05000293/LER-2004-002, High Pressure Coolant Injection System Fuse Failure While System Inoperable for Planned Maintenance and Testing

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High Pressure Coolant Injection System Fuse Failure While System Inoperable for Planned Maintenance and Testing
ML041250413
Person / Time
Site: Pilgrim
Issue date: 04/26/2004
From: Balduzzi M
Entergy Nuclear Operations
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
2.04.037 LER 04-002-00
Download: ML041250413 (6)


LER-2004-002, High Pressure Coolant Injection System Fuse Failure While System Inoperable for Planned Maintenance and Testing
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
2932004002R00 - NRC Website

text

Entergy Entergy Nuclear Operations, Inc.

Pilgrim Nuclear Power Station 600 Rocky Hill Road Plymouth, MA 02360 Michael A. Balduzzi Site Vice President April 26, 2004 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555

SUBJECT:

Entergy Nuclear Operations, Inc.

Pilgrim Nuclear Power Station Docket No.: 50-293 License No.: DPR-35 Licensee Event Report 2004-002-00 LETTER NUMBER:

2.04.037

Dear Sir or Madam:

The enclosed Licensee Event Report (LER) 2004-002-00, "High Pressure Coolant Injection System Fuse Failure While System Inoperable for Planned Maintenance and Testing," is submitted in accordance with 10 CFR 50.73.

There are no commitments contained in this letter.

Please do not hesit t act me if there are any questions regarding this report.

Sincerely, 5

(.4 -

DWE/dm Enclosure: LER 2004-002-00 cc:

Mr. Hubert J. Miller Regional Administrator, Region 1 U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Senior NRC Resident Inspector Mr. Travis Tate, Project Manager Office of Nuclear Reactor Regulation Mail Stop: 0-8B-1 U.S. Nuclear Regulatory Commission 1 White Flint North 11555 Rockville Pike Rockville, MD 20852 INPO Records

-- C

,-- -5 4-

- 1.

NRC Form 366 US. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150G0104 Estimated burden per response to comply with this mandatory information collection LICENSEE EVENT REPORT (LER) request: 50 hrs. Reported lessons learned are incorporated into the licensing process LIE E

and fed back to industry. Forward comments regarding burden estimate to the Records lr nManagement Branch (T-6 F33), U.S. Nuclear Regulatory Commission, Washington, (See reverse fornumberof DC 20555-0001, and to the Paperwork Reduction Project (3150-0104), Office of digits/characters for each block)

Management and Budget. Washington, DC 20503. If an information collection does not display a currently valid 01MB control number, the NRC may not conduct or sponsor, and a person is not required to respond to. the information collection.

FACILITY NAME (1)

DOCKET NUMBER (2)

PAGE (3)

PILGRIM NUCLEAR POWER STATION 05000-293 I of 5 TITLE (4)

High Pressure Coolant Injection System Fuse Failure While System Inoperable for Planned Maintenance and Testing EVENT DATE (5)

LER NUMBER (6)

REPORT DATE (7)

OTHER FACILITIES INVOLVED (8)

YERISEQUENTIAL NUMBER REVISION FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR NUMBER MONTH DAY YEAR N/A 05000 FACILrY NAME DOCT NUMBER 02 26 2004 2004 002 00 04 26 2004 N/A 05000

[

OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUI EMENTS OF 10 CFR: (Check one or more) (I1)

MODE (9)

N 20.2201 (b) 22.2203(a)(3)(i) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii)

POWER 22.2202(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A)

LEVEL (10) l 100 20.2203(a)(1) 20.2203(a)(4)

=

50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(2)(i) 50.36(3Xl)(i)(A) 5_ 0.73(a)(2)Xiii) 50.73(aX2)(ix)(A) 20.2203(a)(2)(ii) 50.36(3)(1)(ii)(A) 50.73(a)(2)(iv0A) 50.73(a)(2)(x) 20.2203(a)(2)(iii) 50.36(cX2) 50.73(a)(2)(v)(A) 73.71(aX4) 20.2203(a)(2)(iv) 50.46(a)(3)(ii)

I_ 0.73(a)(2)(v)(B) 73.71(aX5) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A)

=

_50.73(a)(2)(v)(C)

OTHER 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B)

X 50.73(a)(2)(v)(D)

Specify in Abstract below or in NRC Form 366A LICENSEE CONTACT FOR TIllS LER (12) l NAME TELEPHONE NUMBER (Include Area Code)

Bryan Ford - Licensing Manager l

(508) 830-8403 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN TIlS REPORT (13)

I REPORTABLE l

REPORTABLE

CAUSE

SYSTEM COMPONENT MANUFACTURER TO EPIX

CAUSE

SYSTEM COMPONENT MANUFACTURER TO EPIX X

BJ FU B569 y

j l

lAll SUPPLEMENTAL REPORT EXPECTED (14)

I EXPECTED mo.inTI DAY YEAR YES I

X NO SUBMISSION l(If yes, comnplete EXPECTED SUBMISSION DATE) l l

DATE (15) 1 1

1l ABSTRACT (Urnit to 1400 spaces. i.e.. approxinmtely 15 single-spaced typewritten lines) (16)

On February 26, 2004, the High Pressure Coolant Injection (HPCI) system turbine gland seal condenser (GSC) condensate pump motor became de-energized during post work testing while the HPCI system was inoperable for planned maintenance and testing. An approved analysis has not been conducted to determine the ability of the HPCI turbine to operate for the duration of the system's mission time with the GSC pump inoperable.

The root cause was separation of the fuse element from the fuse end cap (ferrule) that was most likely due to manufacturing defect(s) introduced when the fuse was manufactured (pre-1994). The defect(s) resulted in a weak solder connection between the fuse end cap and fuse element. Inspection of the fuse identified the fusible link to be intact. The fuse was a Bussman Limitron, Class RK1, KWN-R-10 type fuse. The fuse was replaced and the pump was post work tested with satisfactory results.

Corrective actions planned include the following. The scope of fuses to be replaced is being determined, new fuses are being procured, and selected fuses will be replaced with new fuses.

This condition posed no threat to public health and safety.

NRC FORM 366

iU.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUI'.IBER (2)

LER NUMBER (6)

PAGE (3) i SEQUENTIAL REVISION YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000-293 2004 002 00 2 of 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

BACKGROUND The Pilgrim Station core standby cooling systems (CSCS) consist of the high pressure coolant injection (HPCI) system, automatic depressurization system (ADS), residual heat removal (RHR) system low pressure injection (LPCI) mode, and core spray system. The HPCI system is designed to pump water into the reactor vessel for high pressure core cooling. Although not part of the CSCS, the reactor core isolation cooling (RCIC) system is also designed to pump water into the reactor vessel for high pressure core cooling, similar to the HPCI system.

The motive power for water injection into the reactor vessel from the HPCI system is provided by the HPCI turbine-pump (P-205). The turbine is equipped with instrumentation and accessories that include the gland seal condenser (GSC), GSC condensate pump (P-220), and GSC blower. The GSC functions to condense steam from the HPCI turbine gland seal system. A portion of the water from pump P-205 is directed to the GSC for the condensing function. The GSC blower functions to exhaust non-condensible gases from the GSC. Pump P-220 functions to pump condensate from the GSC. Pump -P220 is designed to automatically start if the condensate level in the GSC increases to a preset level, and can be manually started via a control switch in the control room. The control circuit for pump P-220 is powered by 125-volt DC power and is protected and powered by a fuse such that the circuit is de-energized by the electrical opening or removal of the fuse.

Technical Specification (TS) 3.5.C.1 specifies HPCI system operability when irradiated fuel is in the reactor vessel, reactor pressure is greater than 150 psig, and reactor coolant temperature is greater than 365° F. TS 3.5.C.2 specifies a 14-day limiting condition for operation (LCO) from and after the date the system is made or found inoperable for any reason provided that during such 14 days all active components of the ADS, RCIC system, RHR system (LPCI mode), and core spray system are operable. TS 3.5.C.3 specifies a 24-hour timeframe for the initiation of an orderly shutdown (to a cold shutdown condition) if the requirements of Technical Specification 3.5.C cannot be met.

On February 25, 2004, at about 0450 hours0.00521 days <br />0.125 hours <br />7.440476e-4 weeks <br />1.71225e-4 months <br />, the HPCI system was removed from service in accordance with Technical Specification 3.5.C.2 and tagged for planned maintenance and testing. As part of the maintenance activities, a pre-evolution briefing was conducted at about 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br /> for a manual start of the HPCI system. After completing the prerequisites, the HPCI turbine was started in accordance with the procedure at about 0057 hours6.597222e-4 days <br />0.0158 hours <br />9.424603e-5 weeks <br />2.16885e-5 months <br /> on February 26, 2004. The turbine was stopped in accordance with the procedure at about 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />.

EVENT DESCRIPTION

On February 26, 2004 at about 0105 hours0.00122 days <br />0.0292 hours <br />1.736111e-4 weeks <br />3.99525e-5 months <br />, it was identified that the power indicating lamp for the HPCI turbine GSC condensate pump P-220 was not illuminated as expected and that pump P-220 would not operate. The discovery occurred about 5 minutes after the HPCI turbine was stopped in accordance with the procedure for a manual start of the HPCI turbine.

Initial investigation found the fuse to the pump to be electrically open. The fuse was replaced. After the fuse replacement, pump P-220 was tested with satisfactory results.U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER (2)

LER NUMBER (6)

PAGE (3)

SEQUENTIAL REVISION YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000-293 2004 002 00 3 of 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

The NRC Operations Center was notified of the condition on February 26, 2004, at 0838 hours0.0097 days <br />0.233 hours <br />0.00139 weeks <br />3.18859e-4 months <br />, in accordance with 10 CFR 50.72. This action was taken because an approved analysis has not been conducted to determine the ability of the HPCI turbine to operate for its mission time without the operation of the GSC and/or GSC blower and/or GSC condensate pump P-220.

After the completion of the planned maintenance and testing of the HPCI system, the system was returned to operable, standby service by 1818 hours0.021 days <br />0.505 hours <br />0.00301 weeks <br />6.91749e-4 months <br /> on February 27, 2004.

The condition occurred while at 100 percent reactor power with the reactor mode selector switch in the RUN position. The reactor vessel pressure was approximately 1035 psig with the reactor water temperature at the saturation temperature for the reactor pressure.

CAUSE

The cause was the failure of a 10-amp fuse in the 125-volt DC control power circuit for pump P-220.

The fuse was manufactured by Bussman Limitron, Class RK1, KWN-R-1 0; no date code was identified on the fuse.

An examination of the fuse failure and previous fuse failures revealed the fuse elements did not open, indicating the fuse(s) did not experience an overcurrent condition. Further examination indicated each fuse failure was due to separation of the fuse element end tab from the inside end cap (ferrule).

The root cause was separation of the fuse element from the fuse end cap (ferrule) that was most likely due to manufacturing defect(s) introduced when the fuse was manufactured (pre-1994). The defect(s) resulted in a weak solder connection between the fuse end cap and fuse element. The separation occurred as a result of a weak solder connection.

CORRECTIVE ACTION

The following corrective actions have been taken.

The failed fuse was replaced. After the fuse replacement, pump P-220 was tested with satisfactory results.

Pilgrim specific fuse failure history searches were performed to identify premature fuse failures.

Testing has been performed on about 300 spare Bussman KWN-R type fuses. The testing identified 3 additional fuse failures (separation of the fuse element end tab from the inside end cap).

A hold has been placed on all Bussman type KWN-R and type KTK fuses manufactured before 1994 that are in the warehouse inventory.

Corrective actions planned include the following. The scope of fuses to be replaced is being determined, new fuses are being procured, and selected fuses will be replaced with new fuses.

These actions are being tracked in the corrective action program.

NRC FORM 36U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (I)

DOCKET NUMBER (2)

LER NUMBER (6)

PAGE (3) l SEQUENTIAL REVISION YEAR.

NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000-293 2004 002 00 4 of5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

SAFETY CONSEQUENCES

The condition posed no threat to public health and safety.

The power indicating lamp for pump P-220 was discovered not illuminated by the on-shift control room licensed operator at about 0105 hours0.00122 days <br />0.0292 hours <br />1.736111e-4 weeks <br />3.99525e-5 months <br /> on February 27, 2004. The control room panels are walked-down during each shift turnover of the control room operators. The power and position indicating lamps on the control panels, including the indicating lamp for pump P-220, are observed during the shift turnover walkdown and are also observed periodically during each shift by the on-shift licensed operator. The power and position indicating lamps are also observable by other on-shift licensed operators in the control room including the Operations Shift Supervisor. During these activities, the indicating lamp for pump P-220 was illuminated. Therefore, the fuse failure is assumed to have occurred at or near the time of discovery.

The Core Standby Cooling Systems (CSCS) consist of the HPCI system, Automatic Depressurization system (ADS), Core Spray system, and the Residual Heat Removal (RHR) system in the Low Pressure Core Coolant Injection (LPCI) mode. Although not part of the CSCS, the Reactor Core Isolation Cooling (RCIC) system is capable of providing water to the reactor vessel for high pressure core cooling, similar to the HPCI system. During the period the HPCI system was inoperable for planned maintenance and testing, the RHR system was inoperable for the LPCI mode for brief periods when the RHR system was aligned for the suppression pool cooling mode. These brief periods were less than the 24-hour timeframe specified by Technical Specification 3.5.C.3. Except for those periods, the RHR/LCPI mode and the ADS, Core Spray, and RCIC systems were operable. In the unlikely event the RCIC system was to become inoperable while the HPCI system was inoperable and core cooling was necessary, an actuation (automatic or manual) of the ADS would function to reduce reactor vessel pressure for low pressure core cooling provided independently by the RHR (LPCI mode) and/or Core Spray system.

The HPCI system was operable before the system was removed from service when the pump P-220 fuse failure occurred. Although the fuse failure would not have prevented the system from automatically or manually starting and responding as designed, if the fuse failure had occurred when the HPCI system was operating the failure of pump P-220 resulting from the fuse failure could have potentially prevented the system from operating for the duration of the system's mission time.

REPORTABILITY

This report was submitted in accordance with 10 CFR 50.73(a)(2)(v)(D) because the HPCI turbine GSC pump P-220 motor was de-energized. Although the fuse failure occurred after the HPCI system was removed from service in accordance with Technical Specifications, it could not be conclusively determined the system would have operated with a fuse failure and resultant failure of pump P-220 during the system's mission time. An approved analysis has not been conducted to determine the ability of the HPCI turbine to operate for the system's mission time without the operation of the GSC and/or GSC condensate pump P-220 and/or GSC blower.

NKC'Foirn 366A U.S. NUCLEAR REGULATORY COMMIISSION LICENSEE EVENT REPORT (LER)

TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER (2)

LER NUMBER (6)

PAGE (3)

SEQUENTIAL REVISION YEAR NUMBER NUMBER PILGRIM NUCLEAR POWER STATION 05000-293 2004 002 00 5 of 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

SIMILARITY TO PREVIOUS EVENTS A review was conducted of Pilgrim Station Licensee Event Reports (LERs) issued since 1995. The review focused on LERs involving fuse failures. This review identified a similar event reported in LER 2002-001 -00, "HPCI System Inoperable due to Fuse Failure." The cause was a failed fuse (Bussman type KWN-R-10) that is part of the 125-volt DC control power circuit of the normally closed HPCI system injection valve MO-2301-8. Inspection of the failed fuse identified a separation that had occurred at an internal solder connection between the fuse end cap and the fusible link.

ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES The EIIS codes for this report are as follows:

COMPONENTS CODES Fuse FU Pump (P-220)

P SYSTEMS High Pressure Coolant Injection (HPCI) system BJ DC Power system-Class 1 E EJ