CPSES-200400378, Transmittal of the Annual Operating Report for 2003

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Transmittal of the Annual Operating Report for 2003
ML040650376
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 02/27/2004
From: Madden F
TXU Electric
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
CPSES-200400378, RP-85, TXX-04035
Download: ML040650376 (18)


Text

-J -

  • o TXU 14At-ext TXU Energy Mike Blevins Comanche Peak Steam Senior Vice President & Principal Nuclear Officer Electric Station P.O.Box 1002 (E01)

Glen Rose,TX 76043 Tel: 254 897 5209 Fax: 254 897 6652 mike.blevins@txu.com CPSES-200400378 Log # TXX-04035 RP-85 Ref. # 10CFR50.36 February 27, 2004 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)

DOCKET NOS. 50-445 AND 50-446 ANNUAL OPERATING REPORT FOR 2003 Gentlemen:

Attached is the CPSES Annual Operating Report for 2003 prepared and submitted pursuant to guidance provided in C.I.b of U.S. NRC Regulatory Guide 1.16, Revision

4. The attachment also submits the annual Occupational Radiation Exposure Report as required by Technical Specification 5.6.1 contained in Appendix A to the Comanche Peak Steam Electric Station Unit 1 Operating License NPF-87 and Unit 2 Operating License NPF-89.

If you have any questions, please contact Mr. Douglas W. Snow at (254j 897-8448.

S TXU TXX-04035 PAGE 2 OF 2 This communication contains no new licensing basis commitments regarding CPSES Units 1 and 2.

Sincerely, TXU Generation Company LP By: TXU Generation Management Company LLC Its General Partner Mike Blevins By: I/ '(? 2 Fred W. Madden Nuclear Licensing Manager DWS/dws Attachment c- B. S. Mallet, Region IV W. D. Johnson, Region IV M. C. Thadani, NRR Resident Inspectors, CPSES Mail Original copy of Personnel Exposure & Monitoring Report to:

Ms. Sheryl Burrows, REIRS Project Manager Office of Nuclear Regulatory Research U.S. Nuclear Regulatory Commission Washington, DC 20555

1.0

SUMMARY

OF OPERATING EXPERIENCE The Comanche Peak Steam Electric Station (CPSES) is a dual unit pressurized water reactor power plant, supplied by Westinghouse Electric Corporation. It is located in Somervell County in North Central Texas approximately 65 miles southwest of the Dallas-Fort Worth Metropolitan area. Each generating unit core was originally designed for a warranted power output of 3411 Megawatt thermal (MWt). This output, combined with the reactor coolant pump heat output of 14 MWt, gives a warranted NSSS output of 3425 MWt, which is the license application rating. Both units rated thermal power was subsequently increased to 3458 MWt, which represents a 1.4 percent increase in core output (from 3411 to 3458 MWt). The reactor coolant pump heat output considered in the safety analysis was increased to approximately 16 MWt for both units. All safety systems, including the engineered safety features, are designed for operations at a maximum NSSS output of 3579 MWts and an associated maximum core output of 3565 MWt 1.1 CPSES UNIT I CPSES Unit I achieved initial criticality on April 3, 1990. Initial power generation occurred on April 24, 1990, and the plant was declared commercial on August 13, 1990. Since being declared commercial, CPSES Unit I has generated 108,985,123 net Megawatt-hours (MWH) of electricity as of December 31, 2003, with a net unit capacity factor of 80.8% (using MDC). The unit and reactor availability factors were 87.2% and 90.4%, respectively, for the year 2003.

There was no refueling outage for Unit I during 2003.

Figure 1.1-1 provides the generation profile of the average daily net electrical output of Unit 1 for 2003. Table 1.1-1 is a compilation of the monthly summaries of the operating data and Table 1.1-2 contains the yearly and total summaries of the operating data.

During this reporting period there were no failures or challenges to the Safety Valves.

1.2 CPSES UNIT 2 CPSES Unit 2 achieved initial criticality on March 24, 1993. Initial power generation occurred on April 9, 1993, and the plant was declared commercial on August 3, 1993. Since being declared commercial, CPSES Unit 2 has generated 87,055,302 net Megawatt-hours (MWH) of electricity as of December 31, 2003, with a net unit capacity factor of 82.9% (using MDC). The unit and reactor availability factors were 88.0% and 91.2%, respectively, for the year 2003.

On October 4, 2003, the unit began the power ramp down for its seventh refueling outage. The unit entered the refueling outage on the same day.

During the refueling outage, 84 fresh fuel assemblies were loaded for Cycle 8. The refueling outage lasted 25 days and ended on October 29, 2003. Unit 2 reached 100% power on November 6, 2003.

1

During the refueling outage, the major work scope completed included:

  • Reactor Vessel BMI and Alloy 600 Inspections
  • Inspect and replace one RCP cartridge seal
  • Minor Inspection of Main Generator and exciter.
  • Digital Turbine Generator upgrade
  • Fuel Corrosion (Oxide) Measurements to Support the Elevated pH Program Figure 1.2-1 provides the generation profile of the average daily net electrical output of Unit 2 for 2003. Table 1.2-1 is a compilation of the monthly summaries of the operating data and Table 1.2-2 contains the yearly and the total summaries of the operating data During this reporting period there were no failures or challenges to the Safety Valves.

2.0 OUTAGES AND REDUCTIONS IN POWER 2.1 CPSES UNIT 1 Table 2.1 describes unit operating experience including unit shutdowns and provides explanations of significant dips in average power levels for CPSES Unit 1.

2.2 CPSES UNIT 2 Table 2.2 describes unit-operating experience including unit shutdowns and provides explanations of significant dips in average power levels for CPSES Unit 2.

3.0 EXPOSURE AND MONITORING REPORT The personnel exposure and monitoring report for CPSES is provided in Table 3.0.

4.0 IRRADIATED FUEL INSPECTION RESULTS 4.1 CPSES UNIT I There were no irradiated fuel inspections performed on Unit 1 fuel in 2003.

4.2 CPSES UNIT 2 During refueling outage 2RF07, visual examinations of Unit 2, Cycle 7 fuel assemblies were performed by inspection personnel by viewing the assemblies from the edge of Spent Fuel Pool

  1. 2 as assemblies were off-loaded from the core. Visual underwater camera exams were also performed on selected assemblies as part the oxide measurement campaign performed during the outage in support of the demonstration elevated pH program.

From the inspections discussed above, all fuel assemblies appeared to be in good condition with no anomalies observed. During the underwater camera examinations performed during the oxide measurement campaign, the surface of the rods in the lower duty/burnup assemblies generally appeared to contain less crud than observed during underwater camera inspections performed during previous outages. However, some of the higher duty/burnup assemblies contained "streaks" of crud in the upper portion of the fuel assembly.

2

Fuel Clad Corrosion (Oxide) Measurements:

Review of 2RF06 Results:

During the previous Unit 2 refueling outage (2RF06), eight fuel assemblies were inspected for crud deposition and cladding corrosion (oxide thickness). The purpose of this exam was to benchmark crud and corrosion performance before implementation of an elevated RCS pH program in Unit 2 beginning in Cycle 7. All assemblies measured were of the Framatome ANP design with optimized zircaloy4 clad. The measured oxide thickness results were generally as expected with some minor crud deposition observed on most fuel assemblies. A few specific locations contained darker, thicker crud.

2RF07 Results:

The purpose of the oxide measurements performed during 2RF07 was to determine if there had been any significant increase in oxide thickness which could have resulted from operation of the demonstration elevated pH program during Cycle 7. Unit 2, Cycle 7 was operated at a reactor coolant pHt of 7.3 with a maximum lithium concentration of 5 ppm. During this oxide measurement campaign, oxide measurements were again performed on Framatome ANP fuel assemblies that were measured during 2RF06 and on four once-burned Westinghouse supplied fuel assemblies containing ZIRLOGm clad. The Westinghouse supplied assemblies were loaded fresh during 2RF06.

Based on the results of the oxide measurements, the continuation of the demonstration elevated pH program for U2C8 operation was approved. The results of the oxide measurements and crud observations and comparisons to previous campaigns and vendor predictions were reviewed with no significant adverse trends observed. There were no other issues identified that precluded an increase in the pH program for U2C8 operation. Therefore, based upon the review of the data, the continuation of the demonstration Unit 2 elevated pH program was approved and implemented at a constant pHt of 7.4 with a maximum lithium concentration of 6 ppm.

A report containing raw oxide measurement data and a summary of the results and conclusions of the oxide measurement campaign during 2RF07 was transmitted to the Nuclear Regulatory Commission on January 25, 2004 (TXU Energy letter TXX-04016).

5.0 OUTAGE RELATED SINGLE RADIOACTIVITY RELEASE OR RADIATION EXPOSURE TO AN INDIVIDUAL THAT ACCOUNTS FOR MORE THAN 10 PERCENT OF ALLOWABLE ANNUAL VALUES CPSES Units I and 2 did not experience any single release of radioactivity greater than 10% of an allowable dose limit during an outage or forced reduction in power of over 20% of designed power level during 2003.

During 2003 Unit 2 conducted a refueling outage (see section 1.2). During the outage activities, no individual received radiation exposure exceeding 10% of an allowable dose limit in a single exposure event. Exposure is tabulated in Table 6.0.

3

FIGURE 1.1-1 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT I GENERATION PROFILE AVERAGE DAILY UNIT POWER LEVEL for 2003 b

-,om.

F

.4CO

'. I I JAN FEB WNR APR MAY JUN JUL AUG SEP OCT NOV DEC 4

TABLE 1.1-1 (PAGE I OF 2)

COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 1 MONTHLY ELECTRIC POWER GENERATION DATA (2003)

January February March April May June Hours RX was Critical 744 672 727.6 719.0 672.4 720 RX Reserve Shutdown Hours 0 0 0 0 0 0 Hours Generator On-line 744 672 719.1 719.0 662.2 720 Unit Reserve Shutdown Hours 0 0 0 0 0 0 Gross Thermal Energy Generated (MWH) 2,569,380 2,321,038 1,993,313 2,482,903 2,237,614 2,486,938 Gross Electric Energy Generated (MWH) 884,945 798,346 672,342 853,610 765,695 847,178 Net Electric Energy Generated (MWH) 852,609 769,134 641,276 821,591 734,011 814,668 RX Service Factor (%) 100.0 100.0 97.8 100.0 90.4 100.0 RX Availability Factor (%) 100.0 100.0 97.8 100.0 90.4 100.0 Unit Service Factor (%) 100.0 100.0 96.7 100.0 89.0 100.0 Unit Availability Factor (%) 100.0 100.0 96.7 100.0 89.0 100.0 Unit Capacity Factor(%, using MDC net) 99.7 99.5 75.0 99.4 85.8 98.4 Unit Capacity Factor(%, using DER net) 99.7 99.5 75.0 99.4 85.8 98.4 Unit Forced Outage Rate (%) 0.0 0.0 3.3 0.0 0.0 0.0 Hours in Month 744 672 744 719 744 720 5

TABLE 1.1-1 (PAGE 2 OF 2)

COMANCHE PEAK STEAM ELECTRIC STATION - UNIT I MONTHLY ELECTRIC POWER GENERATION DATA (2003)

July Augus September October November December Hours RX was Critical 744 744.0 720.0 745.0 720.0 744.0 RX Reserve Shutdown Hours 0 0.0 0.0 0.0 0 0 Hours Generator On-line 744 744.0 720.0 745.0 720.0 744.0 Unit Reserve Shutdown Hours 0 0 0 0 0 0 Gross Thermal Energy Generated (MWH) 2,569,747 2,564,875 2,486,184 2,573,429 2,471,971 2,569,728 Gross Electric Energy Generated (MWH) 870,587 865,623 843,926 881,215 849,116 883,484 Net Electric Energy Generated (MWH) 837,024 832,085 811,451 846,222 815,618 850,264 RX Service Factor (%) 100.0 100.0 100.0 100.0 100.0 100.0 RX Availability Factor (%) 100.0 100.0 100.0 100.0 100.0 100.0 Unit Service Factor (%) 100.0 100.0 100.0 100.0 100.0 100.0 Unit Availability Factor (%) 100.0 100.0 100.0 100.0 100.0 100.0 Unit Capacity Factor(%, using MDC net) 97.8 97.3 98.0 98.8 98.5 99.4 Unit Capacity Factor(%, using DER net) 97.8 97.3 98.0 98.8 98.5 99.4 Unit Forced Outage Rate (%) 0.0 0.0 0.0 0.0 0.0 0.0 Hours in Month 744 744 720 745 720 744 6

TABLE 1.1-2 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT I ANNUAL ELECTRIC POWER GENERATION DATA (2003)

YEAR CUMULATIVE Hours RX was Critical 8,672.0 103,185 RX Reserve Shutdown Hours 0.0 2,871 Hours Generator On-line 8,653.3 102,316 Unit Reserve Shutdown Hours 0 0 Gross Thermal Energy Generated (MWH) 29,327,119 339,433,298 Gross Electric Energy Generated (MWH) 10,016,067 113,921,660 Net Electric Energy Generated (MWH) 9,625,953 108,985,123 RX Service Factor (%) 99.0 87.9 RX Availability Factor (%) 99.0 90.4 Unit Service Factor (%) 98.8 87.2 Unit Availability Factor (%) 98.8 87.2 Unit Capacity Factor(%, using MDC net) 95.6 80.8 Unit Capacity Factor(%, using DER net) 95.6 80.8 Unit Forced Outage Rate (%) 0.3 3.0 7

FIGURE 1.2-1 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 2 GENERATION PROFILE A.

AVERAGE DAILY UNIT POWER LEVEL for 2003 1 ,'400 1 toJQ 1 ,cCKII 8.000 600 4aa cl JAN FED MAR APR FMAY JUN JUL AUG SEP OCT NOV DEC TABLE 1.2-1 (PAGE 1 OF 2)

COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 2 8

MONTHLY ELECTRIC POWER GENERATION DATA (2003)

January February March April May June Hours RX was Critical 744 672 744.0 719.0 411.0 720.0 RX Reserve Shutdown Hours 0 0 0 0 0 0 Hours Generator On-line 744 672 744.0 719.0 398.2 720.0 Unit Reserve Shutdown Hours 0 0 0 0 0 0 Gross Thermal Energy Generated (MWH) 2,560,486 2,315,078 2,567,032 2,475,564 1,320,086 2,465,263 Gross Electric Energy Generated (MWH) 883,813 799,510 886,240 854,238 452,051 842,521 Net Electric Energy Generated (MWH) 851,597 770,225 853,833 821,864 422,165 809,240 RX Service Factor (%) 100.0 100.0 100.0 100.0 55.2 100.0 RX Availability Factor (%) 100.0 100.0 100.0 100.0 55.2 100.0 Unit Service Factor (%) 100.0 100.0 100.0 100.0 53.5 100.0 Unit Availability Factor (%) 100.0 100.0 100.0 100.0 53.5 100.0 Unit Capacity Factor(%, using MDC net) 99.5 99.7 99.8 99.4 49.3 97.7 Unit Capacity Factor(%, using DER net) 99.5 99.7 99.8 99.4 49.3 97.7 Unit Forced Outage Rate (%) 0.0 0.0 0.0 0.0 0.0 0.0 Hours in Month 744 672 744 719 744 720 9

TABLE 1.2-1 (PAGE 2 OF 2)

COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 2 MONTHLY ELECTRIC POWER GENERATION DATA (2003)

July August September October November December Hours RX was Critical 357.6 744.0 720.0 169.5 720 662.0 RX Reserve Shutdown Hours 0 0 0 0 0 0 Hours Generator On-line 338.6 744.0 720.0 138.1 720 650.4 Unit Reserve Shutdown Hours 0 0 0 0 0 0 Gross Thermal Energy Generated (MWH) 1,117,992 2,547,907 2,473,497 337,438 2,381,926 2,179,147 Gross Electric Energy Generated (MWH) 376,945 856,295 842,366 110,841 823,542 755,006 Net Electric Energy Generated (MWH) 348,869 822,417 809,059 97,540 792,991 723,560 RX Service Factor (%) 48.1 100.0 100.0 22.7 100.0 89.0 RX Availability Factor (%) 48.1 100.0 100.0 22.7 100.0 89.0 Unit Service Factor (%) 45.5 100.0 100.0 18.5 100.0 87.4 Unit Availability Factor (%) 45.5 100.0 100.0 18.5 100.0 87.4 Unit Capacity Factor(%, using MDC net) 40.8 96.1 97.7 11.4 95.8 84.6 Unit Capacity Factor(%, using DER net) 40.8 96.1 97.7 11.4 95.8 84.6 Unit Forced Outage Rate (%) 54.5 0.0 0.0 0.0 0.0 12.6 Hours in Month 744 744 720 745 720 744 10

TABLE 1.2-2 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 2 ANNUAL ELECTRIC POWER GENERATION DATA (2003)

YEAR CUMULATIVE Hours RX was Critical 7,383.1 80,836 RX Reserve Shutdown Hours 0 2,366 Hours Generator On-line 7,308.2 80,286 Unit Reserve Shutdown Hours 0 0 Gross Thernal Energy Generated (MWH) 24,741,416 267,076,710 Gross Electric Energy Generated (MWH) 8,483,368 90,781,110 Net Electric Energy Generated (MWH) 8,123,390 87,055,302 RX Service Factor (%) 84.3 88.6 RX Availability Factor (%) 84.3 91.2 Unit Service Factor (%) 83.4 88.0 Unit Availability Factor (%) 83.4 88.0 Unit Capacity Factor(%, using MDC net) 80.6 82.9 Unit Capacity Factor(%, using DER net) 80.6 82.9 Unit Forced Outage Rate (%) 6.4 3.1 11

TABLE 2.1 (PAGE I OF I)

COMANCHE PEAK STEAM ELECTRIC STATION - UNIT I UNIT OPERATING EXPERIENCE INCLUDING SHUTDOWNS AND POWER REDUCTIONS DURING 2003 METHOD OF TYPE SHUT17ING DOWN F: FORCED DURATION* THE REACTOR OR NO DATE S: SCHEDULED (HOURS) REASON REDUCING POWER CORRECTIVE ACTION/COMMENTS 1 030316 F 24.87 A 2 On March 16, at 2149 hours0.0249 days <br />0.597 hours <br />0.00355 weeks <br />8.176945e-4 months <br />, the Condensate Pump 1-01 tripped, this caused the Feedwater Pumps to trip and a manual reactor trip was initiated. On March 17, at 2241 hours0.0259 days <br />0.623 hours <br />0.00371 weeks <br />8.527005e-4 months <br />, Unit I sync to grid and ramped to approximately 57% power. Unit held at 57% power during pump motor repair. Motor was reinstalled and ramp to full power began on March 30 at 2300. Unit reached full power on March 31 at 1252 hours0.0145 days <br />0.348 hours <br />0.00207 weeks <br />4.76386e-4 months <br />. (Reference LER 1-03-002-00 & SMF-2003-000754) 2 030515 F 81.80 H 3 On May 15 at 0252 hours0.00292 days <br />0.07 hours <br />4.166667e-4 weeks <br />9.5886e-5 months <br /> Unit I experienced an automatic reactor trip due to grid instability and the loss of the 345 KV Switchyard (dual unit trip). Lightning is the suspected cause of the switchyard loss. On May 18 at 1238 hours0.0143 days <br />0.344 hours <br />0.00205 weeks <br />4.71059e-4 months <br /> Unit I synchronized to the grid. On May 19 at 1620 hours0.0188 days <br />0.45 hours <br />0.00268 weeks <br />6.1641e-4 months <br /> Unit I reached full power.

(Reference LER 1-03-003-00)

I) REASON 2) METHOD A: EQUIPMENT FAILURE (EXPLAIN) E: OPERATOR TRAINING AND LICENSE EXAMINATION 1: MANUAL B: MAINT OR TEST F: ADMINISTRATIVE 2: MANUAL SCRAM C: REFUELING G: OPERATIONAL ERROR (EXPLAIN) 3: AUTOMATIC SCRAM D: REGULATORY RESTRICTION II: OTHER (EXPLAIN) 4: OTHER (EXPLAIN)

  • INDICATES SHUTDOWN HOURS/OTHERWISE 'NA' FOR NOT APPLICABLE 12

TABLE 2.2 (PAGE I OF 2)

COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 2 UNIT OPERATING EXPERIENCE INCLUDING SHUTDOWNS AND POWER REDUCTIONS DURING 2003 METHOD OF TYPE SHUTIING DOWN F: FORCED DURATION* THE REACTOR OR NO DATE S: SCHEDULED (HOURS) REASON REDUCING POWER CORRECTIVE ACTION/COMMENTS 1 030515 345.80 H 3 On May 15 at 0252, Unit 2 experienced an automatic reactor trip due to grid instability and the loss of the 345 KV switchyard (dual unit trip). In a post trip inspection a primary water leak was found and repaired. On May 29 Unit 2 synchronized to the grid. On May 30 Unit 2 achieved full power.(Reference LER 1-03-003-00) 2 030709 395.10 A 3 On July 9 at 0108, Unit 2 had an automatic reactor scram due to a Phase B ground on RCP Motor stator. Unit taken to Mode 5 for repairs. Repairs were completed and the unit became critical on July 25 at 0333. The unit returned to service on July 25 at 1214.

(Reference LER 446 03-001-00) 3 030725 10.30 H 4 On July25 at 1317, the Unit 2 turbine was taken off line from 12%

power due to lack of suction pressure on the Main Feedwater Pumps. The reactor remained critical in Mode 2. The unit returned to service at 2334 on the same day. The unit returned to full power on July 26 at 2350. (Reference LER 446 03-002-00) 4a 031004 606.95 C I On October 4 at 0900, Unit 2 began downpowering from full power.

At 1127 on the same day the unit was tripped per procedure entering 2RF07. The refueling outage was completed and the unit returned to power operations with sync to grid on October 29, 2003 at 1724. At the end of the month the unit was at 43% power, ramping to the 45% power-testing plateau.

I) REASON 2) METHOD A: EQUIPMENT FAILURE (EXPLAIN) E: OPERATOR TRAINING AND UCENSE EXAMINATION 1: MANUAL B: MAINT OR TEST F: ADMINISTRATIVE 2: MANUAL SCRAM C: REFUELING G: OPERATIONAL ERROR (EXPLAIN) 3: AUTOMATIC SCRAM D: REGULATORY RESTRICTI0N If: OTIIER (EXPLAIN) 4: OTHER (EXPLAIN)

  • INDICATES SHUTDOWN HOURS/OTIERWISE NA FOR NOT APPUCABLE 13

TABLE 2.2 (PAGE 2 OF 2)

COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 2 UNIT OPERATING EXPERIENCE INCLUDING SHUTDOWNS AND POWER REDUCTIONS DURING 2003 METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION* THE REACTOR OR NO DATE S: SCHEDULED (HOURS) REASON REDUCING POWER CORRECTIVE ACTION/COMMENTS 4b 031101 S C l Unit began the month of November at 43% power ramping to full power after completion of 2RF07. Unit reached full power on November 5 at 0912.

5 031222 F 93.62 A 3 On December 22 at 0827, the Unit 2 turbine and reactor tripped due to an inspection plate that fell and made contact with the generator exciter. The plate caused arching and smoke in the exciter and an automatic turbine/reactor trip. Immediate inspection determined there was no fire but there was damage to the fuses and diodes on the exciter "A" rectifier wheel. After repairs were completed the unit returned to power operations with sync to the grid on December 26 at 0604 and returned to full power on December 27 at 1615.

(Reference LER 2-03-005-00)

I) REASON 2) METHOD A: EQUIPMENT FAILURE (EXPLAIN) E: OPERATOR TRAINING AND LUCENSE EXAMINATION 1: MANUAL B: MAINT OR TEST F: ADMINISTRATIVE 2: MANUAL SCRAM C: REFUEUNG G: OPERATIONAL ERROR (EXPLAIN) 3: AUTOMATIC SCRAM D: REGULATORY RESTRICTION H: OTIlER (EXPLAIN) 4: OTHER (EXPLAIN)

  • INDICATES SHUTDOWN HOURS/OTHERWISE 'NA FOR NOT APPLICABLE 14

TABLE 3.0 COMANCHE PEAK STEAM ELECTRIC STATION - UNITS I AND 2 2003 PERSONNEL EXPOSURE AND MONITORING REPORT

  1. Personne Total Person rem Work & Job Function Saio Utili Contract Station Utility Contract Reactor Operations & Surveillance Maintenance & Construction 93 0 48 0.418 0.000 0.131 Operations 218 0 103 2.768 0.000 0.210 Health Physics & Lab 44 0 36 1.327 0.000 0.230 Supervisory & Office Staff 20 0 2 0.067 0.000 0.037 Engineering Staff 78 0 25 0.565 0.000 0.062 Routine Plant Maintenance Maintenance & Construction 165 0 328 3.830 0.000 21.061 Operations 131 0 16 3.211 0.000 0.430 Health Physics & Lab 34 0 69 1.073 0.000 3.787 Supervisory& Office Staff II 0 0 0.147 0.000 0.000 Engineering Staff 50 0 73 0.986 0.000 8.228 In-service Inspection Maintenance & Construction 15 0 25 0.276 0.000 0.445 Operations 15 0 3 0.104 0.000 0.086 Health Physics & Lab 2 0 8 0.051 0.000 0.087 Supervisory & Office Staff 1 0 0 0.003 0.000 0.000 Engineering Staff 9 0 64 0.551 0.000 5.718
  • Special Plant Maintenance Maintenance & Construction 21 0 100 0.046 0.000 0.650 Operations 20 0 3 0.289 0.000 0.003 Health Physics & Lab 5 0 4 0.018 0.000 0.002 Supervisory & Office Staff 2 0 0 0.014 0.000 0.000 Engineering Staff 5 0 11 0.012 0.000 0.053 Waste Processing Maintenance & Construction 9 0 13 0.008 0.000 0.104 Operations 17 0 4 0.143 0.000 0.228 Health Physics & Lab 29 0 6 0.356 0.000 0.024 Supervisory & Office Staff 0 0 0 0.000 0.000 0.000 Engineering Staff 1 0 0 0.032 0.000 0.000 Refueling Maintenance & Construction 49 0 33 0.206 0.000 1.141 Operations 32 0 4 0.482 0.000 0.012 Health Physics & Lab 18 0 45 0.552 0.000 1.320 Supervisory & Office Staff 2 .0 0 0.004 0.000 0.000 Engineering Staff 16 1 45 0.340 0.001 10.311 Totals Maintenance & Construction 352 0 547 4.786 0.000 23.532 Operations 433 0 133 6.997 0.000 0.969 Health Physics & Lab 132 0 168 3.377 0.000 5.450 Supervisory & Office Staff 36 0 2 0.234 0.000 0.037 Engineering Staff 159 1 218 2.487 0.001 24.371 Grand Totals 1112 1 1068 17.881 0.001 54.359
  • Design Modifications TABLE 6.0 15

2003 COMANCHE PEAK STEAM ELECTRIC STATION - UNITS I AND 2 OUTAGE RELATED RADIATION EXPOSURE TO AN INDIVIDUAL FOR A SINGLE MAINTENANCE ACTIVITY WHICH EXCEEDS 10 PERCENT OF AN ALLOWABLE ANNUAL DOSE LIMIT*

Individual's Maintenance Single Event Total Annual Activity Department Exposure (mrem) Exposure (mrem)

N/A N/A N/A N/A No activities exceeded the allowable 10 percent dose limit.