to recognize adverse conditions with respect to the corrective action program.
Description. On August 19, 2009, a complete loss of offsite power resulted in a reactor
trip. A fault was detected on the La Cygne 345 kV transmission line causing breakers in
the Wolf Creek switchyard to open. However, the carrier communications equipment
failed to block the trip signal on the Rose Hill 345 kV transmission line. The line
deenergized, and the resulting grid instability caused the Benton 345 kV transmission
line to trip, which resulted in a loss of offsite power to Wolf Creek. The carrier
communications equipment did not function as required due to the failure of a coupling
capacitor voltage transformer in the Rose Hill substation. The licensee had received
industry operating experience related to switchyard equipment and its importance to
maintaining a reliable grid, but failed to recognize the significance of switchyard reliability
as evidenced by their failure to effectively screen relevant industry operating experience.
In particular, Condition Report 00007499 was created from a third party recommendation
to develop a monitoring program for coupling capacitor voltage transformers in the
switchyard. This condition report, along with several other switchyard-related condition
reports, were screened to Improvement and Learning Evaluation, which is the lowest
level in the licensees condition reporting system.
The licensee did not take action on several switchyard-related condition reports since
due dates are not typically assigned for implementation of corrective actions for
Improvement and Learning Evaluation condition reports. In Attachment B of
Procedure AP 28A-100, the licensee defines adverse conditions, in part, as conditions
that could negatively impact plant reliability and includes industry operating experience
that is applicable or relevant to Wolf Creek as an example. The inspectors determined
that the licensee had not properly recognized these conditions as adverse conditions.
Also, the team learned that the licensees incident investigation team had determined
that offsite power had numerous interruptions in the past. In their charter, the team was
instructed to inspect previous line losses because regional inspectors noted that the
station had experienced a high number of offsite power interruptions in the recent past.
Based on this observation, the team requested information relating to previous line
losses and learned that since 2004, there had been 31 instances of offsite power
interruptions of at least one line. The team licensee staff had been done in these
instances. The team learned that the cognizant engineer had kept a spreadsheet of all
of these instances and what actions had been taken. The team noted that only 25 of
these instances had been entered into the corrective action program.
Section 2.1 of Procedure AP 28A-100 states that this procedure applies to adverse
conditions that affect equipment, procedures, or personnel and conditions deemed to be
undesirable or questionable. From this, the team concluded that offsite power line
interruptions affecting the availability of offsite power were an adverse condition that
12 Enclosure
affected plant equipment that was undesirable, or at least questionable, and within the
scope of Procedure AP 28A-100.
Section 6.1 of Procedure AP 28A-100 details the licensees guidance for recognizing an
adverse condition. Within this section, Step 6.1.1 instructs Wolf Creek personnel to
initiate a condition report document when they recognize an adverse condition.
Substep 1 of Step 6.1.3 of Procedure AP 28A-100 gives examples of some adverse
conditions. These include:
Step 1.b. A plant or system transient
Step 1.c. An unanticipated actuation or reposition of equipment
The team concluded that offsite power line interruptions comprised an offsite power
system transient. They also concluded that offsite power line interruptions comprised
unanticipated repositioning of equipment.
Based on these conclusions, the team determined that the licensee should have
recognized these conditions as adverse conditions and as a result entered them into
their corrective action program.
The team also observed that all line losses since August 2008 were entered into the
corrective action program. From this, the team concluded that the failure to enter
adverse conditions in the corrective action problem was being addressed by the
licensees ongoing problem identification and resolution improvement initiative and was
not indicative of current performance.
Analysis. The performance deficiency associated with this finding involved the
licensees failure to follow the requirements of Wolf Creek Procedure AP 28A-100.
Specifically, licensee personnel failed to recognize adverse conditions with respect to
the corrective action program which affected the reliability of the offsite power system.
This finding is greater than minor because if left uncorrected, the failure to fully utilize the
corrective action program could become a more significant safety concern. This finding
was more than minor because it impacted the equipment performance attribute of the
Initiating Events Cornerstone objective to limit the likelihood of those events that upset
plant stability and challenge critical safety functions during shutdown as well as power
operations. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and
Characterization of Findings, the inspectors determined that the finding was of very low
safety significance (Green) because it did not contribute to both the likelihood of a
reactor trip and the likelihood that mitigation equipment or functions would not be
available. A crosscutting aspect was not identified for this finding because the
inspectors concluded the deficiency in this area was not indicative of current
performance.
Enforcement. The performance deficiency did not involve a violation of regulatory
requirements because the offsite power sources feeding the Wolf Creek switchyard are
not safety-related. The licensee entered this issue into their corrective action program
as Condition Reports 00022241 and 00022242. Because this finding does not involve a
violation of regulatory requirements and has very low safety significance, it is identified
as FIN 05000482/2009007-01, Failure to Enter Adverse Conditions into the Corrective
Action Program.
13 Enclosure
2. Handling and Evaluation of Noted Conditions
Introduction. The team identified a Green noncited violation of 10 CFR Part 50,
Appendix B, Criterion V, Instructions, Procedures, and Drawings, regarding the
licensees failure to follow the requirements of Procedures AP 28-001, Operability
Evaluations, and AP 26C-004, Technical Specification Operability, associated with
deficiencies resulting from the loss of offsite power induced pressure transient on the
essential service water system. The pressure transient resulted in significant leakage
from the system and required immediate repair.
Description. When the essential service water pumps started following the loss of offsite
power event on August 19, 2009, the resulting pressure surge (water hammer) created
forces that contributed to a three-eighths inch diameter circular hole in essential service
water piping on the 1988 elevation of the auxiliary building. No operability evaluation
was performed immediately following the August 19, 2009, event. Additionally, the
licensee discovered multiple examples of through-wall leakage and essential service
water piping wall thinning attributed to internal corrosion in the summer of 2009. In
April 2008, a loss of offsite power had created a water hammer on the essential service
water system piping resulting in leakage from control room air conditioner and
emergency diesel generator heat exchangers. The air conditioning unit heat exchanger
experienced sufficient forces to stretch the heat exchanger end bell bolting. In
Operability Evaluation GK-08-004, the licensee determined that the piping and heat
exchanger repairs were sufficient to assure continued functionality of the essential
service water system. Operability Evaluation GK-08-004 did not evaluate the essential
service water system as a whole to provide a documented basis for continued
functionality after the water hammer event.
Wolf Creek Procedure AP 26C-004 required that an operability determination be
performed immediately upon determination that a deficiency exists that could affect the
operability of an SSC subject to Technical Specifications. In Step 4.1.1 the procedure
defined deficiency as an all-inclusive term used in reference to any condition or
circumstance that reduces the confidence that a structure, system, or component (SSC)
will perform satisfactorily in service. The August 19, 2009, water hammer was not
discussed in any corrective action document until September 23, 2009, when the NRC
questioned the basis for continued operability of the system. During this inspection on
September 24, 2009, the licensee initiated Operability Evaluation EF 09-007. This
evaluation noted that the essential service water system safety design basis as
described in Updated Safety Analysis Report 9.2.1.2.1.1 defined, in part, the following
system required functions:
- Safety Design Basis Three - Safety functions can be performed assuming a
single active component failure coincident with the loss of offsite power (GDC 44)
- Safety Design Basis Eleven - The essential service water system is protected
from long term organic fouling and corrosion problems
Operability Evaluation EF 09-007 indicated that most of the essential service water
system piping and valves are carbon steel and susceptible to internal localized
corrosion. Wolf Creek relies on internal inspection of the essential service water piping
whenever components within the system are removed for work. As noted above,
several recent piping failures have occurred indicating an increased trend in degradation
14 Enclosure
of the piping wall thickness. There was no operability evaluation for the internal
corrosion until prompting by NRC team inspectors.
The September 24, 2009, operability evaluation concluded that any subsequent
corrosion causing piping leakage would be limited to essential service water flow losses
less than or equal to those that have already occurred, and thus be bounded by the
maximum allowable essential service water leakage (140 gpm) from the ultimate heat
sink system. To address the possible future essential service water system water
hammer events, the licensee is pursuing an engineered solution from a contracted
engineering firm. The licensee is planning increased nondestructive inspection using
ultrasonic detection of degraded wall thickness to determine the extent of condition.
Analysis. The performance deficiency associated with this finding involved the
licensees failure to perform an adequate operability evaluation for the essential service
water system identified nonconforming conditions related to repeated occurrences of
system water hammer and localized internal corrosion. This finding is more than minor
because it is associated with the Mitigating Systems Cornerstone attribute of equipment
performance and adversely affects the objective to ensure equipment availability and
reliability. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and
Characterization of Findings, the issue screened as having very low safety significance
because it was not a design or qualification deficiency that resulted in a loss of
operability or functionality, did not create a loss of system safety function of a single train
for greater than the technical specification allowed outage times, and did not affect
seismic, flooding, or severe weather initiating events. This finding has a crosscutting
aspect associated with the problem identification and resolution area component of the
corrective action program because licensee personnel failed to thoroughly evaluate
problems such that the resolutions address all causal factors and extent of conditions, as
necessary P.1(c).
Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities
affecting quality shall be prescribed by documented instructions or drawings of a type
appropriate to the circumstances and shall be accomplished in accordance with these
instructions or drawings. Contrary to the above, following a water hammer event and
essential service water system pressure boundary leakage in 2009, the licensee failed to
use the operability process immediately upon determination that a deficiency existed that
could have affected the operability of the essential service water system as required by
Step 6.1.4 of Procedure AP 26C-004, Technical Specification Operability. Specifically,
the licensee failed to perform Step 6.1.6 of Procedure AP 26C-004, which calls for
performance of an immediate operability determination. Because of the very low safety
significance and Wolf Creeks action to place this issue in their corrective action program
as Condition Report 00022240, this violation is being treated as a noncited violation in
accordance with Section VI.A.1 of the Enforcement Policy: NCV 05000482/2009007-02,
Failure to Perform an Operability Evaluation.
3. Screening of Conditions in the Corrective Action Program
Introduction. The team identified a Green noncited violation of 10 CFR Part 50,
Appendix B, Criterion V, Instructions, Procedures, and Drawings, regarding the
licensees failure to follow the requirements of Procedure AI 28A-010, Screening
15 Enclosure
Condition Reports, Revision 3A, associated with the effects of a loss of offsite power
induced water hammer of the essential service water system.
Description. On August 19, 2009, a complete loss of offsite power resulted in a water
hammer of the essential service water system which created forces that contributed to a
three-eighths inch diameter circular hole in essential service water piping on the
1988 elevation of the auxiliary building. In June and July of 2009, the licensee identified
that internal corrosion had created through-wall leakage on the 1974 elevation essential
service water piping. In April 2008 a similar loss of offsite power created a water
hammer of the essential service water piping. This occurrence created leakage from
control room air conditioner and emergency diesel generator heat exchangers. The air
conditioning unit heat exchanger experienced sufficient forces to stretch the heat
exchanger end bell bolting. These are four recent examples of system damage to one of
the most risk significant systems at Wolf Creek Generating Station. Condition
Report 2008-004983 describes four additional essential service water system water
hammers in 1993, 1995, 1999, and 2004 that resulted in system damage.
Wolf Creek Procedure AI 28A-010, uses a qualitative risk matrix table to determine
whether identified conditions adverse to quality require a root cause analysis. The
matrix describes that risk vulnerability is a product of the probability of an occurrence
and its potential consequence. A qualitative consequence is determined to be marginal
if system damage or a noncritical equipment failure occurs. A qualitative consequence
is determined to be critical if major system damage occurs, or if an event results in a
loss of production or could have resulted in catastrophic consequences under different
circumstances. The widespread corrosion effects on both trains of the essential service
water system and the vulnerability to large leaks after loss of offsite power induced
essential service water water hammer events could be considered critical by these
definitions. These adverse conditions definitely meet the marginal definition. The
matrix describes a qualitative consequence as probable if the condition is likely to occur
several times in the life of an individual system. This frequency was validated by the
multiple examples described above that resulted in through-wall leaks and damage to
the essential service water system supplied heat exchangers. Using the licensee matrix,
the combination of critical and probable results in requirement to conduct a Level 1,
high, root cause analysis. A combination of marginal and probable results in a
requirement to conduct a Level 2, moderately high, root cause analysis. At the time of
inspection, the licensee had initiated two condition reports addressing essential service
water leakage from these adverse conditions. Condition Report 2008-001660 followed
the April 2008 complete loss of offsite power event and water hammer which resulted in
a Level 4, low risk, basic evaluation. The June, July, and August 2009 essential service
water leakage events were rolled together into Condition Report 00018785 that was
screened as a Level 3, moderately low risk, apparent cause evaluation.
The licensee has inspected only a small portion of the essential service water system
piping to identify the magnitude and location of other likely localized corrosion under
deposits. Possible inspection methods include internal inspections and ultrasonic
measurements.
Analysis. The performance deficiency associated with this finding involved the
licensees failure to follow the requirements of Wolf Creek Procedure AI 28A-010.
Specifically, licensee personnel did not effectively screen condition reports for the
adverse conditions of internal corrosion and loss of offsite power induced water
16 Enclosure
hammers to require a root cause analysis. This finding is greater than minor because if
left uncorrected, the failure to fully utilize the corrective action program could become a
more significant safety concern. The inspectors determined that this finding impacted
the Mitigating Systems Cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial
Screening and Characterization of Findings, the issue screened as having very low
safety significance because it was not a design or qualification deficiency that resulted in
a loss of operability or functionality, did not create a loss of system safety function of a
single train for greater than the technical specification allowed outage times, and did not
affect seismic, flooding, or severe weather initiating events. The cause of this finding is
related to the problem identification and resolution crosscutting component of the
corrective action program because licensee personnel failed to thoroughly evaluate
problems such that the resolutions address causes and extent of conditions P.1(c).
Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities
affecting quality shall be prescribed by documented instructions or drawings of a type
appropriate to the circumstances and shall be accomplished in accordance with these
instructions or drawings. Contrary to the above, prior to September 2009, the licensee
failed to accomplish on activity affecting quality in accordance with documented
instructions. Specifically, as required by Step A.1 of Attachment A to Wolf Creek
Procedure AI 28A-010, Screening Condition Reports, the licensee failed to correctly
determine the appropriate probability associated with occurrences of water hammer
damage and essential service water piping corrosion that resulted in system damage.
Specifically, the licensee did not apply Step A.4.2, Probable, in accordance with the
definition in Step A.4.2, and therefore the licensees application of Step A.6, Qualitative
Risk Matrix, was inappropriate. As a result of the incorrect screening, Condition
Report 00018785 did not require performance of a root cause analysis and did not
evaluate the additive effect of documented loss of offsite power induced water hammers
and internal corrosion. Because of the very low safety significance of this finding and
because the licensee has entered this issue into their corrective action program as Wolf
Creek Condition Report 00022239, this violation is being treated as a noncited violation
in accordance with Section VI.A.1 of the Enforcement Policy:
NCV 05000482/2009007-03, Failure to Correctly Screen Essential Service Water Piping
Leaks for Significance.
1R3 Review of the Licensees Offsite Power System
a. Inspection Scope
The inspectors reviewed the licensees actions for prior instances of loss of the offsite
power lines and whether the licensees actions were commensurate with the number of
previous line failures. Additionally the inspectors assessed the licensees ability to meet
the General Design Criteria requirements for independence of the offsite power lines in
light of conditions surrounding the event.
17 Enclosure
b. Findings
Unresolved Item: 345 kV Offsite Power System Compliance with General Design
Criterion 17
The 345 kV switchyard currently provides both sources of offsite power to the plant. The
original design of the offsite power system included a 345 kV source from the 345 kV
switchyard and a separate 69 kV source from the 69 kV switchyard. In April 1982, the
NRC concluded that the original design was acceptable because the circuits provided
sufficient assurance that redundant and independent sources of offsite power were
provided, as required by General Design Criterion 17. The NRC safety evaluation report
was in two parts. The first described offsite power inside the Standardized Nuclear Unit
Power Plant System design and the second described offsite power to the Wolf Creek
specific Standardized Nuclear Unit Power Plant System (i.e., Wolf Creek). In 1983, Wolf
Creek Generating Station reanalyzed the offsite power system and determined that
changes needed to be made to the Updated Safety Analysis Report. Wolf Creek
Generating Station submitted the revised Updated Safety Analysis Report pages to the
NRC which described the changes to the switchyard and how General Design
Criterion 17 would be met. The significant changes were removing one of the four
proposed 345 kV transmission lines coming into the 345 kV switchyard and adding a
345/69 kV transformer to connect the 345 and 69 kV switchyards. Thus, both offsite
power sources were routed through the common 345 kV switchyard versus from
separate switchyards. In 1985 the NRC concluded that the design changes met the
requirements of General Design Criterion 17 and were acceptable. The removal of this
portion of the USAR was not described in Wolf Creeks submittal and the effective
deletion of the NRCs 1983 safety evaluation report were not described in the NRC
approval. Thus, this Updated Safety Analysis Report change also effectively removed
the second portion of the NRC safety evaluation report from the licensing basis that
described how the plants 345 kV and 69 kV switchyards met the independence
requirements of General Design Criterion 17.
After the NRC approved the offsite power design changes in 1985, Wolf Creek
Generating Station installed an additional 345/13.8 kV transformer. The new
configuration bypassed the 69 kV switchyard and went directly to the onsite XNB01
safety related transformer. In the 10 CFR 50.59 evaluation, Wolf Creek Generating
Station determined that this would be a more reliable source of offsite power than the
previously approved source, which was routed through the 69 kV switchyard. Wolf
Creek Generating Station determined that the new design met General Design
Criterion 17. The inspectors were not able to determine if these design changes were
submitted to the NRC for approval and if the changes, including those in 1983, would
have been accepted as conforming to General Design Criterion 17. Therefore, this issue
is unresolved pending more NRC inspection of the General Design Criterion 17
acceptance criteria applied by Wolf Creek Generating Station and basis and verification
of the removal of the 69 kV system from the offsite power analysis: Unresolved
Item 05000482/2009007-04, 345 kV Offsite Power System Compliance with General
Design Criterion 17.
18 Enclosure
1R4 Review of the Licensees Essential Service Water System
.1 Review of Generic Letter 89-13 and Periodic Verification Program
a. Inspection Scope
The team reviewed the licensees Generic Letter 89-13, Service Water System
Problems Affecting Safety-Related Equipment, program for the essential service water
system including the licensees periodic verification program. As part of their review, the
inspectors examined the licensees response to Generic Letter 96-06, Assurance of
Equipment Operability and Containment Integrity during Design-Basis Accident
Conditions, dated September 30, 1996. Additionally, the inspectors reviewed the
licensees engineering analysis of the system and testing results to ensure the essential
service water system is adequately designed and has the ability to function under
design-basis conditions.
b. Findings and Observations
The team determined that while the licensee had appropriately followed their Generic
Letter 89-13 program for the essential service water system, their implementing
procedures did not result in identifying and correcting pipe wall wastage mechanisms
prior to localized pitting becoming through-wall leaks.
Introduction. The team identified a Green noncited violation of 10 CFR Part 50,
Appendix B, Criterion V, Instructions, Procedures, and Drawings, regarding the
licensees failure to provide adequate guidance to identify and address pitting, corrosion,
and surface-breaking flaw indications in the essential service water system. Previous
licensee self-assessment efforts and associated corrective actions recognized the need
for increased monitoring of piping system pitting and wall thinning but had not translated
the need into the implementing procedures such that the service water monitoring
program could address extent of condition.
Description. From 2005 to 2009, at least five examples of through-wall leakage from the
essential service water piping were documented in the Wolf Creek service water
monitoring and corrective action programs. The cause and extent of condition of
essential service water system leaks were not fully addressed by the licensee due to
procedural inadequacies. This was evident because the licensee monitoring efforts
were unable to ensure the continuous system degradation did not reduce essential
service water pipe wall thickness below the minimum allowed ASME code specifications.
The essential service water system is a critical system for the plant because it is tied to
the ultimate heat sink for the facility and because the system is relied upon to provide
appropriate cooling to the heat exchangers and coolers in safety-related systems
needed for accident mitigation or safe-shutdown of the facility. As documented in the
addendum to Wolf Creek Condition Report 00018785, the Wolf Creek essential service
water system has had a history of corrosion and leakage. The licensee only assessed,
and if necessary corrected, degradation in the essential service water system on a case-
by-case basis, and only after determining that the degradation had progressed to an
unacceptable state; that is, only after actual wall thickness for a component was below
the minimum wall thickness requirement or after the component had leaked.
19 Enclosure
NRC Generic Letter 89-13, applies to all holders of operating licenses for nuclear power
generation facilities, and requested that licensees implement augmented activities for
those service water systems that are tied to the ultimate heat sink and that are used to
provide cooling for safety-related systems and components during operational transients
and postulated design basis accidents. These augmented inspection, surveillance, and
maintenance programs were designed to:
- Significantly reduce the incidence of flow blockage problems as a result of
- Ensure that corrosion, erosion, protective coating failure, silting, and biofouling
cannot degrade the performance of the safety-related systems supplied by
- Confirm that these type of emergency or essential service water systems will
perform their intended function in accordance with the licensing basis for the
plant
- Confirm that maintenance practices, operating and emergency procedures, and
training that involves these types of service water systems are adequate to
ensure that safety-related equipment cooled by the systems will function as
intended
Wolf Creek implements its Generic Letter 89-13 program in accordance with
administrative Procedures ADM-01-100, Lake Water Systems Inspection, Monitoring
and Maintenance Program, and AP-23L-001 Lake Water Systems Corrosion and
Fouling Program, dated March 21, 2005. These procedures refer to augmented
inspection Procedures QCP-20-518, Visual Examinations of Heat Exchangers and
Piping Components, and WCRE-13, Lake Water Systems Structural Integrity
Program. The purpose of these lake water procedures is to detect degradation in the
essential service water system prior to a leakage event. The inspection procedure for
implementing augmented visual examinations of the essential service water system is
Procedure QCP-20-518.
Procedure WCRE-13 is the augmented volumetric inspection procedure.
Procedure WCRE-13 did not consider essential service water piping with intermediate
flow velocities to be susceptible to wall thinning mechanisms. Intermediate flow velocity
sections of pipe are in WCRE-13, but they were not inspected. It also does not identify
silting deposits (under deposits) as possible sources of microbiologically influenced
corrosion in the essential service water system. This is inconsistent with the definition
for tubercles in visual inspection Procedure QCP-20-518 which does identify that silting
tubercles (under deposits) can be a source of microbiologically influenced corrosion.
The August 19, 2009, leak was through intermediate level velocity piping and was
partially caused by pitting and wall-thinning. The inspection team determined that each
of these procedures have inadequacies that have prevented detection, adequate
expansion of extent of condition testing for microbiologically influenced corrosion, and
thus corrective action for pitting related degradation in the essential service water
system. Thus, significant portions of piping would not have received inspection until
after they suffered through wall leaks.
20 Enclosure
These procedure inadequacies were recognized in 2007 Licensee Self-assessment
Number 76, Lake Water Corrosion, Fouling and Chemistry, which identified:
- A need to establish a pit monitoring program for the essential service water
system
- A need to revise Wolf Creeks volumetric inspection Procedure WCRE-13, to be
consistent with the augmented inspection guidelines in EPRI Service Water
Piping Guideline [EPRI Report TR-1010059]
Corrective action procedures also contributed to the inadequate verification of the
essential service water system material condition. Section 6.1.3 of
Procedure AP 28A-100, Condition Reports, did not identify detection of degradation or
corrosion as an adverse condition for generating condition reports at the facility. As a
result, documentation of corrosion on the inside surfaces of the essential service water
system was not normally translated into appropriate condition reports until either a leak
had occurred or essential service water pipe wall thickness had thinned to below the
minimum ASME Code,Section III, wall thickness requirements. Additionally
documentation of corrosion occurring on the outside surfaces of essential service water
system piping did not occur prior to August 2009.
Analysis. The performance deficiency associated with this finding was a failure to
include appropriate essential service water system quality standards and acceptance
criteria in Procedures QCP-20-518, WCRE-13, and AP 28A-100 to address:
- depth sizing relevant surface-breaking flaw indications and abnormal gross
degradation (such as corrosion, erosion, or wear )
- extent of degradation
- blockage as a result of microbiologically influenced corrosion, macrofouling,
silting or corrosion deposits
As a result of the inadequate procedures, appropriate corrective actions could not occur
when essential service water internal surfaces indicated the presence of corrosion. This
finding is greater than minor because if left uncorrected, the failure to fully utilize the lake
water and corrective action programs could become a more significant safety concern.
The inspectors determined that this finding impacted the Mitigating Systems
Cornerstone. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and
Characterization of Findings, the issue screened as having very low safety significance
because it was not a design or qualification deficiency that resulted in a loss of
operability or functionality, did not create a loss of system safety function of a single train
for greater than the technical specification allowed outage times, and did not affect
seismic, flooding, or severe weather initiating events. This finding has a crosscutting
aspect in the area of problem identification and resolution associated with the corrective
action program because licensee personnel failed to take appropriate corrective actions
to address safety issues and adverse trends in a timely manner P.1(d).
Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities
affecting quality shall be prescribed by documented instructions or drawings of a type
21 Enclosure
appropriate to the circumstances and shall be accomplished in accordance with these
instructions or drawings. Contrary to the above, prior to September 2009,
Procedures QCP-20-518, Visual Examinations of Heat Exchangers and Piping
Components, and AP 28A-100, Condition Reports, were not appropriate to the
circumstances because the licensee failed to include appropriate quality standards and
acceptance criteria for corrosion in the essential service water system. As a result of
these procedural deficiencies, the licensee did not evaluate the affect of documented
internal corrosion. Because of the very low safety significance of this finding and
because the licensee has entered this issue into their corrective action program as
Condition Report 00022243 this violation is being treated as a noncited violation in
accordance with Section VI.A.1 of the Enforcement Policy: NCV 05000482/2009007-05,
Failure to Ensure Adequate Acceptance Criteria and Extent of Condition Guidance in
Lake Water and Corrective Action Program Procedures.
.2 Review of the Bases for Insulating Essential Service Water Piping
a. Inspection Scope
The team evaluated the licensees bases for insulating the essential service water
system piping in the auxiliary building. The licensees design drawings and design basis
documentation were reviewed. Also, key personnel from design and system engineering
were interviewed.
b. Findings
No findings of significance were identified.
.3 Review of the Evaluation for Piping Structural Integrity
a. Inspection Scope
The team evaluated the licensees evaluation of the structural integrity of the essential
service water system piping with the 3/8-inch hole which had developed during the
event. In their evaluation, the licensee applied Code Case N-513-2 to the ASME Piping
Code. This code case required the licensee to perform additional monitoring of the
essential service water system piping. The team reviewed acceptability of the chosen
monitoring the licensee adopted. Key personnel from operations, design and system
engineering, maintenance, and the corrective action program were interviewed. The
NRC Office of Nuclear Reactor Regulation also provided technical assistance to the
inspection team during the review of this area (Attachment 3).
b. Findings
No findings of significance were identified.
.4 Review of Essential Service Water System Piping Repairs
a. Inspection Scope
The team evaluated the licensees repairs to the 3/8-inch hole in the essential service
water system piping that occurred during the event. The licensee also discovered
22 Enclosure
another area that was below the minimum wall thickness prescribed by the American
Society of Mechanical Engineering Code after the event. This condition and its repair
was also reviewed by the team. Key personnel from operations, design and system
engineering, maintenance, and the corrective action program were interviewed.
b. Findings
No findings of significance were identified.
1R5 Review of Plant Systems during the Event
.1 Observed Pressure Oscillations in the Auxiliary Feedwater System
a. Inspection Scope
During the event, the senior resident inspector noted there was indication that the
pressure in the auxiliary feedwater system at the suction of the pumps was oscillating.
The team reviewed the acceptability of the observed pressure oscillations observed on
the suction of the auxiliary feedwater pumps and their impact on system operability and
technical specifications. Applicable system piping and instrumentation diagrams along
with system isometrics drawings were reviewed. Also, the team walked down the
auxiliary feedwater system suction piping to verify the drawings and assumptions the
licensee made relative to the indications and their impact on the system. Finally, key
personnel from operations, design and system engineering, maintenance, and the
corrective action program were interviewed.
b. Findings
No findings of significance were identified.
.2 Water Hammer on the Essential Service Water System
a. Inspection Scope
The team verified that a water hammer occurred on the essential service water system
on August 19, 2009. The team noted multiple previous examples of water hammer
occurrences were documented in the licensees corrective action system as mentioned
and detailed in Condition Report 2008-004983.
The team evaluated the licensees procedures for water hammer response and
corrective actions to previous water hammer events. The licensees response to
Generic Letter 96-06, Assurance of Equipment Operability and Containment Integrity
During Design-basis Accident Conditions, was reviewed. Key personnel from
operations, design and system engineering, maintenance, and the corrective action
program were interviewed.
b. Findings
Introduction. The team identified a Green noncited violation of 10 CFR Part 50,
Appendix B, Criterion V, Instructions, Procedures, and Drawings, regarding the
licensees failure to provide adequate guidance to address the impact of a loss of offsite
power event on the essential service water system.
23 Enclosure
Description. On August 19, 2009, a leak of approximately 20 gpm from the essential
service water system piping occurred on the 1988 elevation level of the auxiliary
building concurrent with a loss of offsite power event. This plant area was not frequently
entered by plant personnel. The plants emergency diesel generators started per design
and sequenced on safety loads including two trains of essential service water pumps.
The design of the load sequencing subjects the plant essential service water piping to a
water column separation from the piping high point. Wolf Creek
Procedure STN PE-040G, Transient Event Walkdown, required that several plant
systems subject to expected transient dynamic forces following a reactor trip to have a
post-trip walkdown to identify any structural damage from the off-normal forces. The
walkdown procedure did not identify the essential service water system as vulnerable to
such dynamic forces. However, the procedures Appendix H did allow for operations
shift management to designate additional systems to walk down following reactor trip
events. This procedure was used in a very similar loss of offsite power induced water
hammer on April 7, 2008. That event recognized an essential service water piping
walkdown was needed after leakage from several locations had been identified.
With the current essential service water system design, every loss of offsite power event
at Wolf Creek will result in a water column separation and subsequent re-pressurization
by the loss of normal service water pumps and the sequencing on of the essential
service water pumps. This phenomenon was not specifically described in the licensees
Updated Safety Analysis Report; however, it had been clearly identified in previous Wolf
Creek condition reports (00012990, 00009688, 2008-005075, 2008-004983, and 2008-
001660). This was also evident by Wolf Creeks response to NRC Generic Letter 96-06,
Assurance of Equipment Operability and Containment Integrity During Design-Basis
Accident Conditions, September 30, 1996. Despite the abundant internal operating
experience, Procedure STN PE-040G did not identify essential service water as a
required walkdown system. The post-trip walkdown procedure only required walkdowns
inside the containment building unless specified by operating department shift
supervisors. From the recent implementation of the procedure, outside containment
piping system damage must be self-evident to result in usage of STN PE-040G,
Appendix H. The August 19, 2009, leak was discovered approximately seven hours
after the reactor trip by the NRC resident inspectors and not by the licensee. The
resident inspectors had noted one to three inches of water buildup on the floor one level
below the elevation where the leak had occurred seven hours earlier.
Analysis. The performance deficiencies of this finding are the inadequate walkdown
procedure for post loss of offsite power reactor trips and the failure of the operations
crew to recognize the need to require a walkdown of the essential service water system
in its entirety following the loss of offsite power and reactor trip. This finding is more
than minor because it is associated with the Mitigating Systems Cornerstone attribute of
procedure quality and adversely affects the objective to ensure equipment availability
and reliability. This finding is of very low safety significance because it was not a design
deficiency or qualification deficiency, did not represent a loss of system safety function,
did not represent an actual loss of safety function of one or more non-technical
specification trains of equipment designated as risk-significant, and was not potentially
risk significant due to a seismic, flooding, or a severe weather initiating event. This
finding is related to the area of problem identification and resolution and is associated
with the operating experience crosscutting component because the licensee failed to use
information, including vendor recommendations, and internally generated lessons
24 Enclosure
learned, to support plant safety. Specifically, the licensee failed to implement and
institutionalize operating experience through changes to station walkdown procedures
Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities
affecting quality shall be prescribed by documented instructions or drawings, of a type
appropriate to the circumstances and shall be accomplished in accordance with these
instructions or drawings. Contrary to the above, Procedure STN PE-040G, Transient
Event Walkdown, was not appropriate to the circumstances in that it was not adequate
to detect essential service water system damage on August 21, 2009. Because of the
very low safety significance and Wolf Creeks action to place this issue in their corrective
action program as Condition Report 00022265, this violation is being treated as a
noncited violation in accordance with Section VI.A.1 of the Enforcement Policy:
NCV 05000482/2009007-06, Inadequate Procedure Resulted in Failure to Discover
Essential Service Water System Leakage Following a Water Hammer Event.
.3 Impact on Internal Flood Control Mitigation Capability
a. Inspection Scope
The team noted that water from the essential service water system was entering the
auxiliary building and that the plants room drain pump were powered from non-
emergency sources. In light of this, the team reviewed the design and operation of the
internal flood control features in the plant and their ability to mitigate a leak during a
sustained loss of offsite power event. Pertinent plant drawings were reviewed. Also,
key personnel from operations and engineering were interviewed.
b. Findings
No findings of significance were identified.
.4 Effects of Loss of Power to Plant Radiation Monitors
a. Inspection Scope
During the event, numerous radiation monitors lost power. Due to their design, some
required resetting and other actions to place them back in to operation. The team
reviewed monitors that were unavailable at any time during or after the event and
determine if any of the radiation monitor failures experienced in the event would have
hampered further actions (e.g., implementing the emergency plan). The team reviewed
plant logs, plant computer system data, and the licensees emergency action level
procedures to evaluate the effects. Also, key personnel from radiation protection,
emergency planning, and maintenance were interviewed.
b. Findings
No findings of significance were identified.
25 Enclosure
.5 Partial Loss of Fire Detection System Capability
a. Inspection Scope
The team reviewed the actions taken for the loss of fire detection capability in the
auxiliary building during the event. In their review, the team sought to establish if this
loss of detection capability was anticipated in plant design.
b. Findings
1. Operations Department Actions to Compensate for the Loss of Detection
Introduction. The team identified a Green noncited violation of License
Condition 2.C.(5), Fire Protection, for the failure to establish a compensatory fire watch
in a timely manner per the station fire protection program.
Description. On August 19, 2009, a complete loss of offsite power resulted in a reactor
trip. Immediately after the trip, fire protection trouble alarms came in on fire protection
panel KC-008. The control room supervisor acknowledged the alarms and verified that
every smoke detector in window 109 of the panel was in a trouble alarm state. The
control room supervisor dispatched personnel to verify a fire existed in accordance with
Procedure OFN KC-016, Fire Response. Licensee personnel reported that a fire did
not exist in the location of the alarming smoke detectors. Since there was not an actual
fire, the procedure directed the control room supervisor to exit Procedure OFN KC-016
and enter alarm Procedure ALR KC-888, Fire Protection Panel KC-008 Alarm
Response. Step 4.3.1 required, in part, the operator to take appropriate compensatory
measures per administrative Procedure AP 10-103, Fire Protection Impairment Control,
for the smoke detectors that were in a trouble alarm state.
The control room supervisor was preoccupied with actions related to the reactor trip and
did not perform the required action to initiate a fire protection impairment. The control
room supervisor assigned the action to the nightshift control room supervisor during the
shift turnover. The nightshift control room supervisor subsequently assigned the action
to the nightshift shift engineer. The nightshift shift engineer failed to initiate the
appropriate compensatory measures for the alarming smoke detectors. The next
morning, the NRC senior resident inspector questioned why no impairment had been
established for the alarms on KC-008. The dayshift shift engineer subsequently
discovered the detectors were inoperable and issued the impairment for the 13 affected
fire zones.
The team determined that a significant contributor to the finding was that the licensee did
not follow their procedures as required. Both the dayshift and nightshift control room
supervisors delegated the responsibility of initiating the impairment and failed to verify
that the task was completed. Not having proper compensatory measures in place added
unnecessary risk to the plant.
Analysis. The licensees failure to initiate fire protection impairment and establish an
hourly fire watch for the areas impacted by the inoperable fire detectors was a
performance deficiency. The finding was more than minor since it was associated with
the protection against the external factors attribute of the Mitigating Systems
Cornerstone, and adversely affected the cornerstone objective to ensure the availability,
26 Enclosure
reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences. Using Manual Chapter 0609, Appendix F, Fire Protection
Significance Determination Process, the inspectors determined that this finding had an
adverse affect on the fixed fire protection systems element of fixed fire detection
systems. The inspectors assigned a high degradation rating due to the fact that all the
smoke detectors in the fire zones were inoperable. Because the system was degraded
without compensatory actions for approximately 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> and licensee personnel were
walking through the auxiliary building performing post-trip actions, senior reactor
analysts determined this finding to be of very low safety significance. This finding had a
crosscutting aspect in the area of human performance associated with the work
practices component because the licensee failed to ensure supervisory oversight of work
activities such that nuclear safety is supported H.4(c).
Enforcement. License Condition 2.C.(5) states, in part, that the licensee shall maintain
in effect all provisions of the approved fire protection program as described in the
Standardized Nuclear Unit Power Plant System (SNUPPS) Final Safety Analysis Report
for the facility through Revision 17, the Wolf Creek Site Addendum through Revision 15,
and as approved in the Safety Evaluation Report through Supplement 5. The Wolf
Creek Updated Safety Analysis Report combined the SNUPPS Final Safety Analysis
Report, Revision 17, and the Wolf Creek Site Addendum, Revision 15, into one
document. Updated Safety Analysis Report, Appendix 9.5A, Section B, Administrative
Procedures, Controls and Fire Brigade, states that work control procedures, which
include identification of the need for special action such as a fire watch, are utilized.
Contrary to the above, the licensee failed to utilize work control procedures to identify
the need for a special action (fire watch). Specifically, the licensee did not issue a fire
protection impairment and implement an hourly fire watch within one hour as required by
administrative Procedure AP 10-103, Fire Protection Impairment Control. This issue
and the corrective actions are being tracked by the licensee in Condition
Report 00019320. Because the finding is of very low safety significance and has been
entered into the corrective action program, this violation is being treated as a noncited
violation, consistent with Section VI.A.1 of the NRC Enforcement Policy:
NCV 05000482/2009007-07, Failure to Initiate Timely Fire Protection Impairment
Control Permit and Implement Compensatory Measures.
2. Uncontrolled and Unanalyzed Room Environment Following a Loss of Offsite Power
The Wolf Creek Station Blackout Coping Assessment, Section 4.5, evaluated the Effects
of Loss of Ventilation, associated with the loss of offsite power. Specifically, the
assessment evaluated the loss of auxiliary building ventilation effects on the environment
surrounding the turbine-driven auxiliary feedwater pump room. The evaluation states:
It is shown that the turbine-driven auxiliary feedwater pump room air temperature will
stay below 150 degrees Fahrenheit turbine-pump design specifications provided actions
are taken to open doorways to enhance air circulation. The final steady state
temperature of the room is determined by a NUMARC methodology. This methodology
assumed an open door formula; that is, a need to open the four other doors adjacent to
the corridor outside the turbine-driven auxiliary feedwater pump room. This action was
not performed during the August 19, 2009, loss of offsite power/loss of auxiliary building
ventilation event. Due to this, temperatures in the corridor were recorded above the
assumed maximum of 113 degrees Fahrenheit using the open door formula. With the
doors remaining closed, the calculation determined that the turbine-driven auxiliary
27 Enclosure
feedwater pump room temperatures would rise to 170 degrees Fahrenheit, which is
above that allowable to maintain the rooms equipment operable.
The turbine-driven auxiliary feedwater pump steam drain traps in room 1206/1207 below
the corridor exhausted to the floor drains. During steady-state conditions, the ventilation
system keeps the steam from accumulating in the room. However, during a loss of
offsite power event, the ventilation system no longer functions and the steam heats up
the room. This additional heat source to the corridor was not accounted for in the station
blackout analysis and created conditions not previously analyzed associated with
room 1206/1207. The licensee did not provide an adequate evaluation or adequate
procedural guidance to address the impact of a loss of offsite power on the auxiliary
feedwater system.
The concerns associated with the steam environment in room 1206/1207 below the
auxiliary feedwater pump rooms were:
- The safety related transmitters for condensate storage tank swap-over could be
challenged
- The seismic supports for essential service water piping in the room could be
affected by the increased local temperature
- Manual operator actions to manipulate an essential service water motor operated
valve could be challenged due to visibility and local temperatures
This issue is unresolved pending further NRC inspection of the evaluation by Wolf Creek
Generating Station associated with steam exhausting into rooms 1206/1207 and the
corridor outside the auxiliary feedwater pump rooms following a loss of offsite power:
Unresolved Item 05000482/2009007-08, Uncontrolled and Unanalyzed Room
Environment Following a Complete Loss of Offsite Power.
1R6 Review of the Post-Trip Report
a. Inspection Scope
The team reviewed the licensees post-trip report prepared for analyzing the event. The
report was initially reviewed prior to plant restart and again during the onsite portion of
the special inspection. The team interviewed key personnel from operations and
engineering to discuss the findings of the report.
b. Findings
No findings of significance were identified.
1R7 Review of High Level in Steam Generator Following the Event
a. Inspection Scope
On August 21, 2009, the licensee reported to the NRC a condition in which the level in
Steam Generator A exceeded the 78 percent level. The team reviewed the licensees
report, control room logs, plant computer data, and pertinent plant operating procedures.
Also, key personnel from the operations department were interviewed.
28 Enclosure
b. Findings
Introduction. A self-revealing Green noncited violation of Technical Specification 5.4.1.a,
Procedures, was reviewed involving a failure to monitor and maintain steam generator
water levels resulted in an unanticipated turbine trip signal and feedwater isolation.
Description. On August 21, 2009, while in Mode 3, Wolf Creek control room received
annunciator 112A, S/G LEVEL HIGH TURB TRIP. This was caused by operator
inattention during shift turnover. Steam generator A level had increased to the
78 percent, P-14 feedwater isolation actuation setpoint. This was above the 40 percent
to 60 percent operating band designated in Procedure GEN-OO-005, Minimum Load to
Hot Standby, and created the P-14 feedwater isolation, an engineered safeguards
actuation signal. Control room operators responded to the feedwater isolation by
restoring steam generator water levels to the program band.
The licensee had been having difficulties maintaining steam generator water levels since
the reactor trip from full power on August 19, 2009. These difficulties were due to
staying in Mode 3, steaming the steam generators with no automatic feedwater control,
and atmospheric relief valves periodically releasing steam. The practice established had
been to secure auxiliary feedwater flow as soon as an established operator selectable
alarm indicated that Steam generator A was at 65 percent. This allowed for an
anticipated additional 5 percent level increase due to swell of the introduced colder
auxiliary feedwater and another 5 percent level increase caused by opening of the
atmospheric relief valve.
The licensee determined that the oncoming shift operators had disabled an operator
selectable alarm due to the constant alarms being a distraction. The trip signal and
actuation occurred while the operators were walking down the control boards for shift
turnover. Thus there were no additional operators monitoring the steam generator A
level. Disabling the operator selectable alarm, not having a dedicated operator
monitoring steam generator water levels when in manual control, and intentionally
allowing levels to go above the control band were all contrary to licensee
Procedure AI 21-100, Operations Guidance and Expectations.
Analysis. The performance deficiency associated with this finding involved the failure to
control and maintain steam generator water levels as required in
Procedure GEN-OO-005. This finding was determined to be greater than minor because
it impacted the Initiating Events Cornerstone attribute of human performance and
affected the cornerstone objective to limit the likelihood of those events that upset plant
stability and challenge critical safety functions during shutdown as well as power
operations. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and
Characterization of Findings, this finding was determined to be of very low safety
significance since it did not affect the technical specification limit for reactor coolant
system leakage or mitigation systems safety function, did not contribute to both the
likelihood of a reactor trip and mitigation equipment or functions not being available, and
did not increase the likelihood of a fire or internal/external flooding. The finding has a
crosscutting aspect in the area of human performance associated with the decision
making component because the licensee failed to make safety-significant or risk-
significant decisions using a systematic process, especially when faced with uncertain or
unexpected plant conditions [H.1 (a)].
29 Enclosure
Enforcement. Technical Specification 5.4.1.a, Procedures, required that written
procedures be established and implemented covering activities specified in Appendix A,
Typical Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33, Quality
Assurance Program Requirements (Operation), February 1978. Regulatory Guide 1.33,
Appendix A, Section 2.i, requires procedures for plant shutdown to hot standby.
Contrary to the above, on August 21, 2009, operators failed to implement
Procedure GEN-OO-005, Minimum Load to Hot Standby. Specifically the operators
failed to control and maintain steam generator water levels between 40-60 percent as
required in Step 7.4 of Section 7.0, Final Conditions. Because of the very low safety
significance and Wolf Creeks action to place this issue in their corrective action program
as Condition Report 00019295, this violation is being treated as a noncited violation in
accordance with Section VI.A.1 of the Enforcement Policy: NCV 05000482/2009007-09,
Failure to Adequately Control Steam Generator Water Levels.
1R8 Verification of Meeting Reporting Requirements
a. Inspection Scope
The team reviewed the conditions which occurred due to the event and the reports the
licensee made to the NRC per 10 CFR Part 50.72, Immediate Notification
Requirements for Operating Nuclear Power Plants, and 10 CFR Part 50.73, Licensee
Event Report System. The team also interviewed key personnel from the operations,
licensing, and emergency planning departments to discuss the content of and bases for
their reports.
b. Findings and Observations
No findings of significance were identified. The review of Licensee Event
Report 05000482/2009-002-00 issued for the event are discussed in Section 4OA3 of
this report.
1R9 Review of Compliance with Technical Specifications
a. Inspection Scope
The team reviewed the conditions which occurred during and after the event relative to
the actions taken by the licensee to review the licensees compliance to their technical
specifications. The team also interviewed key personnel from the operations and
licensing departments.
b. Findings and Observations
One finding of significance is documented in Section 4OA7 of this report.
1R10 Review of Licensees Decision to Maintain the Plant in Mode 3 After the Event
a. Inspection Scope
The team reviewed the conditions which occurred after the event, specifically relative to
the licensees decision to keep the plant in a hot standby condition rather than opting to
30 Enclosure
shut down and cool down the plant. The team reviewed plant procedures and
interviewed key personnel from the operations and licensing departments in this effort.
b. Findings and Observations
No findings of significance were identified.
1R11 Review of Application of Emergency Action Level Scheme
a. Inspection Scope
The team reviewed the plant conditions which occurred after the event, specifically
relative to whether the conditions met any entry conditions which would have required
the licensee to declare a Notice of Unusual Event. The team reviewed plant procedures
and interviewed key personnel from the emergency planning, operations, and licensing
departments in this effort.
b. Findings and Observations
NRC inspectors reviewed licensee Procedure APF 06-002-01, Emergency Action
Levels (EAL). The inspectors noted that the offsite power feeds to the 4 kV essential
NB system busses were not restored until 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 50 minutes following the event,
and the licensee did not report a Notice of Unusual Event. The team concluded this was
in accordance with the licensees EAL procedures because those procedures described
that power interruptions to the NB transformers for less than 15 minutes would be
considered momentary power losses and would not be required to be declared as a
Notice of Unusual Event.
The team observed that any interruption of power to the 4 kV essential busses (as
described in their EAL basis document) would have been difficult to recover from in less
than 15 minutes. Because Wolf Creek training documents and the implementing
emergency action level procedure specified restoring power to the NB transformers (and
not the 4 kV busses) and did not emphasize when the 15 minutes to restore power to the
4 kV NB essential bus should start, the inspectors determined that no findings of
significance had occurred.
Because they observed a disparity between the licensees EAL procedure and bases,
the team reviewed the potential scenario of having 15 minutes to restore power to the 4
kV busses alluded to in the EAL bases. The team reasoned that much of the 15 minutes
could be used by the shift manager/emergency coordinator to verify that the crew is
correctly performing its emergency response immediate actions, obtaining emergency
action level procedural guidance, assessing the plant to determine which emergency
action levels may be applicable, diagnosing the plant event effect on the switchyard and
the 4 kV NB essential bus support components and determining what available
personnel can be diverted from the emergency procedures and fire brigade response
duties. The shift manager may also be involved in communications with the
transmission grid operator to understand the grid status during this time. The team
concluded that the time needed to perform these actions coupled with the time to
perform bus power restoration Procedure OFN-NB-030, Loss of AC Bus NB01 (NB02),
could consume much, if not all, of the prescribed 15 minutes to restore power to the
NB busses had the procedure specified that the 15 minutes would start at the initiation of
31 Enclosure
the loss of all offsite power. From this, the inspectors determined that performing the
associated emergency procedures would severely challenge a crews resources making
it questionable whether the crews actual event response would ever be to able restore
offsite power to the 4 kV NB essential busses within 15 minutes, requiring the licensee
would have had to declare a Notice of Unusual Event.
The team also noted other factors specific to the August 19, 2009, loss of offsite power
event which would prolong the time to restore power. During this event, operators took
27 minutes to complete the procedural steps which directed them to transition to bus
restoration Procedure OFN-NB-030. Also, reports from licensee personnel of smoke
near the NB system transformers during the event that day, the presence of actuated fire
alarms in the nearby turbine building and auxiliary building during the event that day, and
the presence of a trouble alarm for each of the NB system transformers were factors
which could have influenced the emergency coordinators decision that power could be
restored to the 4 kV NB essential busses within 15 minutes.
The team shared their observations with the licensee. The licensee entered this
apparent procedural disparity condition into their corrective action program. .
4. OTHER ACTIVITIES
4OA3 Event Follow-up (71153)
(Closed) Licensee Event Report 05000482/2009-002-00: Loss of Offsite Power due to
Lightning
Licensee Event Report 05000482/2009-002-00 was issued on October 17, 2009, after
the onsite portion of the inspection. The events and facts detailed in this Licensee Event
Report were covered and reviewed as part of this special inspection. The licensee has
initiated appropriate corrective actions. No findings of significance were noted. This
Licensee Event Report is closed.
(Closed) Licensee Event Report 05000482/2009-004-00: Feedwater Isolation on High
Water Level in A Steam Generator
Licensee Event Report 05000482/2009-004-00 was issued on October 18, 2009, after
the onsite portion of the inspection. The events and facts detailed in this Licensee Event
Report were covered and reviewed as part of this special inspection. The licensee has
initiated appropriate corrective actions. One finding of significance was noted and is
contained in Section 1R7 of this report. This licensee event report is closed.
4OA6 Meetings, Including Exit
On September 25, 2009, the team presented the preliminary results of this inspection at
the end of the onsite week to Mr. Rick A. Muench, President and Chief Executive Officer,
and other members of his staff who acknowledged the findings. The team verified that
no proprietary information was retained.
On December 22, 2009, the team leader presented the final results of the inspection to
Mr. Matt Sunseri, Vice President Operations and Plant Manager, and other members of
the licensee staff who acknowledged the findings. The team verified that no proprietary
information was retained.
32 Enclosure
4OA7 Licensee-Identified Violations
The following violation of very low safety significance (Green) was identified by the
licensee and is a violation of NRC requirements which meets the criteria of Section VI of
the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a noncited
violation.
Technical Specification 5.4.1, Procedures, required that written procedures be
established and implemented covering activities specified in Appendix A, Typical
Procedures for Pressurized Water Reactors, of Regulatory Guide 1.33, Quality
Assurance Program Requirements (Operation), February 1978. Regulatory Guide 1.33,
Appendix A, Section 6.c, required procedures for combating emergencies and other
significant events. Contrary to the above, from November 2, 2007, to August 19, 2009,
Procedure EMG ES-02, Reactor Trip Response, was inadequate for restoration of
essential service water cooling to instrument air compressors. Specifically, Step 5a,
response not obtained, incorrectly directed operators to locally open valves EFHV0043
and EFHV0044. This action takes the valves out of their normal position and prevents
their automatic isolation on a high flow condition. The unavailability of this automatic
feature makes each train of essential service water inoperable. This finding is greater
than minor because it was associated with the Mitigating Systems Cornerstone attribute
of procedural quality and it affected the cornerstone objective to ensure the availability,
reliability, and capability of systems that respond to initiating events to prevent
undesirable consequences. Using Manual Chapter 0609.04, Phase 1 - Initial
Screening and Characterization of Findings, the issue screened as very low safety
significance because it was not a design or qualification deficiency that resulted in a loss
of operability or functionality, did not create a loss of system safety function of a single
train for greater than the technical specification allowed outage time and did not affect
seismic, flooding, or severe weather initiating events. This finding was entered in the
licensees corrective action program as Condition Report 00019660
33 Enclosure
ATTACHMENT 1
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
T. Birzer, Lake Water Engineering
B. Blecha, Supervisor, Maintenance
W. Camp, Control Room Supervisor
A. Critchly, Corrective Action Technical Specifications
T. Damashek, Superintendent, Operations Support
D. Dees, Superintendent, Operations
B. Dorathy, Supervisor, Systems Engineering
T. Dougan, Quality
D. Erbe, Manager, Security
R. Flannigan, Manager, Regulatory Affairs
M. Free, Senior Nuclear Safety Officer
C. Garcia, Supervisor, Systems Engineering
R. Gardner, Manager Quality, Performance Improvement and Assessment
T. Garrett, Vice President, Engineering
D. Gholson, Reactor Operator
S. Good, Security
S. Hedges, Vice President, Oversight
D. Helm, Supervisor, Supervisor, Systems Engineering
S. Henry, Manager, Operations
R. Hubbard, Shift Manager, Operations
W. Kennamore, Manager Nuclear Engineering
B. Ketchum, Probabilistic Safety Analysis, Nuclear Engineer
M. Kewley, Senior Nuclear Safety Officer
G. Kinn, Supervisor, Nuclear Engineering
S. Koenig, Manager, Corrective Action
B. Masters, Supervisor, Design Engineering
D. McClure, Senior Reactor Operator
R. Muench, President and Chief Executive Officer
B. Muilenburg, Licensing
J. Myers, Reactor Operator
G. Neisis, Manager Design
W. Norton, Manager IPS/Scheduling
G. Pendergrass, Manager Systems Engineering
C. Peterson, Senior Nuclear Safety Officer
D. Phelps, Owners Representative
L. Ratzlaff, Manager Support Engineering
E. Ray, Manager, Chemistry/Health Physics
L. Rockers, Licensing
L. Solorio, Design Engineer
M. Sunseri, Vice President Operations and Plant Manager
B. Vickery, Supply Chain Manager
M. Westman, Manager, Training
S. Yunk, Senior Reactor Operator/Shift Technical Advisor
A1-1 Attachment 1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
05000482/2009007-01 FIN Failure to Enter Adverse Conditions into the Corrective
Action Program (Section 1R2)05000482/2009007-02 NCV Failure to Perform an Operability Evaluation (Section 1R2)05000482/2009007-03 NCV Failure to Correctly Screen Essential Service Water Piping
Leaks for Significance (Section 1R2)05000482/2009007-05 NCV Failure to Ensure Adequate Acceptance Criteria and Extent
of Condition Guidance in Lake Water and Corrective Action
Program Procedures (Section 1R4)05000482/2009007-06 NCV Inadequate Procedure Resulted in Failure to Discover
Essential Service Water System Leakage Following a Water
Hammer Event (Section 1R5)05000482/2009007-07 NCV Failure to Initiate Timely Fire Protection Impairment Control
Permit and Implement Compensatory Measures
(Section 1R5)05000482/2009007-09 NCV Failure to Adequately Control Steam Generator Water Levels
(Section 1R7)
Opened
05000482/2009007-04 URI 345 kV Offsite Power System Compliance with General
Design Criterion 17 (Section 1R3)05000482/2009007-08 URI Uncontrolled and Unanalyzed Room Environment Following
a Complete Loss of Offsite Power (Section 1R5)
Closed
05000482/2009-002-00 LER Loss of Offsite Power due to Lightning (Section 4OA3)
05000482/2009-004-00 LER Feedwater Isolation on High Water Lever in A Steam
Generator (Section 4OA3)
DOCUMENTS REVIEWED
PROCEDURES
NUMBER TITLE REVISION / DATE
0400 Westar Energy, Inc. Transmission Operations Procedure July 28, 2008
0414 Westar Energy, Inc. Transmission Operations Procedure May 1, 2009
A1-2 Attachment 1
PROCEDURES
NUMBER TITLE REVISION / DATE
ADM 01-100 Lake Water Systems Inspection, Monitoring and March 21, 2005
Maintenance
AFP 06-002-01 Emergency Action Levels 12
AI 21-100 Operations Guidance and Expectations 15
AI 26A-003 Regulatory Evaluations (Other Than 10 CFR 50.59) 10
AI 28A-001 Level 1 CR Evaluation (IIT) 10
AI 28A-006 Level 3 Condition Report Evaluation 7
AI 28A-007 Level 2 CR Evaluation 2
AI 28A-008 Level 4 CR Evaluation 2
AI 28A-010 Screening Condition Reports 3A
ALR KC-888 Fire Protection Panel KC-008 Alarm Response 16
ALR 831 ESF Transformer XNB01 3
ALR832 EXF Transformer XNB02 3
ALR 00-019D XNB01 Transformer Trouble 9
ALR 00-022D XNB02 Transformer Trouble 9
ALR 00-127D Condensate Storage Tank Level LoLo 2 7
ALR 00-127E Condensate Storage Tank Level LoLo 1 10A
AP 10-10 Fire Protection Impairment Control. 23
AP 10-100 Fire Protection Program 14
AP 10-103 Fire Protection Impairment Control 11 and 21
AP 10-104 Breach Authorization 22
AP 10-106 Fire Preplans 8
AP 21-001 Conduct of Operations 43
AP 23I-001 Fatigue Management 1
AP 23L-001 Lake Water Supply Corrosion and Fouling Programs March 21, 2005
A1-3 Attachment 1
PROCEDURES
NUMBER TITLE REVISION / DATE
AP 26C-004 Technical Specification Operability 20
AP 28-001 Operability Evaluations 17
AP 28A-100 Condition Reports 10
AP-21C-001 WCGS/Westar Substation 9
APF 06-002-01 Emergency Action Levels 12
BD-EMG C-0 Loss of All AC Power 11
EMG-E-0 Reactor Trip or Safety Injection 24
EMG ES-02 Reactor Trip Response 18
EPP 06-001 Control Room Operations 13
GEN-OO-005 Minimum Load to Hot Standby 62
OFN AF-025 Unit Limitations 27
OFN KC-016 Fire Response 22
OFN-NB-030 Loss of AC Emergency Bus NB01(NB02) 22
STN PE-040G Transient Event Walkdown 1
STS NB-005 Breaker Alignment 4A
STS RE-004 Shutdown Margin Determination 25
SYS NB-201 Transferring NB01 Power Sources 42
SYS NB-202 Transferring NB02 Power Sources 37
QCP 20-518 Visual Examinations of Heat Exchangers and Piping 5A
Components
WCRE-13 Lake Water Systems Structural Integrity Program 5A
DRAWINGS
NUMBER TITLE REVISION
M-12 AL01 Auxiliary Feedwater System Drawing
M-12 AN01 Piping and Instrumentation Diagram Demineralized Water 8
A1-4 Attachment 1
DRAWINGS
NUMBER TITLE REVISION
Storage and Transfer System
M-12 AP01 Condensate Storage and Transfer System 8
M-12 FC02 Auxiliary Turbines System Drawing
M-13 AL01 Piping Isometric Auxiliary Feedwater Pumps Suction Piping 10
10466-J-110- Instrument Loop Diagram for Auxiliary Feedwater Supply 0
0357-W06 Pressure from Condensate Storage Tank
TI 2AC-175 Foxboro Spec 200 Dynamic Compensator 0
Gould Pumps Inc. Floor Drain Tank Pumps 3
765502
CONDITION REPORTS
00003599 00006780 00007499 00007502 00007508
00007509 00007510 00007511 00009519 00009688
00011704 00012990 00013805 00014261 00014930
00015520 00015521 00015574 00015634 00016358
00016901 00016905 00017900 00018217 00018646
00018785 00018817 00019079 00019219 00019248
00019284 00019295 00019308 00019320 00019660
00019716 00019724 00019806 00019918 00019951
00019955 00019960 00020022 00020050 00020068
00020097 00020099 00022247 2007-001531 2007-001780
2007-001993 2007-002009 2007-002162 2007-002656 2007-003350
2007-003378 2007-004125 2007-004126 2007-004127 2007-004128
2007-004129 2007-004130 2007-004131 2007-004132 2008-000116
2008-001448 2008-001450 2008-001456 2008-001457 2008-001458
2008-001459 2008-001479 2008-001481 2008-001485 2008-001494
2008-001511 2008-001642 2008-001660 2008-001797 2008-001819
2008-001932 2008-002280 2008-002785 2008-003745 2008-004536
2008-004592 2008-004983 2008-005075 2009-000250
PERFORMANCE IMPROVEMENT REQUESTS
1994-08237 1995-0558 1997-03965 2002-083 2000-2122
2003-2178 2004-2435 2004-2441 2004-2683 2005-2167
2005-2619 2007-003378 2008-005913
A1-5 Attachment 1
CALCULATIONS
NUMBER TITLE REVISION /
DATE
01030-C-001 Reanalysis of Pipe Stress Calculation P-093A for Containment
Cooler Return Line
01030-C-002 Incorporate Dynamic Loads due to Water Hammer on May 17, 2001
Containment Coolers
FL-01 Flooding of the Auxiliary Building 1
FL-03 Flooding of Individual Aux Bldg Rooms 0
M-FL-04 Summary of Flood Levels in all Auxiliary Building Rooms due 1
to Pipe Break or Crack
XX-E-013 Post Fire Safe Shutdown (PFSSD) Analysis including change 1
notices
XX-E-009 System NB,NG,PG Undervoltage/Degraded Voltage Relay 1
Setpoints, including attachments
XX-E-006 AC System Analysis including attachments and change 5
notices
Engineering Change Package 05818 for Containment Cooler
Support Installations
CORRESPONDENCE
NRC Generic Letter 96-06, Assurance of Equipment Operability and Containment Integrity during
Design-Basis Accident Conditions, September 30, 1996
NRC Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk and the Operability of
Offsite Power, February 1, 2006
ET 07-0003, Wolf Creek Nuclear Operating Corporation Response to NRC Additional Request for
Additional Information RE: NRC Generic Letter 2006-02, Grid Reliability and the Impact on Plant
Risk and the Operability of Offsite Power, January 1, 2007
WM 06-0011, Wolf Creek Nuclear Operating Corporation Response to NRC Generic Letter 2006-
02, Grid Reliability and the Impact on Plant Risk and the Operability of Offsite Power, March 31,
2006
Wolf Creek response to Generic Letter 96-06, January 29, 1997
Letter from Mel Gray, Subject: Request for Additional Information - Generic Letter 96-06,
Assurance of Equipment Operability and Containment Integrity during Design-Basis Accident
Conditions, June 18, 1999
NRC letter: Request for Additional Information Regarding Resolution of Generic Letter 2006-02,
Grid Reliability and the Impact on Plant Risk and the Operability of Offsite Power, December 3,
2006
A1-6 Attachment 1
CORRESPONDENCE
NRC letter: Revised Response Date for Request for Additional Information Regarding Resolution
of Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk and the Operability of
Offsite Power, December 13, 2006
NRC letter: Wolf Creek Generating Station - Closeout Letter for Generic Letter 2006-02, Grid
Reliability and the Impact on Plant Risk and the Operability of Offsite Power, May 10, 2007
NRC Information Notice 2007-01: Recent Operating Experience Concerning Hydrostatic Barriers
NRC Information Notice 2009-16: Spurious Relay Actuations Result in Loss of Power to
Safeguards Buses. (blue added 10-15-09)
NRC Regulatory Guide 1.101, Emergency Planning and Preparedness for Nuclear Power
Reactors, Revision 3
NEI 99-01, Methodology for Development of Emergency Action Levels, Revision 5
NRC Generic Letter 1989-13, Service Water System Problems Affecting Safety-Related
Equipment, January 29, 1990
LICENSEE EVENT REPORTS
NUMBER TITLE DATE
1995-006-00 Loss of Emergency Bus NB02 Due to Degraded Gasket December 7, 1995
on Motor Operator Cabinet
1995-006-01 Loss of Emergency Bus NB02 Due to Degraded Gasket February 1, 1996
on Motor Operator Cabinet
1999-005-00 Engineered Safety Features Actuation Because of Loss June 11, 1999
of Number 7 Transformer
2004-003-00 Automatic Start of B Emergency Diesel Generator Due May 5, 2004
To Start-Up Transformer Cable Ground Fault
2007-001-00 Emergency Diesel Out of Service Longer than Technical September 6, 2007
Specification Allowed Outage Time
2008-004-00 Loss of Offsite Power Event when the Reactor was
Defueled
ACTION PLAN DETAIL REPORTS
NUMBER TITLE DATE
1047 Actions for Switchyard Restoration Issues August 24, 2007
1100 SOER and Non-SOER Evaluation Guidance and SOER January 30, 2008
Effectiveness Reviews
1273 PIR 2007-003378 Action Plan - SOER Effectiveness February 20, 2008
Review
A1-7 Attachment 1
ACTION PLAN DETAIL REPORTS
NUMBER TITLE DATE
1703 CR 2007-004128 Corrective Actions May 13, 2009
1806 Critical Component Review of the Switchyard March 17, 2009
1890 EDG Alarm Acknowledge November 22, 2008
1909 CAP for CR 2008-001797 June 27, 2008
2032 CR 2008-001457 Action Plan February 27, 2009
2186 Revise AP 12-001 December 17, 2008
OPERABILITY EVALUATIONS
NUMBER TITLE REVISION
EF 09-007 Post ESFAS Water Hammer Evaluation 0
GK-08-004 Control Room AC Unit SGK04B and SGK05B Heat 0
Exchangers
OPERATING EXPERIENCE DETAIL REPORTS
NUMBER TITLE DATE
323 Information Notice 2007-14, Loss of Offsite Power and Dual- 9/20/2007
Unit Trip at Catawba Nuclear Generating Station
71 Information Notice 2006-06, Loss of Offsite Power and Station
Blackout are More Probably During Summer Period
WORK ORDERS
07-294733-000 08-302566-000 08-305239-000 08-305240-000 08-305244-000
08-305281-000 08-305289-000 08-305312-000 08-305312-001 08-305313-000
09-305434-001 09-305838-00 09316569-000 09-319476-000 09-320505-000
09-320505-001
HISTORY OF ESSENTIAL SERVICE WATER LEAKS
TIME DESCRIPTION FLOW VELOCITY, POSITION OF LEAK
2002 CCW HX drain leak, galvanic and under 0 Side of vertical pipe
deposit pitting
A1-8 Attachment 1
HISTORY OF ESSENTIAL SERVICE WATER LEAKS
TIME DESCRIPTION FLOW VELOCITY, POSITION OF LEAK
2005 SW discharge bypass line leak, under 0, Stagnant Bottom segment of pipe
deposit corrosion EA129HBC-16
2005 ESW - AFW leak, under deposit 0, Stagnant Bottom segment of pipe
corrosion EF054HBC-8
2007 SGN01D containment air cooler 6 return ~ 6.0 Side of vertical pipe
header, under deposit pitting
2009 ESW B 30 return line, through-wall pit 1.6 Bottom segment of pipe
EF138HBC-30
2009 ESW B 18 supply leak at weld 5.9 Weld area, side of pipe
EF150HBC-18
2009 ESW A 8 room cooler return line leak 0.9/1.6 Bottom segment of pipe
EF049HBC-8
MISCELLANEOUS DOCUMENTS
NUMBER TITLE REVISION / DATE
Posttrip Review Data Package August 19, 2009
Technical Specifications and Bases
Operating License
Control Room Logs August 19-26, 2009
Outage Center Logs August 19-26, 2009
Table 2-2 Offsite Dose Calculation Manual 6
Table 3-2 Offsite Dose Calculation Manual 6
WCAP-12231 Station Blackout Coping Assessment for Wolf Creek April 15, 1989
Generating Station
Safety Evaluation and Request for Additional Information January 16, 1992
Concurring Station Blackout Analysis for the Wolf Creek
Generating Station
Wolf Creek Generating Station - Supplemental Safety June 16, 1992
Evaluation Regarding the Stat ion Blackout Rule
DCP 07687 GE Magne-Blast Circuit Breaker Replacement 5
A1-9 Attachment 1
MISCELLANEOUS DOCUMENTS
NUMBER TITLE REVISION / DATE
Simplified Switchyard Drawing
Zone 117 Device List
Westinghouse Instructions for Metering Accuracy Capacitor June 1982
Voltage Transformer Type PCA-9
Wolf Creek Generating Station License Renewal Application 22
ACE Documents for CR 18785 September 21, 2009
2938 Information on ITIP: Response to NRC Information September 22, 2009
Notice 95-04
2507 Information on ITIP: Response to NRC Information September 22, 2009
Notice 93-83
2275 Information on ITIP: Response to NRC Information September 22, 2009
Notice 93-17
946 Information on ITIP: Response to NRC Information September 22, 2009
Notice 88-75
Switchyard SPV Evaluation
Switchyard SPVs and Mitigating Strategies
Switchyard Component IDs
Notes regarding CR 2008-001457
SER 4-06 INPO Significant Event Re port: Dual-Unit Loss of Off-Site September 25, 2006
Power
2898 CDE Detail Report: Extension Request for CR 2008-005913 May 13, 2009
DOBLE Test Assistant - Autotransfer without Tertiary
Bushing Analysis Test Data
12708 Engineering Disposition: Evaluation of ESW Water Hammer 1
Event Due to Loss of Offsite Power
Licensing Evaluation/Reportability Evaluation Request
2008-023/PIR 2008-001797
93 Operability/Reportability Detail Report November 21, 2008
Line loss spreadsheet March 6, 2004 through
A1-10 Attachment 1
MISCELLANEOUS DOCUMENTS
NUMBER TITLE REVISION / DATE
August 19, 2009
Westar Energy Root Cause Analysis Report: Root Cause March 30, 2009
Analysis Performed at Management Discretion
Incident Investigation Report 09-002 for CR 00019245 October 1, 2009
NRC Question 1, Request 12821
NRC Question 2, Request 12831
NRC Question 3, Request 12841
NRC Question 4, Request 12851
Modification Pipe Support Mod on GN Sys for Water Hammer 2
Package 05818
STN PE-040G Completed Surveillance of Transient Event Walkdown April 7, 2008
LR1007001 Emergency Action Levels and Protective Action
Recommendations Training Material
Updated Safety Analysis Report Section 3.9(N), Table
3.9 (N) - 13 Component Cyclic or Transient Limits
Table 4: Cycle Summary - Current Analysis Period -
11/1/07 through 8/18/08
WCAP 12231, Station Blackout Coping Assessment for Wolf April 15, 1989
Creek Generating Station
Computer Point Trend for Points ALF0002 and AEL0517 August 21, 2009
Change # 12798 Engineering Disposition Evaluation of Essential Service 1
Water Water Hammer Event due to Loss of Offsite Power
Simulator Training Performance Evaluation Summary for October 15, 2008
Crew - D
IIT 09-002 For Condition Report 00019245, Loss of Offsite Power and September 22, 2009
Plant Trip
Post Trip Review Data Package for October 7, 2004
Purchase Order 745187/0 for Engineering Services to March 18, 2009
Address Water Hammer Issues
A1-11 Attachment 1
UNITED STATES
NUCLEAR RE GULATO RY COM M I SSI ON
R EGI ON I V
612 EAST LAMAR BLVD, SUI TE 400
ARLIN GTON, TEXAS 76011-4125
MEMORANDUM TO: Richard Deese, Senior Project Engineer, Team Leader
Projects Branch B
Division of Reactor Projects
David Dumbacher, Senior Resident Inspector
Projects Branch B
Division of Reactor Projects
Jim Medoff, Senior Mechanical Engineer
Division of License Renewal
Office Nuclear Reactor Regulation
FROM: Dwight Chamberlain, Director
Division of Reactor Projects
SUBJECT: CHARTER FOR SPECIAL INSPECTION INVOLVING THE LOSS OF
OFFSITE POWER AND REACTOR TRIP AT WOLF CREEK
GENERATING STATION
In response to the loss of offsite power and subsequent reactor trip which occurred at Wolf
Creek Generating Station on August 19, 2009, a special inspection will be performed. You are
hereby designated as the special inspection team leader.
A. Basis
On August 19, 2009, during stormy weather in the area, Wolf Creek Generating Station
experienced a loss of all 345 kV power to its switchyard. All reactor coolant pumps,
condensate pumps and remaining secondary cooling equipment lost power resulting in
the inability to reject heat to the condenser. The main turbine tripped followed by a
reactor trip. With the condenser unavailable, cooling was supplied by the auxiliary
feedwater system and discharged through the atmospheric relief valves.
With offsite power unavailable, the emergency diesel generators started and powered
emergency loads as required.
Offsite power was noted to have numerous interruptions in the last year, with momentary
line outage occurring relatively frequently. The Rose Hill offsite power line experienced
brief or momentary line outages at least 7 times within the last year. Faulty equipment
on the Rose Hill line which failed to block the effects of the La Cygne line lighting strike
is believed to have led this loss of single offsite power line event into a complete loss of
offsite power.
A2-1 Attachment 2
Also the essential service water system experienced a through-wall leak concurrent with
the event. A 3/8-inch hole was revealed in the header leading to the emergency core
cooling system room coolers as water was discovered streaming from the essential
service water piping after the event. Further evaluation of the area around the hole
uncovered another adjacent area that was below minimum wall. These and previously
identified leaks lead to questioning the reliability of the essential service water system.
A regional Senior Reactor Analyst (SRA) preliminarily estimated the Incremental
Conditional Core Damage Probability for this issue to be 6.1 x 10-6, which falls in the
region which recommends a special inspection. A special inspection will be performed
since there are questions with the reliability of offsite power.
B. Scope
1. Develop a complete sequence of events related to the event.
2. To support review of the problem identification and resolution aspects of the
event:
a. Review operating experience involving prior opportunities to identify and evaluate
action implemented at Wolf Creek from industry Operating Experience.
b. Review the licensees root cause analysis for the event initiator and determine if
it was conducted to a level of detail commensurate with the significance of the
problem.
c. Determine if the licensees corrective actions have addressed the extent of
condition and assess whether these actions are adequate to prevent recurrence.
3. Perform the following to review the licensees offsite power system:
a. Review the licensees actions for prior instances of loss of the offsite power lines
and whether the licensees actions were commensurate with safety for the
number of previous line failures.
b. Assess the licensees ability to meet the General Design Criteria requirements for
independence of the offsite power lines in light of conditions surrounding the
event.
4. Perform the following to review the licensees essential service water system:
a. In light of the leak in the essential service water system that developed, review
the scope and depth of the licensees actions for the monitoring and prevention
of degradation of the essential service water system piping [extent of condition
check]. In this review, verify the licensees commitments to Generic Letter 89-13,
if applicable.
b. Review the licensees bases for insulating the essential service water piping in
the auxiliary building.
c. Review the application of ASME Code Case N-513-2, especially with regard to
choice and acceptability of the additional (extent of condition required by ASME
A2-2 Attachment 2
Code Case and others) ultrasonic testing samples performed for the identified
areas.
d. Evaluate the adequacy of the repairs to the 3/8-inch hole in the essential service
water pipe that occurred during the event and the subsequent below minimum
wall thickness area.
5. Perform the following to review the performance of plant systems during the
event:
a. Review the acceptability of the observed pressure oscillations observed on the
suction of the auxiliary feedwater pumps and their impact on system operability
and technical specifications.
b. Determine if reasonable evidence existed for deduction that a water hammer
event occurred in the essential service water system and whether licensee
actions following the event were sufficient for such an evaluation.
c. Review the design and operation of the internal flood control features in the plant,
in light of being able to handle a slightly larger leak during a sustained loss of
offsite power.
d. Determine if any of the radiation monitor failures experienced in the event would
have hampered further actions (i.e., implementing the emergency plan).
e. Review the actions taken for the loss of fire detection capability in the auxiliary
building during the event. Establish if this loss was anticipated in plant design.
6. Review the post-trip report for adequacy and whether the conclusions the
licensee drew are supported by the report.
7. Review the causes of the high level in Steam Generator A that occurred the day
after the event.
8. Verify the licensee met the proper reporting requirements of 10 CFR 50.72 and
10 CFR 50.73. Determine if the licensee has plans to issue a Licensee Event
Report to document this issue.
9. Review the licensees compliance with the Technical Specifications.
10. Review the licensees decision to maintain the plant in Mode 3 (feeding from the
condensate storage tank with auxiliary feedwater and dumping steam with the
atmospheric relief valves) for an extended period of time.
11. Determine if the licensee correctly applied the Emergency Action Levels and if
the Emergency Action Levels are appropriate.
12. Support assessment of risk significance by performing the following:
a. Collect facts to support an accurate portrayal of exposure time for the LOOP.
b. Collect facts to support proper crediting of the licensees ability to recover offsite
power sources within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> as assumed in the risk assessment. Ensure to
A2-3 Attachment 2
include in the assessment the trouble annunciators that existed on the safety
transformers during the event.
c. Collect facts to support/refute crediting the licensees ability to recover offsite
power within 15 minutes in support of establishing low pressure recirculation for a
reactor coolant pump seal LOCA.
d. Collect facts to verify/refute classification as a grid-centered loss of offsite power
for risk assessment purposes.
e. Verify the risk assessment assumption that no test or maintenance were in
progress at the time of the event.
f. Collect facts to support the senior risk analysts in making a realistic assumption
of the unreliability of the essential service water system.
g. Determine if the difficulties experienced with the startup and main feed pumps on
the prior startup and the startup from this event represented a loss of mitigation
equipment.
h. Verify the function of the main steam isolation valve rupture discs was per design
and did not preclude use of any mitigation equipment when they ruptured.
C. Guidance
Inspection Procedure 93812, Special Inspection, will be used during this inspection. The
inspection should emphasize fact-finding in its review of the circumstance surrounding this
event. It is not the responsibility of the team to examine the regulatory process. Safety
concerns identified that are not directly to the event should be reported to the Region IV office
for appropriate action.
The team will report to the site and begin inspection no later than September 21, 2009. While
onsite, you will provide daily status briefings to Region IV management, who will coordinate with
the Office of Nuclear Reactor Regulation, to ensure that all other parties are kept informed.
Depending on the outcome of the inspection, inspection results will be documented in Special
Inspection Report 05000482/2009007. This report will be issued within 45 days of the
completion of the inspection.
This guidance may be modified should you develop significant new information that warrants
review. Should you require support for the final determination of the risk significance of any
issue, contact Michael Runyan at (817) 860-8142. Should you have any questions concerning
this guidance, contact Vince Gaddy at (817) 860-8141.
A2-4 Attachment 2
ATTACHMENT 3
NRC Technical Review of the August 19, 2009, Self-Revealing Flaw in Essential Service
Water System Piping
General Summary
The Wolf Creeks flaw evaluation is acceptable. The licensee used Code Case N-513-2, the
ASME Code Section XI, Appendix H, and ASME Code,Section III, ND-3600 to perform the flaw
evaluations. The licensee did not use information outside of the ASME Code (other than the
wear rate. (See questions # 4 and discussion below).
In accordance with N-513-2, the licensee will monitor the leakage each shift, perform UT of the
pinhole every 30 days, and perform UT at a minimum 10 locations. The licensee performed a
temporary repair (encapsulation) at the pinhole location and will perform a code repair in the
next refueling outage.
Suggested Questions to Ask the Licensee
1. On page 3 of 5 of the licensees engineering disposition paper, the licensee stated that
Engineering shall be notified of any changes in the leakage or flaw growth. This is an open
ended statement (not useful in terms of NRC regulatory/enforcement actions) because there is
no commitment in the licensees part as to what are the acceptance criteria for the leakage or
flaw growth or the corrective actions that they will do. It is not clear what the licensee would do
if there is a change in the leakage or if there is a flaw growth that extends outside the
encapsulation. It is not clear at what leak rate or flaw growth the licensee will take corrective
action. The licensee needs to clarify the specific acceptance criteria on leak rate and flaw
growth and discuss corresponding actions.
2. The licensee needs to clarify why they used the ASME Code,Section XI, Appendix H to
evaluate the flaw(s) instead of the ASME Code,Section XI, Appendix C, which is required by
Code Case N-513-2. [see the basis of this question below]
3. The licensee stated that it will perform augmented UT on 10 locations (on page 3 of 5 of the
Engineering report). However, it is not clear whether these 10 locations are in the same
degraded pipe or in sister pipes (or pipes in the same system). At a minimum, the licensee
needs to check the wall thickness of the degraded pipe to ensure that there are no other
locations in the pipe that have the corrosion problems. The licensee also needs to UT sister
pipes in the affected piping system. The licensee needs to clarify where are the 10 locations
that will be examined to satisfy the requirements of Code Case N-513-2, paragraph 5.0 [see
discussion below].
4. Appendix 2 of the licensees flaw evaluation calculates the wear rate of the pinhole. The
wear rate was calculated by dividing the difference between the nominal wall thickness (0.322)
and the final wall thickness (which is zero because of the pinhole) by the operating years. This
wear rate method assumes that general corrosion at the pinhole is directly proportional to the
operating time (i.e., a linear relationship) and that corrosion initiated from day one of the
commercial operation. The licensee needs to justify the linear relationship for the wear rate.
[See discussion below]
A3-1 Attachment 3
Discussions
Appendix 1 of the licensees flaw evaluation---
In Appendix 1 of the licensees flaw evaluation, the licensee back-calculated the allowable pipe
thickness based on the stress equations in ASME Code,Section III, ND-3600 with various load
combinations and associated allowable stresses. Using this approach, the licensee calculated
the minimum pipe wall thickness.
The summary page of Appendix 1 shows the minimum thickness for each piping load
combination. The allowable thickness ranges from 0.0035 inches to 0.0595 inches, depending
on the load combinations. The nominal wall thickness is 0.322 inches. The licensee selected
the allowable thickness of 0.1 inches. This is conservative because it is more than the
calculated wall thickness (> 0.0595). If the pipe wall thickness falls below 0.1 inches, the pipe
does not meet the Section III code allowable, does not meet the design conditions, and is,
therefore, inoperable.
The wall thickness at the pinhole location is zero and is below the allowable thickness of 0.1
inches. However, the licensee has used Code case N-513-2 to accept the structural integrity of
the pipe considering the pinhole location (i.e., operable but degraded).
I do not know if the licensee has performed wall thickness measurement on various locations of
the leaking pipe to confirm that the rest of the leaking pipe satisfies the allowable thickness of
0.1 inches. Question # 3 above should confirm this issue.
Appendix 2 of the licensees flaw evaluation
Appendix 2 calculates the wear rate of the pinhole. The wear rate was calculated by dividing
the difference between the nominal wall thickness (0.322) and the final wall thickness (which is
zero because of the pinhole) by the operating years (20 years). This method assumes that
general corrosion at the pinhole is directly proportional to the operating time (i.e., a linear
relationship) and that corrosion initiated from day one of the commercial operation. I do not
know if this linear relationship for the wear rate is correct. In addition, if the inside of the pipe is
coated with epoxy or some protective coating then the corrosion will not initiate until some years
later. If the pipe is not coated inside, it will still take a few years before corrosion initiates. If the
corrosion initiates not from day one but started several years later, the denominator in the above
wear rate equation will be less than 20 year. This will make the wear rate higher and more
conservative. The licensees wear rate may not be conservative because it assumes the
corrosion starts on day one of the commercial operation. The licensee needs to justify its
method of wear rate calculation. [note that N-513-2 does not specify the flaw growth rate for
general corrosion. The flaw growth rate in N-513-2 is for planar flaws which is not applicable to
general corrosion in service water line at wolf creek. Therefore, there is no requirement for the
licensee to use certain wear rate method. All we can do is to ask why they think their method is
acceptable]
Appendices 3 and 4 of the licensees flaw evaluation--
Appendices 3 and 4 analyze the general corrosion/pinhole (which is a nonplanar flaw) as two
planar flaws to show that the pipe with the 2 planar flaws has sufficient fracture toughness to
resist catastrophic failure. Code Case N-513-2, paragraph 3.0(f) allows evaluating a through
wall penetration as two independent planar flawsaxial flaw and circumferential flaw. Appendix
A3-2 Attachment 3
3 of the licensees flaw evaluation evaluates the axial flaw. Appendix 4 of the licensees flaw
evaluation evaluates the circumferential flaw.
Appendices 3 and 4 use information in Section XI, Appendix H instead of Section XI, Appendix
C, which is required by Code Case N-513-2. Code Case N-513-2, paragraph 3.0(c) requires
that for planar flaws in ferritic piping the evaluation procedure of ASME Section XI Appendix C
be used and N-513-2 cites several Appendix C subparagraphs. However, the cited Appendix C
paragraphs do not appear in the 1998 Section through 2000 addenda of the ASME Code,
Section XI, which I suppose is the code of record for Wolf Creek for the current ISI inspection
interval. Therefore, I believe that the licensee used Appendix H of the Section XI to perform the
flaw evaluation because Appendix C in the 1998 edition of the ASME Code, section XI, does not
contain flaw evaluation information that is required by N-513-2.
I have no problem with the licensee using the ASME Code,Section XI, Appendix H for its flaw
evaluation.
Appendix 3 demonstrates that the leaking pipe will not fail catastrophically because the
calculated stress intensity factor (Kmax) of the axial flaw (pinhole) is less than the stress
intensity factor of the pipe material (Kicallowable).
Appendix 4 demonstrates that the leaking pipe will not fail catastrophically because the
calculated stress intensity factor (Kmax) of the circumferential flaw (pinhole) is less than the
stress intensity factor of the pipe material (Kicallowable).
A3-3 Attachment 3