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Category:Annual Operating Report
MONTHYEARCP-202200003, (CPNPP) - Annual Report of Changes in Peak Cladding Temperature2022-05-16016 May 2022 (CPNPP) - Annual Report of Changes in Peak Cladding Temperature CP-202100152, (CPNPP) - 2020 Annual Radioactive Effluent Release Report2021-04-28028 April 2021 (CPNPP) - 2020 Annual Radioactive Effluent Release Report CP-201800383, Amended Annual Report of Changes in Peak Cladding Temperature2018-06-20020 June 2018 Amended Annual Report of Changes in Peak Cladding Temperature CP-201700227, Transmittal of 2017 Radiological Environmental Operating Report2018-04-30030 April 2018 Transmittal of 2017 Radiological Environmental Operating Report CP-201700193, Annual Report of Changes in Peak Cladding Temperature2017-04-12012 April 2017 Annual Report of Changes in Peak Cladding Temperature CP-201600195, Annual Report of Changes in Peak Cladding Temperature2016-03-31031 March 2016 Annual Report of Changes in Peak Cladding Temperature CP-201500263, Annual Report of Changes in Peak Cladding Temperature2015-04-13013 April 2015 Annual Report of Changes in Peak Cladding Temperature ML14127A0682014-04-24024 April 2014 Transmittal of the 2013 Radiological Operating Report CP-201400445, Submittal of the Annual Non-Radiological Environmental Operating Report 20132014-04-24024 April 2014 Submittal of the Annual Non-Radiological Environmental Operating Report 2013 CP-201300391, Submittal of Annual Report of Changes in Peak Cladding Temperature2013-04-25025 April 2013 Submittal of Annual Report of Changes in Peak Cladding Temperature CP-201300553, Submittal of the Annual Non-Radiological, Environmental Operating Report for 20122013-04-25025 April 2013 Submittal of the Annual Non-Radiological, Environmental Operating Report for 2012 ML13123A2512013-04-10010 April 2013 Transmittal of Year 2012 Radiological Environmental Operating Report CP-201300040, Comanche Peak, Units 1 and 2 - Transmittal of Year 2012 Radiological Environmental Operating Report2013-04-10010 April 2013 Comanche Peak, Units 1 and 2 - Transmittal of Year 2012 Radiological Environmental Operating Report CP-201200034, Comanche Peak, Units 1 and 2, Submittal of the Annual Non-Radiological Environmental Operating Report for 20112012-04-30030 April 2012 Comanche Peak, Units 1 and 2, Submittal of the Annual Non-Radiological Environmental Operating Report for 2011 CP-201200315, Annual Report of Changes in Peak Cladding Temperature2012-04-17017 April 2012 Annual Report of Changes in Peak Cladding Temperature CP-201000646, Transmittal of Year 2009 Radiological Environmental Operating Report2010-04-29029 April 2010 Transmittal of Year 2009 Radiological Environmental Operating Report ML0912803742009-04-0909 April 2009 Radioactive Effluent Release Report, January 1, 2008 - December 31, 2008 CP-200900615, Comanche Peak, 2008 Radioactive Effluent Release Report, January 1, 2008 - December 31, 20082009-04-0909 April 2009 Comanche Peak, 2008 Radioactive Effluent Release Report, January 1, 2008 - December 31, 2008 CP-200900472, Submittal of Annual Report of Changes in Peak Cladding Temperature2009-03-31031 March 2009 Submittal of Annual Report of Changes in Peak Cladding Temperature CP-200900345, Annual Operating Report for 20082009-02-26026 February 2009 Annual Operating Report for 2008 CP-200900007, Submittal of Annual Report of Changes in Peak Cladding Temperature2009-01-0808 January 2009 Submittal of Annual Report of Changes in Peak Cladding Temperature CP-200800990, 10CFR50.59 Evaluation Summary Report 0014 (for 08/02/2006 Through 02/01/2008) and Commitment Material Change Evaluation Report 00082008-08-0404 August 2008 10CFR50.59 Evaluation Summary Report 0014 (for 08/02/2006 Through 02/01/2008) and Commitment Material Change Evaluation Report 0008 CP-200800613, Transmittal of Year 2007 Annual Radiological Environmental Operating Report2008-04-24024 April 2008 Transmittal of Year 2007 Annual Radiological Environmental Operating Report CP-200800244, Transmittal of Annual Operating Report for 20072008-02-28028 February 2008 Transmittal of Annual Operating Report for 2007 CP-200800053, Submittal of Annual Report of Changes in Peak Cladding Temperature for Comanche Peak Steam Electric Station (CPNPP) Units 1 and 22008-01-10010 January 2008 Submittal of Annual Report of Changes in Peak Cladding Temperature for Comanche Peak Steam Electric Station (CPNPP) Units 1 and 2 CPSES-200700859, Submittal of the Annual Non-Radiological Environmental Operating Report for 20062007-04-27027 April 2007 Submittal of the Annual Non-Radiological Environmental Operating Report for 2006 ML0712300732007-04-26026 April 2007 Radioactive Effluent Release Report CPSES-200700451, Annual Operating Report for 20062007-02-28028 February 2007 Annual Operating Report for 2006 CPSES-200600395, Annual Operating Report for 20052006-02-24024 February 2006 Annual Operating Report for 2005 CPSES-200500638, Correction to Annual Operating Report for 20042005-03-17017 March 2005 Correction to Annual Operating Report for 2004 CPSES-200500361, Annual Operating Report for 20042005-02-25025 February 2005 Annual Operating Report for 2004 CPSES-200500104, Annual Report of Changes in Peak Cladding Temperature2005-01-10010 January 2005 Annual Report of Changes in Peak Cladding Temperature CPSES-200401138, Environmental Protection Plan Annual Environmental Operating Report for 20032004-04-21021 April 2004 Environmental Protection Plan Annual Environmental Operating Report for 2003 CPSES-200401136, Transmittal of the Annual Radiological Environmental Operating Report for 20032004-04-21021 April 2004 Transmittal of the Annual Radiological Environmental Operating Report for 2003 CPSES-200400378, Transmittal of the Annual Operating Report for 20032004-02-27027 February 2004 Transmittal of the Annual Operating Report for 2003 CPSES-200300852, Annual Environmental Operating Report for 20022003-04-29029 April 2003 Annual Environmental Operating Report for 2002 CPSES-200300849, Annual Radiological Environmental Operating Report for 20022003-04-29029 April 2003 Annual Radiological Environmental Operating Report for 2002 CPSES-200300346, Annual Operating Report for 20022003-02-28028 February 2003 Annual Operating Report for 2002 CPSES-200201244, (CPSES) Transmittal of the Annual Radiological Environmental Operating Report for 20012002-04-18018 April 2002 (CPSES) Transmittal of the Annual Radiological Environmental Operating Report for 2001 CPSES-200200643, Clarification to Annual Operating Report for 20012002-03-15015 March 2002 Clarification to Annual Operating Report for 2001 CPSES-200200528, Annual Operating Report for 20012002-02-28028 February 2002 Annual Operating Report for 2001 2022-05-16
[Table view] Category:Letter type:CPSES
MONTHYEARCPSES-201001000, Operator Licensing Examination Data, Form 5362010-07-28028 July 2010 Operator Licensing Examination Data, Form 536 CPSES-200901377, Operator Licensing Examination Data2009-09-29029 September 2009 Operator Licensing Examination Data CPSES-200701127, Response to Request for Additional Information Related to License Amendment Request (LAR) 06-009, Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times.2007-11-15015 November 2007 Response to Request for Additional Information Related to License Amendment Request (LAR) 06-009, Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times. CPSES-200701495, Withdrawal of License Amendment Request (LAR) 06-007, Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times for Offsite Circuits2007-10-22022 October 2007 Withdrawal of License Amendment Request (LAR) 06-007, Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times for Offsite Circuits CPSES-200701530, Additional Information in Connection with the Indirect Transfer of Facility Operating Licenses and Conforming License Amendments2007-10-0909 October 2007 Additional Information in Connection with the Indirect Transfer of Facility Operating Licenses and Conforming License Amendments CPSES-200701496, Information Required by Order Approving the Indirect Transfer of Facility Operating Licenses and Conforming License Amendments2007-10-0202 October 2007 Information Required by Order Approving the Indirect Transfer of Facility Operating Licenses and Conforming License Amendments CPSES-200701351, Transmittal of First-Half 2007 Fitness-for-Duty Program Performance Data2007-08-29029 August 2007 Transmittal of First-Half 2007 Fitness-for-Duty Program Performance Data CPSES-200701076, Revision to the Operating License and Technical Specifications 1.0, Use and Application and 3.7.17, Spent Fuel Assembly Storage to Revise Rated Thermal Power from 3458 Mwt to 3612 Mwt2007-08-28028 August 2007 Revision to the Operating License and Technical Specifications 1.0, Use and Application and 3.7.17, Spent Fuel Assembly Storage to Revise Rated Thermal Power from 3458 Mwt to 3612 Mwt CPSES-200701302, Relief Request B-4 to the Unit 2 Inservice Inspection (ISI) Program Plan from the 1998 Edition of ASME Code, Section XI, Through 2000 Addenda (Interval Start Date - August 03, 2004, Second Interval)2007-08-22022 August 2007 Relief Request B-4 to the Unit 2 Inservice Inspection (ISI) Program Plan from the 1998 Edition of ASME Code, Section XI, Through 2000 Addenda (Interval Start Date - August 03, 2004, Second Interval) CPSES-200701324, Supplement to License Amendment Request (LAR) 07-003 Revision to Technical Specification 3.1, Reactivity Control Systems, 3.2, Power Distribution Limits, 3.3, Instrumentation, and 5.6.5 B, Core Operating Limits2007-08-16016 August 2007 Supplement to License Amendment Request (LAR) 07-003 Revision to Technical Specification 3.1, Reactivity Control Systems, 3.2, Power Distribution Limits, 3.3, Instrumentation, and 5.6.5 B, Core Operating Limits CPSES-200701323, License Amendment Request 07-006, Revision to Technical Specification 3.1.4, Rod Group Alignment Limits, Table 3.3.1-1, Reactor Trip System Instrumentation, Table 3.3.2-1, Engineered Safety Feature Actuation System..2007-08-16016 August 2007 License Amendment Request 07-006, Revision to Technical Specification 3.1.4, Rod Group Alignment Limits, Table 3.3.1-1, Reactor Trip System Instrumentation, Table 3.3.2-1, Engineered Safety Feature Actuation System.. CPSES-200701279, Mitigation of Alloy 82/182 Pressurizer Butt Welds in 20082007-08-0303 August 2007 Mitigation of Alloy 82/182 Pressurizer Butt Welds in 2008 CPSES-200701284, (Cpses), Operator Licensing Examination Data2007-08-0202 August 2007 (Cpses), Operator Licensing Examination Data CPSES-200701238, Submittal of the CPSES Units 1 and 2 Large and Small Break LOCA Analyses2007-07-31031 July 2007 Submittal of the CPSES Units 1 and 2 Large and Small Break LOCA Analyses CPSES-200701178, Supplement to Application for Order Approving Indirect Transfer of Control of Licenses and License Amendments to Reflect Proposed Licensee Name Change (TAC Nos. MD5289 and MD5280), Enclosures 1, 4, 5, 6 & 72007-07-20020 July 2007 Supplement to Application for Order Approving Indirect Transfer of Control of Licenses and License Amendments to Reflect Proposed Licensee Name Change (TAC Nos. MD5289 and MD5280), Enclosures 1, 4, 5, 6 & 7 CPSES-200701126, Response to Request for Additional Information to License Amendment Request (LAR) 06-007 Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times for Offsite Circuits2007-07-18018 July 2007 Response to Request for Additional Information to License Amendment Request (LAR) 06-007 Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times for Offsite Circuits CPSES-200701174, Submittal of Twelfth Refueling Outage (1RF12) Inservice Inspection Summary Report (1998 Edition of ASME Code Section XI Through 2000 Addenda, Interval Start Date - 08/03/2000, Second Interval)2007-07-17017 July 2007 Submittal of Twelfth Refueling Outage (1RF12) Inservice Inspection Summary Report (1998 Edition of ASME Code Section XI Through 2000 Addenda, Interval Start Date - 08/03/2000, Second Interval) CPSES-200701065, Response to NRC Generic Letter 2007-01, Inaccessible or Underground Power Cable Failures That Disable Accident Mitigation Systems or Cause Plant Transients.2007-06-21021 June 2007 Response to NRC Generic Letter 2007-01, Inaccessible or Underground Power Cable Failures That Disable Accident Mitigation Systems or Cause Plant Transients. CPSES-200700951, (Cpses), Unit 1, Pressurizer Weld Overlay 60 Day Report and Update for Unit 1 Reactor Pressure Vessel Head Replacement Regarding Revised Order EA-03-0092007-06-19019 June 2007 (Cpses), Unit 1, Pressurizer Weld Overlay 60 Day Report and Update for Unit 1 Reactor Pressure Vessel Head Replacement Regarding Revised Order EA-03-009 CPSES-200701059, Submittal of Startup Report, Cycle 132007-06-13013 June 2007 Submittal of Startup Report, Cycle 13 CPSES-200700738, License Amendment Request (LAR) 07-001 Revision to Technical Requirements Surveillance 13.3.33.2 Frequency for the Turbine Stop and Control Valves2007-05-22022 May 2007 License Amendment Request (LAR) 07-001 Revision to Technical Requirements Surveillance 13.3.33.2 Frequency for the Turbine Stop and Control Valves CPSES-200700915, Supplemental Response to Request for Information on Generic Letter 2003-01, Control Room Habitability2007-05-0707 May 2007 Supplemental Response to Request for Information on Generic Letter 2003-01, Control Room Habitability CPSES-200700871, Transmittal of Year 2006 Radioactive Effluent Release Report2007-04-30030 April 2007 Transmittal of Year 2006 Radioactive Effluent Release Report CPSES-200700859, Submittal of the Annual Non-Radiological Environmental Operating Report for 20062007-04-27027 April 2007 Submittal of the Annual Non-Radiological Environmental Operating Report for 2006 CPSES-200700517, Application for Order Approving Indirect Transfer of Control of Licenses and License Amendments to Reflect Proposed Licensee Name Change2007-04-18018 April 2007 Application for Order Approving Indirect Transfer of Control of Licenses and License Amendments to Reflect Proposed Licensee Name Change CPSES-200700719, Nuclear Liability Insurance2007-04-10010 April 2007 Nuclear Liability Insurance CPSES-200700605, License Amendment Request (LAR) 07-003, Revision to Technical Specifications 3.1, Reactivity Control Systems, 3.2, Power Distribution Limits, 3.3, Instrumentation, & 5.6.5b, Core Operating Limits Report2007-04-10010 April 2007 License Amendment Request (LAR) 07-003, Revision to Technical Specifications 3.1, Reactivity Control Systems, 3.2, Power Distribution Limits, 3.3, Instrumentation, & 5.6.5b, Core Operating Limits Report CPSES-200700708, Evaluation of Pressurizer Weld Overlay Confirmatory Analyses2007-04-0505 April 2007 Evaluation of Pressurizer Weld Overlay Confirmatory Analyses CPSES-200700691, Core Operating Limits Report, Cycle 132007-04-0404 April 2007 Core Operating Limits Report, Cycle 13 CPSES-200700663, Transmittal of the Annual Radiological Environmental Operating Report for 20062007-03-30030 March 2007 Transmittal of the Annual Radiological Environmental Operating Report for 2006 CPSES-200700607, Property Damage Insurance2007-03-29029 March 2007 Property Damage Insurance CPSES-200700606, Decommissioning Report2007-03-29029 March 2007 Decommissioning Report CPSES-200700573, Request to Withdraw Relief Request A-72007-03-22022 March 2007 Request to Withdraw Relief Request A-7 CPSES-200700571, Supplement to License Amendment Request (LAR) 05-06; Revision to Technical Specification 5.6.5 Revise Listing of LOCA and Non-LOCA Analysis Methodologies (TAC Nos. MD0185/0186)2007-03-19019 March 2007 Supplement to License Amendment Request (LAR) 05-06; Revision to Technical Specification 5.6.5 Revise Listing of LOCA and Non-LOCA Analysis Methodologies (TAC Nos. MD0185/0186) CPSES-200700515, Day Response to NRC Generic Letter 2007-01, Inaccessible or Underground Power Cable Failures That Disable Accident Mitigation Systems or Cause Plant Transients.2007-03-0909 March 2007 Day Response to NRC Generic Letter 2007-01, Inaccessible or Underground Power Cable Failures That Disable Accident Mitigation Systems or Cause Plant Transients. CPSES-200700454, Transmittal of Second-Half 2006 Fitness-For-Duty Program Performance Data2007-02-28028 February 2007 Transmittal of Second-Half 2006 Fitness-For-Duty Program Performance Data CPSES-200700451, Annual Operating Report for 20062007-02-28028 February 2007 Annual Operating Report for 2006 CPSES-200700422, Response to Request for Additional Information Related to Txu Power'S Request for Review of Previously Submitted Topical Reports2007-02-22022 February 2007 Response to Request for Additional Information Related to Txu Power'S Request for Review of Previously Submitted Topical Reports CPSES-200700414, Transmittal of Inservice Inspection Program Plan, Revision 5 (Unit 1: ASME Code Section XI 1998 Edition, 1999 and 2000 Addenda, Interval Start Date - 08/13/200, Second Interval)2007-02-22022 February 2007 Transmittal of Inservice Inspection Program Plan, Revision 5 (Unit 1: ASME Code Section XI 1998 Edition, 1999 and 2000 Addenda, Interval Start Date - 08/13/200, Second Interval) CPSES-200700391, Inspection and Mitigation of Alloy 82/182 Pressurizer Butt Welds2007-02-20020 February 2007 Inspection and Mitigation of Alloy 82/182 Pressurizer Butt Welds CPSES-200700346, Guarantees of Payment of Deferred Premiums, Submits Form 10-Q for the Period Ending September 30, 20062007-02-0808 February 2007 Guarantees of Payment of Deferred Premiums, Submits Form 10-Q for the Period Ending September 30, 2006 CPSES-200700229, Comanche, Response to Request for Additional Information, Relief Request B-6 for the Unit 1 Inservice Inspection (ISI) Program Plan from the 1998 Edition of ASME Code, Section XI, Through 2000 Addenda (Interval Start Date..2007-02-0202 February 2007 Comanche, Response to Request for Additional Information, Relief Request B-6 for the Unit 1 Inservice Inspection (ISI) Program Plan from the 1998 Edition of ASME Code, Section XI, Through 2000 Addenda (Interval Start Date.. CPSES-200700169, Inspection and Mitigation of Alloy 82/182 Pressurizer Butt Welds2007-01-30030 January 2007 Inspection and Mitigation of Alloy 82/182 Pressurizer Butt Welds CPSES-200700147, Response to Request for Additional Information Regarding Resolution of Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk and the Operability of Offsite Power2007-01-29029 January 2007 Response to Request for Additional Information Regarding Resolution of Generic Letter 2006-02, Grid Reliability and the Impact on Plant Risk and the Operability of Offsite Power CPSES-200700127, Submittal of Unit 2 Ninth Refueling Outage (2RF09) Inservice Inspection (ISI) Summary Report (Unit 2: 1998 Edition of ASME Code Section XI, Through 2000 Addenda, Interval Start Date - August 3, 2004, Second Interval)2007-01-24024 January 2007 Submittal of Unit 2 Ninth Refueling Outage (2RF09) Inservice Inspection (ISI) Summary Report (Unit 2: 1998 Edition of ASME Code Section XI, Through 2000 Addenda, Interval Start Date - August 3, 2004, Second Interval) CPSES-200700146, License Amendment Request (LAR) 06-007, Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times for Offsite Circuits2007-01-18018 January 2007 License Amendment Request (LAR) 06-007, Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times for Offsite Circuits CPSES-200700130, License Amendment Request (LAR) 06-009, Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times for Diesel Generators2007-01-18018 January 2007 License Amendment Request (LAR) 06-009, Revision to Technical Specification (TS) 3.8.1, AC Sources - Operating, Extension of Completion Times for Diesel Generators CPSES-200700099, Annual Report of Changes in Peak Cladding Temperature2007-01-10010 January 2007 Annual Report of Changes in Peak Cladding Temperature CPSES-200602339, License Amendment Request (LAR) 06-010, Revision to Technical Specification 5.5.16, Containment Leakage Rate Testing Program.2006-12-19019 December 2006 License Amendment Request (LAR) 06-010, Revision to Technical Specification 5.5.16, Containment Leakage Rate Testing Program. CPSES-200602340, License Amendment Request (LAR) 06-012, Revision to Technical Specification 3.7.5, Auxiliary Feedwater System, TS 3.8.1, AC Sources - Operating, & TS 3.8.9, Distribution Systems - Operating.2006-12-19019 December 2006 License Amendment Request (LAR) 06-012, Revision to Technical Specification 3.7.5, Auxiliary Feedwater System, TS 3.8.1, AC Sources - Operating, & TS 3.8.9, Distribution Systems - Operating. 2010-07-28
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Text
TXU SPower TXIJJ Pbwer LMlIke BLevins Comaincte Peak Steamm Senior Vice Ptesident &
Metie N~ucear Officer Ref. #10CFR50.36 P. G.. Box IG02 ((EQIý Gitem Rose, TX T60~43 1Telt 254 897 5209 Fax:c 254 897 6652 rn 54e. h evi nsCat .crnacm CPSES-200700451 Log # TXX-07050 RP-85 February 28, 2007 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555
SUBJECT:
COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)
DOCKET NOS. 50-445 AND 50-446 ANNUAL OPERATING REPORT FOR 2006
Dear Sir or Madam:
By means of the Attachment to this letter, TXU Generation Company LP (TXU Power) hereby submits the CPSES Annual Operating Report for 2006, prepared and submitted pursuant to guidance provided in C. 1.b of U.S. NRC Regulatory Guide 1.16, Revision 4.
This communication contains no new licensing basis commitments regarding CPSES Units 1 and 2. Should you have any questions, please contact Robert Kidwell at (254) 897-5310.
AUOJ A member of the STARS (Strategic Teaming and Resource Sharing) Alliance Callaway 9 Comanche Peak a Diablo Canyon
- Palo Verde o South Texas Project
TXX-07050 Page 2 of 2 Sincerely, TXU Generation Company LP By: TXU Generation Management Company LLC Its General Partner Mike Blevins By: j4272 7 4
- red W. Madden Director, Oversight and Regulatory Affairs RJK Attachment c - B. S. Mallett, Region IV M. C. Thadani, NRR Resident Inspectors, CPSES
Attachment to TXX-07050 COMANCHE PEAK STEAM ELECTRIC STATION ANNUAL OPERATING REPORT 2006 TXU Generation Company LP.
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Attachment to TXX-07050 TABLE OF CONTENTS 1.0 Summary of Operating Experience 2.0 Outages and Reductions in Power 3.0 Deleted (Reference 69 FR 35067 & TSTF-369) 4.0 Irradiated Fuel Inspection Results 5.0 Deleted (Reference 69 FR 35067 & TSTF-369) 2
Attachment to TXX-07050 1.0
SUMMARY
OF OPERATING EXPERIENCE The Comanche Peak Steam Electric Station (CPSES) is a dual unit pressurized water reactor power plant, supplied by Westinghouse Electric Corporation. It is located in Somervell County in North Central Texas approximately 65 miles southwest of the Dallas-Fort Worth Metropolitan area. Each generating unit core was originally designed for a warranted power output of 3411 Megawatt thermal (MWt). This output, combined with the reactor coolant pump heat output of 14 MWt, gives a warranted NSSS output of 3425 MWt, which is the license application rating. Both units rated thermal power was subsequently increased to 3458 MWt, which represents a 1.4 percent increase in core output (from 3411 to 3458 MWt). The reactor coolant pump heat output considered in the safety analysis was increased to approximately 16 MWt for both units. All safety systems, including the engineered safety features, are designed for operations at a maximum NSSS output of 3579 MWt and an associated maximum core output of 3565 MWt.
1.1 CPSES UNIT 1 CPSES Unit 1 achieved initial criticality on April 3, 1990. Initial power generation occurred on April 24, 1990, and the plant was declared commercial on August 13, 1990. Since being declared commercial, CPSES Unit 1 has generated 137,519,035 net Megawatt-hours (MWH) of electricity as of December 31, 2006, with a net unit capacity factor of 83.26% (using MDC). The cumulative unit and reactor availability factors were 88.39% and 91.04% respectively, as of December 31, 2006.
The was no refueling outage for Unit 1 in 2006 Figure 1.1 provides the generation profile of the average daily net electrical output of Unit 1 for 2006. Table 1.1 is a compilation of the yearly and total summaries of the operating data.
During this reporting period there were no failures or challenges to the Safety Valves.
1.2 CPSES UNIT 2 CPSES Unit 2 achieved initial criticality on March 24, 1993. Initial power generation occurred on April 9, 1993, and the plant was declared commercial on August 3, 1993. Since being declared commercial, CPSES Unit 2 has generated 115,917,723 net Megawatt-hours (MWH) of electricity as of December 31, 2006, with a net unit capacity factor of 85.74% (using MDC). The cumulative unit and reactor availability factors were 89.57% and 92.09% respectively, as of December 31, 2006.
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Attachment to TXX-07050 On October 7, 2006, the unit began a power ramp down for its ninth refueling outage. The unit entered the refueling outage on the same day. During the refueling outage, 88 fresh fuel assemblies were loaded for Cycle 10. The refueling outage lasted 18 days 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> and ended on October 26, 2006. Unit 2 reached 100% power on November 2, 2006.
During the refueling outage, the major work scope completed included:
" Fuel rod oxide (corrosion) measurements in support of the CPSES elevated pH pilot program.
" Identification of leaking fuel assemblies
- Alloy 600 Inspections of the Reactor Vessel BMI's
- Reactor Head Penetration Volumetric Inspections
- GSI-191 containment sump modifications
- Digital upgrade to the Turbine-Generator Protection System controls
- SSW Train Bravo pump and motor replacement
- Performed 5-year inspection on Diesel Generator Figure 1.2 provides the generation profile of the average daily net electrical output of Unit 2 for 2006. Table 1.2 is a compilation of the yearly and the total summaries of the operating data.
During this reporting period there were no failures or challenges to the Safety Valves.
2.0 OUTAGES AND REDUCTIONS IN POWER 2.1 CPSES UNIT 1 Table 2.1 describes unit operating experience including unit shutdowns and provides explanations of significant dips in average power levels for CPSES Unit 1.
2.2 CPSES UNIT 2 Table 2.2 describes unit-operating experience including unit shutdowns and provides explanations of significant dips in average power levels for CPSES Unit 2.
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Attachment to TXX-07050 3.0 EXPOSURE AND MONITORING REPORT Deleted (Reference 69 FR 35067 & TSTF-369).
4.0 IRRADIATED FUEL INSPECTION RESULTS 4.1 CPSES UNIT 1 Though there was no Unit 1 refueling outage during 2006, a follow-on reconstitution and inspection campaign was performed on three once-burned Unit 1, Cycle 11 (U1C 11) failed assemblies N24, N17, and N46 in late July, 2006. The results of the follow-on campaign are provided below:
Assembly N46 - This assembly was re-examined using the ultrasonic testing (UT) equipment, however, none of the UT scans produced data indicative of a leaking rod and, therefore, no repairs or further inspections were performed. It is likely that this assembly, contains a very tight defect.
Assembly N 17 - One failed rod was detected and was successfully removed and replaced with a stainless steel rod. High magnification visual examination of this rod showed indications of debris wear scars. An adjacent non-leaking fuel rod was also removed and replaced with a stainless steel rod as a precaution. No wear scars were observed on that rod however.
Assembly N24 - One failed fuel rod was located and successfully removed and replaced with a stainless steel rod. High magnification visual examination of this rod showed indications of a debris wear scar near the location of visible debris in the assembly. The debris was removed prior to the reconstitution attempt. Also, near the bottom end plug, the failed rod visual examination revealed a severe through-wall debris scar. An adjacent non-leaking rod was also removed and showed debris wear scars. This rod location was also reloaded with a stainless steel rod.
It was concluded that assemblies N 17 and N24 were successfully reconstituted and are acceptable for re-use. It was also concluded that debris was the likely cause of all of the U1C 11 fuel failures.
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Attachment to TXX-07050 4.2 CPSES UNIT 2 Inspection personnel performed visual examination of Unit 2, Cycle 9 fuel assemblies as each assembly was withdrawn from the Fuel Building upender during core off-load operations. All fuel assemblies appeared to be in good condition with no anomalies observed, including the assemblies identified as failed by in-mast sipping (IMS).
IMS Results During 2RF09 core offload, IMS inspections were performed on all U2C9 assemblies. The results provided clear indications of two failed fuel assemblies, both of which were scheduled for discharge during the refueling outage. UT and visual inspections of the failed rods are currently scheduled for the upcoming Unit 1 refueling outage in March, 2007.
Clad Oxide Measurements During 2RF09, fuel clad oxide thickness measurements were performed in support of the pilot elevated pH program (constant 7.4) on Unit 2. This was the third oxide measurement campaign performed on Unit 2 in support of the program. Although the final results of the measurements are still under review and analyses, overall, the measurements results were as expected and well within regulatory limits.
Based on these preliminary results, the elevated pH program at CPSES was continued.
5.0 OUTAGE RELATED SINGLE RADIOACTIVITY RELEASE OR RADIATION EXPOSURE TO AN INDIVIDUAL THAT ACCOUNTS FOR MORE THAN 10 PERCENT OF ALLOWABLE ANNUAL VALUES Deleted (Reference 69 FR 35067 & TSTF-369) 6
Attachment to TXX-07050 FIGURE 1.1 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 1 GENERATION PROFILE AVERAGE DAILY UNIT POWER LEVEL for 2006 1,400 1,200 1,000 0) 800 600 400 200 0
JAN FEB MAR APR MAY JUN JUL AUG SEP OCT NOV DEC, 7
Attachment to TXX-07050 TABLE 1.1 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 1 ANNUAL ELECTRIC POWER GENERATION DATA (2006)
YEAR CUMULATIVE Hours RX was Critical 8,760.00 127,898.75 RX Reserve Shutdown Hours 0 2,870.89 Hours Generator On-line 8,760.00 126,959.37 Gross Thermal Energy Generated (MWH) 30,254,772.00 424,045,360.20 Gross Electric Energy Generated (MWH) 10,672,575.00 143,550,327.00 Net Electric Energy Generated (MWH) 10,297,952.00 137,519,035.00 RX Service Factor (%) 100.00 89.05 RX Availability Factor (%) 100.00 91.04 Unit Service Factor (%) 100.00 88.39 Unit Availability Factor (%) 100.00 88.39 Unit Capacity Factor (%, using MDC net) 102.22 83.26 Unit Capacity Factor (%, using DER net) 102.22 83.26 Unit Forced Outage Rate (%) 0.00 2.44 8
Attachment to TXX-07050 FIGURE 1.2 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 2 GENERATION PROFILE AVERAGE DAILY UNIT POWER LEVEL for 2006 1,400 1,200 1,000 800 600 400 200 0
JAN FEB MAR APR MAY JUN JUL AUG SEP OCT NO)V DEC 9
Attachment to TXX-07050 TABLE 1.2 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 2 ANNUAL ELECTRIC POWER GENERATION DATA (2006)
YEAR CUMULATIVE Hours RX was Critical 8,286.92 105,906.79 RX Reserve Shutdown Hours 0.00 2,366.46 Hours Generator On-line 8,260.75 105,310.82 Gross Thermal Energy Generated (MWH) 28,323,583.20 352,879,084.80 Gross Electric Energy Generated (MWH) 9,981,348.00 120,795,508.00 Net Electric Energy Generated (MWH) 9,598,204.00 115,917,723.00 RX Service Factor (%) 94.60 90.08 RX Availability Factor (%) 94.60 92.09 Unit Service Factor (%) 94.30 89.57 Unit Availability Factor (%) 94.30 89.57 Unit Capacity Factor (%, using MDC net) 95.28 85.74 Unit Capacity Factor (%, using DER net) 95.28 85.74 Unit Forced Outage Rate (%) 0.62 2.43 10
Attachment to TXX-07050 TABLE 2.1 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 1 UNIT OPERATING EXPERIENCE INCLUDING SHUTDOWNS AND POWER REDUCTIONS DURING 2006 METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION* THE REACTOR OR NO DATE S:SCHEDULED (HOURS) REASON REDUCING POWER CORRECTIVE ACTION/COMMENTS 1 11/30/2006 F 1.42 A 4 On November 30, 2006 at 0010, the operators initiated a manual turbine runback from 100% reactor power to 57% reactor power, when Heater Drain Valve 1-LV-2509 failed causing a decrease in Main Feedwater Pump suction pressure. On November 30, 2006 at 0622, 1-LV-2509 repairs were completed and Unit I returned to 100% reactor power
- 1) REASON 2) METHOD A: EQUIPMENT FAILURE (EXPLAIN) E: OPERATOR TRAINING AND LICENSE EXAMINATION 1: MANUAL B: MAINT OR TEST F: ADMINISTRATIVE 2: MANUAL SCRAM C: REFUELING G: OPERATIONAL ERROR (EXPLAIN) 3: AUTOMATIC SCRAM D: REGULATORY RESTRICTION H: OTHER (EXPLAIN) 4: OTHER (EXPLAIN)
- INDICATES SHUTDOWN HOURS/OTHERWISE "NA" FOR NOT APPLICABLE 11
Attachment to TXX-07050 TABLE 2.2 COMANCHE PEAK STEAM ELECTRIC STATION - UNIT 2 UNIT OPERATING EXPERIENCE INCLUDING SHUTDOWNS AND POWER REDUCTIONS DURING 2006 METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION* THE REACTOR OR NO DATE S: SCHEDULED (HOURS) REASON REDUCING POWER CORRECTIVE ACTION/COMMENTS 1 10/07/2006 S 447.95 C 2 On October 7, 2006 at 0900, unit commenced a power ramp down to 60 MWe turbine power to enter 2RF09. On October 7, 2006 at 1200, operators initiated manual reactor trip per procedure to enter MODE 3. Unit exited MODE 6 after core reload on October 20, 2006 and entered MODE 5 at 2120. On October 25, 2006 unit entered MODE 2 and the reactor was critical at 0952. The unit entered MODE I and was synchronized to the grid on October 26, 2006 at 0357, ending 2RF09 with duration of 18 days and 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />. Unit returned to full power on November 2, 2006 at 1000.
2 10/27/2006 F 14.57 A 2 On October 27, 2006 at 0309 a manual reactor trip occurred after an automatic turbine trip on P-14, HI-HI steam generator level in SG 2-02, during post-outage load rejection testing from 29% reactor power. After repairs were completed, the unit entered MODE 2 on October 27, 2006 and the reactor was critical at 1416. The unit entered MODE I on October 27, 2006 and was synchronized to the grid at 1742.
3 10/29/2006 F 36.73 A 2 October 29, 2006 at 1520, operators manually tripped the reactor from 80%
reactor power, due to decreasing steam generator level in SG 2-03; Feedwater Regulating Valve, 2-FV-0530, controller had failed. After repairs were completed, the unit entered MODE 2 on October 30, 2006 and the reactor was critical at 2326. The unit entered MODE I on October 31, 2006 and was synchronized to the grid at 0404.
I) REASON 2) METHOD A: EQUIPMENT FAILURE (EXPLAIN) E: OPERATOR TRAINING AND LICENSE EXAMINATION I: MANUAL B: MAINT OR TEST F: ADMINISTRATIVE 2: MANUAL SCRAM C: REFUELING G: OPERATIONAL ERROR (EXPLAIN) 3: AUTOMATIC SCRAM D: REGULATORY RESTRICTION H: OTHER (EXPLAIN) 4: OTHER (EXPLAIN)
. INDICATES SHUTDOWN HOURS/OTHERWISE "NA" FOR NOT APPLICABLE 12