ML043060486

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IR 05000313-04-004, 05000368-04-004, on 06/24/2004 - 09/23/2004, ANO, Units 1 and 2; Adverse Weather Protection, Fire Protection, Maintenance Risk Assessments and Emergent Work Control, Operability Evaluations, Surveillance Testing, and Eve
ML043060486
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 10/28/2004
From: Troy Pruett
NRC/RGN-IV/DRP/RPB-D
To: Forbes J
Entergy Operations
References
IR-04-004
Download: ML043060486 (53)


See also: IR 05000313/2004004

Text

October 28, 2004

Jeffrey S. Forbes, Vice President,

Operations

Arkansas Nuclear One

Entergy Operations, Inc.

1448 S.R. 333

Russellville, Arkansas 72801-0967

SUBJECT: ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT

05000313/2004004 AND 05000368/2004004

Dear Mr. Forbes:

On September 23, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Arkansas Nuclear One, Units 1 and 2, facility. The enclosed integrated

report documents the inspection findings, which were discussed on September 28, 2004, with

you and other members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

This report documents one unresolved item concerning the potential unavailability of an

emergency diesel generator in Unit 1 due to a lube oil leak. This finding has potential safety

significance greater than very low safety significance. This finding did represent an immediate

safety concern until July 3, 2004, when your staff repaired a fitting associated with a

temperature switch. Also, this report documents one apparent violation regarding the potential

unavailability of a containment spray pump in Unit 2 due to a loose connection in the breaker

circuitry. This finding has potential safety significance greater than very low safety significance.

This finding did represent an immediate safety concern until August 9, 2004, when your staff

repaired the connection in the breaker circuitry.

In addition, the report documents three NRC-identified and two self-revealing findings of very

low safety significance (Green). Four of these findings were determined to involve violations of

NRC requirements. However, because of the very low safety significance and because they

are entered into your corrective action program, the NRC is treating these five findings as

noncited violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy.

Additionally, one licensee-identified violation, which was determined to be of very low safety

significance, is listed in Section 4OA7 of this report. If you contest these noncited violations,

you should provide a response within 30 days of the date of this inspection report, with the

basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control

Entergy Operations, Inc.

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Desk, Washington DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas

76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,

Washington DC 20555-0001; and the NRC Resident Inspector at Arkansas Nuclear One,

Units 1 and 2, facility.

In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Troy W. Pruett, Chief

Project Branch D

Division of Reactor Projects

Dockets: 50-313

50-368

Licenses: DPR-51

NPF-6

Enclosure:

NRC Inspection Report 05000313/2004004 and 05000368/2004004

w/Attachment: Supplemental Information

cc w/enclosure:

Senior Vice President

& Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Vice President

Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Manager, Washington Nuclear Operations

ABB Combustion Engineering Nuclear

Power

12300 Twinbrook Parkway, Suite 330

Rockville, MD 20852

Entergy Operations, Inc.

- 3 -

County Judge of Pope County

Pope County Courthouse

100 West Main Street

Russellville, AR 72801

Winston & Strawn

1400 L Street, N.W.

Washington, DC 20005-3502

Bernard Bevill

Radiation Control Team Leader

Division of Radiation Control and

Emergency Management

Arkansas Department of Health

4815 West Markham Street, Mail Slot 30

Little Rock, AR 72205-3867

James Mallay

Director, Regulatory Affairs

Framatome ANP

3815 Old Forest Road

Lynchburg, VA 24501

Entergy Operations, Inc.

- 4 -

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

Senior Resident Inspector (RWD)

Branch Chief, DRP/D (TWP)

Senior Project Engineer, DRP/D (GEW)

Staff Chief, DRP/TSS (KMK)

RITS Coordinator (KEG)

DRS STA (DAP)

Matt Mitchell, OEDO RIV Coordinator (MAM4)

ANO Site Secretary (VLH)

ADAMS: / Yes

G No Initials: TWP_____

/ Publicly Available G Non-Publicly Available

G Sensitive / Non-Sensitive

R:\\_ANO\\2004\\AN2004-04RP-RWD.wpd

RIV:RI:DRP/D

RI:DRP/D

SRI:DRP/D

C:DRS/PEB

C:DRS/PSB

JLDixon

ELCrowe

RWDeese

LJSmith

MPShannon

T - TWPruett

T - TWPruett

T - TWPruett

/RA/

/RA/

10/6/04

10/6/04

10/6/04

10/25/04

10/25/04

C:DRS/EMB

C:DRS/OB

C:DRP/D

JAClark

ATGody

TWPruett

/RA/

/RA/

/RA/

10/25/04

10/25/04

10/28/04

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets:

50-313, 50-368

Licenses:

DPR-51, NPF-6

Report:

05000313/2004004 and 05000368/2004004

Licensee:

Entergy Operations, Inc.

Facility:

Arkansas Nuclear One, Units 1 and 2

Location:

Junction of Hwy. 64W and Hwy. 333 South

Russellville, Arkansas

Dates:

June 24, 2004 to September 23, 2004

Inspectors:

E. Crowe, Resident Inspector

R. Deese, Senior Resident Inspector

J. Dixon, Resident Inspector

J. Drake, Operations Engineer

P. Gage, Senior Operations Engineer

G. Replogle, Senior Reactor Inspector

Approved By:

Troy W. Pruett, Chief, Project Branch D

Division of Reactor Projects

Enclosure

CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R01

Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R04

Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R05

Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R06

Flood Protection Measures . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R11

Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R12

Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

1R13

Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 10

1R14

Operator Performance During Nonroutine Plant Evolutions and Events . . . . . 13

1R15

Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

1R16

Operator Workarounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R19

Post-Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1R22

Surveillance Testing

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

1R23

Temporary Plant Modifications

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30

4OA7 Licensee-Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30

ATTACHMENT: SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-3

Enclosure

SUMMARY OF FINDINGS

IR 05000313/2004004, 05000368/2004004; 6/24/04 - 9/23/04; Arkansas Nuclear One, Units 1

and 2; Adverse Weather Protection, Fire Protection, Maintenance Risk Assessments and

Emergent Work Control, Operability Evaluations, Surveillance Testing, and Event Followup.

This report covered a 3-month period of inspection by resident inspectors, a maintenance rule

inspector, and two operations inspectors. Four Green noncited violations, one Green finding,

one apparent violation with potential safety significance greater than Green, and one

unresolved item with potential safety significance greater than Green were identified. The

significance of most findings is indicated by their color (Green, White, Yellow, or Red) using

Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the

significance determination process does not apply may be Green or be assigned a severity

level after NRC management's review. The NRCs program for overseeing the safe operation

of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight

Process, Revision 3, dated July 2000.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green. A self-revealing finding associated with an inadequate maintenance

procedure occurred when the Unit 2 main generator reverse power relays

contributed to a turbine trip and a reactor trip. The licensee had not incorporated

vendor recommended maintenance on the reverse power relays, and as a result,

one of the reverse power relays actuated with no reverse power condition

present. Corrective actions taken or planned by the licensee have been entered

into the licensee's corrective action program as Condition Report ANO-2-2002-

2173.

The finding is more than minor because it was analogous to Example 4.b. in

Appendix E, Examples of Minor Issues, of Manual Chapter 0612, Power

Reactor Inspection Reports, because a procedural error contributed to a reactor

trip. This finding affected the initiating events cornerstone. Using the Phase 1

worksheet in Manual Chapter 0609, Significance Determination Process, the

finding is of very low safety significance because, although it resulted in a reactor

trip, all mitigating systems remained available (Section 4OA3).

Cornerstone: Mitigating Systems

TBD. An unresolved item was identified for the failure to take timely corrective

action to repair an oil leak on a temperature switch for the Unit 1 Emergency

Diesel Generator K-4A in May 2004. This failure resulted in the oil leak

progressively worsening and ultimately developing into a leak which challenged

the emergency diesel generator safety function. The fitting was repaired and the

leakage is no longer a safety concern. This finding involved problem

identification and resolution crosscutting aspects associated with operations and

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Enclosure

engineering personnel not recognizing the significance of the degraded condition

and not implementing timely corrective actions to repair the leak. Corrective

actions taken or planned by the licensee have been entered into the licensees

corrective action program as Condition Report ANO-1-2004-1705.

This finding is unresolved pending a review of the duration of the condition and

the completion of a significance determination. This finding affected the

mitigating systems cornerstone. The finding was more than minor because it

directly impacted the availability and reliability of an emergency diesel generator

which is used to mitigate the loss of AC power to the respective safety-related

bus. Using Appendix A, "Technical Basis For At Power Significance

Determination Process, of Manual Chapter 0609, Significance Determination

Process, and the Phase 2 worksheets from Risk-Informed Inspection Notebook

for Arkansas Nuclear One - Unit 1, the finding was determined to potentially

have greater than very low safety significance because the failure could have

resulted in an actual loss of the safety function of the Train A emergency diesel

generator during a loss of offsite power event (Section 1R15).

TBD. The inspectors identified an apparent violation of 10 CFR Part 50,

Appendix B, Criterion XV, "Nonconforming Materials, Parts, or Components," for

the failure to establish controls to prevent a circuit breaker with a loose

connection from being installed in Unit 2. A loose connection in the Containment

Spray Pump 2P-35A breaker was not identified prior to installation in the plant

even though there were several undocumented instances where similar loose

connections were discovered during receipt inspections of other breakers in its

group. This issue involved problem identification and resolution crosscutting

aspects associated with maintenance technicians not identifying the cause of the

breaker failure and not documenting nonconformances. Corrective actions taken

or planned by the licensee have been entered into the licensee's corrective

action program as Condition Report ANO-2-2004-1712.

This finding is being considered an apparent violation pending completion of its

significance determination. The finding is more than minor because it affected

the mitigating systems cornerstone objective of ensuring the reliability of systems

that respond to initiating events to prevent undesirable consequences. Using

Appendix A, Technical Basis For At Power Significance Determination Process,

of Manual Chapter 0609, Significance Determination Process, and the Phase 2

worksheets from Risk-informed Inspection Notebook for Arkansas Nuclear

One - Unit 2, the finding was determined to potentially have greater than very

low safety significance because the loose connection could have resulted in an

actual loss of the safety function of the Unit 2 Train A containment spray pump

during small break loss of coolant accident or stuck open relief valve events

(Section 1R22).

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Enclosure

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion III, Design Control, for the failure of the licensee to

correctly translate the design basis heat removal requirements for the Unit 1

intake structure into specifications for the ventilation opening sizes.

Measurements of the openings by the inspectors were smaller than those

assumed in the licensees heat removal calculations. Analyses using the smaller

dimensions resulted in a 13 percent reduction in the heat removal capability.

The licensee has taken action to update their calculation with the correct opening

sizes. Corrective actions taken or planned by the licensee have been entered

into the licensees corrective action program as Condition Report ANO-1-2004-

1829.

This finding is more than minor because it was analogous to Example 3.i of

Appendix E, Examples of Minor Issues, to Inspection Manual Chapter 0612,

Power Reactor Inspection Reports, in that the licensee's engineering staff had

to reperform analyses due to a significant dimensional discrepancy. This finding

affected the mitigating systems cornerstone. Using the Phase 1 worksheets in

Manual Chapter 0609, Significance Determination Process, the inspectors

consider this finding to have very low safety significance because it did not result

in an actual loss of safety function (Section 1R01).

Green. The inspectors identified a noncited violation of Unit 2 operating license

Condition 2.C.(3)(b), Fire Protection, for the failure to perform hydrostatic

testing on approximately 80 to 90 percent of the carbon dioxide fire

extinguishers. The licensee failed to implement a plan to ensure carbon dioxide

fire extinguishers would not exceed their hydrostatic retest expiration dates in

response to NRC Information Notice 2001-004, Neglected Fire Extinguisher

Maintenance Causes Fatality. This issue involved problem identification and

resolution crosscutting aspects associated with fire protection technicians failing

to correct adverse conditions in a timely manner. Corrective actions taken or

planned by the licensee have been entered into the licensees corrective action

program as Condition Report ANO-1-2004-1544.

This finding is more than minor because, if left uncorrected, it would become a

more significant safety concern in that internal degradation of the fire

extinguishers could continue without any means of detection until the

extinguishers were unable to perform their intended functions. Using

Appendix F, Determining Potential Risk Significance of Fire Protection and

Post-Fire Safe Shutdown Inspection Findings, of Manual Chapter 0609,

Significance Determination Process, the inspectors determined the issue is of

very low safety significance because the fire protection elements performance

and reliability was minimally impacted (Section 1R05).

Green. The inspectors identified two examples of a noncited violation of

10 CFR 50.65(a)(4) for the failure to consider the external risk from changing

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Enclosure

weather conditions (tornado warning) while a Unit 2 emergency diesel generator

was out of service for maintenance and the failure to perform an adequate risk

assessment of the removal of a high energy line break barrier between the

turbine building and the Unit 1 South switchgear room. This finding involved

problem identification and resolution crosscutting aspects associated with

operations and engineering personnel not implementing corrective actions to

address the extent of condition from a previous noncited violation documented in

NRC Inspection Report 05000313/2004003. Corrective actions taken or planned

by the licensee have been entered into the licensees corrective action program

as Condition Reports ANO-C-2004-1279 and ANO-C-2004-1402.

The inspectors determined that these issues are more than minor because, if left

uncorrected, they would become a more significant safety concern in that actions

to manage increases in risk may not be implemented. This finding affected the

mitigating systems cornerstone. Using the Phase 1 worksheet in Manual

Chapter 0609, Significance Determination Process, the example involving

changing weather conditions was determined to have very low safety

significance because the finding did not result in a loss of function per Generic Letter 91-18, Revision 1, Information to Licensees Regarding NRC Inspection

Manual Section on Resolution of Degraded and Nonconforming Conditions.

Next, using Appendix A, Technical Basis For At Power Significance

Determination Process, of Manual Chapter 0609, Significance Determination

Process, and the Phase 2 worksheets from Risk-informed Inspection Notebook

for Arkansas Nuclear One - Unit 1, the finding involving the high energy line

break barrier was determined to be of very low safety significance because the

only affected initiator was a main steam line break and a redundant train of

safety related switchgear always remained available during the short exposure

time for the condition (Section 1R13).

Cornerstone: Barrier Integrity

Green. A self-revealing violation of Unit 1 Technical Specification 3.9.2, Nuclear

Instrumentation, occurred when one of the two required source range nuclear

neutron monitors failed during core alterations. The licensee continued

movement of spent fuel assemblies from the reactor vessel for approximately

11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> following the failure of the instrument. Corrective actions taken or

planned by the licensee have been entered into the licensees corrective action

program as Condition Report ANO-1-2004-0989.

The finding is more than minor because it affects the barrier integrity cornerstone

objective of providing reasonable assurance that physical design barriers protect

the public from radionuclide releases caused by accidents or events. Using

Appendix G, Shutdown Operations Significance Determination Process, of

Manual Chapter 0609, Significance Determination Process, the finding was

determined to have very low safety significance because the instrument failure

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Enclosure

did not affect the licensee's ability to maintain reactor coolant system inventory,

terminate a leak path, or recover decay heat removal (Section 4OA3).

B.

Licensee-Identified Violations

A violation of very low safety significance which was identified by the licensee has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensee's corrective action program. This violation and corrective

actions are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent rated thermal power and remained there

throughout the inspection period.

Unit 2 began the inspection period at 100 percent rated thermal power and remained there until

August 29, 2004, when operators reduced power to 10 percent rated thermal power and

removed the main generator from service to correct a lowering flow condition in the main

generator stator water cooling system. On August 31 the unit resumed 100 percent power

operation and remained there for the rest of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01

Adverse Weather Protection (71111.01)

Readiness for Seasonal Susceptibilities

a.

Inspection Scope

The inspectors completed a review of the licensee's readiness of seasonal

susceptibilities involving extreme high temperatures. The inspectors (1) reviewed plant

procedures, the Updated Final Safety Analysis Report, and Technical Specifications to

ensure that operator actions defined in adverse weather procedures maintained the

readiness of essential systems; (2) walked down portions of the below listed systems to

ensure that adverse weather protection features were sufficient to support operability

including the ability to perform safe shutdown functions; (3) evaluated operator staffing

levels to ensure the licensee would maintain the readiness of essential systems required

by plant procedures; and (4) reviewed the corrective action program to determine if the

licensee identified and corrected problems related to adverse weather conditions.

Week of July 19, 2004, Units 1 and 2, service water system

The inspectors completed one sample.

b.

Findings

Introduction. The inspectors identified a Green noncited violation (NCV) of

10 CFR Part 50, Appendix B, Criterion III, Design Control, for the failure to correctly

translate the Unit 1 intake structure ventilation design bases into specifications.

Description. Arkansas Nuclear One, Unit 1, Calculation 93-D-5015-01, Unit 1 Intake

Structure Natural Convection, Revision 1, addressed the cooling of the components in

the Unit 1 intake structure during a design basis accident. These components, which

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Enclosure

include the service water pumps, rely on natural convection through doors and openings

in the structure for cooling since the intake structure does not contain emergency

powered ventilation fans. The inspectors measured the dimensions of the openings

relied upon for natural convection and noted that the openings were not as large as

those assumed in the calculation. The inspectors noted that engineering personnel had

not considered the flow obstruction caused by the open louvers on the structures

access doors. Additionally, the inspectors noted that engineering personnel did not

consider restrictions in air flow caused by support beams for the missile shields on the

structures roof along with the air flow restriction caused by the placement of two of the

shields adjacent to vertical walls. The calculation assumed openings for the doors and

roof openings for the intake structure would allow a free flow area for ventilation of

30 square feet. Dimensions measured by the inspectors yielded an area of 23 square

feet. The inspectors concluded that the licensees calculation for design basis cooling of

the intake structure was nonconservative because the openings which would allow the

convection air flow were not as large as assumed in the calculation. As part of their

corrective actions, the licensee performed more precise measurements and updated

their calculation showing that heat removal was 13 percent less than previously

assumed with the openings that existed in the intake structure.

Analysis. The inspectors determined that this finding is more than minor because it is

analogous to Example 3.i of Appendix E, Examples of Minor Issues, of Manual

Chapter 0612, Power Reactor Inspection Reports, because the licensee's engineering

staff had to reperform a calculation to assure accident analysis requirements were met

after identification of a significant dimensional discrepancy. The finding affected the

mitigating systems cornerstone. Using the Phase 1 worksheets in Manual

Chapter 0609, Significance Determination Process, the issue was determined to have

very low safety significance because it did not result in an actual loss of safety function.

The inspectors determined that even though the calculation was nonconservative,

adequate convection flow would have been available to cool components in the Unit 1

intake structure.

Enforcement. Criterion III of 10 CFR Part 50, Appendix B, Design Control, states, in

part, that measures shall be established to assure that the design basis is correctly

translated into specifications. Contrary to the above, engineering personnel did not

correctly translate the design basis heat removal requirements for the Unit 1 intake

structure into the proper specifications for the size of openings in the intake structure.

Because of the very low safety significance of the finding and because the licensee has

entered these issues into their corrective action program in Condition

Report ANO-1-2004-1829, the inspectors treated this as a NCV, consistent with

Section VI.A of the NRC Enforcement Policy, NCV 05000313/2004004-01,

Nonconservative Calculation of Design Basis Intake Structure Ventilation.

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Enclosure

1R04

Equipment Alignment (71111.04)

a.

Inspection Scope

Partial System Walkdowns. The inspectors (1) walked down portions of the three below

listed risk important systems and reviewed plant procedures and documents to verify

that critical portions of the selected systems were correctly aligned; and (2) compared

deficiencies identified during the walk down to the licensee's corrective action program

to ensure problems were being identified and corrected.

July 27, 2004, Unit 2 Inverters 2Y22 and 2Y24 and their associated portion of the

AC and DC distribution systems, the inspectors performed a partial system

walkdown of accessible portions of these distribution systems during periodic

maintenance on Swing Inverter 2Y2224.

August 24, 2004, Unit 1 emergency feedwater (EFW) system, the inspectors

performed a partial system walkdown of accessible portions of the Train B

portion of the system during periodic maintenance on the steam driven EFW

pump (Train A).

September 8, 2004, Unit 1 EFW system, the inspectors performed a partial

system walkdown of accessible portions of the Train A portion of the system

during periodic maintenance on the Train B portion of the EFW system.

The inspectors completed three samples.

Complete Walkdown. The inspectors (1) reviewed plant procedures, drawings, the

Updated Final Safety Analysis Report, Technical Specifications, and vendor manuals to

determine the correct alignment of the system; (2) reviewed outstanding design issues,

operator work arounds, and corrective action program documents to determine if open

issues affected the functionality of the system; and (3) verified that the licensee was

identifying and resolving equipment alignment problems.

August 11-12, 2004, Unit 1 decay heat system, the inspectors performed a

complete system walkdown of accessible portions of the system. This walkdown

was performed during the period when Decay Heat System Pump P-34A was

taken out of service for scheduled maintenance.

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

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Enclosure

1R05

Fire Protection (71111.05AQ)

a.

Inspection Scope

Annual Inspection. The inspectors observed a fire brigade drill on August 14, 2004, to

evaluate the readiness of licensee personnel to prevent and fight fires, including the

following aspects: (1) use of protective clothing, (2) use of breathing apparatuses,

(3) placement and use of fire hoses, (4) entry into the fire area, (5) use of fire fighting

equipment, (6) brigade leader command and control, (7) communications between the

fire brigade and control room, (8) searches for fire victims and fire propagation,

(9) smoke removal, (10) use of prefire plans, and (11) adherence to the drill scenario.

The licensee simulated a fire in the Unit 2 controlled access dress out area (Fire

Zone 2136 of the 386' elevation of the auxiliary building).

The inspectors completed one sample.

Quarterly Inspection. The inspectors walked down the six below listed plant areas to

assess the material condition of active and passive fire protection features, their

operational lineup, and their operational effectiveness. The inspectors (1) verified that

transient combustibles and hot work activities were controlled in accordance with plant

procedures; (2) observed the condition of fire detection devices to verify they remained

functional; (3) observed fire suppression systems to verify they remained functional;

(4) verified that fire extinguishers and hose stations were provided at their designated

locations and that they were in a satisfactory condition; (5) verified that passive fire

protection features (electrical raceway barriers, fire doors, fire dampers, steel fire

proofing, penetration seals, and oil collection systems) were in a satisfactory material

condition; (6) verified that adequate compensatory measures were established for

degraded or inoperable fire protection features; and (7) reviewed the corrective action

program to determine if the licensee identified and corrected fire protection problems.

June 24, 2004, Unit 1 computer room, Fire Zone 160-B

August 12, 2004, Unit 1 East decay heat removal pump room, Fire Zone 10-EE

August 13, 2004, Unit 1 West decay heat removal pump room, Fire Zone 14-EE

September 9, 2004, Unit 1 control room, Fire Zone 129-F

September 20, 2004, Unit 2 North electrical equipment room, Fire Zone 2091-BB

September 20, 2004, Unit 2 lower North electrical penetration room, Fire

Zone 2112-BB

The inspectors completed six samples.

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Enclosure

b.

Findings

Introduction. The inspectors identified a Green NCV of the Unit 2 operating license for

the failure to perform hydrostatic testing of the carbon dioxide fire extinguishers.

Description. On June 24, 2004, the inspectors requested documentation of the latest

hydrostatic test for a carbon dioxide fire extinguisher in Fire Zone 160-B. In response to

this request, the licensee initiated CR ANO-1-2004-1544 which received an apparent

cause evaluation. From this evaluation, the inspectors noted that the licensee had

initiated corrective actions to determine the number of fire extinguishers with expired

hydrostatic retest dates in 2001, following the receipt of NRC Information Notice 2001-004, Neglected Fire Extinguisher Maintenance Causes Fatality. The

licensees inspection effort was stopped due to the large number of fire extinguishers

with expired hydrostatic retesting dates (approximately 80 to 90 percent). The licensee

decided that a wholesale repair/replacement plan was needed; however, the plan was

never developed and implemented. While reviewing the corrective actions associated

with CR ANO-1-2004-1544, the inspectors determined that no fire extinguishers had

received the required hydrostatic test during the past 3 years because the licensee had

suspended the maintenance work orders.

The licensees fire hazard analysis described manual fire protection features as hose

stations and carbon dioxide fire extinguishers in 97 of the 149 fire zones listed in the

analysis. Currently, there are 228 carbon dioxide fire extinguishers strategically located

in Units 1 and 2 that are afforded to fire watches and fire brigade members for the

manual suppression of fires in the above 97 fire zones.

Analysis. The inspectors determined the issue was more than minor because, if left

uncorrected, it would become a more significant safety concern in that internal

degradation of the fire extinguishers would continue without any means of detection until

the extinguisher was unable to perform its intended function as defined in the fire hazard

analysis. Using Appendix F, Determining Potential Risk Significance of Fire Protection

and Post-Fire Safe Shutdown Inspection Findings, of Manual Chapter 0609,

Significance Determination Process, the inspectors assumed that the issue affected

the mitigating systems cornerstone and had very low safety significance (Green)

because this fire protection elements performance and reliability was minimally

impacted. This issue involved problem identification and resolution crosscutting aspects

associated with fire protection technicians failing to correct adverse conditions in a

timely manner.

Enforcement. Arkansas Nuclear One, Unit 2 facility operating license

Condition 2.C.(3)(b) states, in part, that Entergy Operations, Inc. shall implement and

maintain in effect all provisions of the approved fire protection program as described in

Amendment 9A to the Safety Analysis Report and as approved in the safety evaluation

dated March 31, 1992. Arkansas Nuclear One, Unit 2 Safety Analysis Report,

Appendix 9A, Fire Protection Program, states, in part, the ANO fire protection systems

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Enclosure

consist of numerous components including portable extinguishers. Safety Analysis

Report, Section 9.5.1, Fire Protection Systems (FPS) - Codes and Standards, states,

in part, that the fire protection system is designed in substantial compliance with the

requirements of the National Fire Codes of the National Fire Protection Association

(NFPA 1977). NFPA 10, Standard for Portable Fire Extinguishers, Chapter 7,

Hydrostatic Testing, states, in part, that fire extinguishers shall be hydrostatically

retested at intervals not exceeding those specified in Table 7.2, which establishes the

test interval for carbon dioxide fire extinguishers as 5 years.

Contrary to the above, the licensee failed to perform hydrostatic retesting of carbon

dioxide fire extinguishers every 5 years. Because of the very low safety significance and

because the licensee included this condition in the corrective action program as

CR ANO-1-2004-1544, this violation is being treated as an NCV, consistent with

Section VI.A of the NRC Enforcement Policy, NCV 05000368/2004004-02: Failure to

Perform Required Hydrostatic Testing of Pressurized Fire Extinguishers.

1R06

Flood Protection Measures (71111.06)

a.

Inspection Scope

Semi-annual Internal Flooding. The inspectors (1) reviewed the Updated Final Safety

Analysis Report, the flooding analysis, and plant procedures to assess seasonal

susceptibilities involving internal flooding; (2) reviewed the corrective action program to

determine if the licensee identified and corrected flooding problems; (3) verified that

operator actions for coping with flooding can reasonably achieve the desired outcomes;

and (4) walked down the below listed areas to verify the adequacy of (a) equipment

seals located below the floodline; (b) floor and wall penetration seals; (c) watertight door

seals; (d) common drain lines and sumps; (e) sump pumps, level alarms, and control

circuits; and (f) temporary or removable flood barriers.

August 12, 2004, Unit 1, decay heat removal vault

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification Program (71111.11)

.1

Quarterly Review.

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Enclosure

a.

Inspection Scope

The inspectors observed testing and training of senior reactor operators and reactor

operators on September 14, 2004, in the Unit 2 simulator to (1) identify deficiencies and

discrepancies in the training; (2) assess operator performance; and (3) assess the

evaluator's critique. The training scenario involved plant conditions where an

inadvertent containment isolation actuation signal, from a single train, resulted in a loss

of all feedwater to the steam generators. The loss of all feedwater was followed with a

faulted steam generator, requiring the crew to address increased containment

temperature and pressure during natural circulation cooldown of the reactor coolant

system.

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

.2

Biennial Inspection.

a.

Inspection Scope

The inspectors (1) evaluated examination security measures and procedures for

compliance with 10 CFR 55.49; (2) evaluated the licensees sample plan of the written

examinations for compliance with 10 CFR 55.59 and NUREG-1021, as referenced in the

facility requalification program procedures; and (3) evaluated maintenance of license

conditions for compliance with 10 CFR 55.53 by review of facility records (medical and

administrative), procedures, and tracking systems for licensed operator training,

qualification, and watchstanding. In addition, the inspectors reviewed remedial training

for examination failures for compliance with facility procedures and responsiveness to

address failed areas.

Furthermore, the inspectors (1) interviewed 10 personnel, including operators,

instructors/evaluators, and training supervisors, regarding the policies and practices for

administering requalification examinations; (2) observed the administration of two

dynamic simulator scenarios to one requalification crew; and (3) observed four

evaluators administer six performance measures, including four in the control room

simulator in a dynamic mode and two in the plant under simulated conditions.

The inspectors also reviewed the remediation process and the results of the biennial

written examination. The results of the examinations were assessed to determine the

licensees appraisal of operator performance and the feedback of performance analysis

to the requalification training program. The inspectors interviewed members of the

training department and operating crews to assess the responsiveness of the licensed

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Enclosure

operator requalification program. The inspectors also observed the examination

security maintenance for the operating tests during the examination week.

Additionally, the inspectors assessed the Arkansas Nuclear One, Unit 2,

plant-referenced simulator for compliance with 10 CFR 55.46 using Baseline Inspection

Procedure 71111.11 (Section 03.11). This assessment included the adequacy of the

licensees simulation facility for use in operator licensing examinations and for satisfying

experience requirements as prescribed by 10 CFR 55.46. The inspectors reviewed a

sample of simulator performance test records (transient tests, surveillance tests,

malfunction tests, and scenario-based tests), simulator discrepancy report records, and

processes for ensuring simulator fidelity commensurate with 10 CFR 55.46. The

inspectors also interviewed members of the licensees simulator configuration control

group as part of this review.

In addition to the biennial review for Unit 2, the inspectors reviewed the test results of

the Unit 1 annual operating examination for 2004. Since this was the first half of the

biennial requalification testing cycle, the licensee had not yet administered the written

examination. These results were assessed to determine if they were consistent with

NUREG 1021 guidance and Manual Chapter 0609, Appendix I, Operator

Requalification Human Performance Significance Determination Process,

requirements. This review included examination test results for 10 crews which included

56 licensed individuals.

b.

Findings

No findings of significance were identified.

.3

Examination Security

a.

Inspection Scope

The inspectors identified a minor violation of 10 CFR 55.49 for the licensee's failure to

provide examination security. The examiners reviewed examination security during the

onsite examination administration week for compliance with NUREG-1021 requirements.

Plans for simulator security and licensed operator control were reviewed.

b.

Findings

One examination security issue was identified by the licensee during the administration

of the simulator static section of the written examination. A licensee representative, on

the NRC examination security agreement, was inadvertently administered the same

static examination as the one the individual had previously validated. This action was

prohibited by NUREG-1021 and the security agreement. The error was immediately

identified by the individual and reported to the cognizant instructor.

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Enclosure

Subsequent to the identification of the administrative error, a static examination that the

affected individual had not been exposed to was selected and approved for

administration to the individual. The licensee performed a review of track records for all

Unit 2 licensed operators and verified no other individual was administered, or was

scheduled to be administered, any part of the biennial examination in which the

individuals had previously participated in the validation process. Immediate licensee

followup and short-term corrective actions were discussed with the inspector and

NRC regional management and conservatively confirmed that no potential for

communicating examination content existed, which would have the possible impact of

compromising the licensed operator requalification examination.

As stated, in part, in 10 CFR 55.49, the integrity of an examination is considered

compromised if any activity, regardless of intent, would have affected equitable and

consistent administration of the examination. Although this finding constitutes a

violation of minor significance that is not subject to enforcement in accordance with

Section IV of the NRCs Enforcement Policy, it is being documented as required by

NUREG-1021, Operator Licensing Examination Standards for Power Reactors,

Revision 8, Section ES 501, paragraph E.3.a. The licensee documented the problem in

CR ANO-2-2004-1370.

1R12

Maintenance Effectiveness (71111.12)

.1

Quarterly Reviews

a.

Inspection Scope

The inspectors reviewed the two below listed maintenance activities to (1) verify the

appropriate handling of structure, system, and component (SSC) performance or

condition problems; (2) verify the appropriate handling of degraded SSCs functional

performance; (3) evaluate the role of work practices and common cause problems;

and (4) evaluate the handling of SSCs issues reviewed under the requirements of the

Maintenance Rule, 10 CFR Part 50, Appendix B, and Technical Specifications.

Unit 2 engineered safety feature (ESF) inverter condition of momentary

out-of-synchronization of the power supplies.

Unit 1 auxiliary building heating, ventilation, and air conditioning system decay

heat vault cooler failures

The inspectors completed two samples.

b.

Findings

No findings of significance were identified.

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Enclosure

.2

Biennial Maintenance Rule Implementation

a.

Inspection Scope

Periodic Evaluation Reviews

The inspectors reviewed the licensee's last two Maintenance Rule (10 CFR 50.65,

Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power

Plants) periodic assessments. In addition, the inspectors reviewed the licensees

overall implementation of the Maintenance Rule. As part of the inspection, the

inspectors reviewed the licensees maintenance rule scope, (a)(1) determinations,

performance criteria, program definitions, use of industry operating experience, and

maintenance rule related self assessments. The inspectors verified the establishment of

appropriate goals, corrective actions, and the impact of risk monitoring. The inspectors

reviewed the conclusion reached by the licensee with regard to the balance of reliability

and unavailability for specific maintenance rule functions. The minimum sample for the

biennial inspection will consist of four SSCs/functions (of high risk significance to the

extent available) that have suffered degraded performance or condition. The inspectors

selected the following four problematic systems for a detailed review:

Repeated cracking of Alloy 600 nozzles

Repeated cracking of Unit 1, Control Rod Drive Mechanism Nozzle 56

Repetitive problems with emergency diesel generator starting air receivers

Failure of Reactor Coolant Pump P-32C

Identification and Resolution of Problems

The inspectors reviewed selected corrective action documents associated with

maintenance rule related findings. The inspectors verified that the licensee took, or

planned, appropriate corrective measures for identified issues.

The inspectors completed 4 samples.

b.

Findings

No findings of significance were identified.

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

Risk Assessment and Management of Risk. The inspectors reviewed the below listed

assessment activities to verify (1) the performance of risk assessments when required

by 10 CFR 50.65 (a)(4) and licensee procedures prior to changes in plant configuration

for maintenance activities and plant operations; (2) the accuracy, adequacy, and

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Enclosure

completeness of the information considered in the risk assessment; (3) the licensee

recognizes, and/or enters as applicable, the appropriate licensee-established risk

category according to the risk assessment results and licensee procedures; and (4) the

licensee identified and corrected problems related to maintenance risk assessments.

April 12, 2004, Unit 1, removal of fire/high energy line break Door 48 for the

Service Water Pump P-4B cable replacement

July 5, 2004, Unit 2, planned maintenance during the week

July 12, 2004, Unit 2, planned maintenance during the week

August 9, 2004, Unit 1, planned maintenance during the week

August through September 2004, site modifications affecting the local start of the

alternate AC diesel generator

The inspectors completed five samples.

Emergent Work Control. The inspectors (1) verified that the licensee performed actions

to minimize the probability of initiating events and maintained the functional capability of

mitigating systems and barrier integrity systems; (2) verified that emergent work-related

activities such as troubleshooting, work planning/scheduling, establishing plant

conditions, aligning equipment, tagging, temporary modifications, and equipment

restoration did not place the plant in an unacceptable configuration; and (3) reviewed

the corrective action program to determine if the licensee identified and corrected risk

assessment and emergent work control problems for the below listed activity:

July 21, 2004, Unit 2, emergent maintenance to replace a degraded cell on

ESF Battery 2D11

The inspectors completed one sample.

b.

Findings

Introduction. The inspectors identified two examples of a Green NCV of

10 CFR 50.65(a)(4) for the failure to perform adequate risk assessments.

Description. The licensee failed to consider the external risk from changing weather

conditions in previous risk assessments. During the week of July 5, 2004, the licensee

performed maintenance on the Unit 2 Emergency Diesel Generator (EDG) 2K-4A. On

July 7, 2004, the licensee tagged out the EDG and subsequently the National Weather

Service issued a thunderstorm warning. The inspectors questioned licensee personnel

on how their risk assessments took into account weather as an external event

contributor to risk during maintenance activities. In addition, the inspectors reviewed

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Enclosure

Common Operations Directive COPD024, Risk Assessment Guidelines, Change 12,

which the licensee uses to implement 10 CFR 50.65 (a)(4), Operating

Procedure 1107.001, Electrical System Operations, Revision 60, and Operating

Procedure 2107.001, Electrical System Operations, Revision 48. The inspectors

determined that, except for the specific instances of a missile or external flood barrier

being removed, the licensee had not considered the increase in risk from changing

weather conditions during maintenance activities. The inspectors noted that Regulatory

Guide 1.160, "Monitoring the Effectiveness of Maintenance in Nuclear Power Plants,"

endorsed NUMARC 93-01, "Nuclear Energy Institute Industry Guideline for Monitoring

the Effectiveness of Maintenance at Nuclear Power Plants." Section 11 of

NUMARC 93-01 specified that emergent conditions (weather) could change the

conditions of previously performed assessments and that the evaluation should be

reperformed to address the changed conditions.

The inspectors determined that the licensee's corrective actions in response to

NCV 05000313/2004003-03, Failure to adequately assess risk due to external

conditions, were incomplete. While the inspectors noted that the licensee had updated

COPD024, Risk Assessment Guidelines, and both units natural emergencies

procedures (Operating Procedures 1203.025 and 2203.008), the inspectors found that

the revised procedures were still deficient because, even with the changes, the potential

still existed for risk to not be re-evaluated based on changing weather conditions.

The inspectors determined that the licensee failed to consider the additional risk to the

plant from having a high energy line break (HELB) door removed. During the week of

April 12, 2004, the licensee removed Door 48 to facilitate the installation of new power

cables for the Unit 1 Service Water Pump P-4B. HELB Door 48 provided a barrier

between the turbine building and the Unit 1 South switchgear room. The inspectors

reviewed Common Operations Directive COPD024, Risk Assessment Guidelines,

Change 12, and found that the document stated that HELB door requirements are not

modeled quantitatively or qualitatively. Upon questioning the licensee, the inspectors

determined that the licensee addressed HELB doors being removed through an

engineering request, which included impact statements and contingency actions. As the

licensee documented in CR ANO-C-2004-1402, the engineering request may not in all

cases address an increase in risk from a 10 CFR 50.65(a)(4) perspective. While the

licensee did station a continuous fire watch (Door 48 is also a fire barrier door), the

engineering request did not address the increase in overall plant risk due to the lack of

separation between the turbine building and a safety-related switchgear room.

Analysis. The inspectors determined that both examples affected the mitigating

systems cornerstone and that the finding was more than minor because, if left

uncorrected, it would become a more significant safety concern in that actions to

manage increases in risk may not be implemented. Using the Phase 1 worksheets in

Manual Chapter 0609, Significance Determination Process, the example involving

changing weather conditions was determined to have very low safety significance

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Enclosure

because the finding did not result in a loss of function per Generic Letter 91-18,

Revision 1, Information to Licensees Regarding NRC Inspection Manual Section on

Resolution of Degraded and Nonconforming Conditions.

The example involving the high energy line break door was analyzed using the Phase 1

worksheets in Manual Chapter 0609, Significance Determination Process, from which

the inspectors determined that the finding affected the mitigating systems and barrier

integrity cornerstones. As a result, the inspectors performed a Phase 2 analysis using

Appendix A, "Technical Basis For At Power Significance Determination Process, of

Manual Chapter 0609, Significance Determination Process, and the Phase 2

worksheets from Risk-Informed Inspection Notebook for Arkansas Nuclear

One - Unit 1. In this determination, the inspectors postulated a break which would

disable the Train A 4160 VAC switchgear and that operations personnel would not be

able to recover the switchgear. The inspectors assumed that the only affected event

was a main steam line break and that the exposure time for the condition was 5 days.

The Phase 2 analyses demonstrated that the finding was of very low safety significance.

Using Appendix H, Containment Integrity Significance Determination Process, of

Manual Chapter 0609, the inspectors determined that the finding was of very low safety

significance because of the low core damage probability determined from the Phase 2

analysis.

Enforcement. 10 CFR 50.65(a)(4) requires, in part, that the licensee shall assess and

manage the increase in risk that may result from proposed maintenance activities.

Contrary to this, the licensee did not adequately assess risk from maintenance activities

during adverse weather conditions and following the removal of a HELB barrier.

Because of the very low safety significance and because the licensee included this

condition in the corrective action program as ANO-C-2004-1279 and ANO-C-2004-1402,

this violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000313/2004004-03; 05000368/2004004-03, Failure to

Adequately Assess Risk.

1R14

Operator Performance During Nonroutine Plant Evolutions and Events

(71111.14, 71153)

a.

Inspection Scope

The inspectors (1) reviewed operator logs, plant computer data, and/or strip charts for

the below listed evolutions to evaluate operator performance in coping with nonroutine

events and transients; (2) verified that operator response was in accordance with the

response required by plant procedures and training; and (3) verified that the licensee

has identified and implemented appropriate corrective actions associated with personnel

performance problems that occurred during the nonroutine evolutions sampled.

July 21, 2004, Unit 2, the licensee replaced a degraded cell in ESF Battery 2D11

-14-

Enclosure

August 29, 2004, Unit 2, the licensee reduced reactor power to 10 percent rated

thermal power and removed the turbine generator from operation to allow

replacement of the degraded stator water cooling filter which was causing

reduced cooling flow to the main turbine generator

The inspectors completed two samples.

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors (1) reviewed plants status documents such as operator shift logs,

emergent work documentation, deferred modifications, and standing orders to

determine if an operability evaluation was warranted for degraded components;

(2) referred to the Updated Final Safety Analysis Report and design basis documents to

review the technical adequacy of licensee operability evaluations; (3) evaluated

compensatory measures associated with operability evaluations; (4) determined

degraded component impact on any Technical Specifications; (5) used the significance

determination process to evaluate the risk significance of degraded or inoperable

equipment; and (6) verified that the licensee has identified and implemented appropriate

corrective actions associated with degraded components.

CR ANO-1-2004-0989

Unit 1 source range Nuclear Instrument NI-502

failure during core alterations of the reactor vessel

CR ANO-1-2004-1705

Unit 1 EDG K-4B lube oil leak at temperature

switch TSH-5271

CR ANO-1-2004-2076

Unit 1 service water pumps corrosion at wet end to

pump column flange coupling

CR ANO-2-2004-0779

Alternate AC diesel generator DC Battery 2D-55

service capacity concerns

CR ANO-2-2004-1235

Unit 2 Excore C DC power supply voltage on plant

protection system cabinet indicating low

-15-

Enclosure

CR ANO-2-2004-1277

Unit 2 ESF Battery 2D11 low cell voltage on Cell 25

The inspectors completed six samples.

b.

Findings

Introduction. An unresolved item was identified for the repeated failures of licensee

personnel to promptly identify and correct degraded conditions associated with Unit 1

EDG K-4B Temperature Switch TSH-5271.

Description. In 1990, the temperature switch for the lubricating oil scavenging pump

discharge (TSH-5271) was discovered leaking by the licensee. A leak repair was

attempted by tightening the fitting which resulted in the threaded fitting breaking.

Licensee personnel attempted to replace the switch fitting, but because no exact

replacement fittings were readily available, they implemented a different fitting

arrangement. The replacement fitting arrangement consisted of two 1/2 to 3/8-inch

fittings coupled together to replace one 1/2 to 1/2-inch fitting. This new arrangement

was smaller in diameter at the 3/8-inch threaded coupling and consequently not as

robust. The replacement occurred without engineering personnel questioning the

adequacy of the strength of the smaller fitting. The cantilever configuration of the fitting

and switch in a high vibration environment was also not questioned by engineering

personnel. The inspectors questioned the licensee concerning the EDG manufacturer's

involvement related to the replacement configuration. No evidence was found that the

EDG manufacturer was contacted.

The new fittings prevented oil leakage until 1995 when a leak was discovered and

corrected. No additional problems were noted until June 2003 when a 3 drop per minute

(dpm) leak was noticed by operations personnel during an EDG surveillance test. In

September 2003 maintenance personnel disassembled and tightened the fitting using

sealant to stop the leak. No leakage was observed during the next four surveillance

runs.

During the January 12, 2004, surveillance run, the fitting developed a 10 dpm leak,

which prompted licensee personnel to initiate another work order for repair of the leak.

This work order was scheduled to be completed during the EDG outage in

February 2005. The leak rate remained at 10 dpm during the next four surveillance

runs.

On May 18, 2004, 1 week following the May surveillance run, the fitting began leaking at

4 dpm with the engine secured. CR ANO-1-2004-1442 was generated to document the

condition and was closed without adjusting the priority to the last existing work order,

which was still scheduled to be performed in February 2005.

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Enclosure

During the May 31, 2004 surveillance run, operations personnel quantified the new leak

rate at 136 dpm with the engine running. CR ANO-1-2004-1520 was generated to

document the increased leak rate. This CR did not adequately address the significance

of the increased leak rate on the operability of the EDG and the possibility of the leak

becoming worse. Corrective actions assigned by this CR rescheduled leak repairs to

August 2004.

During the June 28, 2004, surveillance run, the leak rate increased to 400 dpm with the

engine running. A system engineer present during the surveillance run of the EDG was

asked by operations personnel to evaluate the leakage by writing an additional CR. No

CR was written and the repair activity was not rescheduled.

On July 2, 2004, operations personnel noted an increase in the leak rate from 6 to

14 dpm with the engine secured and generated CR ANO-1-2004-1700. In response to

this CR, the licensee began planning for immediate repairs. During a walkdown on

July 3, 2004, operations personnel discovered the fitting leaking at 600 dpm with the

engine secured. Operations personnel declared the EDG inoperable and began repairs.

Maintenance personnel discovered a 300 degree circumferential crack in the 3/8-inch

section of one of the two fittings upon disassembly of the temperature switch. The

licensee sent the fitting to an independent lab for failure analysis. The independent lab

determined the failure of the fitting to be caused by high torque and vibration fatigue.

The inspectors reviewed the licensees actions in response to the increasing leak rates

and determined that after the observation of leakage on May 18, 2004, the licensee did

not promptly identify a degrading leak. As a result, timely action was not taken to repair

the leak.

Analysis. This finding has the potential to be more than minor because it affected the

mitigating systems cornerstone objective of ensuring the availability and reliability of

systems that respond to initiating events to prevent undesirable consequences. Using

the Phase 1 worksheets in Manual Chapter 0609, Significance Determination Process,

the inspectors determined that the finding may represent a loss of one train of a

Technical Specification component for greater than the allowed outage time. As a

result, the inspectors performed a Phase 2 analysis using Appendix A, Technical Basis

For At Power Significance Determination Process, of Manual Chapter 0609,

Significance Determination Process, and the Phase 2 worksheets from Risk-Informed

Inspection Notebook for Arkansas Nuclear One - Unit 1. The inspectors assumed that

(1) the leak rate would have increased on EDG K-4B as the amount of run time

accumulated on the engine between September 23, 2003 and July 3, 2004, (2) the EDG

would not have performed its safety function without exigent corrective actions to repair

the fitting or replenish the lube oil, (3) the duration for not meeting the 6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> offsite

power recovery time, given the leak rate, was approximately 32 days, (4) licensee

personnel would not have acted to replenish lube oil inventory until it manifested itself in

a large leak at the temperature switch, and (5) licensee actions to replenish lube oil

inventory were not credited because of the difficulty in retrieving the oil, transporting the

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Enclosure

oil, and filling the sump. Using these assumptions, the inspectors determined that the

finding had potentially greater than Green safety significance. The dominate core

damage sequence involved a loss of offsite power with a failure of the EDGs and the

failure to recover offsite power.

The duration of the condition and the application of the assumptions is under review by

the regional senior risk analysts. Therefore, this finding is considered an unresolved

item. This issue is not an immediate safety concern because on July 3, 2004, the

licensee removed the EDG from service and repaired the degraded fitting with the

original design, thereby restoring structural integrity to the EDG K-4B lube oil system.

This finding involved problem identification and resolution crosscutting aspects

associated with operations and engineering personnel not recognizing the significance

of the degraded condition and not implementing timely corrective actions to repair the

leak.

Enforcement. From May 18 to July 2, 2004, the licensee did not promptly identify and or

implement actions to repair a degrading fitting on Temperature Switch TSH-5271. The

licensee entered this condition in their corrective action program as

CR ANO-1-2004-1705. Pending the determination of the duration of the condition and a

review of the safety significance by the regional senior reactor analyst, this finding is

considered an unresolved item (URI)05000313/2004004-04, Untimely Corrective

Action to Fix Oil Leak Renders Emergency Diesel Generator Inoperable.

1R16

Operator Workarounds (71111.16)

a.

Inspection Scope

Selected Operator Workarounds: The inspectors reviewed the two below listed operator

workarounds to (1) determine if the functional capability of the system or human

reliability in responding to an initiating event is affected; (2) evaluate the effect of the

operator workaround on the operators ability to implement abnormal or emergency

operating procedures; and (3) verify that the licensee has identified and implemented

appropriate corrective actions associated with operator workarounds.

Selected Operator Workarounds 1-04-09, Unit 1 Train A and B decay heat check

valve back leakage

CR ANO-2-2004-1624, Unit 2 high pressure safety injection pressurization

system pump operation

The inspectors completed two samples.

b.

Findings

No findings of significance were identified.

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Enclosure

1R19

Post-Maintenance Testing (71111.19)

a.

Inspection Scope

The inspectors selected the five below listed postmaintenance test activities of risk

significant systems or components. For each item, the inspectors (1) reviewed the

applicable licensing basis and/or design-basis documents to determine the safety

functions; (2) evaluated the safety functions that may have been affected by the

maintenance activity; and (3) reviewed the test procedure to ensure it adequately tested

the safety function that may have been affected. The inspectors either witnessed or

reviewed test data to verify that acceptance criteria were met, plant impacts were

evaluated, test equipment was calibrated, procedures were followed, jumpers were

properly controlled, the test data results were complete and accurate, the test

equipment was removed, the system was properly realigned, and deficiencies during

testing were documented. The inspectors also reviewed the corrective action program

to determine if the licensee identified and corrected problems related to

post-maintenance testing.

Week of August 9, 2004, Unit 2 EDG 2K-4A, reviewed Work Order

Package 0004283802 for replacement of Cylinder 5 and 9 temperature elements

August 26, 2004, Unit 1 EFW Pump P-7A, reviewed Procedure 1106.006,

Emergency Feedwater Pump Operation, Supplement 12, Steam Driven

Emergency Feedwater Pump Test (Quarterly), Revision 64, which was

performed following maintenance on the turbine driven pump

September 2, 2004, Unit 1 Decay Heat Pump P-34A, reviewed

Procedure 1104.004, Decay Heat Removal Operating Procedure,

Supplement 1, Low Pressure Injection (Decay Heat) Pump and Components

Quarterly, Revision 71, which was performed following maintenance on the

pump

September 22, 2004, Unit 2 High Pressure Injection Pump 2P-89A, reviewed

Procedure 2104.039, HPSI System Operation, Supplement 1, 2P-89A

Quarterly Test, Revision 42, which was performed following maintenance on the

pump

September 23, 2004, Unit 1 Reactor Building Spray Pump P-35A, reviewed

Procedure 1104.005, Reactor Building Spray System Operation, Supplement 3,

RB Spray Pump P-35A Quarterly Test (Red Train), Revision 42, which was

performed following maintenance on the pump

The inspectors completed five samples.

-19-

Enclosure

b.

Findings

No findings of significance were identified.

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedure

requirements, and Technical Specifications to ensure that the eight below listed

surveillance activities demonstrated that the SSCs tested were capable of performing

their intended safety functions. The inspectors either witnessed or reviewed test data to

verify that the following significant surveillance test attributes were adequate:

(1) preconditioning; (2) evaluation of testing impact on the plant; (3) acceptance criteria;

(4) test equipment; (5) procedural adherence; (6) jumper/lifted lead controls; (7) test

data; (8) testing frequency and method demonstrated Technical Specification

operability; (9) test equipment removal; (10) restoration of plant systems; (11) fulfillment

of ASME Code requirements; (12) updating of performance indicator data,

(13) engineering evaluations, root causes, and bases for returning tested SSCs not

meeting the test acceptance criteria were correct; (14) reference setting data;

and (15) annunciator and alarm setpoints. The inspectors also verified that the licensee

identified and implemented any needed corrective actions associated with the

surveillance testing.

September 5, 2003, alternate AC diesel generator 18 month surveillance test per

Procedure 2104.037, Revision 6

April 13, 2004, Unit 1, source range channel linear amplifier calorimetric

calibration per Procedure 1304.055, Revision 12

May 21, 2004, Unit 2, Containment Spray Pump 2P-35A Quarterly Test per

Procedure 2104.005, Supplement 1, Revision 42

May 27, 2004, Unit 1, EFW Steam Admission Valve CV-2663 stroke testing per

Procedure 1106.006, Revision 64

July 9, 2004, Unit 2, low pressure safety injection and refueling water tank

motor-operated valve stroke testing per Procedure 2104.040, Revision 35

July 11, 2004, Unit 2, service water valve quarterly stroke test performed per

Procedure 2104.029, Revision 54

July 15, 2004, Unit 1, Continuous Air Monitors RE-7460 and RE-7461 quarterly

testing per Procedure 1304.181, Revision 8, (RCS leakage detection

surveillance)

-20-

Enclosure

July 27, 2004, Unit 2, Swing Inverter 2Y2224 periodic testing performed per

Procedure/Work Plan 2416.046, Revision 3. During the performance of this

procedure, the technicians increased the Inverter Output Overvoltage Alarm,

setpoint per ER ANO-2003-0644-000 (Work Order Package 0038659,

Revision 1) and replaced critical status lights per ER ANO-2003-0618-000 (Work

Order Package 00035555, Revision 1). The installation of the new lights

addressed existing problems of short bulb life and the inability of operators to

replace burned bulbs

The inspectors completed eight samples.

b.

Findings

Introduction. The inspectors identified an Apparent Violation of 10 CFR Part 50,

Appendix B, Criterion XV, Nonconforming Materials, Parts, or Components, for the

licensee's failure to establish controls to prevent a breaker with a loose connection from

being installed in Unit 2.

Description. During a quarterly surveillance test on May 20, 2004, Unit 2 Containment

Spray Pump 2P-35A failed to start. This was the first instance of this pump failing to

start since the licensee replaced the 4160 VAC breaker in 2001. Licensee personnel

conducted troubleshooting to diagnose the cause of the pump failure and found

elevated resistance across the contacts for Relay LS-9 in the breaker's closing circuit.

Convinced that this was the cause of the breaker failure, the licensee replaced

Relay LS-9 and returned the breaker and pump to service. During postmaintenance

testing, the breaker was cycled satisfactorily 11 times and the pump started with the

breaker racked-in.

On June 3, 2004, engineering personnel contacted the breaker vendor, Siemens, to

inform them of their findings with the high resistance across the contacts. The vendor

refuted the licensee's finding stating that any resistance would have been burned

through by the 250 volts DC supplied to the breaker's closing circuit during the start

sequence. The vendor recommended that the licensee check other parts of the circuit

to identify the cause of the failed breaker.

On August 9, 2004, the licensee racked out the containment spray pump breaker for

further troubleshooting and discovered that a spade-lug connection leading to the

anti-pump relay in the closing circuitry was loose. The spade was not completely

inserted into the lug, giving intermittent elevated resistance readings to the relay

technicians who were troubleshooting the breaker. The inspectors noted that the

licensee delayed additional inspections of the breaker even though the vendor had

provided information which contradicted their cause of the breaker's failure mechanism.

-21-

Enclosure

During conversations after the discovery, one licensee technician noted that he had

discovered five or six similar loose connections while performing receipt inspections of

this group of breakers in 2000. The inspectors questioned whether a condition report

had been written to document the discovery of loose connections during the receipt

inspection process. The licensee explained that the receipt inspection procedure for the

breakers instructed the technicians to tighten loose connections as necessary. As a

result, the technician simply inserted the spade into the lug for the loose connections he

discovered and did not document the deficiency on the receipt inspection sheet. The

technician did inform other technicians performing receipt inspections of the deficiency.

Because the loose connections were not recorded individually, a deficiency report was

not generated, and corrective actions to inspect all other spade-lug connections in the

group of breakers was not initiated. As a result, a breaker with a loose connection was

installed into the plant for the Unit 2 Containment Spray Pump 2P-35A.

The inspectors noted that Maintenance Action Item 26147 (used to inspect the

breakers) required that all deficiencies be recorded. The inspectors concluded that the

loose connections should have been documented. The inspectors noted that after the

failure of the pump to start on May 21, 2004, the degraded circuit connection was not

discovered and was left in place for 2 additional months, until August 9, due to licensee

personnel incorrectly considering Relay LS-9 as the cause of the failure of the

containment spray pump to start.

Analysis. The inspectors determined that this finding is more than minor because it is

analogous to Example 5.c of Appendix E, Examples of Minor Issues, of Manual

Chapter 0612, Power Reactor Inspection Reports, because a nonconforming

component was installed in the plant and the system it was in was returned to service.

Using the Phase 1 worksheets in Manual Chapter 0609, Significance Determination

Process, the inspectors determined that the finding effected the mitigating systems and

barrier integrity cornerstones. As a result, the inspectors performed a Phase 2 analysis

using Appendix A, "Technical Basis For At Power Significance Determination Process,

of Manual Chapter 0609, Significance Determination Process, and the Phase 2

worksheets from Risk-Informed Inspection Notebook for Arkansas Nuclear

One - Unit 2. The Phase 2 analysis determined that the finding was potentially of

greater than Green safety significance. The inspectors assumed that the duration was

greater than 30 days and that operations personnel would be able to recover the

containment spray pump by starting it from the switchgear room. The dominate core

damage sequences involved a loss of AC or DC busses, a failure of emergency

feedwater, and a failure of containment spray recirculation. Specifically, the small break

loss of coolant accident and stuck open relief valve sequences were most limiting. A

review of the Phase 2 analysis and performance of a Phase 3 analysis by a regional

senior reactor analyst is needed to determine the final safety significance of the finding.

This issue is not an immediate safety concern because on August 9, 2004, the licensee

removed the Containment Spray Pump from service and repaired the loose connection,

thereby restoring electrical continuity to the containment spray pump 2P-35A breaker

-22-

Enclosure

circuitry. This issue involved problem identification and resolution crosscutting aspects

associated with maintenance technicians not identifying the cause of the breaker failure

and not documenting deficiencies in the corrective action program.

Enforcement. 10 CFR Part 50, Appendix B, Criterion XV, requires that licensees

establish measures to control components which do not conform to requirements in

order to prevent their inadvertent use. Contrary to the above, licensee personnel did not

establish adequate measures during the breaker receipt inspection process in

October 2000 to prevent breakers with loose circuit connections from being installed in

the plant. As a result, the breaker was installed in the cubicle for the Unit 2 containment

spray pump breaker in February 2001. Pending determination of the findings final

safety significance, this violation is being treated as Apparent Violation (AV), consistent

with Section VI.A of the NRC Enforcement Policy: AV 05000368/2004004-05, Failure to

Identify and Correct a Loose Circuit Connection in Containment Spray Pump Circuitry.

1R23

Temporary Plant Modifications (71111.23)

a.

Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, plant drawings,

procedure requirements, and Technical Specifications to ensure that the one temporary

modification listed below was properly implemented. The inspectors (1) verified that the

modification did not have an affect on system operability/availability; (2) verified that the

installation was consistent with the modification documents; (3) ensured that the

post-installation test results were satisfactory and that the impact of the temporary

modification on permanently installed SSCs were supported by the test; (4) verified that

the modifications were identified on control room drawings and that appropriate

identification tags were placed on the affected drawings; (5) verified that appropriate

safety evaluations were completed; and (6) examined drawings, procedures, and

operations logs for temporary modifications that have not been so designated. The

inspectors verified that the licensee identified and implemented any needed corrective

actions associated with temporary modifications.

Weeks of August 2 and 9, 2004, Unit 2 green train high pressure safety injection

header, temporary alteration of a high pressure safety injection pressurization

system. The pressurization system was evaluated under Engineering Request

ER ANO-2000-3275-003.

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

-23-

Enclosure

1EP6 Drill Evaluation (71114.06)

a.

Inspection Scope

For the below listed drill and simulator-based training evolutions contributing to

drill/exercise performance and emergency response organization performance

indicators, the inspectors (1) observed the training evolution to identify any weaknesses

and deficiencies in classification, notification, and protective action requirements

development activities; (2) compared the identified weaknesses and deficiencies against

licensee identified findings to determine whether the licensee is properly identifying

failures; and (3) determined whether licensee performance is in accordance with the

guidance and acceptance criteria of NEI 99-02, Regulatory Assessment Indicator

Guidelines, Revision 2.

September 15, 2004, the inspectors evaluated the licensees performance in the

Unit 2 simulator, emergency operating facility, and the technical support center

during a quarterly emergency plan drill that involved a loss of lake level, loss of

the emergency cooling pond, degradation of the service water system, and a

reactor coolant system leak into the component coolant water system which

resulted in the release of radioactivity from the containment building to the

environment.

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

a.

Inspection Scope

The inspectors sampled licensee submittals for the two performance indicators listed

below on both units for the period from July 1, 2003, through June 30, 2004. The

inspectors verified (1) the accuracy of the performance indicator data reported during

that period; and (2) used the performance indicator definitions and guidance contained

in NEI Document 99-02, Regulatory Assessment Indicator Guidelines, Revision 2, to

verify the basis in reporting for each data element.

-24-

Enclosure

Reactor Safety Performance Indicators

Safety system unavailability, auxiliary feedwater system

Safety system unavailability, residual heat removal system

The inspectors reviewed operator log entries, daily shift manager reports, plant

computer data, CRs, maintenance action items, maintenance rule data, and

performance indicator data sheets to determine whether the licensee adequately verified

the performance indicators listed above. This number was compared to the number

reported for the performance indicator during the past 3 quarters. Also, the inspectors

interviewed licensee personnel responsible for compiling the information.

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1

Annual Sample Review

a.

Inspection Scope

The inspectors chose one issue for more in depth review to verify that licensee

personnel had taken corrective actions commensurate with the significance of the

issues. The issues and their bases for their selection are described below:

The 10 CFR 50.65(a)(4) implementation procedure, COPD024, Risk

Assessment Guidelines, has had a number of revisions during the past quarter

due to both NRC and licensee identified weaknesses and violations.

CR ANO-C-2004-0548 documented the changes as a result of failing to

reperform risk assessments due to changing external events (weather related

issues).

When evaluating the effectiveness of the licensees corrective actions for these issues,

the following attributes were considered:

Complete and accurate identification of the problem in a timely manner

commensurate with its significance and ease of discovery

Evaluation and disposition of operability and reportability issues

Consideration of extent of condition, generic implications, common cause, and

previous occurrences

-25-

Enclosure

Classification and prioritization of the resolution of the problem commensurate

with its safety significance

Identification of root and contributing causes of the problem for significant

conditions adverse to quality

Identification of corrective actions which are appropriately focused to correct the

problem

Completion of corrective actions in a timely manner commensurate with the

safety significance of the issue

b.

Findings

The inspectors determined that the licensee's corrective actions in response to NCV 05000313/2004003-03, Failure to adequately assess risk due to external conditions,

were incomplete. While the inspectors noted that the licensee had updated COPD024,

Risk Assessment Guidelines, and both units natural emergencies procedures

(Operating Procedures 1203.025 and 2203.008), the inspectors found that the revised

procedures were still deficient because, even with the changes, the potential still existed

for risk to not be re-evaluated based on changing weather conditions (See

Section 1R13).

.2

Cross-References to Problem Identification and Resolution Findings Documented

Elsewhere

Section 1R05 documents a condition where the licensee failed to identify and correct

conditions adverse to safety in that carbon dioxide fire extinguishers were not being

hydrostatically retested on a 5-year interval as required by NFPA 10 requirements.

Section 1R13 and 4OA2 documents a condition where operations and engineering

personnel did not implement corrective actions to address the extent of condition from a

previous maintenance rule noncited violation documented in NRC Inspection Report 05000313/2004003 and 05000368/2004003.

Section 1R15 documents a condition where the licensee did not take timely corrective

actions to assure that oil leakage was repaired on the Unit 1 Emergency Diesel

Generator K-4B.

Section 1R22 documents a condition where maintenance technicians did not document

loose connections in circuitry associated with the breaker for the Unit 2 Containment

Spray Pump 2P-35A or identify the cause of the breaker failure in a timely manner.

-26-

Enclosure

.3

Observations with the Substantive Crosscutting Issue in Problem Identification and

Resolution

As a result of numerous findings dealing with the licensees corrective action program

(CAP), the NRC staff identified a substantive crosscutting issue in the area of problem

identification and resolution during its annual assessment for inspections conducted

in 2003. In this inspection quarter, inspectors made the following observations

pertaining to the specific areas listed below, which were identified as areas with

implementation problems.

Problem Identification and Entry into the CAP. The inspectors noted that the issue with

Unit 2 Containment Spray Pump 2P-35A was never entered into the corrective action

program or its counterpart for the licensees receipt inspection program. As a result, a

breaker with a loose connection was installed into the plant as described in

Section 1R22.

Prioritizing and Evaluating Conditions in the CAP. The inspectors noted that a leaking

oil condition from a fitting on the Unit 1 EDG K-4B was not adequately prioritized or

evaluated which affected the reliability of the EDG as described in Section 1R15.

Implementing Effective Corrective Actions. The inspectors identified an example where

a plan to ensure all fire extinguishers were adequately hydrostatically tested per

NFPA code was not implemented and, therefore, the periodicity of these tests had

lapsed as described in Section 1R05. Additionally, the inspectors identified an example

where operations and engineering personnel did not implement corrective actions to

address the extent of condition from a previous maintenance rule noncited violation

documented in NRC Inspection Report 05000313/2004003.

4OA3 Event Followup (71153)

.1

(Closed) LER 05000313/2004001-01, Operation Prohibited by Technical Specifications

due to an Undetected Inoperable Channel of Required Source Range Nuclear

Instrumentation during Core Alterations Caused by a Signal Processing Unit Circuit

Breaker Failure

a.

Inspection Scope

The inspectors reviewed the LER, corrective action documents CR ANO-1-2004-0645

and CR ANO-1-2004-0989, Unit 1 station operating logs, plant procedures, and plant

computer trends. This review verified that the cause of the April 29, 2004 source range

nuclear neutron monitor failure was identified and corrective actions were appropriate.

The monitor failure was caused by a faulty circuit breaker which provided power to the

process panel that drives the source range instrument. The inspectors also reviewed

the corrective action database for other past failures related to source range nuclear

neutron monitors.

-27-

Enclosure

b.

Findings

Introduction. A self-revealing Green NCV of Unit 1 Technical Specification 3.9.2 was

identified due to an inoperable source range nuclear neutron monitor which reduced the

number of operable instruments below the requirements of Technical Specifications

during core alterations.

Description. On April 29, 2004, at 10:51 p.m. shortly after completion of core offload for

Refueling Outage 1R18, operators discovered that one of two redundant trains of

source range nuclear neutron monitors was inoperable. The operators reviewed plant

computer historical data and determined the green train source range nuclear neutron

monitor had failed at 10:52 a.m. on April 29, 2004. As a result, for approximately

11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />, movement of spent fuel assemblies from the reactor vessel had occurred with

only one of the required two source range nuclear neutron monitors operable.

Operators stationed to monitor the source range instruments did not notice the failure of

the green train instrument.

Analysis. The finding is more than minor because it affects the barrier integrity

cornerstone objective of providing reasonable assurance that physical design barriers

protect the public from radionuclide releases caused by accidents or events attributable

to configuration control. Using Appendix G, Shutdown Operations Significance

Determination Process, of Manual Chapter 0609, Significance Determination Process,

the finding was determined to have very low safety significance (Green) because it did

not affect the licensee's ability to maintain reactor coolant system inventory, terminate a

leak path, or recover decay heat removal.

Enforcement. Unit 1 Technical Specification 3.9.2, Nuclear Instrumentation, requires

that one source range neutron nuclear monitor be operable in Mode 6. Additionally,

Technical Specification 3.9.2 requires that one additional source range neutron nuclear

monitor be operable during core alterations. Contrary to the above, on April 29, 2004,

the licensee performed core alterations (removed fuel from the reactor vessel) with only

one source range neutron nuclear monitor operable for 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br />. Because the finding

was determined to have very low safety significance and has been entered in the

licensee's corrective actions program as CR ANO-1-2004-0989, this violation is being

treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000313/2004004-06, Core Alterations with Less than Two Operable Source

Range Neutron Nuclear Monitors.

-28-

Enclosure

.2

(Closed) LER 05000368/2002002-00, Automatic Actuation of the Reactor Protection

System Caused by a Main Turbine Trip due to Failure of the Main Generator Reverse

Power Relay Resulted in a Reactor Trip

a.

Inspection Scope

The inspectors reviewed the LER and corrective action document CR ANO-2-2002-2173

to verify the cause of the December 19, 2002, Unit 2 reactor trip and that corrective

actions were reasonable. The reactor trip was caused by a main turbine trip which

resulted from the failure of the main generator reverse power relay. The inspectors

reviewed plant parameters and verified that licensee staff properly implemented the

appropriate plant procedures and that plant equipment performed as required. The

inspectors also reviewed the cause of the sequence of events dating back to the original

procurement of the failed relay and associated operational experience.

b.

Findings

Introduction. A self-revealing Green finding was identified for an inadequate

maintenance procedure which did not include vendor recommended maintenance for

the Unit 2 main generator reverse power relay.

Description. The licensee installed General Electric (GE) Model GGP relays for their

reverse power relays in Unit 2. These relays were designed to receive input from

current and voltage transformers on the main generator output which in turn were

designed to provide rotary motion of a vertical shaft. An arm containing a moving

contact at its end was attached to the shaft using a clutch (essentially a set screw).

Rotary action was designed to occur instantly upon sensing a reverse power condition.

On December 19, 2002, while the plant was operating at 100 percent rated thermal

power, the reverse power relay inadvertently operated with no reverse power condition

present, resulting in a Unit 2 reactor trip. Inspection of the relay identified that the clutch

had been slipping. This slippage eventually wore the shafts pivot bearing completely

away and allowed the contact on the arm to close, which caused the relay to actuate on

reverse power even though no reverse power condition existed.

Follow-up correspondence between GE and the licensee uncovered that the licensee

had not been performing the clutch tightness test required by GE

Document GEK-34117, Polyphase Power Directional Relay for Anti-Motoring

Protection. Consequently, maintenance personnel were not aware that the clutch on

the relay was slipping. This GE document was used to develop master preventative

Maintenance Procedure ANO PM-070, Protective Relays, and the specific

maintenance procedures for these reverse power relays. A review of these documents

revealed that the clutch tightness check recommended by Document GEK-34117 was

not included in the applicable ANO preventative maintenance engineering evaluation or

maintenance procedures.

-29-

Enclosure

Analysis. This finding is greater than minor because it was analogous to Example 4.b in

Appendix E, Examples of Minor Issues, of Manual Chapter 0612, Power Reactor

Inspection Reports, in that a procedural error caused a reactor trip. This finding

affected the initiating events cornerstone. Using the Phase 1 worksheet in Manual

Chapter 0609, Significance Determination Process, the finding was determined to

have very low safety significance (Green) because, although it resulted in a reactor trip,

all mitigating systems remained available to the operators.

Enforcement. No violation of regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because it occurred on

nonsafety secondary plant equipment. Licensee personnel entered this issue into the

corrective action program as CR ANO-2-2002-2173: FIN 05000368/2004004-07,

Inadequate Maintenance Procedure for the Main Generator Reverse Power Relays.

.3

(Closed) LER 05000368/2004001-00, Wide-Range Containment Water Level

Transmitter in the off Position Rendering One of Two Technical Specification Channels

Inoperable

On March 16, 2004, a waste control operator found the power switch for one of the wide

range containment water level transmitters in the off position. This rendered the

corresponding Technical Specification required wide range containment water level

indicator inoperable. During the investigation, the licensee determined that the

transmitter had been secured on October 9, 2003, during the latter stages of the

previous refueling outage and, therefore, had been secured greater than the allowed

outage time per Technical Specification 3.3.3.6. The licensee determined that the most

probable cause of the mispositioning was an accidental bump by an individual exiting

the containment building. The inspectors reviewed CR ANO-2-2004-0551 and its

associated root cause evaluation report and determined this finding constituted a

violation of Unit 2 Technical Specification 3.3.3.6. The inspectors determined this

violation to be of minor safety significance that is not subject to enforcement action in

accordance with Section IV of the NRCs Enforcement Policy, because the redundant

channel was available, the containment sump level detection system was available, and

the transmitter was located in an area that is easily accessible and; had the need arisen,

an operator could have been dispatched to investigate and restore power. This LER is

closed.

4OA5 Other Activities

1.

Temporary Instruction 2515/154, Spent Fuel Material Control and Accounting at

Nuclear Power Plants

-30-

Enclosure

a.

Inspection Scope

The inspectors collected the data specified in Phases I and II of the temporary

instruction. The data was forwarded to the individuals identified in the temporary

instruction for consolidation and assessment.

b.

Findings

No findings of significance were identified.

4OA6 Meetings, Including Exit

The maintenance rule inspector presented the inspection results of the maintenance

effectiveness inspection to Mr. J. Forbes, Vice President, Operations, and other

members of licensees management staff on August 19, 2004. The licensee

acknowledge the findings presented.

The operations inspectors presented the inspection results of the operations

requalification inspection to Mr. J. Forbes, Vice President, Operations, and other

members of licensees management at the conclusion of the inspection on

September 8, 2004. The licensee acknowledged the findings presented.

The resident inspectors presented the inspection results of the resident inspections to

Mr. J. Forbes, Vice President, Operations, and other members of the licensee's

management staff on September 28, 2004. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements which meet the criteria of Section VI.A of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

10 CFR 50.65(a)(4) requires, in part, that the licensee shall assess and manage the

increase in risk that may result from the proposed maintenance activities. Contrary to

this, while performing a routine risk assessment the licensee discovered they had not

modeled the Unit 1 decay heat vault room coolers into their equipment out of service

quantitative risk assessment program to assess plant risk, nor had they evaluated them

by any qualitative means. Consequently, the licensees risk assessments for

maintenance activities which affected the decay heat vault room coolers were

-31-

Enclosure

inadequate. This condition is described in the corrective action program as

CRs ANO-1-2004-1948, ANO-1-2004-1813, and ANO-1-2004-1283. This finding is of

very low safety significance because one of the two coolers provides 100 percent

cooling capability and one cooler was always available.

ATTACHMENT: SUPPLEMENTAL INFORMATION

A-1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

B. Berryman, Manager, Planning and Scheduling

J. Bradford, Supervisor, Nuclear Training

R. Byford, Training

S. Cotton, Manager, Training

S. Cupp, Supervisor, Simulator Training

J. Eichenberger, Manager, Corrective Actions and Assessments

C. Eubanks, General Manager, Plant Operations

J. Forbes, Vice President, Arkansas Nuclear One

F. Forrest, Manager, Operations, Unit 1

D. Fowler, Quality Assurance

R. Gordon, Manager, System Engineering

W. Greeson, Acting Manager, Engineering Programs and Components

A. Hawkins, Licensing Specialist

A. Heflin, Manager, Operations, Unit 2

P. Higgins, Supervisor, Nuclear Training

G. Hines, Maintenance Rule Coordinator

J. Hoffpauir, Manager, Maintenance

R. Holeyfield, Manager, Emergency Planning

D. James, Acting Director, Nuclear Safety Assurance

S. Kaufmann, Access Authorization, Fitness For Duty

J. Kowalewski, Director, Engineering

T. Mayfield, Supervisor, Training, Unit 2

J. Miller, Manager, Nuclear Engineering

K. Nichols, Manager, Design Engineering

P. Partridge, Manager, Technical Support

K. Perkins, Supervisor, System Engineering

S. Pyle, Licensing Specialist

R. Scheide, Licensing Specialist

C. Tyrone, Manager, Quality Assurance

F. Vanbuskirk, Licensing

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000313/2004004-04

URI

Untimely Corrective Action to Fix Oil Leak Renders

Emergency Diesel Generator Inoperable (Section 1R15)05000368/2004004-05

AV

Failure to Identify and Correct a Loose Circuit Connection in

Containment Spray Pump Circuitry (Section 1R22)

A-2

Attachment

Opened and Closed

05000313/2004004-01

NCV

Nonconservative Calculation of Design Basis Intake

Structure Ventilation (Section 1R01)05000368/2004004-02

NCV

Failure to Perform Required Hydrostatic Testing of

Pressurized Fire Extinguishers (Section 1R05)05000313/2004004-03

05000368/2004004-03

NCV

Failure to Adequately Assess Risk Due to External

Conditions or HELB Doors Removed (Section 1R13)05000313/2004004-06

NCV

Core Alterations with Less than Two Operable Source

Range Nuclear Neutron Monitors (Section 4OA3)05000368/2004004-07

FIN

Inadequate Maintenance Procedure for the Main Generator

Reverse Power Relays (Section 4OA3)

Closed

05000368/2002002-00

LER

Automatic Actuation of the Reactor Protection System

Caused by a Main Turbine Trip due to Failure of the Main

Generator Reverse Power Relay Resulted in a Reactor Trip

(Section 4OA3)05000313/2004001-01

LER

Operation Prohibited by Technical Specifications due to an

Undetected Inoperable Channel of Required Source Range

Nuclear Instrumentation During Core Alterations Caused by

a Signal Processing Unit Circuit Breaker Failure

(Section 4OA3)05000368/2004001-00

LER

Wide-Range Containment Water Level Transmitter in the

off Position Rendering One of Two Technical Specification

Channels Inoperable (Section 4OA3)

Discussed

None

A-3

Attachment

LIST OF DOCUMENTS REVIEWED

In addition to the documents called out in the inspection report, the following documents were

selected and reviewed by the inspectors to accomplish the objectives and scope of the

inspection and to support any findings:

Section1R01: Adverse Weather Protection

Engineering Calculation

89-D-2001-08, Intake Structure Ventilation Post Modification Evaluation With Worst Case Heat

Load Under Accident Conditions, Revision 0

89-D-2001-09, Unit 2 Intake Structure Environmental Temperature Study, Revision 0

93-D-5015-01, Unit 1 Intake Structure Natural Convection, Revision 1

Operating Procedures

1104.050, Turbine Building, Intake Structure, and Miscellaneous Ventilation, Revision 2

1203.012I, Annunciator K10 Corrective Action, Revision 40

Section 1R04: Equipment Alignment

Operating Procedures

1104.004, Decay Heat Removal Operating Procedure, Revision 71

2107.002, ESF Electrical System Operation, Revision 16

2107.003, Inverter and 120 VAC Electrical System Operation, Revision 19

Plant Drawings

209 Sheet 4, Revision 14; 210 Sheet 1, Revision 139; and 232 Sheet 1, Revision 99

Section 1R05: Fire Protection

CRs

ANO-1-2004-1544 and ANO-C-2004-0755

Engineering Calculation

85-E-0053-15, Revision 45

A-4

Attachment

Plant Documents

Arkansas Nuclear One Fire Hazards Analysis Report, Revision 8

ANO Pre-Fire Plan for Fire Zone 2136-I and 2119-H, Revision 1

Plant Drawings

FP-101, Fire Zone Fuel Handling Floor Plan El. 404 '- 0" and 422' - 6", Sheet 1, Revision 16

FP-105, Fire Zone Plan Below Grade EL 335' - 0", Sheet 1, Revision 18

FP-106, Fire Zone Plan at Elev. 317' - 0" & Section B-B, Sheet 1, Revision 12

FP-2103, Fire Zones Intermediate Floor Plan at Elev. 368' - 0" and 372' 0", Sheet 1,

Revision 25

FP-2104, Fire Zone Ground Floor Plan at Elev. 354' - 0", Sheet 1, Revision 29

Section 1R06: Flood Protection Measures

Engineering Calculations

92-R-0024-01 and 92-R-0034-01

Plant Drawings

FP-105, Fire Zone Plant Below Grade EL 335" - 0", Sheet 1, Revision 18

FP-106, Fire Zone Plant at Elev. 317' - 0" & Section B-B, Sheet 1, Revision 12

Section 1R11: Licensed Operation Requalification Program

Operating Procedures

1903.010, Emergency Action Level Classification, Revision 37

Training Scenario

ES-2-023, Dynamic Exam Scenario, Revision 2

Biennial

Procedures:

DG-TRNA-202-CORETEST, Simulator Core Reload Acceptance Test, Revision 1

DG-TRNA-202-EXAMSEC, Simulator Exam Security Guidelines, Revision 0

DG-TRNA-202-SIMCONTROL, Simulator Modification Control, Revision 0

ENS-TQ-201, Systematic Approach to Training Process, Revision 3

ENS-TQ-202, Simulator Configuration Control, Revision 1

A-5

Attachment

OP-1063008, Operations Training Sequence, May 29, 2003

OP-1064032, Simulator Training, November 20, 2003

Written Examinations

A2EXM-LOR-ANNUAL-RO-TEST 1

A2EXM-LOR-ANNUAL-RO-TEST 2

A2EXM-LOR-ANNUAL-RO-TEST 3

A2EXM-LOR-ANNUAL-RO-TEST 4

A2EXM-LOR-ANNUAL-RO-TEST 5

A2EXM-LOR-ANNUAL-RO-TEST 6

A2EXM-LOR-ANNUAL-SRO-TEST 1

A2EXM-LOR-ANNUAL-SRO-TEST 2

A2EXM-LOR-ANNUAL-SRO-TEST 3

A2EXM-LOR-ANNUAL-SRO-TEST 4

A2EXM-LOR-ANNUAL-SRO-TEST 5

A2EXM-LOR-ANNUAL-SRO-TEST 6

Static Scenarios (written examination)

SS-001, SS-003, SS-006, SS-008, SS-010, and SS-017

Dynamic Examination Scenarios

ES-2-008, Revision 2; ES-2-009, Revision 3; ES-2-010, Revision 4; ES-2-011, Revision 6;

ES-2-013, Revision 3; ES-2-018, Revision 8; ES-2-023, Revision 2; ES-2-024, Revision 1;

and ES-2-026, Revision 4

Job Performance Measures

A2JPM-RO-SFPFL, Revision 6

A2JPM-RO-EDDCG, Revision 3

A2JPM-SRO-EAL5, Revision 0

A2JPM-RO-CVCS7, Revision 4

A2JPM-RO-RCP02, Revision 4

A2JPM-RO-EFW02, Revision 10

A2JPM-RO-FWCS1, Revision 6

A2JPM-RO-SIT05, Revision 2

A2JPM-RO-EFW03, Revision 5

A2JPM-SRO-EAL2, Revision 0

A2JPM-RO-FPEM2, Revision 10

A2JPM-RO-2RS2, Revision 4

A2JPM-RO-AAC01, Revision 2

A2JPM-RO-CCWSA, Revision 9

A2JPM-RO-CPC02, Revision 1

A2JPM-RO-CVCS2, Revision 2

A-6

Attachment

Training Evaluation Action Requests

2003-420 and 2004-146

Miscellaneous

Simulator Fidelity Report for 2003/2004

Annual Performance Testing Data for 2003

Plant Data from Loss of both Main Feedwater Pumps

Steady State Data

Transient Data

Core Performance Data

Section 1R12: Maintenance Effectiveness

CRs

ANO-1-1999-0109, ANO-2-2001-0622, ANO-2-2001-1404, ANO-1-2002-0066,

ANO-1-2002-0428, ANO-2-2002-0005, ANO-2-2002-0389, ANO-2-2002-1574,

ANO-C-2002-0151, ANO-C-2002-0395, ANO-C-2003-0640, and ANO-2-2004-0779

Operating Procedures

2107.002, ESF Electrical System Operation, Revision 16

2107.003, Inverter and 120 VAC Electrical System Operation, Revision 19

Biennial

CRs

ANO-2-2001-0092, ANO-1-2002-1155, ANO-1-2002-1191, ANO-1-2002-1489,

ANO-2-2002-1102, ANO-1-2003-0062, ANO-1-2004-1964, and ANO-2-2004-1132

Operating Procedures

1202.005, Inadequate Core Cooling, Revision 4

1203.003, Control Rod Drive Malfunction Action, Revision 20

DC-121, Maintenance Rule, Revision 1

LI-102, Corrective Action Process, Revision 4

Miscellaneous

ALO-2004-00037, Maintenance Rule Self-Assessment, July 2, 2004

Maintenance Rule (a)(1) Systems, as of August 16, 2004

Maintenance Rule Scope, as of August 16, 2004

A-7

Attachment

System Performance Criteria, August 10, 2004

Entergy Nuclear South Maintenance Rule Desk Top Guide, Revision 1

Entergy Nuclear South System Engineering Desk Guide, Revision 0

Engineering Report A-SE-2002-001-0, ANO Units 1 & 2 and Structures - 2002 Maintenance

Rule Periodic Assessment, approved October 22, 2003

Engineering Report A-SE-2004-001-0, ANO Units 1 & 2 and Structures - 2003 Maintenance

Rule Periodic Assessment, approved May 24, 2004

ANO Units 1 & 2 Availability and Reliability Data, through June, 2004

U1 & U2 Joint Expert Panel Meeting, dated March 8, 2001

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

CRs

ANO-2-2004-1188, ANO-2-2004-1302, ANO-C-2004-1279, ANO-C-2004-1402,

and ECH-2004-0307

Operating Procedures

1107.001, Electrical System Operations, Revision 60

2107.001, Electrical System Operations, Revision 48

Plant Documents

CE-P-05.07, Data Analysis for At-Power PSA Models, Revision 0

COPD024, Risk Assessment Guidelines, Change 11

COPD024, Risk Assessment Guidelines, Change 12

COPD024, Risk Assessment Guidelines, Change 13

Section 1R15: Operability Evaluations

CRs

ANO-C-2001-0018, ANO-C-2001-0678, ANO-C-2001-0698, ANO-C-2003-0360,

ANO-2-2004-0011, ANO-2-2004-0779, ANO-2-2004-1235, and ANO-C-2004-0483

Operating Procedures

1025.063, Control of Troubleshooting, Attachment 1, Revision 1

2104.037, Alternate AC Diesel Generator Operations, Revision 7

A-8

Attachment

2104.037, Alternate AC Diesel Generator Operations, Supplement 1, Revision 7

2304.102, Unit 2 High Linear and High Log Power Levels Excore Safety Channel C,

Revision 47

2304.102, Unit 2 High Linear and High Log Power Levels Excore Safety Channel C,

Supplement 2, Revision 47

Work Order Packages

00048303 01, 50284683 01, 50685110 01, and 50973125 01

Section 1R16: Operator Workarounds

CRs

ANO-1-2002-1853, ANO-1-2004-1817, ANO-1-2004-1832, ANO-1-2004-1974,

ANO-2-2004-1061, ANO-2-2004-1118, ANO-2-2004-1120, ANO-2-2004-1388,

ANO-2-2004-1558, and ANO-2-2004-1624

Operating Procedures

1104.004, Decay Heat Removal Operating Procedure, Revision 71

2104.039, HPSI System Operation, Revision 42

Section 1R19: Postmaintenance Testing

CRs

ANO-2-2004-0780

Operating Procedures

2304.134, Unit 2 EDG 2K4A Instrumentation Calibration, Sections 1 through 7, 8.10.2, and 9,

Revision 11

Work Order Packages

00042838 02, 50243449 01, 50571411 01, 50965925 01, 50965964 01, 50966657 01,

50966693 01, 50966736 01, 50966740 01, 50966830 01, 50966878 01, 50971621 01,

50972991 01, 50972992 01, and 50973104 01

Section 1R22: Surveillance Testing

CRs

ANO-1-2004-0645, ANO-1-2004-0989, ANO-2-2004-1187, ANO-2-2004-1186, and

ANO-2-2004-1200

A-9

Attachment

Engineering Calculation

ANO-2003-0618-000 and ANO-2003-0644-000

Operating Procedures

1304.181, Unit 1 RCS Radiation Leak Detection System Quarterly Test, Revision 8

2104.029, Service Water System Operations, Revision 54

2104.037, Alternate AC Diesel Generator Operations, Revision 6

2104.040, LPSI System Operations, Revision 35

2416.046, Unit 2 (2Y11, 2Y13, 2Y1113, 2Y22, 2Y24, and 2Y2224) Inverter Inspection, Test

and Maintenance Instructions, Revision 3

Work Order Packages

00035555 01, 00036437 01, 00038659 01, 50278828 01, 50336059 01, 50573018 01,

50747792 01, 50972347 01, and 50973055 01

Section 1R23: Temporary Plant Modifications

CRs

ANO-2-2004-0065, ANO-2-2004-0253, ANO-2-2004-0406, ANO-2-2004-0420,

ANO-2-2004-0446, ANO-2-2004-0472, ANO-2-2004-0671, ANO-2-2004-0694,

ANO-2-2004-0722, ANO-2-2004-0784, ANO-2-2004-1120, ANO-2-2004-1121,

and ANO-C-2004-0597

ER

ANO-2000-3275-003

Operating Procedures

1000.028, Control of Temporary Alterations, Revision 23

2104.039, HPSI System Operation, Revision 42

Work Orders

50276366 01 and 50276364 01

A-10

Attachment

Section 4OA2: Identification and Resolution of Problems

CRs

ANO-C-2004-0548

Operating Procedures

1015.047, Condition Reporting Operability and Immediate Reportability Determinations,

Revision 1

1203.025, Natural Emergencies, Revision 19

2203.008, Natural Emergencies, Revision 9

4OA3: Event Followup

CRs

ANO-1-1998-0300, ANO-1-2004-0645, and ANO-1-2004-0989

Operating Procedures

1107.003, Inverter and 120V Vital AC Distribution, Revision 12

1203.021, Loss of Neutron Flux Indication, Revision 8

1502.004, Control of Unit 1 Refueling, Revision 34

Section 4OA7: Licensee-Identified Violations

CRs

ANO-1-1998-0358, ANO-1-2004-0645, and ANO-1-2004-1373

A-11

Attachment

LIST OF ACRONYMS

ANO

Arkansas Nuclear One

AV

apparent violation

CAP

corrective action program

CFR

Code of Federal Regulations

CR

condition report

dpm

drops per minute

EDG

emergency diesel generator

EFW

emergency feedwater

ESF

engineered safety features

HELB

high energy line break

GE

General Electric

LER

licensee event report

NCV

noncited violation

NFPA

National Fire Protection Association

SSC

structure, system, or component

URI

unresolved item