ML040330908
ML040330908 | |
Person / Time | |
---|---|
Site: | Waterford |
Issue date: | 02/02/2004 |
From: | Howell A NRC/RGN-IV/DRP |
To: | Venable J Entergy Operations |
References | |
EA-03-230 IR-03-007 | |
Download: ML040330908 (55) | |
See also: IR 05000382/2003007
Text
February 2, 2004
EA 03-230
Joseph E. Venable
Vice President Operations
Waterford 3
Entergy Operations, Inc.
17265 River Road
Killona, Louisiana 70066-0751
SUBJECT: WATERFORD STEAM ELECTRIC STATION, UNIT 3 - NRC INTEGRATED
INSPECTION REPORT 05000382/2003007
Dear Mr. Venable:
On December 31, 2003, the NRC completed an inspection at your Waterford Steam Electric
Station, Unit 3. The enclosed report documents the inspection findings which were discussed
on January 5, 2003, with you and other members of your staff. This inspection examined
activities conducted under your license as they relate to safety and compliance with the
Commissions rules and regulations and with the conditions of your license. Within these areas,
the inspection consisted of selected examination of procedures and representative records,
observations of activities, and interviews with personnel.
The report discusses a finding that appears to have Greater than Green safety significance. As
described in Section 4OA3.1 of this report, the issue involved the failure to establish appropriate
instructions and accomplish those instructions for installation of a fuel line for Train A
emergency diesel generator in May of 2003. This failure resulted in uneven and excessive
scoring of the tubing that ultimately led to a complete 360 degree failure of the fuel supply line
on September 29, 2003, during a monthly surveillance test, which rendered the Train A
emergency diesel generator inoperable. This finding was assessed based on the best available
information, including influential assumptions, using the applicable Significance Determination
Process and was preliminarily determined to be a Greater than Green Finding. The final
resolution of this finding will convey the increment in the importance to safety by assigning the
corresponding color i.e, White (a finding with some increased importance to safety, which may
require additional NRC inspection), Yellow (a finding with substantial importance to safety that
will result in additional NRC inspection and potentially other NRC action) or Red (a finding of
high importance to safety that will result in increased NRC inspection and other NRC action).
Because the preliminary safety significance is greater than Green, the NRC requests that
additional information be provided regarding the nonrecovery probability for the Train A
emergency diesel generator and any other considerations you have identified as impacting the
safety significance determination.
Entergy Operations, Inc. -2-
This finding does not present an immediate safety concern based on your immediate and long
term corrective actions. These actions included a complete re-design and installation of the
fuel line that had prematurely failed.
This finding is also an apparent violation of NRC requirements and is being considered for
escalated enforcement action in accordance with the General Statement of Policy and
Procedure for NRC Enforcement Actions (Enforcement Policy), NUREG-1600. The current
enforcement policy is included on the NRCs website at
http://www.nrc.gov/what-we-do/regulatory/enforcement.html.
Before the NRC makes a final decision on this matter, we are providing you an opportunity
(1) to present to the NRC your perspectives on the facts and assumptions, used by the NRC to
arrive at the finding and its significance, at a Regulatory Conference or (2) submit your position
on the finding to the NRC in writing. If you request a Regulatory Conference, it should be held
within 30 days of the receipt of this letter and we encourage you to submit supporting
documentation at least one week prior to the conference in an effort to make the conference
more efficient and effective. If a Regulatory Conference is held, it will be open for public
observation. If you decide to submit only a written response, such submittal should be sent to
the NRC within 30 days of the receipt of this letter.
Please contact Mr. William Jones at (817) 860-8147 within 10 days of the date of this letter to
notify the NRC of your intentions. If we have not heard from you within 10 days, we will
continue with our significance determination and enforcement decision and you will be advised
by separate correspondence of the results of our deliberations on this matter.
Since the NRC has not made a final determination in this matter, no Notice of Violation is being
issued for the inspection finding at this time. In addition, please be advised that the
characterization of the apparent violation described in the enclosed inspection report may
change as a result of further NRC review.
In addition, the enclosed report documents four NRC-identified findings of very low safety
significance (Green). These findings were determined to involve violations of NRC
requirements. However, because of the very low safety significance and because they are
entered into your corrective action program, the NRC is treating these four findings as non-cited
violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy. These NCVs
are described in the subject inspection report. If you contest the violations or significance of
these NCVs, you should provide a response within 30 days of the date of this inspection report,
with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document
Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, U.S.
Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas
76011; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington,
DC 20555-0001; and the NRC Resident Inspector at the Waterford Steam Electric Station,
Unit 3 facility.
In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure(s), and your response will be made available electronically for public inspection in the
Entergy Operations, Inc. -3-
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Should you have any questions concerning this inspection, we will be pleased to discuss them
with you.
Sincerely,
/RA/
Arthur T. Howell III, Director
Division of Reactor Projects
Docket: 50-382
License: NPF-38
Enclosure:
NRC Inspection Report
050000382/2003007
w/attachment: Supplemental Information
cc w/enclosure:
Senior Vice President and
Chief Operating Officer
Entergy Operations, Inc.
P.O. Box 31995
Jackson, MS 39286-1995
Vice President, Operations Support
Entergy Operations, Inc.
P.O. Box 31995
Jackson, MS 39286-1995
Wise, Carter, Child & Caraway
P.O. Box 651
Jackson, MS 39205
General Manager, Plant Operations
Waterford 3 SES
Entergy Operations, Inc.
17265 River Road
Killona, LA 70066-0751
Entergy Operations, Inc. -4-
Manager - Licensing Manager
Waterford 3 SES
Entergy Operations, Inc.
17265 River Road
Killona, LA 70066-0751
Chairman
Louisiana Public Service Commission
P.O. Box 91154
Baton Rouge, LA 70821-9154
Director, Nuclear Safety &
Regulatory Affairs
Waterford 3 SES
Entergy Operations, Inc.
17265 River Road
Killona, LA 70066-0751
Michael E. Henry, State Liaison Officer
Department of Environmental Quality
Permits Division
P.O. Box 4313
Baton Rouge, LA 70821-4313
Parish President
St. Charles Parish
P.O. Box 302
Hahnville, LA 70057
Winston & Strawn
1400 L Street, N.W.
Washington, DC 20005-3502
Entergy Operations, Inc. -5-
Electronic distribution by RIV:
Regional Administrator (BSM1)
DRP Director (ATH)
DRS Director (DDC)
Senior Resident Inspector (MCH)
Branch Chief, DRP/E (WBJ)
Senior Project Engineer, DRP/E (VGG)
Staff Chief, DRP/TSS (PHH)
RITS Coordinator (NBH)
Debby Jackson, OEDO RIV Coordinator (DAJ1)
WAT Site Secretary (AHY)
Dale Thatcher (DFT)
G. F. Sanborn, D:ACES (GFS)
K. D. Smith, RC (KDS1)
F. J. Congel, OE (FJC)
OE:EA File (RidsOeMailCenter)
ADAMS: W Yes G No Initials: __wbj____
W Publicly Available G Non-Publicly Available G Sensitive W Non-Sensitive
R:\_WAT\2003\WT2003-07RP-MCH.wpd
RIV:RI:DRP/E SRI:DRP/E C:DRS/PSB C:DRS/OB
GFLarkin MCHay TWPruett ATGody
T - WBJones T - WBJones E - WBJones /RA/
1/28/04 1/28/04 1/28/04 1/27/04
C:DRS/EB SRA C:DRP/E D:DRP
CSMarschall MFRunyan WBJones ATHowell
/RA/ /RA/ /RA/ /RA/
1/28/04 2/2/04 1/28/04 2/2/04
OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket: 50-382
License: NPF-38
Report: 05000382/2003007
Licensee: Entergy Operations, Inc.
Facility: Waterford Steam Electric Station, Unit 3
Location: Hwy. 18
Killona, Louisiana
Dates: September 21 through December 31, 2003
Inspectors: M. C. Hay, Senior Resident Inspector
G. F. Larkin, Resident Inspector
M. P. Shannon, Senior Health Physicist
P. C. Gage, Senior Operations Engineer
T. O. McKernon, Senior Operations Engineer
J. F. Drake, Operations Engineer
V.G. Gaddy, Senior Project Engineer
D. R. Carter, Health Physicist
W. C. Sifre, Reactor Inspector, Engineering Branch
T. McConnell, Reactor Inspector, Engineering Branch
Accompanying V. X. Thomas, Intern, NRC Headquarters
Personnel:
Approved By: A. T. Howell III, Director, Division of Reactor Projects
ATTACHMENT: Supplemental Information
Enclosure
CONTENTS
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2
1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
1R11 Licensed Operator Requalification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
1R12 Maintenance Rule Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
1R13 Maintenance Risk Assessments and Emergent Work Evaluation . . . . . . . . . . . 9
1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9
1R16 Operator Workarounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
1R20 Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14
2OS1 Access Control to Radiological Significant Areas . . . . . . . . . . . . . . . . . . . . . . . 14
2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18
4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19
4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23
4OA4 Crosscutting Aspects of Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33
4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33
4OA6 Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36
4OA7 Licensee Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36
ATTACHMENT: SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 37
Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
Items Opened, Closed, and Discussed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2
List of Acronyms . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-8
SUMMARY OF FINDINGS
IR05000382/2003-007; 09/21/2003-12/27/2003; Waterford Steam Electric Station, Unit 3;
Postmaintenance Testing, Access Control to Radiological Significant Areas, Identification and
Resolution of Problems, and Event Followup.
The report covered a 15-week period of inspection by resident inspectors, a senior health
physicist, a health physicist, two senior operations engineers, an operations engineer, a senior
project engineer, and a reactor engineer. The inspection identified one potential greater than
green finding and four green findings. The significance of most findings is indicated by their
color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance
Determination Process. Findings for which the Significance determination process does not
apply may be Green or be assigned a severity level after NRC management review. The
NRCs program for overseeing the safe operation of commercial nuclear power reactors is
described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A. NRC-Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
- TBD. A self-revealing apparent violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, was identified for the
failure to establish appropriate instructions and accomplish those instructions for
installation of a fuel line for Train A emergency diesel generator in May 2003.
This failure resulted in uneven and excessive scoring of the tubing that ultimately
led to a complete 360 degree failure of the fuel supply line on September 29,
2003, during a monthly surveillance test.
This finding is unresolved pending completion of a significance determination.
The finding was greater than minor because it directly impacted the availability
and reliability of an emergency diesel generator which is used to mitigate the
loss of AC power to the respective safety related bus. The finding was
determined to have a potential safety significance greater than very low
significance because the failure resulted in an actual loss of the safety function
of the Train A emergency diesel generator for an extended period of time
(Section 4OA3).
- Green. The inspectors identified a noncited violation of 10 CFR Part 50,
Appendix B, Criterion XVI, for the failure to establish adequate corrective actions
to prevent recurrence of voiding conditions affecting the operability of the low
pressure safety injection system following shutdown cooling operations.
This finding is greater than minor because it affected the mitigating system
objective to ensure the reliability and availability of the low pressure safety
injection system to respond to an initiating event. The problem if left uncorrected
would become a more significant safety concern. The significance of this finding
was determined to be of very low safety significance because low pressure
safety injection Train B was inoperable for less than the Technical Specification
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allowed outage time and Train A was determined to be degraded but operable in
accordance with Generic Letter 91-18 guidance (Section 4OA2).
Cornerstone: Barrier Integrity
- Green. The inspectors identified a noncited violation of 10 CFR Part 50,
Appendix B,Section XI, "Test Control," for the failure to establish adequate test
controls for leak testing main steam isolation Valves 1 and 2. This performance
deficiency contributed to both valves being declared inoperable due to system
leaks creating a low pressure condition in the valve actuating systems.
This finding is more than minor because it affected the Barrier Integrity
Cornerstone objective of providing reasonable assurance of the functionality of
containment. The finding was only of very low safety significance because it did
not represent an actual reduction of the atmospheric pressure control function of
the reactor containment, it did not result in an actual open pathway affecting the
physical integrity of reactor containment, and the main steam isolation valves
were inoperable for less time than the allowed Technical Specification outage
time (Section 1R19).
- Green. The inspectors identified a noncited violation of 10 CFR Part 50,
Appendix B, Criterion XVI, for the failure to implement effective corrective actions
resulting in recurrences of pressure boundary leakage due to primary water
stress corrosion cracking of Alloy 600 reactor coolant system nozzles.
This finding was greater than minor because it affected the reactor safety barrier
integrity cornerstone objective for providing reasonable assurance that the
physical design barriers protect the public from radionuclide releases caused by
accidents or events. Using NRC Manual Chapter 0609 Significance
determination process Phase 1 Screening Worksheet this performance
deficiency affected the reactor coolant system barrier function requiring a
Phase 2 analysis. The results of the Phase 2 and 3 analysis determined that this
finding was of very low safety significance based on the cracks being axial in
nature (does not contribute substantially to a loss of coolant accident) and the
leaks resulted in a build up of only minor boric acid residue indicative of only
trace amounts of through wall leakage. The leak rates identified were well within
the capacity of a single charging pump (4OA2).
Cornerstone: Occupational Radiation Safety
- Green. The inspector identified a noncited violation of Technical
Specification 6.12.1 because Entergy failed to barricade a high radiation area.
Specifically, on October 27, 2003, the inspector observed that the high radiation
area rope barricading the regenitive heat exchanger room was stretched across
the entrance way at a height of approximately 79 inches, which would not
obstruct the entry of station workers. General area radiation levels within the
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room were as high as 420 millirem per hour. The finding is in Entergys
corrective action program as Condition Report CR-WF3-2003-03164.
The finding is greater than minor because it affected the Occupational Radiation
Safety cornerstone objective to ensure adequate protection of worker health and
safety from exposure to radiation and the finding is associated with the
cornerstone attribute (Program & Process). The finding involved an individuals
potential for unplanned or unintended dose. When processed through the
Occupational Radiation Safety Significance Determination Process the finding
was determined to be of very low safety significance because the finding was not
associated with ALARA planning or work controls, there was no overexposure or
a substantial potential for overexposure, and the ability to assess dose was not
compromised (Section 2SO1).
B. Licensee-Identified Violations
Violations of very low safety significance, which were identified by Entergy have been
reviewed by the inspectors. Corrective actions taken or planned by Entergy have been
entered into Entergy's corrective action program. These violations and corrective action
tracking numbers are listed in Section 4OA7 of this report.
Enclosure
Report Details
Summary of Plant Status: The plant began the period on September 21, 2003, at 97 percent
power and coasted down to 75 percent power on October 20, 2003. The plant was shutdown
for a scheduled refueling outage on October 20, 2003. On November 20, 2003, operators
commenced a reactor startup to perform low power physics testing. The main turbine
generator was placed online on November 22, 2003, and the refueling outage ended on
November 24, 2003. Power was increased and reached approximately 100 percent on
November 25, 2003. Power remained at that level until December 19, 2003, when power was
reduced to 95 percent power for moderator temperature coefficient testing. Following testing,
power was increased to 100 percent.
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R01 Adverse Weather Protection (71111.01)
a. Inspection Scope
The inspectors completed one adverse weather protection inspection during this
inspection period. On December 19, 2003, the inspectors completed a walkdown of
components and systems susceptible to freezing using Procedure OP-002-007, Freeze
Protection and Temperature Maintenance, Revision 10, to verify that the onset of cold
weather would not affect the mitigating systems. This inspection included a review of
condition reports associated with heat tracing and other cold weather protection
measures to determine their impact on the systems. Additionally, the inspectors
discussed adverse weather preparations with various Entergy Operations, Inc. (Entergy)
personnel.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment (71111.04)
.1 Partial System Walkdowns
a. Inspection Scope
The inspectors performed the following two partial system equipment alignment
inspections during this inspection period:
- On November 3, 2003, the inspectors walked down the accessible portions of
the spent fuel pool cooling system, Train A. The walkdown was completed
following a full core offload to verify that cooling water flow to the spent fuel pool
was adequate to maintain adequate cooling for the spent fuel. The inspectors
performed the walkdown using Procedure OP-002-006, Fuel Pool Cooling and
Purification, Revision 15. The inspectors had reviewed the ability of the spent
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fuel pool cooling system to remove the decay heat of the spent fuel during
refueling outages involving a full core offload during the previous inspection
period (NRC Inspection Report 05000382/2003006) and as documented in
Section 1R07 to this report.
- On December 18, 2003, the inspectors performed a partial equipment alignment
inspection of the reactor auxiliary building cable vault area and switchgear area
ventilation system Train B while the switchgear area ventilation system Train A
was inoperable. A review of selected maintenance work orders and corrective
action documents was performed to assess the material condition and
performance of the system. System configuration was assessed using
Operating Procedure OP-003-026, Cable Vault and Switchgear HVAC,
Revision 7. A walkdown of accessible portions of the system was performed to
assess material condition, such as system leaks and housekeeping issues, that
could adversely affect system operability.
b. Findings
No findings of significance were identified.
.2 Complete System Walkdowns
a. Inspection Scope
The inspectors performed a complete alignment inspection of the safety related nitrogen
system. A walkdown of the mechanical and electrical components in the system was
performed to verify that the system was configured and operated in accordance with
Operating Procedure OP-003-019, Nitrogen System, Revision 12. The inspectors
reviewed the nitrogen system design requirements in the Updated Final Safety Analysis
Report to verify the systems ability to provide back up source of compressed gas for
various safety-related valves was adequate. The inspectors reviewed Engineering
Request ER-W3-97-0547-000 and select condition reports written on the nitrogen
system since October 1, 2000, to verify that degraded conditions were identified at the
appropriate threshold and that corrective actions were implemented in a timely manner.
b. Findings
No findings of significance were identified.
1R05 Fire Protection (71111.05)
a. Inspection Scope
The inspectors conducted six inspections to assess whether Entergy had implemented a
fire protection program that adequately controlled combustibles and ignition sources
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within the plant, effectively maintained fire detection and suppression capabilities, and
maintained passive fire protection features in good material condition.
The following areas were inspected:
- Fire Zone RAB 2, 15, 16, 17 and 18 on October 1, 2003
- Fire Zone RAB 1A, 1B, 5, 6 and 7 on October 6, 2003
- Fire Zone RAB 35, 36, 37, 38 and 39 on November 20, 2003
- Fire Zone RAB 1A, 8, 11, 12 and 13 on November 28, 2003
- Fire Zone RAB 1A, 5, 6, 7 and 8 on December 18, 2003
- Fire Zone RAB 35, 36, 37, 38, and 39 on December 30, 2003
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance (71111.07)
a. Inspection Scope
As discussed in NRC Inspection Report 05000382/200306, Section 1R07, the
inspectors previously reviewed documentation, analysis, and design basis
documentation relative to the ability of the spent fuel pool cooling system to remove
decay heat of the spent fuel during refueling outages involving a full core offload.
During this inspection period (as discussed in Section 1R04 of this report) on
November 3, 2003, the inspectors walked down the accessible portions of the spent fuel
pool cooling system Train A. The walkdown was completed following a full core offload
to verify that cooling flow to the spent fuel pool was adequate to maintain spent fuel pool
temperature.
b. Findings
No findings of significance were identified.
1R08 Inservice Inspection Activities (71111.08)
.1 Nondestructive Examination Activities
The inspectors observed the ultrasonic system calibration and observed ultrasonic and
magnetic particle examinations. The inspectors observed 13 examinations, which are
listed below.
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System Component/Weld Examination Method
Identification
RCS cold leg 07-013 Ultrasonic
RCS cold leg 07-013 Magnetic Particle
RCS cold leg 07-016 Ultrasonic
RCS cold leg 07-016 Magnetic Particle
RCS Hot leg 06-010 Magnetic Particle
RCS Hot leg 06-011 Magnetic Particle
Main Feed Header B 46-011 Ultrasonic
Main Feed Header B 46-012 Ultrasonic
Main Feed Header B 46-020 Ultrasonic
- 2 Steam Generator 04-030 Magnetic Particle
Nozzle
Containment 55-050 Ultrasonic
During the review of these examinations, the inspectors verified that the correct
nondestructive examination (NDE) procedure was used, examinations and conditions
were as specified in the procedure, and test instrumentation or equipment was properly
calibrated and within the allowable calibration period. The inspectors also reviewed the
documentation to determine if the indications revealed by the examinations were
compared against the American Society of Mechanical Engineers (ASME) Code
specified acceptance standards, and that the indications were appropriately
dispositioned. The nondestructive examination certifications of those personnel
observed performing examinations or identified during review of completed examination
packages were reviewed by the inspectors.
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The inspectors also observed the ultrasonic and eddy current examination of two leaking
pressurizer heater sleeves. In each case the flaws were clearly identified as short axial
flaws near the sleeve/pressurizer interface. The two pressurizer heater sleeves were
repaired using a MNSA-2 clamp.
b. Findings
No findings of significance were identified.
.2 Steam Generator Tube Inspection Activities
a. Inspection Scope
The inspection procedure specified, with respect to in situ pressure testing, performance
of an assessment of in situ screening criteria to assure consistency between assumed
NDE flaw sizing accuracy and data from the Electric Power Research Institute (EPRI)
examination technique specification sheets. It further specified assessment of
appropriateness of tubes selected for in situ pressure testing, observation of in situ
pressure testing, and review of in situ pressure test results.
The inspectors selected and reviewed the acquisition technique sheets and their
qualifying EPRI examination technique specification sheets to verify that the essential
variables regarding flaw sizing accuracy had been identified and qualified through
demonstration.
The inspection procedure specified comparing the estimated size and number of tube
flaws detected during the current outage against the previous outage operational
assessment predictions to assess Entergys prediction capability. The inspectors
reviewed Report ER-W3-2003-0534-000, Steam Degradation Assessment and Repair
Criteria for RF12. The purposes of the report were: (1) to provide a comprehensive
review and overall plan for detection and assessment of degradation to be addressed
during Refueling Outage RF12; and, (2) to provide predictions as to the type and extent
of degradation expected to be found.
The inspection procedure specified confirmation be made that the steam generator tube
eddy current testing (ECT) scope and expansion criteria meet technical specification
requirements, EPRI guidelines, and commitments made to the NRC. The inspectors
review determined that the steam generator tube ECT scope and expansion criteria
were being met.
The inspection procedure also specified that, if Entergy identified new degradation
mechanisms, then verify that Entergy had fully enveloped the problem in an analysis
and had taken appropriate corrective actions before plant startup. At the time of this
inspection, no new degradation mechanisms had been identified.
Enclosure
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The inspection procedure also required confirmation that all areas of potential
degradation were being inspected, especially areas which were known to represent
potential ECT challenges (e.g., top-of-tubesheet, tube support plates, and U-bends).
The inspectors confirmed that all known areas of potential degradation, including
ECT challenged areas, were included in the scope of inspection and were being
inspected.
The inspection procedure further required that repair processes being used were
approved in the technical specifications for use at the site. At the time of this inspection,
Entergy had not performed or used the designated Technical Specification approved
repair processes, thus there was no opportunity to observe implementation of any
potential repairs (e.g., plugging operations) or in-situ pressure testing.
The inspection procedure also required confirmation that the Technical Specification
plugging limit was being adhered to, and determination whether depth sizing repair
criteria were being applied for indications other than wear or axial primary water stress
corrosion cracking in dented tube support plate intersections. The inspectors confirmed
that Entergy was adhering to these specifications. The inspectors also determined that
Entergy, in response to Information Notice 2002-21, did account for crack-like
indications in dented tube support plate intersections by including these parameters in
their ECT computer programming, and the acquisition and analysis technique sheets.
Further, the ECT data analysts had been presented with specialized training associated
with this type of indication.
The inspection procedure stated that if steam generator leakage greater that three
gallons per day was identified during operations or during postshutdown visual
inspections of the tubesheet face, then assess whether Entergy had identified a
reasonable cause and corrective actions for the leakage based on inspection results.
The inspectors did not conduct any assessment because this condition did not exist.
The inspection procedure required confirmation that the ECT probes and equipment
were qualified for the expected types of tube degradation and assessment of the site
specific qualification of one or more techniques. The inspectors observed portions of all
ECT performed. During these examinations, the inspectors verified that: (1) the probes
appropriate for identifying the expected types of indications were being used; (2) probe
position location verification was performed; (3) calibration requirements were adhered
to; and, (4) probe travel speed was in accordance with procedural requirements. The
assessment of site specific qualifications of the techniques being used, including a
listing of the specific techniques and qualifications reviewed, is addressed and identified
in the table above.
Finally, the inspection procedure specified the review of one to five samples of ECT data
if questions arose regarding the adequacy of ECT data analyses. The inspectors did
not identify any results where ECT data analyses adequacy was questionable.
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b. Findings
No findings of significance were identified.
.3 Identification and Resolution of Problems
a. Inspection Scope
The inspectors reviewed inservice inspection related condition reports issued during the
current and past refueling outage, and verified that Entergy identified, evaluated,
corrected, and trended problems. In this effort, the inspectors evaluated the
effectiveness of Entergys corrective action process, including the adequacy of the
technical resolutions.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification (71111.11)
.1 Biennial Inspection
a. Inspection Scope
The inspectors: (1) evaluated examination security measures and procedures for
compliance with 10 CFR 55.49; (2) evaluated Entergys sample plan of the written
examinations for compliance with 10 CFR 55.59 and NUREG-1021, as referenced in the
facility requalification program procedures; and (3) evaluated maintenance of license
conditions for compliance with 10 CFR 55.53 by review of facility records (medical and
administrative), procedures, and tracking systems for licensed operator training,
qualification, and watchstanding. In addition, the inspectors reviewed remedial training
for examination failures for compliance with facility procedures and responsiveness to
address areas failed.
Furthermore, the inspectors: (1) interviewed 12 personnel, including operators,
instructors/evaluators, and training supervisors, regarding the policies and practices for
administering requalification examinations; (2) observed the administration of two
dynamic simulator scenarios to one requalification crew; and (3) observed four
evaluators administer six job performance measures, including three in the control room
simulator in a dynamic mode and two in the plant under simulated conditions.
The inspectors also reviewed the remediation process for two individuals. The
inspectors also reviewed the results of the annual licensed operator requalification
operating examination for 2002 and 2003. The biennial written examinations that were
administered in September and October 2003 were also reviewed. The results of the
examinations were assessed to determine Entergys appraisal of operator performance
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and the feedback of performance analysis to the requalification training program. The
inspectors interviewed members of the training department and operating crews to
assess the responsiveness of the licensed operator requalification program. The
inspectors also observed the examination security maintenance for the operating tests
during the examination week.
Additionally, the inspectors assessed the Waterford 3 plant referenced simulator for
compliance with 10 CFR 55.46 using Baseline Inspection Procedure IP 71111.11
(Section 03.11). The inspectors assessed the adequacy of Entergys simulation facility
for use in operator licensing examinations and for satisfying experience requirements as
prescribed in 10 CFR 55.46. The inspectors reviewed a sample of simulator
performance test records (transient tests, surveillance tests, malfunction tests, and
scenario-based tests), simulator work request records, and processes for ensuring
simulator fidelity commensurate with 10 CFR 55.46. The inspectors also interviewed
members of Entergys simulator configuration control group as part of this review.
b. Findings
No findings of significance were identified.
.2 Quarterly Inspection
a. Inspection Scope
On October 7, 2003, the inspectors observed a licensed operator simulator training
exercise. During the exercise the inspectors evaluated the operators ability to
recognize, diagnose, and respond to a steam generator tube leak followed by tube
rupture. Additional challenges included loss of component cooling water Pump B,
containment spray Pump B failing to start, failure of pressure level Channel X, reactor
coolant Pump 2B lower seal failure, two stuck control element assemblies, and high
pressure safety injection Pump A failure to start. The inspectors observed and
evaluated the following areas:
- Understanding and interpreting annunciator and alarm signals
- Diagnosing events and conditions based on signals or readings
- Understanding plant systems
- Use and adherence of Technical Specifications
- Crew communications including command and control
- The crews and evaluators critiques
b. Findings
No findings of significance were identified.
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1R12 Maintenance Rule Implementation (71111.12)
a. Inspection Scope
During the inspection period, the inspectors reviewed Entergys implementation of the
Maintenance Rule. The inspectors considered the characterization, safety significance,
performance criteria, and the appropriateness of goals and corrective actions. The
inspectors assessed Entergys implementation of the Maintenance Rule to the
requirements outlined in 10 CFR 50.65, and Regulatory Guide 1.160, Monitoring the
Effectiveness of Maintenance at Nuclear Power Plants, Revision 2. The inspectors
reviewed the following system that displayed performance problems:
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)
a. Inspection Scope
The inspectors reviewed risk assessments for planned or emergent maintenance
activities to determine if Entergy met the requirements of 10 CFR 50.65(a)(4) for
assessing and managing any increase in risk from these activities. The following two
risk evaluations were reviewed:
- On October 3, 2003, and December 11, 2003, planned maintenance was
performed on the digital fault recorders and protective relays in the 230 kV
switchyard associated with offsite power to the Waterford 3 nuclear plant.
- On September 29 through September 30, 2003, during emergent repairs
performed on emergency diesel generator, Train A. Repairs consisted of
replacing a failed fuel line as discussed in Section 4OA3 of this report.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
a. Inspection Scope
The inspectors reviewed the technical adequacy of two operability evaluations to verify
that they were sufficient to justify continued operation of a system or component. The
inspectors considered that, although equipment was potentially degraded, the operability
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evaluation provided adequate justification that the equipment could still meet its
Technical Specification, Updated Final Safety Analysis Report, and design-bases
requirements and that the potential risk increase contributed by the degraded equipment
was thoroughly evaluated. The following evaluations were reviewed:
- Operability evaluation addressing dye penetrant indications on the reactor vessel
head incore instruments nozzles (Condition Report CR-WF3-2003-3307)
- Operability evaluation addressing degraded shutdown cooling suction inside
containment isolation valve (Condition Report CR-WF3-2003-2991)
b. Findings
No findings of significance were identified.
1R16 Operator Workarounds (71111.16)
a. Inspection Scope
The inspectors performed two reviews of operator workarounds. One review was
performed prior to the plant being shutdown for a refueling outage that began
October 20, 2003. The second review was performed immediately following the
refueling outage during full power operations. The reviews evaluated the individual and
cumulative effects of current operator workarounds to assess the associated impact
affecting the operators ability to respond in a correct and timely manner to plant
transients and accidents.
b. Findings
No findings of significance were identified.
1R19 Postmaintenance Testing (71111.19)
a. Inspection Scope
The inspectors reviewed 3 postmaintenance tests for selected risk-significant systems to
verify their operability and functional capabilities. The inspectors considered whether
testing met design and licensing bases, Technical Specifications, and licensee
procedural requirements. The inspectors reviewed the testing results for the following
three components:
- Nitrogen Gas Pressure Indicating Switch NG IPIS0941B following emergent
repairs on September 16, 2003, due to the failure of Nitrogen Accumulator 2
Outlet Valve NG-610 to properly cycle
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- Emergency diesel generator, Train A, following a failed fuel oil tubing line on
September 30, 2003
- Main steam isolation Valves (MSIVs) 1 and 2 actuating system leak tests
performed following system modifications in November 2003
b. Findings
Introduction. The inspectors identified a noncited violation of 10 CFR Part 50,
Appendix B,Section XI, "Test Control," for the failure to establish adequate test controls
for leak testing MSIVs 1 and 2. This performance deficiency contributed to both valves
being declared inoperable due to system leaks creating a low pressure condition in the
valve actuating systems.
Description. On December 6, 2003, control room operators declared MSIV 1 inoperable
after identifying that the valve actuating system nitrogen pressure was less than the
acceptance criteria of 2520 psig. The inspectors reviewed operator logs and noted that
MSIV 2 had previously been declared inoperable for the same reason at 1:29 a.m. on
November 20, 2003. Entergy had completed a refueling outage and control room
operators declared MSIV 1 operable November 19, 2003, at 11:10 p.m., and MSIV 2
operable November 20, 2003, at 12:01 a.m. The inspectors reviewed work orders and
noted that MSIV 1 valve actuating nitrogen system had been recharged due to low
system pressure on December 1, 2003.
The inspectors reviewed the work history of the MSIVs and noted that both valves had
received a modification that installed a high accuracy pressure instrument in the
nitrogen actuating system. The nitrogen actuating system is a safety related system
having a safety function to close each MSIV within 7 seconds following a main steam
line isolation signal. The inspectors reviewed the postmaintenance test instructions and
noted that the work order specified a leak test of the modified system be performed at
normal system operating pressure. After reviewing operator logs and discussions with
maintenance personnel that performed the leak tests, the inspectors determined that the
leak tests were not performed at normal system pressure. Normal system nitrogen
pressure is approximately 2600 psig and the inspectors determined that the leak tests
were performed at approximately 1200 psig for MSIV 1and 930 psig for MSIV 2. The
individual that performed the test did not recall the pressure that the leak tests were
performed at nor did the individual recall the normal system operating pressure. The
inspectors determined that Entergy had failed to establish adequate test controls for
leak testing the piping connections following the modification. This resulted in the failure
to identify system leaks that eventually resulted in both valves being declared
Analysis. The deficiency associated with this finding was inadequate testing controls.
The inadequate test controls failed to ensure that leak tests of the nitrogen actuating
systems for the MSIVs were performed at normal system pressure (2600 psig)
following modification to the systems. This performance deficiency resulted in the
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failure to identify system leaks which contributed to the valves being declared
inoperable. This finding is more than minor because it affected the Barrier Integrity
Cornerstone objective of providing reasonable assurance of the functionality of
containment. The finding was evaluated using the Phase 1 significance determination
process worksheet. The finding was only of very low safety significance because it did
not represent an actual reduction of the atmospheric pressure control function of the
reactor containment, it did not result in an actual open pathway affecting the physical
integrity of reactor containment, and the main steam isolation valves were inoperable for
less time than the allowed Technical Specification outage time.
Enforcement. 10 CFR Part 50, Appendix B, Criterion XI, "Test Control," states, in part,
that a test program shall be established to assure that all testing required to
demonstrate that structures, systems, and components will perform satisfactorily in
service. The failure to establish testing controls to ensure the MSIVs would perform
satisfactorily in service is a violation of 10 CFR Part 50, Appendix B, Criterion XI.
Because the failure to establish adequate testing controls was of very low safety
significance and has been entered into Entergys corrective action program as Condition
Reports 2003-3716 and 2003-3837, this violation is being treated as a noncited
violation, consistent with Section VI.A of the NRC Enforcement Policy:
NCV 50-382/2003007-01, Inadequate Test Controls of MSIVs.
1R20 Refueling and Outage Activities (71111.20)
a. Inspection Scope
Refueling Outage 12 began on October 20, 2003, and ended on November 24, 2003.
During the outage, the inspectors observed shutdown, cooldown, refueling, startup, and
maintenance activities to verify that Entergy maintained the plant capabilities within the
applicable Technical Specification requirements and within the scope of the outage risk
plan. Specific performance activities evaluated included:
- Clearance Activities - ensured tags were properly hung and equipment
appropriately configured to support the function of the clearance
- Reactor Water Inventory Controls - verified that flow paths, equipment
configurations, and alternative means for inventory addition were appropriate to
prevent inventory loss
- Reactivity Controls - ensured compliance with Technical Specifications and
verified that activities, which could affect reactivity, were reviewed for proper
control within the outage risk plan
- Refueling Activities - assessed compliance with Technical Specifications, verified
proper tracking of fuel assemblies from the spent fuel pool to the core, and
confirmed that foreign material exclusion was maintained
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- Reduced Inventory and Midloop Conditions - verified that commitments to
Generic Letter 88-17 were in place, that plant configuration was in accordance
with those commitments, and that distractions from unexpected conditions or
emergent work did not affect operator ability to maintain the required reactor
vessel level
- Monitored Shutdown Cooling System - verified that operating parameters were
established and maintained within the required range
- Reactor Coolant System Instrumentation Indication - verified that reactor coolant
system pressure, level, and temperature instrumentation were installed and
configured to provide accurate indication
- Spent Fuel Pool Cooling System Operation - assessed outage work for potential
impact on the ability of the operations staff to operate the spent pool cooling
system during and after core offload
- Containment Closure - reviewed control of containment penetrations to ensure
that containment closure could be achieved within required times during various
portions of the outage Reduced Inventory
- Heatup and Startup Activities - ensured that Technical Specifications and
administrative procedure prerequisites for mode changes were met prior to
changing modes or plant configurations
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing (71111.22)
a. Inspection Scope
The inspectors observed or reviewed the following surveillance test to ensure the
system was capable of performing its safety function and to assess its operational
readiness. Specifically, the inspectors considered whether the following surveillance
test met Technical Specifications, the Updated Final Safety Analysis Report, and
licensee procedural requirements:
- Surveillance Procedure OP-903-026, Emergency Core Cooling System Valve
Lineup Verification, Revision 12, performed on November 21, 2003. This
surveillance verified that the appropriate valve lineup was established for low
pressure safety injection system and verified the system was vented and filled
with water.
Enclosure
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b. Findings
As discussed in Section 4OA2 of this report, the inspectors identified a noncited
violation of 10 CFR Part 50, Appendix B, Criterion XVI, for the failure to establish
adequate corrective actions to prevent recurrence of voiding conditions affecting the
operability of the low-pressure safety injection system following shutdown cooling
operations.
2. RADIATION SAFETY
Cornerstone: Occupational Radiation Safety
2OS1 Access Control to Radiological Significant Areas (71121.01)
a. Inspection Scope
To review and assess Entergy's performance in implementing physical and
administrative controls for airborne radioactivity areas, radiation areas, high radiation
areas, the inspector interviewed supervisors, radiation workers, and radiation protection
personnel involved in high dose rate and high exposure jobs during the 2003 refueling
outage. The inspector discussed changes to the access control program with the
Radiation Protection Manager. The inspector also conducted plant walkdowns within
the controlled access area and conducted independent radiation surveys of selected
work areas. The following items were reviewed and compared with regulatory
requirements:
- Area postings, radiation work permits (RWPs), radiological surveys, and other
controls for airborne radioactivity areas, radiation areas, and high radiation areas
- High radiation area key control
- Setting, use, and response of electronic personnel dosimeter alarms
- Prejob briefings for the pressurizer heater replacement and upper guide
structure movement work activities
- Conduct of work by radiation protection technicians and radiation workers in
areas with the potential for high radiation dose work associated with refueling
outage activities
- Dosimetry placement when work involved a significant dose gradient (primary
steam generator and reactor head detensioning activities)
- Controls involved with the storage of highly radioactive items in the spent fuel
pool
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- Audits and self-assessments involving high radiation area controls and staff
performance
- Summary of corrective action documents written since the last inspection and
selected documents relating to high radiation area incidents, radiation protection
technician and radiation worker errors, repetitive, and significant individual
deficiencies
- Controls in place to ensure compliance with 10 CFR 20.1703(f)
There were no internal dose events which exceeded 50 millirem committed effective
dose equivalent during this inspection period; therefore, this aspect to the inspection
procedure could not be completed. Performance indicator reviews associated with
occupational exposure control effectiveness are documented in Section 4OA1 of this
report. No licensee event reports or special reports were required in this inspectable
area since the previous inspection. The inspector completed all 21 of the required
samples.
b. Findings
Introduction. The inspector identified a Green, noncited violation of Technical
Specification 6.12.1 because Entergy failed to barricade a high radiation area to prevent
inadvertent entry.
Description. On October 27, 2003, during tours of the reactor containment building the
inspector noted that the high radiation area rope barricading the regenitive heat
exchanger room located on the 21-foot elevation was stretched across the entrance way
at a height of approximately 79 inches, which would not obstruct the entry of station
workers. General area radiation levels were as high as 420 millirem per hour.
Analysis. The inspector determined that Entergys failure to properly barricade a high
radiation area as required by Technical Specification 6.12.1 is a performance deficiency.
Traditional enforcement does not apply because the issue did not have any actual safety
consequences or potential for impacting the NRCs regulatory function and was not the
result of any willful violation of NRC requirements or licensees procedures. The finding
is greater than minor because it is associated with the Occupational Radiation Safety
Cornerstone attribute: program and process, and affected the cornerstone objective to
provide adequate protection to workers health and safety from exposure to radiation.
When the issue was processed through the Occupational Radiation Safety Significance
Determination Process it was determined to be a Green finding because it was not an
ALARA planning and control issue, there was no overexposure or substantial potential
for an overexposure and the ability to assess dose was not compromised.
Enforcement. Technical Specification 6.12.1. states, in part, that each high radiation
area in which the intensity of radiation is greater than 100 millirem per hour but less than
1000 millirem per hour shall be barricaded.
Enclosure
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The failure to place a high radiation barricade to obstruct entry to the regenitive heat
exchanger room is a violation of Technical Specification 6.12.1. Because the finding is
of very low safety significance and was entered into the corrective action program as
Condition Report CR-WF3-2003-03164, this violation was treated as a noncited
violation, consistent with Section VI.A of the NRC Enforcement Policy:
NCV 50-382/2003007-02, Failure to barricade a high radiation area.
2OS2 ALARA Planning and Controls (71121.02)
a. Inspection Scope
To assess Entergys program to maintain occupational exposures as low as is
reasonably achievable (ALARA), the inspector reviewed work activities conducted during
Refueling Outage 12, and attended the pre-job ALARA brief and observed radiological
work associated with the replacement of the chemical volume control system filter.
The inspector interviewed radiation protection staff members and other radiation
workers to determine the level of planning, communication, ALARA practices, and
supervisory oversight integrated into work planning and work activities. In addition, the
following items were reviewed and compared with procedural and regulatory
requirements:
- Current 3-year rolling average collective exposure
- Six ALARA prejob, in progress, and postjob reviews and associated radiation
work permit packages from Refueling Outage 12 which resulted in some of the
highest personnel collective exposures
- Site specific trends in collective exposures, historical data, and source-term
measurements
- Site specific ALARA program procedures
- ALARA work activity evaluations, exposure estimates, and exposure mitigation
requirements
- Work activity intended dose against actual dose received and the reasons for
any inconsistencies
- Assumptions and basis for annual collective exposure estimates, the
methodology for estimating work activity exposures, and intended dose
outcomes
- Method for adjusting exposure estimates, or re-planning work, when unexpected
changes in job scope or emergent work were encountered
Enclosure
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- Use of engineering controls to achieve dose reductions and the benefits afforded
by using shielding
- Historical trends and current status of tracked plant source terms and
contingency plans due to changes in fuel performance or primary plant chemistry
- Radiation worker performance during work activities in radiation, high radiation or
airborne radioactivity areas
- Declared pregnant workers declared during the assessment period and
monitoring controls and exposure result
- Self-assessments and audits related to the ALARA program since the last
inspection
- Resolution through the corrective action process of problems identified through
postjob reviews and postoutage report critiques
- The effectiveness of self-assessment activities with respect to identifying and
addressing repetitive deficiencies or significant individual deficiencies
- Summary of corrective action documents written since the last inspection and
selected documents relating to exposure tracking, higher than planned exposure
levels, radiation worker practices, repetitive, and significant individual
deficiencies against the corrective action program
The inspector completed 16 sample requirements.
b. Findings
No findings of significance were identified.
4. OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
a. Inspection Scope
The inspectors sampled licensee submittals for the performance indicators listed below
for the period from April 2002 through September 2003. To verify the accuracy of the
performance indicator data reported during that period, performance indicator definitions
and guidance contained in NEI 99-02, "Regulatory Assessment Indicator Guideline,"
Revision 2, were used to verify the basis in reporting for each data element.
Enclosure
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Occupational Radiation Safety Cornerstone
- Occupational Exposure Control Effectiveness Performance Indicator
Licensee records reviewed included corrective action documentation that identified
occurrences of locked high radiation areas (as defined in Technical
Specification 6.12.2), very high radiation areas (as defined in 10 CFR 20.1003), and
unplanned personnel exposures (as defined in NEI 99-02). Additional documents
reviewed included ALARA records and whole body counts of selected individual
exposures. The inspector interviewed licensee personnel that were accountable for
collecting and evaluating the performance indicator data. In addition, the inspector
toured plant areas to verify that high radiation, locked high radiation, and very high
radiation areas were properly controlled. The inspector completed one of the required
inspection samples.
Public Radiation Safety Cornerstone
- Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
Radiological Effluent Occurrences
Licensee documents reviewed included radiological effluent release corrective action
records and annual effluent release reports during the past four quarters (no licensee
event or special reports were submitted) to determine if any doses resulting from liquid
or gaseous effluent releases exceeded performance indicator thresholds. The
inspectors interviewed licensee personnel that were accountable for collecting and
evaluating the performance indicator data. The inspector completed one of the required
inspection samples.
Barrier Integrity Cornerstone
- Unplanned Scrams
Licensee documents reviewed included control room logs, reactor power profile
obtained from the plant computers, and licensee quarterly operating reports. The
inspector completed one of the required inspection samples.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)
Section 2OS2 evaluated the effectiveness of Entergy's problem identification and
resolution processes regarding exposure tracking, higher than planned exposure levels,
and radiation worker practices. Section 1RO8.3 evaluated the effectiveness of
Enclosure
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Entergys problem identification and resolution process regarding inservice inspection-
related condition reports issued during the current and past refueling outages. No
findings of significance were identified.
.1 Voiding in the Low Pressure Safety Injection System
a. Inspection Scope
On December 19, 2003, the inspectors completed a review of Entergys actions
regarding voiding in the low pressure safety injection system. Entergys previous
actions to address voiding conditions affecting the emergency core cooling systems for
a number of years are documented in NRC Inspection Report 05000382/2002005. The
long-term voiding issues have contributed to equipment failures along with operations,
engineering, and radiological challenges. The inspectors conducted interviews with
responsible engineers, operators, and managers and reviewed relevant documents and
drawings.
b. Findings
Introduction. The inspectors identified a noncited violation of 10 CFR Part 50,
Appendix B, Criterion XVI, for the failure to establish adequate corrective actions to
prevent recurrence of voiding conditions affecting the operability of the low pressure
safety injection system following shutdown cooling operations.
Description. On November 21, 2003, following restart from Refueling Outage 12,
Entergy performed ultrasonic testing on low pressure safety injection system, Trains A
and B, per Procedure OP-903-026, Emergency Core Cooling System Valve Lineup
Verification, Revision 12, to determine if the piping was water solid. The ultrasonic
testing identified gas voids at Containment Penetration 38 and Vent Valve SI-134A that
resulted in the low pressure safety injection system Train A being inoperable in
accordance with the procedural acceptance criteria. Subsequently, ultrasonic testing
identified gas voids in the low pressure safety injection system, Train B, at Vent
Valves SI-133B and SI-134B and at Containment Penetrations 36 and 37. The gas void
at Vent Valve SI-134B rendered low pressure safety injection system Train B inoperable.
The inspectors noted that one day following Refueling Outage 11, a gas void was
identified in low pressure safety injection system Train B, which required Train B to be
declared inoperable (Documented in NRC Inspection Reports 05000382/2002002 and
05000-382/2002005). Entergy determined that the root cause for gas voiding in the low
pressure safety injection system was an inadequate plan to vent the gas following the
low pressure safety injection system realignment from shutdown cooling to the safety
injection mode. Entergy placed this degraded condition into their corrective action
process as Condition Report 2002-00818. Corrective actions assigned were to vent and
sweep the low pressure safety injection system with less gas saturated water from the
Enclosure
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refueling water storage pool. Additionally, procedural guidance requiring operators to
ensure work orders were generated to vent and fill the low pressure safety injection
system following shutdown cooling operations was implemented.
Following the identification of gas voids on November 21, 2003, engineering and
operations personnel stated that although work orders were written, operations failed to
accomplish the vent and fill tasks in a timely manner resulting in the accumulation of
voids that rendered the systems inoperable per the proceduralized acceptance criteria.
The inspectors determined that the failure to effectively implement the corrective actions
directed by Condition Report 2002-00818 resulted in unacceptable voids in the low
pressure safety injection system. This failure resulted in a recurrence of a significant
condition adverse to quality and was determined to be a violation of 10 CFR Part 50,
Appendix B, Corrective Action.
Analysis. The deficiency associated with this finding was the failure to establish
corrective measures to prevent recurrence of a significant condition adverse to quality.
Specifically, corrective actions established to address unacceptable gas voids identified
in the low pressure safety injection system following Refueling Outage 11 were not
effectively implemented and failed to prevent recurrence following Refueling Outage 12.
This finding is greater than minor because it affected the mitigating system objective to
ensure the reliability and availability of the low pressure safety injection system to
respond to an initiating event. The problem if left uncorrected would become a more
significant safety concern. The significance of this finding was determined to be of very
low safety significance because Train B was inoperable for less than the Technical
Specification allowed outage time and Train A was determined to be degraded but
operable in accordance with Generic Letter 91-18 guidance.
Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires,
in part, that measures be established to assure that conditions adverse to quality are
promptly identified and corrected. In the case of significant conditions adverse to
quality, the measures shall assure that the cause of the condition is determined and
corrective action taken to preclude repetition. The failure to establish corrective
measures to prevent recurrence of unacceptable void accumulations in the low pressure
safety injection system following shutdown cooling operations is a violation of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action." Because this finding is of very
low safety significance and has been entered into Entergys corrective action program
as Condition Reports 2003-3740, -3858, and -3901, this violation is being treated as a
noncited violation consistent with Section VI.A of the NRC Enforcement Policy: NCV 05000382/2003007-03, Ineffective Corrective Actions to Prevent Recurrence of Voiding
Conditions.
Enclosure
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.2 Alloy 600 Nozzle Cracking
a. Inspection Scope
During refueling Outage 12 (October 20, 2003, through November 24, 2003) Entergy
identified pressure boundary leakage emanating from three Alloy 600 reactor coolant
system nozzles. The inspectors reviewed Entergys corrective actions associated with
the multiple nozzle failures. Additionally, the inspectors reviewed the corrective and
preventive maintenance history of the reactor coolant system Alloy 600 nozzles. The
inspectors also reviewed previous corrective actions addressing pressure boundary
leakage to evaluate their effectiveness in preventing recurrence.
b. Findings
Introduction. The inspectors identified a noncited violation of 10 CFR Part 50,
Appendix B, Criterion XVI, for the failure to implement effective corrective actions
resulting in recurrences of pressure boundary leakage due to primary water stress
corrosion cracking of Alloy 600 reactor coolant system nozzles.
Discussion. Entergy identified three reactor coolant system Alloy 600 nozzle leaks
during Refueling Outage 12. The nozzles affected were the reactor coolant system hot
Leg 2 Instrument Nozzle RC-IPT-0106B and two pressurizer heater sleeve Nozzles C-1
and C-3. Each nozzle leak was determined by Entergy to be the result of primary water
stress corrosion cracking. Each nozzle leak was repaired prior to the end of the
refueling outage.
The inspectors reviewed the history of the Alloy 600 nozzles at Waterford 3 and noted
that multiple failures had previously occurred due to primary water stress corrosion
cracking. In Refueling Outage 9, three hot leg nozzles and two pressurizer top nozzles
were found leaking. In Refueling Outage 10, one pressurizer heater sleeve nozzle was
found leaking. The inspectors reviewed Condition Reports 1999-00204, 1999-00232,
1999-00234, 2000-1250, 2003-03130, and 2003-03110. Review of these corrective
action documents revealed that no replacement plans had been established by Entergy
to repair or replace the Alloy 600 nozzles throughout the reactor coolant system that
were susceptible to primary water stress corrosion cracking. The inspectors noted that
Condition Report 2000-1250 stated, Due to the nature of primary water stress corrosion
cracking and the use of Inconel 600 at Waterford 3, recurrence of similar leaks is
considered beyond Waterford 3 control. The inspectors noted that with the current
materials and ongoing actions, that Waterford 3 would be susceptible to future pressure
boundary leakage caused by primary water stress corrosion cracking of Alloy 600 nozzle
material. Operation of Waterford 3 with reactor coolant system boundary leakage is a
condition prohibited by plant Technical Specification 3.4.5.2.a during Modes 1, 2, 3, and
4.
The inspectors noted that Entergy had not initiated actions to prevent the occurrence of
pressure boundary leakage, through the Inconel 600 material nozzles, during either
Enclosure
-22-
Refueling Outages 11 or 12. The inspectors also noted that no inspections other than
visual examinations to find leakage were being performed by Entergy to detect
degradation of the nozzles that would allow for repairs or replacement prior to reactor
coolant system pressure boundary leakage occurring. The inspectors determined that
Entergy had not established adequate measures to prevent recurrence of reactor
coolant system pressure boundary leakage, due to primary water stress corrosion
cracking of Alloy 600 nozzles, a significant condition adverse to quality.
Analysis. The deficiency associated with this finding was the failure to establish
corrective measures to prevent recurrence of a significant condition adverse to quality.
Specifically, Entergy had not established corrective measures to preclude multiple
occurrences of reactor coolant system pressure boundary leakage, during an operating
cycle, due to primary water stress corrosion cracking of Alloy 600 nozzle material. This
finding was greater than minor because it affected the reactor safety barrier integrity
cornerstone objective for providing reasonable assurance that the physical design
barriers protect the public from radionuclide releases caused by accidents or events.
Using NRC Manual Chapter 0609 significance determination process Phase 1
Screening Worksheet this performance deficiency affected the reactor coolant system
barrier function requiring a Phase 2 analysis. The results of the Phase 2 and 3 analysis
determined that this finding was of very low safety significance based on the cracks
being axial in nature (does not contribute substantially to a loss of coolant accident) and
the leaks resulted in a buildup of only minor boric acid residue indicative of only trace
amounts of through wall leakage. The leak rates identified were well within the capacity
of a single charging pump.
Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires,
in part, that measures be established to assure that conditions adverse to quality are
promptly identified and corrected. In the case of significant conditions adverse to
quality, the measures shall assure that the cause of the condition is determined and
corrective action taken to preclude repetition. The failure to establish corrective
measures to prevent recurrence of reactor coolant system pressure boundary leakage
due to primary water stress corrosion cracking of Alloy 600 nozzle material is considered
a violation of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action." Because
this finding is of very low safety significance and has been entered into Entergys
corrective action program as Condition Reports 2003-03130 and 2003-03110, this
violation is being treated as a noncited violation consistent with Section VI.A of the NRC
Enforcement Policy: NCV 05000382/2003007-04, Ineffective Corrective Actions to
Prevent Recurrence of PWSCC of Alloy 600 material.
Enclosure
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4OA3 Event Followup (71153)
.1 Failure of the Train A Emergency Diesel Generator
Description of Event
On September 29, 2003, during the performance of a monthly surveillance run, the
Train A emergency diesel generator experienced a fuel line failure. Approximately
3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> into the surveillance an operator in the Train A diesel room observed the fuel
line break and immediately shutdown the diesel locally in approximately 15 seconds.
The operator reported seeing a solid stream of fuel oil being discharged from the fuel
line break located on the left cylinder bank side of the diesel generator. Approximately
70 gallons of fuel oil was discharged from the line break. Waterford personnel
performed a field inspection and identified that the 3/4 inch stainless steel fuel supply
tube had sheared 360 degrees where the tube inserted into a Swagelok compression
fitting.
Entergy assembled a root cause analysis team to investigate the cause of the failure
and develop a corrective action plan. Plant personnel replaced the failed tubing,
retested the Train A emergency diesel, and restored the diesel to operable status on
September 30, 2003. Examination of the failed tubing indicated that fatigue failure
resulted in the break where the tip of the back ferrule of the compression fitting
contacted the tubing. Entergy determined the Train B emergency diesel generator was
not susceptible to the same failure mechanism since the fuel lines were the original lines
having never been replaced by Entergy.
a. Inspection Scope
The inspector reviewed the sequence of events related to the emergency diesel
generator fuel oil line failure.
The inspector assessed Entergys immediate actions and subsequent evaluation of the
Train A emergency diesel generator failure that occurred on September 29, 2003.
The inspector evaluated pertinent industry operating experience and potential
precursors to the failure of emergency diesel generator fuel oil line at the Swagelock
fitting.
The inspector reviewed and assessed Entergys corrective actions to verify that they
have adequately evaluated and addressed the extent of condition including generic
implications.
The inspector reviewed Entergys root cause evaluation determination for
independence, completeness, and accuracy.
Enclosure
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The inspector, along with a senior reactor analyst inspector, assessed the safety
significance associated with the Train A emergency diesel generator failure.
b. Findings
Introduction. A self-revealing apparent violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, was identified for the failure to
establish appropriate instructions and accomplish those instructions for proper
installation of a fuel line for Train A emergency diesel generator in May of 2003. This
failure resulted in uneven and excessive scoring of the tubing that ultimately led to a
complete 360 degree failure of the fuel supply line on September 29, 2003, during a
monthly surveillance test.
Description. In May of 2003, Entergy performed an overhaul on the Train A emergency
diesel generator. During this overhaul the fuel oil header left/right bank cross connect
tubing and associated fittings were replaced to repair a small fuel oil leak that had been
discovered previously. The tubing was 316 grade stainless steel, 3/4 inch outer
diameter, with a nominal wall thickness of 0.049 inches. The tubing was bent by
mechanical craft personnel at four locations and spanned approximately 5 feet. The
replacement compression fittings were manufactured by Swagelok. After approximately
28.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> of runtime, following the May overhaul, failure of the replaced fuel oil line
occurred on September 29, 2003 during a monthly surveillance test. Entergy noted that
a complete 360 degree failure of the tubing occurred at the compression fitting that
attached the fuel line to the diesel engine left cylinder bank.
Entergy sent the failed specimen to two laboratories for examination to determine the
root cause of the failure. Both labs concluded that fatigue failure of the tubing occurred
at the point where the back ferrule of the compression fitting contacted the outer tubing
surface. It was noted that the tube failure was along the front edge of the back ferrule
and that the outer circumference of the tubing along the fracture was unevenly scored,
up to 30 percent of the tubing thickness. According to Swagelok, a correct installation
would result in an evenly scored tube, approximately 10 percent of the tubing thickness.
Entergy determined that improper alignment of the tubing in the compression fitting and
potential over tightening of the compression fitting resulted in the uneven and excessive
scoring. With these conditions established, the vibrational stresses subjected to the
flawed tubing connection experienced during operation of the diesel generator resulted
in fatigue failure of the tubing on September 29, 2003.
The inspectors reviewed Entergys analysis of the event contained in document CR-
WF3-2003-02759. Entergy concluded that the installation of the replacement tubing
offered minimal margin for error when considering the following design attributes:
- Specified material is thin walled (0.049 inches)
- Large bore tubing $ 1/2 inch
- Configuration is complex containing multiple tube bends
Enclosure
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- Swagelok fittings produce tube scoring
- Vibration is present
Entergy determined that all these factors played a role in causing the tubing failure when
coupled with the tubing not being correctly installed into the Swagelok compression
fitting. Entergy determined that the extent of condition for this type of failure mechanism
was isolated to the Train A emergency diesel generator. A review of past events
revealed that there had been isolated tubing leaks or failures located at Swagelok
fittings that had all occurred greater than three years previous to the failure on
September 29, 2003. The inspectors reviewed these instances and found that there
were slight differences between the identified failure mechanisms, but did note that one
common corrective action was to provide additional training to mechanical maintenance
personnel on how to appropriately install a Swagelok compression fitting application.
The inspectors noted that Entergy relied on skill of the craft to install the fittings with no
detailed instructions or quality control checks provided to ensure the fittings were made
correctly. The inspectors noted that the Swagelok manual contained detailed
instructions for installing the fitting and also recommended the use of a depth marking
tool that could be used to ensure proper tube alignment within the compression fitting.
In review of the training materials and discussions with maintenance department
personnel the inspectors noted that not all Swagelok recommended installation practices
were being implemented by Entergy, including use of the depth marking tool. The
inspectors discussed these observations with licensee senior management who
indicated that they were evaluating enhancements that included more detailed
instructions.
Analysis. The deficiency associated with this event was the failure to establish
appropriate measures to ensure proper installation of a replacement fuel oil line on the
Train A emergency diesel generator in May of 2003. This failure resulted in uneven and
excessive scoring of the tubing that ultimately led to a complete 360 degree failure of
the fuel supply line on September 29, 2003. The finding was greater than minor
because it directly impacted the availability and reliability of an emergency diesel
generator which is used to mitigate the loss of AC power to the respective safety related
bus. The finding was determined to be potentially greater than Green based on a
Phase 1, Phase 2, and Phase 3 analysis.
Significance determination process Phase 1:
In accordance with NRC Inspection Manual Chapter 0609, Appendix A,
Significance Determination of Reactor Inspection Findings for At-Power
Situations, the inspectors conducted a significance determination Phase 1
screening and determined that the finding resulted in loss of the safety function
of the Train A emergency diesel generator for greater than the Technical
Specification allowed outage time. Therefore, a Significance determination
process Phase 2 evaluation was required.
Enclosure
-26-
Significance determination process Phase 2:
The Risk-Informed Inspection Notebook for Waterford Nuclear Plant Unit 3,
Revision 1, September 2, 2003, was utilized for the Phase 2 evaluation of the
inoperable Train A emergency diesel generator. The following steps and the
associated findings are listed below:
- Select or define the applicable initiating event scenarios:
Table 2, Initiators and System Dependency for Waterford Nuclear Plant,
Unit 3, was reviewed to determine that the loss of offsite power (LOOP)
initiating event scenario was the only scenario that needed to be
analyzed due to the failure of the Train A emergency diesel generator.
- Estimate the likelihood of scenario initiating events and conditions:
The performance deficiency was assumed to exist for greater than
30 days based on the failure of the diesel generator being expected to
occur within its mission time. The mechanism leading to the fuel line
break was fatigue failure caused by vibration that only occurred while the
engine was running. No degradation was assumed to occur while the
engine was idle. Therefore, the diesel was destined to fail approximately
28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> after the fuel line was replaced in May of 2003. Using Table 1,
Categories of Initiating Events for Waterford Nuclear Plant, Unit 3, the
initiating event likelihood for loss of offsite power was determined to be
valued at 2.
- Estimate the remaining mitigation capability:
Using the significance determination process worksheet for loss of offsite
power (Table 3.6, SDP Worksheet for Waterford Nuclear Power Plant,
Unit 3 - Loss of Offsite Power (LOOP)), Sequences 1, 2, and 3, the
following results were assigned for each:
Sequence 1: LOOP-EFW - 6
Sequence 2: LOOP-EDG-REC8 - 6
Sequence 3: LOOP-EDG-TDEFW-REC1 - 6
Estimate the risk significance of the inspection finding:
NRC Inspection Manual Chapter 0609, Significance Determination
Process, Appendix A, Attachment 1, Counting Rule Worksheet, was
utilized using three sequences that resulted in values of 6. Since Step 10
was greater than zero, the risk significance of the inspection finding was
determined to be at low to moderate safety significance (White).
Enclosure
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As a result of the White finding in the Phase 2 evaluation, a Phase 3 evaluation
was performed.
Significance Determination Process Phase 3 Analysis
The following table presents the running history of the A emergency diesel
generator from the time of the maintenance until the run failure.
Date Event Run Time Run Time Total Run
(PMT) (Surveillance) Time for
Day
May 16-17, EDG A 39 min 4:15 4:54
2003 Maintenance
Outage
June 9, 2003 Monthly 4:46 4:46
Surveillance
July 8, 2003 Monthly 5:23 5:23
Surveillance
August 4, 2003 Monthly 4:36 4:36
Surveillance
September 2, PMT 20 0:20
2003
September 2, Monthly 5:02 5:02
2003 Surveillance
September 29, Monthly 2:48 (fuel oil 2:48
2003 Surveillance line break)
Cumulative run 27 hours3.125e-4 days <br />0.0075 hours <br />4.464286e-5 weeks <br />1.02735e-5 months <br />
time since 49 minutes
tubing total run
replaced. time for
EDG A
Assumptions:
- The mechanism leading to the fuel line leak was fatigue failure caused by
vibration that occurred while the engine was running. No degradation
occurred while the engine was idle. Therefore, the diesel was destined to
fail after 28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> of run time, regardless of how this time was accrued.
Enclosure
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- The primary period of risk was the 27 days of standby service while the
EDG had only 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, 48 minutes of run time remaining. Prior to this
period, the EDG had approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or more of run time
remaining, and a failure after 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> of accident recovery would have
been much less important because of the higher probability of recovering
offsite power or the Train B EDG. The analyst evaluated the 27 day high-
risk period and applied an adjustment factor based on information
received from Entergy to account for the other periods of exposure.
- Based on information received from Entergy, a nonrecovery probability of
0.6 was applied to each cutset that contained a Train B EDG fail-to-start
basic event, but no recovery was assumed for fail-to-run or
test/maintenance situations.
- Based on information received from Entergy, a nonrecovery probability of
0.1 was applied for the Train A EDG, after its failure from a fuel line
failure. This assumption was based on a statistical analysis performed by
Entergy and a walk-through simulation, where a maintenance technician
procured the necessary tools and manufactured a replacement fuel line
segment in approximately 25 minutes. Although this assumption was
used in this analysis, the analyst recognized that certain factors such as
stress, lack of procedures, diversion to other tasks, having only
emergency lighting, and the presence of excess fuel oil could make the
fuel line repair more likely to fail than once in every 10 attempts. A
sensitivity analysis was performed that did not provide recovery credit.
- The postprocessing application of the non-recovery probabilities for
EDG A and B were applied only to SBO sequences 2 and 13 in
accordance with the technical advice of Idaho National Engineering and
Environmental Laboratory (INEEL). Other sequences included recoveries
inherent to the model. SBO sequences 2 and 13 comprised
approximately 80 percent of the change in risk.
as noted above, therefore, to prevent the SPAR model from imputing a
higher failure rate for EDG B, the basic event for EDG A fail-to-run
was set to a probability of 1.0 in lieu of setting it to TRUE.
- Because EDG A would have run for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 48 minutes during the
final 27 days of the exposure period, the analyst changed the LOOP
initiating event frequency in both the base and evaluation cases to reflect
the probability that offsite power would be restored prior to the diesel
failure. This is based on the first-order assumption that if offsite power is
recovered prior to the diesel failure, the recovery will be successful.
Using the NUREG-5496 for Waterford 3, the frequency weighted average
probability of recovering offsite power in 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, 48 minutes is
Enclosure
-29-
80 percent. Therefore, the LOOP frequency was changed from 5.2E-
6/hr. to 1.04E-6/hr. Inherent to the analysis was the bounding
assumption that if EDG B fails, it will do so before the failure of EDG A.
To be consistent, the basic event OEP-XHE-NOREC-ST (Operator fails
to recover offsite power in the short term) was set to a probability of 1.0 in
both the base and evaluation cases, since this is implied in the
adjustment to the loss of offsite power frequency.
Quantification of the Change in Risk:
The analyst used SAPHIRE 6.79 software and the Waterford SPAR, Revision 3i
model, further revised by INEEL to include updated offsite power recovery
curves and reactor coolant pump seal failure probabilities.
The update was accomplished to make LOOP recovery times consistent with
NUREG-5496, which reported generally longer times of offsite power recovery
than previous studies. As a protocol, the mission time assigned to the
emergency diesel generator was made equal to the time after a LOOP needed to
achieve a 95 percent probability of recovering offsite power. As a consequence,
the mission time assigned to the emergency diesel generators was extended to
15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />, making the fail-to-run emergency diesel generator events more
important in the calculation. The NRC recently used a similar update to evaluate
an event at the Salem plant in Region I.
To update the base model the following change sets were inserted:
- OEP-XHE-NOREC-ST set to a probability of 1.0
The result obtained was 6.84E-9/hr.
This result was further adjusted to account for the 0.6 non-recovery probability of
the EDG B fail-to-start events in SBO sequences 2 and 13. The total CDF of
these cutsets was 1.44E-10/hr. Therefore the adjusted base model result is:
- 6.84E-9/hr. - 1.44E-10/yr. (1 - 0.6) = 6.78E-9/hr.
To evaluate the risk associated with the performance deficiency, the following
change sets were applied:
- OEP-XHE-NOREC-ST set to a probability of 1.0
- EPS-DGN-FR-DG3A (Diesel Generator 3A-S Fails to Run) set to a
probability of 1.0
Enclosure
-30-
The result obtained was 2.62E-8/hr.
Adjustments were made to cutsets containing SBO sequences 2 and 13 with
either an EDG A FTR or EDG B FTS events, as follows:
SBO sequences 2 and 13 exclusively contain the basic event OEP-XHE-
NOREC-BD (Operators fail to recover AC power before battery depletion)
The recovery of both EDGs applies to the total CDF of cutsets containing OEP-
XHE-NOREC-BD and EPS-DGN-FS-DG3B (EDG B fails to start) and EPS-DGN-
FR-DG3A (Diesel Generator 3A-S Fails to Run) =1.23E-9/hr. Application of
0.1 non-recovery probability for EDG A and 0.6 non-recovery probability for
EDG B results in a total CDF reduction of 1.23E-9/hr. (1.0 - (0.1) (0.6)) = 1.16E-
9/hr.
The recovery of EDG A only applies to the total CDF of cutsets that contain
OEP-XHE-NOREC-BD and EPS-DGN-FR-DG3A (EDG A fails to run), excluding
the cutsets in the group above that contain EPS-DGN-FS-DG3B.
The total CDF of this group is 1.48E-8. Application of 0.1 non-recovery
probability for EDG A results in a total CDF reduction of 1.48E-8/hr. (1.0 - 0.1) =
1.33E-8/hr.
Therefore, the revised CDF for the evaluation case is:
- 2.62E-8/hr. - 1.16E-9/hr. - 1.33E-8/hr. = 1.17E-8/hr.
The change in frequency attributable to the performance deficiency is:
- 1.17E-8/hr. - 6.78E-9hr. = 4.92E-9/hr.
The exposure period of 27 days consists of 648 hours0.0075 days <br />0.18 hours <br />0.00107 weeks <br />2.46564e-4 months <br />. Therefore the delta CDF
of the performance deficiency is:
- 4.92E-9/hr. (648 hour0.0075 days <br />0.18 hours <br />0.00107 weeks <br />2.46564e-4 months <br />s/yr.) = 3.19E-6/yr.
Consideration of other periods of exposure
The analyst evaluated only the final 27 days of exposure when EDG A had only
approximately three hours of run time remaining. Some risk was also incurred
when the EDG had additional run time remaining. In Entergys evaluation the
percentage of the total calculated risk associated with the final 27-day exposure
period was 61.2%. The analyst adjusted the CDF result obtained above by this
percentage to approximate the risk incurred during the entire exposure period.
Enclosure
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Adjusted CDF = 3.19E-6/yr (1/0.612) = 5.21E-6/yr
External Initiators:
The analyst concluded that external initiators would have a negligible impact on
the final result.
High winds or other weather conditions that could cause a loss of offsite power
were included in the updated database used to estimate the LOOP frequency,
and equipment important to mitigating the consequences of these occurrences
are adequately protected from these events.
Seismic events at the plant are rare and of low magnitude, and the plant is
isolated by being situated on a floating island. A seismic event is not likely to
cause an earlier failure of the fuel line fitting because the entire skid would move
as a unit and would not be subjected to the differential stresses caused by the
vibrations of a running engine.
Internal flooding would not likely cause a loss of offsite power or failure of the
Train B EDG and would therefore have little impact on the analysis.
Fires that could cause a loss of offsite power were isolated to two fire areas, both
with frequencies more than two orders of magnitude less than the LOOP
frequency. A fire initiating in the Train A EDG room as a consequence of the
as-found fuel spill was very unlikely because of the lack of sufficient ignition
temperatures on surfaces exposed to the spill. Additionally, a fire in this room
would only affect the operation of the Train A EDG and would not impede
operator access to other mitigating system components. The room contained
automatic detection and suppression devices.
In summary, the overall effect of external initiators would be very small compared
to the internal result.
Large early release frequency:
The analyst reviewed the finding for impact on large early release using
Inspection Manual Chapter 0609, Appendix H. On a loss of power, all
containment isolation and purge valves fail closed. There existed no other
conditions involving containment integrity. Therefore LERF, though slightly
increased because of the increase in delta-CDF, was well below the E-7/yr.
threshold. This is because a release would have occurred only in the event of a
concurrent containment boundary failure.
Enclosure
-32-
Sensitivity Considerations:
If recovery of EDG A is not credited, the resulting delta CDF is 2.00E-5/yr. If
recovery is not credited for either EDG, the result is 2.05E-5/yr.
Conclusion:
The condition was of low to moderate safety significance (WHITE). If credit is
not applied for recovery of EDG A, the result is one of substantial safety
significance (YELLOW).
Enforcement. 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and
Drawings, states in part, that Activities affecting quality shall be prescribed by
documented instructions, procedures, or drawings, of a type appropriate to the
circumstances and shall be accomplished in accordance with these instructions,
procedures, or drawings. The failure to establish appropriate instructions and
accomplish those instructions for installation of the fuel line for Train A emergency diesel
generator resulting in the fuel line failure on September 29, 2003, is a violation of
10 CFR Part 50, Appendix B, Criterion V. Pending determination of the findings final
safety significance, this finding is identified as Apparent Violation (AV)05000382/2003007-05, Failure to establish appropriate instructions and implement
those instructions.
.2 (Closed) Licensee Event Report 50-382/2003-001-00: Loose Breaker Fuse Rendered
One Bank of Pressurizer Proportional Heaters Inoperable
On July 24, 2003, Entergy identified that a loose control power fuse for the Control
Element Drive Motor Generator Set B breaker rendered one bank of pressurizer
proportional heaters inoperable beyond the allowed outage time of Technical
Specification 3.4.3.1. This was determined to be a violation of Technical
Specification 3.4.3.1 (See section 40A7 for details). This finding is more than minor
because it had a credible impact on safety, in that if the redundant group of proportional
heaters did not function, reactor coolant system pressure control under natural
circulation conditions could not be ensured. This finding affects the Mitigating Systems
Cornerstone. Using the significance determination process, this issue was determined
to have a very low safety significance, since only one train of proportional heaters is
required to control reactor coolant system pressure under natural circulation conditions
and operators could manually align the heaters to their emergency power source locally
had the automatic transfer failed during a loss of normal power event. This issue was
entered into Entergys corrective action process as Condition
Report CR-WF3-3003-2076.
Enclosure
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.3 (Closed) Licensee Event Report 50-382/2003-003-00: Reactor Coolant System
Boundary Leakage Due to Primary Water Stress Corrosion Cracking
During Refueling Outage 12, Entergy identified three indications of reactor coolant
system pressure boundary leakage. The first indication was identified on
October 24, 2003, on the hot leg #2 instrument nozzle connected to instrument RC-IPT-
0106B. The other two indications of leakage were identified on October 26, 2003.
These indications were identified on pressurizer heater sleeves C-1 and C-3. This issue
is addressed in Section 4OA2.2 of this report.
4OA4 Crosscutting Aspects of Findings
Section 1R19 of the report describes a human performance crosscutting issue where
personnel failed to establish appropriate postmaintenance testing criteria following a
modification to the main steam isolation valve nitrogen actuating system.
Section 4OA3 of the report describes a human performance crosscutting issue where
maintenance personnel performed improper installation of the EDG Train A fuel oil line.
4OA5 Other Activities
.1 Reactor Pressure Vessel Head and Vessel Head penetration Nozzles (Temporary
Instruction 2515/150, Revision 2)
a. Inspection Scope
The inspectors verified that Entergys susceptibility ranking was high based on the
calculated effective degradation years being 16.95 years through Cycle 12. Entergy
used plant specific temperature data in their susceptibility ranking calculation.
The inspectors noted that examinations were performed by contract Westinghouse and
Entergy personnel. Contract personnel had been qualified using licensee qualification
procedures and all personnel had been qualified using procedures that satisfied
applicable requirements of SNT-TC-1A and ASME Section XI. Westinghouse personnel
performed eddy current testing and ultrasonic examinations. Entergy personnel
performed dye penetrant testing.
The reactor vessel had 102 penetrations (1 reactor head vent, 10 incore instrument
nozzles, and 91 control element drive mechanisms). Entergy performed dye penetrant,
ultrasonic, and eddy current examinations on the penetrations to identify flaws. The
reactor head vent was analyzed using eddy current testing. The control element drive
mechanisms were analyzed using ultrasonic testing. The incore instruments were
analyzed using a combination of eddy current testing, ultrasonic testing, and dye
penetrant testing. Entergy also performed a bare metal visual inspection of 83 vessel
head penetrations. A bare metal visual inspection of the remaining 19 could not be
performed due to concerns with damaging the head vent line. However, Entergy did
Enclosure
-34-
perform a complete inspection of the reactor vessel head using a boroscope. The
inspectors observed the accessible areas of the vessel head and observed selected
portions of the videotaped results of the boroscope data. No evidence of boric acid
leakage was noted.
The inspectors reviewed the results of the eddy current testing of the reactor head vent,
the results of 9 ultrasonic tests on control element drive mechanism, and results of eddy
current, dye penetrant, and ultrasonic tests of 2 incore instruments nozzles. All the
examinations were performed in accordance with approved procedures. The inspectors
reviewed testing results for incore Instrument Penetrations 94 and 98. No indications
were identified on incore Instrument Penetration 98. However, dye penetrant
examinations did identify a 1/2-inch rounded indication at the nozzle to toe weld of
Instrument Penetration 94. This indication exceeded the code criteria for allowable
indication size. This indication was removed mechanically. Additional indications were
also identified on incore Instrument Penetrations 92 and 93. Indications on Instrument
Penetration 92 were rounded 3/32-inch indications on the nozzle to weld toe. The
indication on Instrument Penetration 93 was a 3/16-inch linear indication at the nozzle to
weld toe. This indication exceeded the code criteria for allowable indication size. The
indications were also removed by mechanical removal. The indications were believed to
be weld flaws. No evidence of leakage was found. Followup examinations after repair
revealed no relevant indications. Entergy initiated Condition Report 2003-3307 based
on the results of the of the dye penetrant examinations.
The inspectors reviewed eddy current test results of the reactor head vent penetration
and control element driven mechanism (CEDM) Penetrations 18, 21, 30, 44, 52, 53, 56,
66, and 87. No indications or evidence of leakage were identified.
Entergy used ultrasonic examinations data to provide an assessment of leakage into the
interference fit zone. Guidance for performing this assessment was contained in
Procedure WDI-UT-013, CRDM/ICI UT Analysis Guidelines, Revision 3.
Entergy also performed visual inspections of the top of the cooling shroud. These
inspections were performed using a video camera and a boroscope. No indications of
boric acid buildup were noted.
The inspectors reviewed the approved relaxation requests from the NRC
Order EA-03-009, "Establishing Interim Inspection Requirements for Reactor Pressure
Vessel Heads at Pressurized Water Reactors."
- Relaxation request dated July 1, 2003, allowed Entergy to use eddy current
testing to inspect the vent line nozzle and J-groove weld instead of ultrasonic
testing. The relaxation was approved on October 2, 2003.
Enclosure
-35-
- Relaxation request dated September 15, 2003, allowed the control element drive
mechanism nozzles to be inspected using a three-step alternative involving an
analysis technique, ultrasonic testing, and augmented surface examination. This
request was approved November 12, 2003.
- Relaxation request dated October 24, 2003, allowed ultrasonic testing and
surface examinations of the incore instrument nozzles. This relaxation request
was approved on November 7, 2003.
b. Findings
No findings of significance were identified.
.2 Reactor Containment Sump Blockage (Temporary Instruction 2515/153, Revision 0)
a. Inspection Scope
On November 17, 2003, the inspectors completed a detailed walkdown of the safety
injection sump, drainage paths to the safety injection sump, and evaluated insulation
and material coatings used in containment that could contribute to sump blockage in a
postaccident scenario. The inspectors verified that the safety injection sump screen
was free of adverse gaps and breaches to prevent debris from entering the safety
injection system suction piping. The inspectors assessed Entergys containment foreign
material management control program and verified that Entergy maintained adequate
cleanliness standards to prevent debris transport that could lead to potential blockage of
the safety injection sumps screens. The safety injection sump design and the
containment drainage arrangement was assessed using applicable sections of the
Updated Final Safety Analysis Report, contractor test modeling of the safety injection
system sump and interviews with civil, mechanical, and system engineers. The
inspectors will complete the inspection of Entergys compensatory measures in
response to degraded containment sump performance following development of training
and procedures scheduled to be completed in April 2004.
b. Findings
No findings of significance were identified.
.3 (Closed URI 05000382/0310-01): Possibility of flooding both emergency diesel
generator fuel oil storage tank rooms in the event of a flood and subsequent loss of
offsite power.
a. Inspection Scope
As discussed in NRC Inspection Report 05000382/2003010 a potential finding was
identified in that both emergency diesel generators could be lost due to potential
flooding in the emergency diesel generator fuel oil storage tank rooms due to leaking
Enclosure
-36-
check valves installed in the industrial waste nonsafety-related drain systems connected
to the rooms. The inspectors reviewed Entergys analysis of this potential condition and
discussed the results of the analysis with the responsible system engineers.
b. Findings
No findings of significance were identified.
4OA6 Meetings
Exit Meeting Summary
On December 5, 2003, the inspector presented the ALARA Planning and Controls
inspection results to Mr. J. Venable, Site Vice-President and other members of his staff
who acknowledged the findings. The inspectors confirmed that proprietary information
was not provided or examined during the inspection. The inspector asked Entergy
whether any materials examined during the inspection should be considered proprietary.
No proprietary information was identified.
The inspectors presented the results of the inservice inspection effort to Mr. R. Fili,
Engineering Program Manager and other members of licensee management on
November 6, 2003. Entergy management acknowledged the inspection findings. The
inspectors asked Entergy whether any materials examined during the inspection should
be considered proprietary. Several documents were proprietary information as identified
by Entergy. The inspectors informed Entergy that these documents would be destroyed
upon completion of their review.
The resident inspectors presented the integrated inspection results to Mr. J. Venable,
Site Vice-President and other members of Entergy management at the conclusion of the
inspection on January 5, 2004. Entergy acknowledged the findings presented. The
inspectors asked Entergy whether any materials examined during the inspection should
be considered proprietary. No proprietary information was identified.
4OA7 Licensee Identified Violations
The following violation of very low safety significance (Green) was identified by Entergy
and is a violation of NRC requirements, which meets the criteria of Section VI of the
NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
Technical Specification 3.4.3.1 requires at least two groups of pressurizer proportional
heaters be operable. With one group of pressurizer proportional heaters inoperable,
Entergy must restore the other group within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
The proportional heaters remained inoperable for about 4 days while the unit was in
Mode 1. Entergy had failed to meet Technical Specification requirements. This issue
was determined to be more than minor because pressurizer proportional heaters help to
ensure the capability of systems that respond to initiating events and was of very low
Enclosure
-37-
safety significant because only one train of proportional heaters is required to control
reactor coolant system pressure under natural circulation conditions and operators could
manually align the heaters to their emergency power source locally had the automatic
transfer failed during a loss of normal power event. This violation is being treated as a
noncited violation, consistent with Section VI.A of the NRC Enforcement Policy. This
issue was entered into Entergys corrective action process as Condition
Report CR-WF3-3003-2076.
ATTACHMENT: SUPPLEMENTAL INFORMATION
Enclosure
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
S. Anders, Superintendent, Plant Security
T. Brumfield, Manager Quality Assurance
L. Dauzat, Supervisor, Radiation Protection
J. R. Douet, General Manager, Plant Operations
R. Fili, Engineering Program Manager
R. Fletcher, Operations Training Supervisor
C. Fugate, Assistant Manager, Operations
T. Gaudet, Director, Planning and Scheduling
B. Greeson, Code Program Supervisor, Arkansas Nuclear One
B. Houston, Manager, Radiation Protection
R. Jones, Simulator Support Supervisor
P. Kelly, Supervisor, Radiation Protection
C. Lambert, Director, Engineering
J. Laque, Manager, Maintenance
R. Murillo, Engineer, Licensing
R. Osborne, Manager, System Engineering
W. H. Pendergrass, Assistant Operations Manager (Support)
K. Peters, Director, Nuclear Safety Assurance/Emergency Preparedness
G. Pierce, Chemistry Superintendent
G. Scott, Engineer, Licensing
G. Sen, Manager, Licensing
T. E. Tankersley, Manager, Training
J. Venable, Vice President, Operations
K. T. Walsh, Manager, Operations
D. Weber, Codes Program Steam Generator Engineer
NRC
V. Gaddy, Senior Project Engineer, Region IV
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
05000382/2003007-01 NCV Inadequate Test Controls of MSIVs (Section 1R19)05000382/2003007-02 NCV Failure to barricade a high radiation area (Section 2OS1)05000382/2003007-03 NCV Ineffective Corrective Actions to Prevent Recurrence of
Voiding Conditions (Section 4OA2.1)05000382/2003007-04 NCV Ineffective Corrective Actions to Prevent Recurrence of
PWSCC of Alloy 600 material (Section 4OA2.2)
A-1 Attachment
05000382/2003007-05 AV Failure to establish appropriate instructions and
implement those instructions (Section 4OA3.1)
Closed
05000382/2003007-01 NCV Inadequate Test Controls of MSIVs (Section 1R19)05000382/2003007-02 NCV Failure to barricade a high radiation area (Section 2OS1)05000382/2003007-03 NCV Ineffective Corrective Actions to Prevent Recurrence of
Voiding Conditions (Section 4OA2.1)05000382/2003007-04 NCV Ineffective Corrective Actions to Prevent Recurrence of
PWSCC of Alloy 600 material (Section 4OA2.2)05000382/2003010-01 URI Possibility of flooding both emergency diesel generator
fuel oil storage tank rooms in the event of a flood and
subsequent loss of offsite power (Section 4OA5.3)
05000382/2003-001-00 LER Loose Breaker Fuse Rendered One Bank of Pressurizer
Proportional Heaters Inoperable (Section 4OA3.2)
05000382/2003-003-00 LER Reactor Coolant System Pressure Boundary Leakage
Due to Primary Water Stress Corrosion Cracking
(Section 4.OA3.3)
LIST OF DOCUMENTS REVIEWED
Procedures
DC-317, Entergy Steam Generator Administrative Procedure, Revision 1
NOECP-252, Steam Generator Eddy Current Inservice Testing, Revision 8
NOECP-257, Steam Generator Secondary Side Inspection, Revision 3
EPS-001-W, Steam Generator ECT Data Analysis For Waterford 3, Revision 1
QAP-393, Manual Ultrasonic Examination of Welds in Vessels, Revision 3
NDE 9.04, Ultrasonic Examination of Ferritic Piping for ASME Section XI, Revision 3
NDE 9.31, Magnetic Particle Examination (MT) for ASME Section XI, Revision 3
NDE 9.40, Liquid Penetrant Examination (PT), Revision 1
NDE 9.41, Liquid Penetrant Examination (PT) for ASME Section XI, Revision 1
Miscellaneous Documents
ER-W3-2003-0534-000, Steam Degradation Assessment and Repair Criteria for RF12
A-2 Attachment
Eddy Current Acquisition Technique Sheets
WTR-01-03
WTR-A-03
Procedures:
TQ-201, Systematic Approach to Training Process, Revision 1
TQ-202, Simulator Configuration Control, Revision 1
DG-TQ-201, Design and Development Phase, Revision 2
DG-TQ-201, Implementation Phase, Revision 1
DG-TQ-201, Evaluation Phase, Revision 3
DG-TRNW-001, Operator Training Simulator Deskguide, Revision 8
DG-TRNW-003, Operator Training Examination Development and Administration, Revision 6
TDG-SIM-003, Simulator Steady State and Transient Testing, Revision 1
TDG-SIM-016, Configuration Management, Revision 6
TDG-SIM-017, Conducting a Simulator Outage, Revision 1
Simulator Documents:
Simulator Fidelity Report for 2003
Annual Performance Testing Data for 2002
Transient data
Steady State data
Plant Data from Main Turbine Trip on 14 February 2003
Plant Data from Loss of 2B RCP in 1999
Core Performance Data
Miscellaneous:
Licensed operator annual/biennial examination development model
Licensed operator requal sample plan and two-year guide
Biennial exam testable subject matter
Training Review Group Meeting Minutes, June 4, 2002
Training Review Group Meeting Minutes, September 9, 2002
Training Review Group Meeting Minutes, January 7, 2003
Training Review Group Meeting Minutes, February 25, 2003
Training Review Group Meeting Minutes, June 3, 2003
Simulator Scenarios:
E-68
E-70
E-71
E-91
P-76
SRO-EP-EMERG-1
RO-CPC-NORM-11
RO-CS-EMERG-7
NAO-SDC-NORM
A-3 Attachment
NAO-CED-OFFNORM-2
RO-PPO-OFFNORM-5
Written Examinations:
WWEX-LOR-03061R
WWEX-LOR-03061S
WWEX-LOR-03062R
WWEX-LOR-03062S
Training Evaluation Reviews:
WLP-OPS-SAF00, 2/28/2002
WLP-OPS-REQ22, 2/25/02
WLP-LOR/AOR-REQ21, 2/26/02
WLP-LOR/PPO30, 5/29/02
WSEM-OPS-COACH, 2/28/02
WLP-LOR-LOG00; 8/22/02
WLP-TYH11; 7/8/02
WLP-LOR-PPO020; 5/29/02
WLP-LOR-TYR09; 5/29/02
WLP-LOR-PPE20; 7/1/02
WLP-OPS-CLR00; 2/28/02
WLP-OPS-SP00; 7/10/02
WLP-OPS-CED00; 5/7/03
WLP-LOR-PPO10, PPO40; 2/13/03
WLP-LOR-TYR08; 1/14/03
WLP-OPS-CLR; 7/29/03
WLP-OPS-TS04; 8/21/03
WLP-OPS-RF00; 8/26/03
WLP-OPS-COL; 7/10/03
WLP-OPS-IC01; 6/24/03
Operations Training Coaching Cards for Functional Recovery Procedure Usage:
30097
30119
30331
30353
30354
30808
30836
31068
31767
31800
Management Observation Cards for Technical Specification Recognition:
37335
37456
37496
37612
37614
A-4 Attachment
Procedures
Operating Procedure OP-901-521, "Severe Weather and Flooding," Revision 3
Surveillance Procedure OP-903-026, Emergency Core Cooling System Valve Lineup
Verification, Revision 12
Operating Instruction OI-004-000, Operation Shift Logs, Revision 28
Administrative Procedure UNT-007-059, Foreign Material Exclusion, Revision 2
Operating Procedure OP-901-521, "Severe Weather and Flooding," Revision 3
Surveillance Procedure STA-001-005, Leakage Testing of Air and Nitrogen Accumulators for
Safety Related Valves, Revision 6
Surveillance Procedure OP-903-119, Secondary Auxiliaries Quarterly IST Valve Tests,
Revision 7
Surveillance Procedure OP-903-027, Inspection of Containment, Revision 6
Administrative Procedure LI-102, Corrective Action Process, Revision 2
Corrective Action Documents
CR 2003-2076, CR 2003-2089, CR 2003-3858, CR 2003-3911, CR 2003-3901, CR 2003-3729,
CR 2002-0818, CR 1999-0167, CR 1998-1033, CR 2003-3837, CR 2003-3716, CR 2003-3884,
CR 2003-3839, CR 2003-3849, CR 2003-3204, CR 2003-3152, CR 2003-3763, CR 2003-3459,
CR 2003-3458, CR 2003-3536, CR 2003-2674, CR 2003-2900, CR 2003-0201,CR 2003-2615,
CR 2001-0135, CR 2003-0643, CR2003-2589, CR 2003-3515, CR 2003-3897, CR 2003-3379,
CR 2003-3523, CR 2003-3533, CR 2003-3400, CR 2003-3425, CR 2003-3142, CR 2003-3083,
CR 2003-3082, CR 2000-1250, CR 2003-3130, CR 2003-3110, CR 2003-2863, CR 2003-3508,
Other
Engineering Calculation EC-M88-024, Accumulator V, VIII, IX and X Calculation, Revision 3
Engineering Request ER-W3-97-547-00-01, Safety Function of Target Rock Solenoid Valves
and Pressure Regulating Valves in the SC3 Portion of the NG System, Revision 1
Design Engineering Procedure NOECP-451, Conducting Engineering Inspection of Reactor
Containment Building Protective Coatings
Program Section CEP-IST-001, Inservice Testing Plan, Revision 2
Engineering Request ER-W3-00-0890, MSIV Design Basis, Revision 2
A-5 Attachment
NRC Generic Letter 98-04, Potential for Degradation of the Emergency Core Cooling System
and the Containment Spray System After a Loss-Of -Coolant Accident Because of Construction
and Protective Coating Deficiencies and Foreign Material in Containment, dated July 14, 1998
Engineering Calculation EC-S96-012, Si Sump Water Volume and Boron Concentration for
TSP Calculation, Revision A
Engineering Calculation MN(Q)-6-35, Safety Injection System Sump and Screen, Revision 1
NEI 02-01, Condition Assessment Guidelines: Debris Sources Inside PWR Containment,
Revision 1
Engineering Calculation EC-M91-011, NPSH for Safeguard Pumps in Recirculation Mode with
Valve SI-106a(B) Failed Open, Revision 2
NRC Bulletin 2003-01, Potential Impact of Debris Blockade on Emergency Sump Recirculation
at Pressurized-Water Reactors, dated June 9, 2003
Western Canada Hydraulic Laboratories LTD, Model Testing of the Safety Injection System
Sump, dated June 1982
Information Notice 90-10, Primary Water Stress Corrosion Cracking (PWSCC) of INCONEL
600, dated February 23, 1990
Engineering Request ER-W3-99-01-0184-02-12, Weld Repair of Inconel Instrument Nozzles
on the Pressurizer, Revision 12
Work Order Package
31122, 50334786, 13532, 13531, 33801, 33381, 50285047, 32863, 19905, 28970
Condition Reports:
CR-WF3-2002-1806, CR-WF3-2002-1851, CR-WF3-2003-322, CR-WF3-2003-814,
CR-WF3-2003-1080, CR-WF3-2003-1290,CR-WF3-2003-1405, CR-WF3-2003-1426,
CR-WF3-2003-1521,CR-WF3-2003-1602, CR-WF3-2003-2268, and CR-WF3-2003-2607
Procedures:
UNT-001-016 Radiation Protection, Revision 1
RP-103 Access Control, Revision 2
RP-105 Radiation Work Permits, Revision 4
RP-108 Radiation Protection Posting, Revision 1
HP-001-107 High Radiation Area Access Control, Revision 16
Radiation Work Permits:
2003-1502 RCP 1B Seal Replacement
2003-1613 Replacement of Pressurizer Heaters
2003-1702 Reactor Disassembly
A-6 Attachment
Self-Assessment and Quality Assurance:
QS-2003-W3-002
QS-2003-W3-013
Radiation Work Permits
2003-1511 Steam Generator Primary Side Work
2003-1512 Steam Generator Secondary Side Work
2003-1600 Health Physics Surveys and Job Coverage
2003-1610 Erect/Dismantle Scaffolding in RCB
2003-1705 Reactor Re-Assembly
2003-1713 Work involving Non-Destructive Examination under Reactor Head Shield Frame
Procedures
RP-102 Radiological Control, Revision 3
RP-105 Radiation Work Permits, Revision 4
RP-109 Hot Spot Program, Revision 0
RP-110 ALARA Program, Revision 1
RP-205 Prenatal Monitoring, Revision 2
HP-001-101 ALARA Program Implementation, Revision 13
HP-001-114 Installation of Temporary Shielding, Revision 8
Condition Reports
2002-1616, 2002-1759, 2003-0396, 2003-0535, 2003-1853, 2003-1936, 2003-2211, 2003-
2989, 2003-3168, 2003-3253, 2003-3282, 2003-3286, 2003-3361, 2003-3405, 2003-3703,
2003-3718, and ECH-2003-0347
Self-Assessment and Quality Assurance
W3F3-2003-0012 Radiation Protection
W3F3-2003-133 RWP Revisions
QS-2002-W3-092 RWP/ALARA Radiation Practices
WT-ECH-2003-074 RF12 Radiation Protection Outage Readiness
Radiation Protection Assessment dated November 18-22, 2002
Procedures:
QAP-410, Reactor Vessel Head VT Examination (Alloy 600), Revision 2
MRS-SSP-1534, Reactor Vessel Head Penetration Inspection Tool Operation, Revision 0
WDI-STD-101, RVHI Vent Tube J-Weld Eddy Current Examination, Revision 2
A-7 Attachment
WDI-ET-003, IntraSpect Eddy Current Imaging Procedure for Inspection of Reactor Vessel
head Penetrations, Revision 5
WDI-ET-004, IntraSpect Eddy Current Analysis Guidelines for Inspection of Reactor Vessel
Head Penetrations, Revision 3
WDI-UT-010, IntraSpect Ultrasonic Procedure for Inspection of Reactor Vessel Head
Penetrations, Time of Flight, Longitudinal Wave & Shear Wave, Revision 6
WDI-UT-011, IntraSpect NDE Procedure for Inspection of Reactor Vessel Head Vent Tubes,
Revision 4
WDI-UT-013, CRDM.ICI Analysis Guidelines, Revision 3
WDI-STD-122, RVHI CEDM Bottom OD Inspection, Revision 0
WCAL-02, Pulser/Receiver Linerarity Procedure, Revision 2
Calculation:
ECM03-010, Calculation of RPV Head Effective Degradation Years
LIST OF ACRONYMS
NRC Nuclear Regulatory Commission
CFR Code of Federal Regulations
NRR Nuclear Reactor Regulation
MSIV main steam isolation valve
A-8 Attachment