ML030630314

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IR 05000346-02-013 and IR 05000346-02-014; on 09/03-11/08/02, and 09/23-11/13/02; Firstenergy Nuclear Operating Company; Davis-Besse Nuclear Power Station. System Health Assurance - Reports
ML030630314
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 02/26/2003
From: Grobe J
NRC/RGN-III
To: Myers L
FirstEnergy Nuclear Operating Co
References
FOIA/PA-2003-0376 IR-02-013, IR-02-014
Download: ML030630314 (106)


See also: IR 05000346/2002013

Text

February 26, 2003

Mr. Lew Myers

Chief Operating Officer

FirstEnergy Nuclear Operating Company

Davis-Besse Nuclear Power Station

5501 North State Route 2

Oak Harbor, OH 43449-9760

SUBJECT: DAVIS-BESSE NUCLEAR POWER STATION

NRC SPECIAL INSPECTION - SYSTEM HEALTH ASSURANCE - REPORTS

NO. 50-346/02-13(DRS) and 50-346/02-14(DRS)

Dear Mr. Myers:

On November 13, 2002, the NRC completed a special inspection at your Davis-Besse Nuclear

Power Station. This inspection reviewed your actions to resolve Restart Checklist Item No. 5.b,

associated with assuring the capability of safety significant structures, systems and components

to support safe and reliable plant operation. Specifically, this inspection focused on review of

activities as described in the Davis-Besse System Health Assurance Plan. The plan consisted

of three review programs: an Operational Readiness Review (ORR), a System Health

Readiness Review (SHRR), and a Latent Issues Review (LIR). Our inspection of this plan

included reviewing the plans and procedures for the ORR, SHRR, and LIR, monitoring the work

of the SHRR and LIR teams in-progress, monitoring Nuclear Oversight activities, attending

review board meetings, and reviewing Condition Reports generated by the teams as reviews

were conducted and discrepancies were identified. The inspectors also monitored training of

reviewers, conducted walkdowns of selected systems, examined emergent issues, reviewed

independent self-assessments of systems, and reviewed two SHRR reports. In addition, to

assess the quality of your staffs reviews, the NRC conducted an in-depth design and

performance capability review of the Service Water, High Pressure Injection, and 4160 Volt AC

Electrical Distribution systems. The enclosed reports document the findings of this special

inspection, which were discussed with you and other members of your staff during an exit

meeting on November 13, 2002.

Report No. 50-346/02-13(DRS) discusses the review of the plans, procedures, and

implementation of the System Health Assurance Plan. No violations of NRC rules or

regulations were identified. The inspectors concluded that the System Health Assurance Plan

was well-designed, plans and procedures were appropriate to the circumstances, the program

was rigorously implemented, and quality assurance review by the Nuclear Oversight

Department was adequate. At the close of the inspection, only two of the 36 anticipated review

reports had been completed. The inspectors reviewed the System Health Readiness Review

Report for the 125/250 Volt DC Electrical Distribution system and concluded that the review had

been performed acceptably.

L. Myers -2-

Report No. 50-346/02-14(DRS) discusses the in-depth design and performance capability

review of the Service Water, High Pressure Injection, and 4160 Volt Electrical Distribution

systems. The inspectors identified four findings, one with multiple examples, of very low safety

significance (Green) that were determined to involve violations of NRC requirements. The first

finding involved failure to complete Technical Specification surveillance requirement 4.2.5.H,

associated with High Pressure Injection pump flow following modifications that could alter

system flow characteristic. The second finding involved examples of failure to assure that

applicable regulatory requirements and the design basis for structures, systems, and

components were correctly translated into specifications, drawings, procedures, and

instructions related to a non-conservative TS value for the 90 percent degraded voltage relay, a

non-conservative relay setpoint calculation for the 59 percent undervoltage relay, an inadequate

analytical basis for the setpoint to swap the service water system discharge path, a lack of a

design basis analysis for containment isolation valve backup air supply accumulators, and

inadequate blowdown provisions for Containment Air Cooler backup air accumulators. The

third finding involved a service water surveillance test that did not use worst case values to

bound the design basis conditions. The fourth finding involved failure to take prompt corrective

actions for incorrect service water pump discharge check valve test acceptance criteria. In

addition, the inspectors identified seventeen issues where design control may have been

inadequate; however, at the close of the inspection, insufficient information was available to

draw a conclusion regarding the acceptability of these items which are identified as unresolved

items in the report. Additional analyses, in most cases by your staff, are necessary to generate

the information needed to resolve the issues.

Because of the very low safety significance of the findings and because these issues have

been entered into your corrective action program, the NRC is treating these issues as

Non-Cited Violations in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If

you deny these Non-Cited Violations, you should provide a response with a basis for your

denial, within 30 days of the date of this inspection report, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the

Regional Administrator, Region III; the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Davis-Besse Nuclear Power Station.

The results of our review of the Service Water system were consistent with your Latent Issues

Review and a corporate Nuclear Oversight self-assessment. All three efforts identified a

significant number of deficiencies in calculations, analyses, and testing which will require

resolution prior to restart. We are also aware that the Latent Issues Reviews on the component

cooling, emergency diesel, auxiliary feedwater, and reactor coolant systems identified similar

deficiencies. As a result of these findings, we have concluded that the Latent Issues Reviews

were performed in a manner sufficient to reasonably determine whether or not systems were

capable of performing their safety functions during future plant operation.

Because the majority of the System Health Assurance Plan reports were not ready for review

by the close of the inspection and because the findings of the Latent Issues Review program

dictate the need to expand the scope of system reviews, Restart Checklist item 5.b will remain

open and subject to continued inspection.

L. Myers -3-

In accordance with 10 CFR Part 2.790 of the NRCs "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

John A. Grobe, Chairman

Davis-Besse Oversight Panel

Docket No. 50-346

License No. NPF-3

Enclosures: 1. NRC Special Inspection Report

No. 50-346/02-13(DRS)

2. NRC Special Inspection Report

No. 50-346/02-14(DRS)

cc w/encls: B. Saunders, President - FENOC

Plant Manager

Manager - Regulatory Affairs

M. OReilly, FirstEnergy

Ohio State Liaison Officer

R. Owen, Ohio Department of Health

Public Utilities Commission of Ohio

President, Board of County Commissioners

Of Lucas County

President, Ottawa County Board of Commissioners

D. Lochbaum, Union of Concerned Scientists

L. Myers -3-

In accordance with 10 CFR Part 2.790 of the NRCs "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

John A. Grobe, Chairman

Davis-Besse Oversight Panel

Docket No. 50-346

License No. NPF-3

Enclosures: 1. NRC Special Inspection Report

No. 50-346/02-13(DRS)

2. NRC Special Inspection Report

No. 50-346/02-014(DRS)

cc w/encls: B. Saunders, President - FENOC

R. Fast, Plant Manager

Manager - Regulatory Affairs

M. OReilly, FirstEnergy

Ohio State Liaison Officer

R. Owen, Ohio Department of Health

Public Utilities Commission of Ohio

President, Board of County Commissioners

Of Lucas County

President, Ottawa County Board of Commissioners

D. Lochbaum, Union of Concerned Scientists

DOCUMENT NAME: G:DRS\ML030630314.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE RIII E RIII N RIII RIII

NAME MFarber:sd RGardner CLipa JGrobe

DATE 01/24/03 01/24/03 02/20/03 02/26/03

OFFICIAL RECORD COPY

L. Myers -4-

ADAMS Distribution:

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ENCLOSURE 1

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-346

License No: NPF-3

Report No: 50-346/02-013

Licensee: FirstEnergy Nuclear Operating Company

Facility: Davis-Besse Nuclear Power Station

Location: 5501 North State Route 2

Oak Harbor, OH 43449

Dates: September 3 through November 13, 2002

Inspectors: M. Farber, Senior Reactor Inspector

J. Jacobson, Senior Mechanical Engineer

G. Hausman, Senior Reactor Inspector

Approved by: Ronald N. Gardner, Chief

Electrical Engineering Branch

Division of Reactor Safety

SUMMARY OF FINDINGS

IR 05000346-02-013; FirstEnergy Nuclear Operating Company; on 09/03-11/08/02;

Davis-Besse Nuclear Power Station. System Health Assurance Plan Implementation Inspection

The report covers a special inspection, by three regional inspectors, of the Davis-Besse Nuclear

Power Station System Health Assurance Building Block. The NRCs program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649,

Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspector Identified Findings

None

B. Licensee Identified Findings

None

2

REPORT DETAILS

4. OTHER ACTIVITIES

4OA3 Event Follow-up (93812)

Background

On March 6, 2002, Davis-Besse personnel notified the NRC of degradation (corrosion)

of the reactor vessel head material adjacent to a control rod drive mechanism (CRDM)

nozzle. This condition was caused by coolant leakage and boric acid corrosion of the

head material induced by an undetected crack in the adjacent CRDM nozzle. The

degraded area covered in excess of 20 square inches where the low-alloy structural

steel was corroded away, leaving the thin stainless steel cladding layer. This condition

represented a loss of the reactor vessels pressure retaining design function, since the

cladding was not considered as pressure boundary material in the structural design of

the reactor pressure vessel. While the cladding did provide a pressure retaining

capability during reactor operations, the identified degradation represented an

unacceptable reduction in the margin of safety of one of the three principal fission

product barriers at the Davis-Besse Nuclear Power Station (reference NRC

report 50-346/02-03(DRS)).

The System Health Assurance (SHA) Plan is one of seven building blocks identified as

part of the licensees Return to Service Plan. The intent of the SHA plan was to review

plant systems prior to restart to ensure that these systems were in a condition that

would support safe and reliable information. The plan consisted of three review

programs: an Operational Readiness Review (ORR), a System Health Readiness

Review (SHRR), and a Latent Issues Review (LIR). NRC inspectors reviewed the

activities as described in the SHA plan. Given the high public interest in this subject

area at Davis Besse, and therefore the need to clearly communicate the rationale for

NRC staff conclusions regarding the effectiveness of licensee extent of condition

inspections, this report documents the inspectors observations.

a. Inspection Scope

The inspectors reviewed the plans and procedures for the ORR, SHRR, and LIR,

monitored the work of the SHRR and LIR teams in-progress, monitored Nuclear

Oversight activities, attended review board meetings, and reviewed Condition

Reports (CR) generated by the teams as reviews were conducted and discrepancies

were identified. The inspectors also monitored training of reviewers, conducted

walkdowns of selected systems, examined emergent issues, reviewed independent

self-assessments of systems, and reviewed two SHRR reports.

1

b. Observations and Findings

b.1 Operational Readiness Reviews

a. Introduction

The inspectors examined the Operational Readiness Review (ORR) program, CRs

issued as a result of the reviews, and the final ORR report.

b. Description

The licensee initiated the ORR program before the NRC implemented the Manual

Chapter 0350 process for Davis-Besse. The licensee developed this program to

ensure that selected systems and programs were in a condition that would support safe

and reliable plant operation through the forthcoming operating cycle (cycle 14) and

beyond. The ORR was initiated by the Plant Manager and consisted of a panel

composed of system engineers and representatives of other site organizations.

Forty-one systems and eight programs were selected for review, based on risk

significance, Maintenance Rule performance, materiel condition, and operator burden.

The ORRs were patterned on the licensees Quarterly System Health Report and

covered the selection criteria plus significant issues or corrective actions, mode

restraints, latent issues, and operating experience.

ORRs were nearly completed when the SHA plan was in development. The ORR was

incorporated into the SHA plan to ensure that all system review efforts were captured

under one program, that findings were retained and properly documented, and that

appropriate corrective actions were specified. After the reviews were completed, a

CR was generated by the Quality Assurance (QA) Department documenting concerns

with the administration and tracking of action items identified during the ORR.

Subsequently, a rigorous validation program for ORR was conducted to ensure that the

program was adequately documented, that new issues or changes were identified, and

that issues were entered into the corrective action program. Forty-two CRs were

generated which listed the issues and related outstanding corrective actions for

40 systems and two programs.

c. Observations and Findings

No findings were identified. The ORR was a proactive effort at system assessment.

The concept of a multi-disciplined panel consisting of management and supervisory

personnel reviewing the system engineers analysis of system condition was

well-conceived. While the system engineers analyses and panel reviews appeared

thorough, the project lacked rigor in the recording, tracking, and statusing of issues and

action items which were identified by the program. The QA condition report (02-02941)

noted that action items were not documented in CRs, that action items were overdue,

with no formal tracking mechanism to ensure completion, and that ORR action items

were not screened for inclusion in the Restart Action List. The subsequent validation

effort identified issues that were not evident in the original ORR. The validation effort

2

introduced the necessary rigor to the documentation process and resulted in a

complete, concise tabulation of issues.

b.2 System Health Readiness Reviews

a. Introduction

The inspectors reviewed the plans and procedures for SHRRs, reviewed the charters for

the various panels and boards established to oversee the SHA plan, monitored reviews

in progress, interviewed reviewers, examined scoping and testing memos, walked down

systems, observed meetings of the Engineering Assessment Board, Restart Station

Review Board, and Restart Senior Management Team, reviewed CRs that were related

to SHRRs, and examined emergent issues, i.e., issues not directly related to SHRR, but

identified as a result of walkdowns or examining SHRR documents.

b. Description

b.2.1 Procedure and Process

SHRRs were performed for 31 systems categorized as risk-significant under the

licensees Maintenance Rule program. The intent of SHRRs was to assess the

material condition of the systems and to determine whether process or programmatic

issues existed that could potentially have an adverse impact on system operability or

functionality. Five, more risk-significant systems were reviewed under the LIR program

which will be discussed later in this report. SHRRs were conducted using procedures

EN-DP-01503, System Walkdown, and EN-DP-01504, System Health Readiness

Review. Revisions to these procedures were issued during the course of reviews; these

revisions are listed at the end of this report.

The inspectors reviewed both procedures noted above, along with the charters for

the Engineering Assessment Board, Restart Safety Review Board, and Restart Senior

Management Team. EN-DP-01503, System Walkdown, provided a structured process

for conducting system walkdowns and recording deficiencies, and provided lists of

potential problems and conditions as criteria for identifying deficiencies. EN-DP-01504,

System Health Readiness Review, provided training requirements, documents to be

reviewed, a structure and process for defining the scope of the reviews, establishing the

testing necessary to support safety functions, selecting data sources and conducting

data source reviews, criteria and process for expanding the review scope, and

preparation, review, and approval of the final report.

c.2.1 Observations and Findings

No findings were identified. The inspectors determined that both procedures were

well-written, logical, complete, and appropriate to the circumstances. One minor

procedural problem was identified. The inspectors learned from interviews, CRs, and

schedule reviews, that walkdowns and document reviews were being conducted in

parallel with the development of the scoping and testing letters. There was no formal

mechanism in the SHRR procedure to ensure that changes mandated by EAB to either

3

the scoping or testing memoranda would be reflected back into the walkdowns or

document reviews. This resulted in the potential that approved changes might not be

completely reviewed. The licensee issued a procedure revision to address this issue.

No other problems were identified.

b.2.2 Training

Requirements for training SHA reviewers were specified in the SHRR procedure. This

training covered system design and licensing basis, site-specific databases, Generic

Letter 91-18 (Operability Determinations), the system walkdown procedure, FirstEnergy

Principles and Expectations, and the system health readiness review process.

The inspectors reviewed training records, met with instructors, and attended a training

session for reviewers.

c.2.2 Observations and Findings

No findings were identified. The inspectors considered the training provided for SHA

reviewers to be well-developed, adequately administered, and appropriate to the

circumstances. Training records were properly maintained, and documented the

training and qualification of all SHA reviewers. Through the combination of interviews

and attending training sessions, the inspectors determined that instructors were

qualified, knowledgeable of the SHA program, and well-prepared to lead the training

sessions.

During one training session, the inspector observed that several class members were

apparently disinterested and not paying attention. At the end of the session, when the

instructor was questioning the class to assess the level of retention, these individuals

were unable to answer the instructors questions. The inspector brought this to the

attention of licensee management. The class was subsequently retrained and tested to

ensure that training objectives were met.

b.2.3 System Walkdown

Complete system walkdowns, covering the entire scope of the system, were required

under the SHRR procedure. These were conducted using EN-DP-01503, System

Walkdowns. The walkdowns were led by the SHRR team leader, generally conducted

by the entire team, and deficiencies were identified on CRs. To assess the quality of

SHRR walkdowns, the inspectors conducted a plant-wide walkdown which included

SHRR and LIR systems. The intent was to compare inspector-identified deficiencies to

those of the walkdown team. The inspectors assessment of the quality of the walkdown

was based, in part, on the number and significance of discrepancies found by the

inspectors, but not by the teams. After the inspectors walkdown was completed, the

inspectors reviewed a sample of the CRs issued to assess the number and significance

of discrepancies identified by the walkdown teams.

4

c.2.3 Observations and Findings

No findings were identified. The inspectors identified a very small number of minor

discrepancies not identified by the SHRR walkdown teams; the licensee issued CRs to

document the inspectors observations.

Among the discrepancies was inconsistency in the lubrication of manually-operated

valves. The inspectors noted that for three identical manual valve operators, one

appeared to be over-greased, one appeared to be satisfactory, and one valve operator

did not have a grease fitting installed. This became an emergent issue which is

discussed in Section b.2.6 below. Another discrepancy was inconsistency in greasing of

seismic support struts. The inspectors noted that one seismic strut near a Component

Cooling Water pump was over-greased while the grease fittings on a nearby strut were

painted over. This became an emergent issue which is also discussed in Section b.2.6

below.

The inspectors concluded that the system walkdowns conducted by the licensee using

EN-DP-01503, System Walkdowns, were thorough and appropriate to the

circumstances. This conclusion was based on the following:

  • the number of deficiencies identified by the walkdown teams;
  • the inspectors did not identify any significant deficiencies missed by the licensee;

and

  • the number of deficiencies found by the inspectors, but not by the teams, was

very small.

b.2.4 Engineering Assessment Board (EAB)

The role of the EAB was defined in DBE-0001, Engineering Assessment Board

Role/Policy in Support of the Return to Service Plan. The EABs mission was to provide

senior level oversight and technical review of engineering products and processes.

EABs charter included:

  • assist site and engineering management with oversight of Return to Service

activities;

  • provide technical review of engineering products as requested by engineering

management;

  • review Return to Service Building Blocks;
  • ensure implementation of the FENOC Engineering Principles and Expectations;
  • provide qualitative assessment of products to identify engineering progress; and
  • provide feedback to engineering management and staff.

The inspectors reviewed DBE-0001 to understand the role EAB was expected to play,

interviewed the leadership and members of the EAB, examined EAB documented

reviews and comments on a large number of engineering products, and attended

several EAB meetings where SHA engineering products were reviewed.

5

c.2.4 Observations and Findings

No findings were identified. The inspectors determined that the EAB made significant

contributions to the quality of SHA engineering products. The EAB had several specific

responsibilities in both the SHRR and LIR programs. For brevity, EAB activities will only

be discussed in this section.

EAB responsibilities in the SHA included review and concurrence with:

  • scope, including the identified system boundaries, the selected components, and

justification for their selection;

  • identified testing or review of other information that assessed on a periodic

frequency, the systems risk significant maintenance rule functions;

  • recommendations for expanding the scope of review when problems are found;

and

  • final report to ensure the reviews complied with the procedure and were

complete, findings were adequately documented, and activities were in place to

address issues.

EAB membership was composed of very experienced consulting engineers; a large

percentage had in excess of 30 years of nuclear experience. EAB subcommittees were

established to oversee System Health, Program Review, and Management and Human

Performance. Early in the SHA program, through its review and comments on system

scope and boundaries, EAB established a high standard for completeness, accuracy,

and depth of detail. EAB members were provided engineering products which were

examined in detail. EAB then met with the author and the supervisor who presented the

product and responded to EAB questions and comments. In all the meetings that the

inspectors attended, EAB members were clearly well-prepared. Questions and

comments ranged from process to procedural to technical to philosophical; all were

in-depth, focused on the product, and challenging. The inspectors examination of

documented reviews of testing memos and completed reports showed that this level of

review and comment was consistent with all products.

b.2.5 Report Review

The inspectors reviewed the licensees completed System Health Readiness Review

Report for the 125/250 VDC System. The inspectors review was to verify that the

activities performed by the licensee during the SHRR reports preparation, review, and

approval were completed in accordance with EN-DP-01504, System Health Readiness

Review, Revision 2.

c.2.5 Observations and Findings

No findings were identified. However, the inspector identified two CRs that were

considered potential restart items, a fuse issue that may be generic to all electrical

systems, and several minor editorial errors.

6

The two CRs were CR 01-01232, Crack in Battery Post Seal Ring, dated June 22,

2001, and CR 02-00412, DC Voltage Drop Calculation, dated February 8, 2002.

  • Condition Report 01-01232 identified a broken battery post seal nut on cell 21 of

the 2P battery. The system engineer concurred that the CR should be changed

to a recommend for restart item because the 2P battery must be taken

out-of-service to complete the CRs corrective action. Since the 2P battery was

being disassembled during the current outage for corrosion product removal

(CR 02-03354), this outage would be the appropriate time to replace the broken

battery post seal nut.

  • Condition Report 02-00412, stated that DC Calculation C-EE-002.01.010 did not

adequately address small loads on the dc system. Based on the CR and SHRR

report, the inspectors could not conclude that this issue was not a restart item.

The system engineer concurred with the inspectors that the CR and the report

did not clearly indicate whether the issue involved an actual addition of loads to

the battery or was only concerned with the voltage drop of the circuits supplying

the small loads. Further review revealed that the issue involved voltage drops

and was properly classified.

The potential generic fuse issue was identified by CR 02-04586, SHRR: 1992 PCAQR

Corrective Action Not Yet Completed - Fuse Size, dated August 23, 2002, which was

identified as a recommend for restart item by the system engineer. This CR was

written following the 125/250 VDC SHRR walk-down, where several switches were

identified with a maintenance information tag (sticker) stating PCAQR 92-0030. The

PCAQR addressed several circuits throughout the plant where the installed fuse did not

match that specified by drawing E-2014. Drawing E-2014 was the licensees controlled

fuse drawing. All the fuses identified by the 1992 PCAQR were evaluated and

determined to be acceptable for continued operation with the understanding that the

fuses would be replaced upon fuse failure with the correct fuse. However, the E-2014

drawing was not annotated to identify that upon fuse failure the fuse was to be replaced

per the PCAQR. The inspectors were concerned that this issue may be generic to all

electrical systems and not just the 125/250 VDC system. The system engineer

concurred with the inspectors that the PCAQR identified fuses in other plant systems

that should be replaced and that he would ensure that the other affected systems

system engineer would be made aware of this issue.

Subsequent to the NRC inspectors inspection, the 125/250 VDC system engineer

issued Milestone #14-1, System Health Readiness Review for 125/250 VDC System,

Amendment 2, Revision 00, dated November 14, 2002, which resolved the inspectors

concerns identified above.

It was the intent of this inspection to review five completed SHRR reports. At the close

of this inspection, two reports had been issued. One of those was discussed above.

The inspectors will return to examine four additional reports when all 31 have been

formally completed; results of that inspection will be documented in a separate

inspection report.

7

b.2.6 Emergent Issues

Issues, not directly related to SHA, but needing licensee attention, were identified

throughout the course of the inspection as inspectors walked down systems, reviewed

condition reports, interviewed licensee staff, or examined other system health

documents. The inspectors monitored the licensees response to these issues to gain

insights on the licensees ability to understand the issue, determine the extent of

condition, assess significance, and identify and implement appropriate corrective

actions.

c.2.6 Observations and Findings

During the plant-wide walkdown, the inspectors noted inconsistencies in lubrication of

identical manual valve operators. A CR was issued and the licensee staff began to

examine the issue. In discussions with the staff, it was revealed that although the need

had been recognized, the station had no program for consistent maintenance of critical

manual valves. The licensees staff committed to develop such a program. During a

review of Condition Report 02-02397, the inspector noted in the description of the

condition, that the station had no preventive maintenance program for molded-case

circuit breakers. In discussions with the staff, it was revealed that the need had been

recognized, but the program had not been developed or implemented. The licensee

staff indicated plans to develop such a program. With these two issues as background,

the inspectors questioned the extent of component-based reliability or maintenance

programs and learned that the station only had a very small number. Further

discussions with the licensees staff revealed that an October 1999 self-assessment had

revealed this condition and recommended the establishment of component-based

programs. No action appeared to have been taken. This concern was presented to

licensee management, who acknowledged the concern and directed that a CR,

documenting the lack of response to the 1999 self-assessment, be issued. Resolution

of CR 02-08742 was in progress at the close of the inspection.

During the plant-wide walkdown, the inspectors identified inconsistencies in lubrication

of seismic support struts. A CR was issued and the licensee evaluated the condition.

The licensee identified that all the seismic supports supplied to the plant during

construction used a dry-film lubricant, intended to last for the life of the plant. Greasing

was unnecessary but if the strut was greased, it would then need periodic regreasing.

The licensee was unable to determine when the strut had been greased or if it had been

regreased. A condition report was issued to conduct an extent of condition and to

evaluate operability impacts of greasing and then failing to regrease these struts.

Resolution of CR 02-06765 was in progress at the close of the inspection.

During review of the licensees self-assessment conducted on the High Pressure

Injection (HPI) system, the inspectors examined a table of late commitments.

Commitment 10752, dated November 21, 1979, to submit information on HPI protection

against deadheading during a small-break loss-of-coolant accident, was listed as

pending. The licensee acknowledged that the commitment tracking system was

problematic and in need of corrective action. In response to the inspectors technical

questions on this issue, the licensee staff assembled a closure package which consisted

8

of the November 21, 1979 NRC letter requesting information on the topic, the

licensees December 28, 1979 response, and procedures involving HPI operation.

The licensees December 1979 letter did not properly address the issue of HPI

deadheading during small-break loss-of-coolant accident. Two of the procedures were

for Integrated Leak Rate Test and contained steps for leaving the HPI recirculation

valves open during the test. The current HPI operating procedure, included in the

package, contained a caution that during HPI operation taking suction on the

containment sump, the recirculation valves must be closed. This is exactly the

alignment which could lead to deadheading the HPI pumps during a protracted

small-break loss-of-coolant accident. None of the information in the closure package

properly addressed the issue. The inspectors expressed their concerns to management

regarding this inadequate response. The NRC team inspection, documented in

Inspection Report 50-346/2002014, independently raised questions about deadheading

the HPI pumps during a small-break loss-of-coolant accident. Consequently, the

licensees analysis, generated as a result of the team inspection, will address the

technical issue.

b.3 Latent Issues Reviews

a. Introduction

The inspectors reviewed the plans and procedures for LIRs, monitored reviews in

progress, interviewed reviewers, examined scoping and testing memos, walked down

systems, reviewed CRs issued that were related to LIRs, and examined emergent

issues, i.e., issues not directly related to LIR, but identified as a result of walkdowns or

examining LIR documents. LIRs were conducted on the Reactor Coolant, Auxiliary

Feedwater, Component Cooling, Emergency Diesel Generator, and Service Water

systems.

b. Description

b.3.1 Procedure and Process

LIRs were performed for five systems listed above, all of which were categorized as

risk-significant under the licensees Maintenance Rule program. The intent of LIRs,

as stated in the System Health Assurance Plan, was to provide reasonable

assurance that five systems could perform their safety and accident mitigation

functions. LIRs were conducted using procedures EN-DP-01503, System Walkdown,

and EN-DP-01505, Latent Issues Review. Revisions to these procedures were issued

during the course of reviews; these revisions are listed at the end of this report.

The inspectors reviewed both procedures noted above. EN-DP-01503, System

Walkdown, provided a structured process for conducting system walkdowns and

recording deficiencies, and provided lists of potential problems and conditions as criteria

for identifying deficiencies. EN-DP-01505, Latent Issues Review, provided training

requirements, documents to be reviewed, a structure and process for defining the scope

of the reviews, establishing the testing necessary to support safety functions, selecting

data sources and conducting data source reviews, criteria and process for expanding

9

the review scope, and preparation, review, and approval of the final report. These are

identical to the SHRR; however, the LIR went into greater detail, included a greater span

of data sources, and contained design basis inspection attributes that the SHRR did not.

The LIR was also more tightly structured to ensure consistency of review across the five

systems.

c.3.1 Observations and Findings

No findings were identified. The inspectors determined that both procedures were

well-written, logical, complete, and appropriate to the circumstances. The LIR

procedure had the same minor procedural problem as the SHRR procedure, in that

there was no formal mechanism in the LIR procedure to ensure that changes mandated

by EAB to either the scoping or testing memoranda would be reflected back into the

walkdowns or document reviews. As with the SHRR procedure, this was addressed in a

procedure revision.

b.3.2 Team Leader Meeting

The licensee held a weekly meeting with LIR team leaders to review progress, discuss

review approaches, identify common issues, and resolve problems. The inspectors

attended one meeting.

c.3.2 Observations and Findings

The meeting was attended by all team leaders, assistant team leaders, system health

assurance supervisors, and engineering management. The meeting was well organized

and conducted; there was a prepared agenda which was followed. There was a good

exchange of information, team leaders and supervisors spoke frankly about progress,

problems, and emerging issues.

b.3.3 System Walkdown

The inspectors performed a walkdown of the auxiliary feedwater system and

reviewed the results of the licensees previous walkdown efforts. The purpose of

the walkdown was to assess the physical condition of the system and verify the

quality and thoroughness of the licensees previous efforts. The licensees procedure

EN-DP-01503, Revision 2, System Walkdowns, was reviewed prior to the walkdown.

c.3.3 Observations and Findings

Overall, the licensees walkdown efforts were found to be effective. The materiel

condition of the auxiliary feedwater system appeared to have issues which required

corrective actions.

The System Walkdowns procedure provided reasonable guidance for identifying any

materiel degradations and cleanliness deficiencies in the system. The licensees

walkdown efforts identified numerous issues, especially in the areas of environmental

qualification and high energy line break. The inspector identified three conditions

10

adverse to quality which had not been previously identified by the licensees effort:

Fitting leakage and boric acid build up was found on tubing from CW-275J and sample

cooler S6B2. The licensee issued condition report CR 02-06268 to document the

leakage. Fluid leakage from a hydraulic snubber near orifice AF-4630 was noted. The

licensee issued condition report CR 02-06273 to document the leakage. Bearing lube

oil supply and return lines were found rubbing together on auxiliary feedpump 1-1. The

licensee issued condition report CR 02-06274 to document this condition.

b.3.4 Emergent Issues

As the LIRs progressed, the licensee began to analyze and trend the CRs that were

being written. This collective significance review was expanded to include

self-assessment results, EAB program reviews, SHRR issues, and the NRC team

inspection. The collective significance review revealed a number of problem areas

common to all five of the LIRs. Among these problem areas were design basis

validation, environmental qualification, high energy line break, missing or flawed

calculations, calculation control, accident analysis, system descriptions, and

configuration management.

The identification of these common problem areas resulted in the recognition by

licensee management that the scope of the SHA needed to be expanded. The

inspectors reviewed the CRs issued as a result of the collective significance review,

examined the list of common problem areas and the underlying data, and met

repeatedly with SHA staff to monitor the status of the review and development of

expansion plans.

c.3.4 Observations and Findings

No findings were identified. The licensee examined several expansion plan methods for

feasibility, effectiveness, efficiency, scope, and depth of review. At the close of this

inspection, a final plan had not been adopted. The inspectors will continue to monitor

the licensees progress on this issue.

One of the proposed expansion methods involved use of the Design Basis Document

Validation Program (DBDVP), which the licensee had committed to complete in

response to the NRCs October 1996 10 CFR 50.54.f letter on adequacy and availability

of design bases information. The licensee compared deficiencies identified during the

LIR to those identified during the DBDVP. The expectation was that if there was good

correlation on findings between the two programs, then the findings of the DBDVP

would be used as the basis for expansion. The licensees examination of the DBDVP

concluded that there was insufficient correlation between the two programs to support

using DBDVP for expansion plans. In addition, the licensees review identified problems

with the DBDVP; the program had not been completed and a portion of the deficiencies

identified had not been properly corrected.

The inspectors reviewed all of the related correspondence, the DBDVP instruction, the

Design Basis Validation Report of the Service Water System, and the Service Water

System Description. The inspectors also interviewed licensee staff members who had

11

been involved with the project. The project, though a commitment to NRC in response

to the 10 CFR 50.54.f letter, was delayed about two years due to engineering resource

considerations. The licensee, on recognizing that station resources would remain a

restraint, elected to contract for the reports. Two engineering organizations were

contracted to prepare the validation reports and work on the project was commenced.

From all of the systems validated, there were slightly more than 1000 identified

deficiencies. These were characterized as either high, medium, or low significance

and work was initiated to correct them. At the close of this inspection, approximately

200 deficiencies had not been corrected. The inspectors reviewed the deficiency

tracking list and open item log sheets for the service water and found where the

resolution of an issue assigned a high significance rating was inadequate. The issue

concerned rated flow in the service water system description that didnt include all

possible flows. The prescribed resolution for this deficiency was that it was to be

corrected in the system description. It failed to recognize that the analyses related to

rated service water flow or using rated service water flow needed to be examined. This

deficiency was noted by both the LIR team and the NRC team inspection. As corrective

action, the licensee plans to:

  • establish an event time line of identified deficiencies and opportunities to improve

design information availability and adequacy;

  • identify why the DBDVP was not completed;
  • confirm that the DBDVP discovery phase was adequate; and
  • evaluate why the DBDVP and other, prior programs and activities did not resolve

the identified discrepancies.

b.3.5 Report Review

Planning for this inspection included a detailed review of all five LIRs. This was

considered an import review effort because these were the most in-depth of all the

licensees reviews and conclusions drawn on the quality of the LIRs would be an

important considered in assessing the over quality of the SHA effort .

c.3.5 Observations and Findings

At the close of this inspection, none of the LIR reports had been reviewed or approved

by licensee management and were therefore unavailable for inspection. The inspectors

will return to examine these reports when they have been formally completed; results of

that inspection will be documented in a separate inspection report.

b.4 Quality Assessment Oversight

a. Introduction

During development of the Restart Action Plan and the related seven building blocks,

licensee management recognized the necessity of quality assurance oversight

throughout the process. Consequently, as the building block plans were being

developed, the Nuclear Quality Assessment (NQA) organization prepared a plan for

oversight of restart activities. The plan, entitled Nuclear Quality Assessment Oversight

12

of Davis-Besse Return to Service Plan, Revision 1, was approved by the Vice President

of FirstEnergy Oversight on July 22, 2002. The stated mission was to provide oversight

and verify the adequacy of activities conducted as part of the Return to Service Plan.

For each of the seven building blocks, the NQA plan contained specific objectives to be

accomplished through monitoring and assessment of key activities. The inspectors

reviewed the NQA oversight plan, met periodically with NQA staff and management,

reviewed Quality Field Observations (QFO), reviewed CRs written by NQA staff, and

reviewed the three independent system reviews performed by the NQA staff.

b. Description

b.4.1 Planning

To meet the objectives spelled out in the oversight plan, the NQA staff developed a

comprehensive program of review and monitoring during the development and

implementation of SHA processes. The program included review of training, attendance

at ORR, EAB, Restart Safety Review Board, and Restart Senior Management Team

meetings, in-line review and comment for SHRR and LIR inspection plan and procedure

development, assessment of scope and testing for SHRR and LIR, oversight of

walkdowns, independent system health readiness reviews conducted in accordance with

the SHRR procedure, and a comparison between the SHRR team and NQA results for

the selected system.

c.4.1 Observations and Findings

No findings were identified. The inspectors determined that NQA had developed a

comprehensive oversight program to assess the implementation of the SHA plan.

During initial discussion with NQA staff and management, the inspectors recognized

that while there was a provision for generation of a quarterly roll-up of QFOs, NQA had

not established how the comprehensive results of monitoring and reviews of SHA

implementation would be documented for presentation to senior licensee management.

After deliberation, NQA management elected to prepare a complete roll-up report of

assessment activities, findings and observations, and conclusions after the SHA

programs were completed. The inspectors considered this acceptable.

b.4.2 Monitoring

The NQA plan directed frequent monitoring of walkdowns, briefings, LIR and SHRR

team meetings, and review boards. These activities were documented through issuance

of QFOs, in accordance with NOP-LP-2004, Internal Assessment Process, and

issuance of CRs in accordance with NOP-LP-2001, Condition Report Process.

c.4.2 Observations and Findings

The inspectors review of CRs and QFOs confirmed the frequency and depth of NQA

involvement in process and procedure development; NQA comments and concerns

strengthened the review programs.

13

b.4.3 Independent System Review

The NQA plan for oversight directed the independent performance of three SHRRs

using EN-DP-01504, System Health Readiness Reviews. These independent reviews

were to be conducted by NQA staff and the results compared to the findings of the

SHRR teams for the selected systems, which were 125/250VDC Electrical Distribution,

Station and Instrument Air, and Decay Heat Removal/Low Pressure Injection. The

inspectors reviewed the reports of the three independently performed reviews and the

comparative analysis for the 125/250VDC Electrical Distribution system, which was

issued as a QFO.

c.4.3 Observations and Findings

No findings were identified. The inspectors found that the independent reviews had

been conducted in accordance with the SHRR procedure. The inspectors determined

that the findings between the two reviews were essentially similar; this was borne out by

the review of the comparative analysis.

b.5 Self-Assessment

a. Introduction

After being informed that the HPI, 4160VAC Electrical Distribution, and Service

Water systems had been selected for examination by the NRC design team inspection

(Inspection Report 50-346/02-14(DRS)), the licensee elected to perform

self-assessments of the three systems. NRC encourages licensees to perform

self-assessments as a means of identifying and correcting their own issues.

b. Description

The licensee conducted the self-assessments under the guidance of the FENOC

Focused Self-Assessment Guideline, Revision 0, issued December 2001. Each

system was reviewed by a separate team led by a member of the licensees staff,

and composed of licensee and consultant engineers. As is typical of these types of

self-assessments, the licensee used NRC Inspection Procedure 71111.21, Safety

System Design and Performance Capability, to conduct the system reviews.

c. Findings and Observations

No findings were identified. The inspectors reviewed the Focused Self-Assessment

Guideline, the staffing of the three review teams, and the completed reports for all three

systems. The reports were thorough and identified some significant issues with each of

the three systems.

14

4OA6 Management Meetings

Exit Meeting Summary

The inspectors presented the inspection results to Mr. L. Myers and other members of

licensee management and staff at the conclusion of the inspection on November 13,

2002. The licensee acknowledged the information presented.

15

KEY POINTS OF CONTACT

DAVIS-BESSE

D. Baker, Life Cycle Management (A) Manager

R. Cooper, Consultant

R. Fast, Plant Manager

J. Grabnar, Design Basis Engineering Manager

E. Grindahl, Quality Assurance

D. Gudger, Learning Organization Manager

D. Haskins, Human Resources Manager

S. Loehlein, Quality Assurance Manager

E. Matranga, Plant Engineering

P. McCloskey, Regulatory Affairs Manager

D. Miller, Compliance Supervisor

G. Mountain, Licensing Engineer

L. Myers, Chief Operating Officer

L. Pearce, Vice President, Oversight

J. Powers, Engineering Director

P. Roberts, Maintenance Manager

M. Roder, Operations Manager

J. Rogers, Plant Engineering Manager

C. Price, Business Manager

R. Schrauder, Services Director

B. Saunders, President, FENOC

L. Thornsberry, Plant Engineering

S. Wise, Operations Superintendent

NUCLEAR REGULATORY COMMISSION

J. Grobe, Chairman, Davis-Besse Oversight Panel

C. Lipa, Chief, Reactor Projects Branch 4

S. Thomas, Senior Resident Inspector

16

LIST OF ACRONYMS USED

AIT Augmented Inspection Team

CR Condition Report

CRDM Control Rod Drive Mechanism

DBDVP Design Basis Document Validation Program

EAB Engineering Assessment Board

HPI High Pressure Injection

LIR Latent Issues Review

NQA Nuclear Quality Assessment

NRC Nuclear Regulatory Commission

ORR Operational Readiness Review

PCAQR Potential Conditions Adverse to Quality Report

PDR Public Document Room

QA Quality Assurance

SHA System Health Assurance

SHRR System Health Readiness Review

URI Unresolved Item

17

LIST OF DOCUMENTS REVIEWED

The following is a list of licensee documents reviewed during the inspection, including

documents prepared by others for the licensee. Inclusion on this list does not imply that NRC

inspectors reviewed the documents in their entirety, but that selected sections or portions of the

documents were evaluated as part of the overall inspection effort. Inclusion on this list does not

imply NRC acceptance of the document, unless specifically stated in the inspection report.

Procedures

EN-DP-01503 System Walkdown, Revision 02, August 10, 2002

EN-DP-01504 System Health Readiness Review, Revision 00, August 21, 2002

EN-DP-01504 System Health Readiness Review, Revision 02, October 16, 2002

EN-DP-01505 Latent Issues Reviews, Revision 00, September 3, 2002

EN-DP-01505 Latent Issues Reviews, Revision 03, October 8, 2002

EN-DP-01506 Borated Water System Inspections (Outside Containment), September 3,

2002

DBE-0001 Engineering Assessment Board Role/Policy in Support of the Return to

Service Plan, Revision 0, June 28, 2002

NG-EN-00324 Boric Acid Corrosion Control, July 20, 2002

NG-VP-00100 Restart Action Plan Process, Revision 01, August 23, 2002

NG-VP-00100 Restart Action Plan Process, Revision 02, August 23, 2002

NOP-ER-2001 Boric Acid Corrosion Control Program, July 20, 2002

NOP-LP-2001 Condition Report Process, Revision 1,

System Health Readiness Review Scoping Memos

Steam Feed Rupture Control System Scope Memo, September 19, 2002

125/250 VDC System Scope Memo, August 26, 2002

High Pressure Injection System Scope Memo, September 16, 2002

Anticipatory Reactor Trip System Scope Memo, September 11, 2002

EDG Ventilation System Scope Memo, September 20, 2002

Condition Reports Generated from Inspection

02-05578 LIR Training Effectiveness

02-06565 SHRR LIR Review of Change Initiating Documents

02-06261 SHRR Boron Identified on CS17 Packing Area

02-06621 SHRR LIR Reviews Initiated before Scoping Approved

02-06723 SHRR LIR NRC Concern regarding Sites Lubrication

02-06765 Sway Strut Bushing Grease Fittings, September 26, 2002

02-07011 SHRR LIR NRC Concerns about System Review Scoping

02-07869 NRC Inspectors Concern Regarding Supervisor Comment for CR, October 11,

2002

02-08432 Containment Design Basis Calculation, October 21, 2002

02-08742 Inadequate Followup to Self Assessment 1999-0076, October 28, 2002

02-09036 Greasing of Struts, November 5, 2002

18

Condition Reports (CR)

02-02397 IPR: Breaker Reliability Program, May 31, 2002

02-03157 HELB in Turbine Building Effects on AFP Rooms, July 11, 2002

02-03369 Quality Expectations, July 17, 2002

02-03828 SHRR: ARTS Walkdown Findings from 8-7-02 for PSL4535A, B, C, D, August 7,

2002

02-03895 LIR-EDG-Two Instrument Tubing Lines Damaged, August 7, 2002

02-03923 SHRR Walkdown DH Train 1 DW143 Demin Water Valve Leakby, August 9,

2002

02-03925 SHRR Walkdown Decay Heat Train 1 Cooler Room - Scaffold Pole, August 9,

2002 02-02941 Operational Readiness Review Action Items, July 2, 2002

02-04021 SHRR Walkdown Finding During Containment System Walkdown, August 11,

2002

02-04041 SHRR Walkdown Items - RPS CTMT Press SW Sensing Line Guard, August 8,

2002

02-04033 Failure to Process Condition Reports through SRO Review in a Timely Manner,

August 12, 2002

02-04047 SHRR Walkdown Items - Outboard Electrical Penetration Cabinet Generic

Issues, August 9, 2002

02-04085 LIR-EDG - EDG 1 Air Intake Filter Can Use Paint to Overcoat Rusting,

August 11, 2002

02-04198 LIR-EDG 1 - Elec Maintenance Tag on Hand Switch (C3617), August 12, 2002

02-04473 SHRR - I&C Comment Regarding Test Points during Walkdown, August 13,

2002

02-04501 LIR - EDG 2 Cable Pull Wire Left in Place, August 17, 2002

02-04521 LIR - EDG 2 Panel C3616 Test Switch TS-3 Plastic Cover Broken, August 17,

2002

02-04543 SHRR: Battery Room 2 Deficiencies, August 20, 2002

02-04546 SHRR: Interlock for DC Panel Supply Breakers, August 20, 2002

02-04572 LIR-EDG-DO119 Piping Needs to be Cleaned and Painted, August 16, 2002

02-04578 LIR-EDG-EDG1-2 Day Tank Room Needs General Clean & Painting All Equip &

Floor, August 16, 2002

02-04581 LIR-EDG-HISNP 1951A Switch Label is Missing, Label Start/Stop, August 16,

2002

02-04635 LIR-Emergency Diesel Generator 1-2, August 17, 2002

02-04782 Potential Omission of LCO for Delay Time of Fuel Movement to Spent Fuel Pool,

August 22, 2002

02-04812 LIR CCW - Lack of Identification Tags on Instrumentation Valves, August 22,

2002

02-05066 LIR-AFW-ST138, August 23, 2002

02-05092 LIR-AFW-Service Water valve SW6392, August 23, 2002

02-05101 ORR - System Condition Report for Steam Feed Rupture Control System,

August 27, 2002

02-05103 ORR - System Condition Report for Condensate System, August 26, 2002

02-05125 ORR - System Condition Report for Non-nuclear Instrumentation, August 19,

2002

19

02-05132 ORR - System Condition Report for Integrated Control System, August 19, 2002

02-05135 ORR - System Condition Report for RPS, DSS, and NI, August 19, 2002

02-05137 ORR - System Condition Report for Decay Heat Removal/LPI System,

August 28, 2002

02-05138 ORR - System Condition Report for Radiation Monitoring System, August 27,

2002

02-05140 ORR - System Condition Report for Switchyard and Transformers, August 24,

2002

02-05141 ORR - System Condition Report for Main Feedwater Pumps/Turbines/Piping

System, August 26, 2002

02-05143 ORR - System Condition Report for 125/250 VDC System, August 17, 2002

02-05144 ORR - System Condition Report for Main Steam System, August 26, 2002

02-05146 ORR - System Condition Report for Anticipatory Reactor Trip System,

August 15, 2002

02-05147 LIR Design Basis Recovery, August 28, 2002

02-05149 ORR - System Condition Report for Motor Driven Feedwater Pumps, August 26,

2002

02-05150 ORR - System Condition Report for Emergency Diesel Generator, August 21,

2002

02-05157 BWST Level Shift Log Acceptance Criteria May Not Meet TS 3.5.4.A

Requirements, August 28, 2002

02-05191 SHRR: 480VAC MCC & MCCB Maintenance Issues, August 28, 2002

02-05408 SHRR: Testing Review - Trip Alarm Excluded from RPS Procedures,

September 4, 2002

02-05409 SHRR: Testing Review-Not Verifying Ch Trip Light on Reactor Trip Module,

September 4, 2002

02-06040 Issues Identified during SHRR Final Report Presentation, September 14, 2002

02-06259 SHRR LIR System Health Assurance Reviews, September 19, 2002

02-06313 LIR - EDG Exciter/Voltage Regulator PM May Not be Adequate, September 20,

2002

02-06398 Some Safety-Related Breakers Lacking Pms, September 20, 2002

02-06436 SSDPC Collective Significance of Issues from SW Self Assessment and LIR,

September 21, 2002

02-06582 LIR-RCS: 273R11 Does Not Reflect the As-Built Plant Configuration,

September 24, 2002

02-06770 LIR-AFW-CR 95-0703 Action to Prevent Recurrence Missing, September 26,

2002

02-06819 Inaccurate Input Provided by Contractor for NRC Correspondence,

September 26, 2002

Correspondence

Log 4928 Ltr: James M. Taylor to R. J. Farling, Request for Information Pursuant to 10

CFR 50.54(f) Regarding Adequacy and Availability of Design Bases Information,

October 9, 1996

Log 4954 Memo: Ledyard B. Marsh, Meeting with NEI and Licensees to Discuss Generic

Letter (GL) 96-06, Assurance of Equipment Operability and Containment

Integrity during Design-Basis Accident Conditions, November 22, 1996

20

Serial 2438 Ltr: Centerior Energy to USNRC, Response to NRC Request for Information

Regarding Adequacy and Availability of Design Bases Information Regarding

Adequacy and Availability of Design Bases Information, February 11, 1997

Log 5004 Ltr: Allen G. Hansen to John K. Wood, Response to October 9, 1996 Request for

Information Pursuant to 10 CFR 50.54(f) Regarding Adequacy and Availability of

Design Bases Information, Davis-Besse Nuclear Power Station, Unit No. 1

(TAC No. 97583), February 25, 1997

Log 5024 Ltr: Allen G. Hansen to John K. Wood, Planned Design Inspection, Davis-Besse

Nuclear Power Station, Unit No. 1, March 27, 1997

Serial 2455 Ltr: Centerior Energy to USNRC, Plan And Schedule for Completion of the

DBNPS Design Basis Validation Program, March 31, 1997

Log 5173 Ltr: Allen G. Hansen to John K. Wood, Davis-Besse Nuclear Power Station,

Unit 1 - Design Inspection - NRC Inspection Report No. 50-346/97-201

(TAC No. M99129), November 19, 1997

Serial 2623 Ltr: Guy G. Campbell to USNRC, Status of the Design Basis Validation Program

and the Planned Program to Convert to the Improved Standard Technical

Specifications, December 17, 1999

Other Documents

Davis-Besse Return to Service Plan, Revision 2, August 6, 2002

Nuclear Quality Assessment Oversight of Davis-Besse Return to Service,

Revision 1, July 22, 2002

RSMT Davis-Besse Restart Senior Management Team Charter, Revision 00,

June 24, 2002

Davis-Besse Restart Overview Panel Charter, Revision 0, June 7, 20002

RSRB Davis-Besse Restart Station Review Board Charter, Revision 00, June 24,

2002

Davis-Besse System Health Assurance Plan, Revision 2, August 5, 2002

Davis-Besse System Health Assurance Plan, Revision 3, September 9, 2002

System Health Assurance Discovery Action Plan, Revision 0, August 5, 2002

System Health Assurance Discovery Action Plan, Revision 2, October 15,

2002

FENOC Engineering Principles and Expectation, July 10, 2002

NED 87-10338 Memo, Sway Strut Bushing Grease Fittings, July 29, 1987

Manual Valve Component Reliability Template Basis Document

ENDP-01506 Leakage Reduction Program Manual, Revision 00, July 18, 2001

Design Basis Document Validation Program, Revision 1, August 21, 1997

SD-018 System Description for Service Water System, Revision 2, August 4, 1995

Design Basis Document Validation Report of the Service Water (SW) for

Davis-Besse Power Plant by Sargent & Lundy, LLC, December 23, 2000

Training Lesson Plan - Borated Water System Inspections (Outside

Containment), September 5, 2002

TM-108 Job Familiarization Guidelines - Mechanical Boric Acid Corrosion Control

Inspector (Applicable to EN-DP-01501 Only), July 22, 2002

Focused Self-Assessment Guideline, Revision 0, December 2001

SA 2002-0093 Davis-Besse NPS Self-Assessment Service Water System Report,

October 22, 2002

21

SA 2002-0094 Davis-Besse NPS Self-Assessment High Pressure Injection System Report,

October 22, 2002

SA 2002-0095 Davis-Besse NPS Self-Assessment 4160 VAC System Report, October 22,

2002

Quality Assurance Review of System Health Readiness Review for Decay

Heat Removal/Low Pressure Injection System, September 27, 2002

Quality Assurance Review of System Health Readiness Review for

125/250 VDC System, Revision 0, October 5, 2002

Quality Assurance Review of System Health Readiness Review for Station

and Instrument Air System, Revision 0, November 6, 2002

Davis-Besse Operation Readiness Report, Revision 0, October 29, 2002

NPE-99-0076 Plant Equipment Reliability Self-Assessment, October 22, 1999

22

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-346

License No: NPF-3

Report No: 50-346/02-14(DRS)

Licensee: FirstEnergy Nuclear Operating Company

Facility: Davis-Besse Nuclear Power Station

Location: 5501 North State Route 2

Oak Harbor, OH 43449

Dates: September 23 through November 13, 2002

Inspectors: B. Bartlett, Lead Inspector

J. Ellegood, Resident Inspector

R. Daley, Reactor Inspector

R. Deese, Resident Inspector

D. Prevatte, Mechanical Consultant

M. Shlyamberg, Mechanical Consultant

Approved by: Ronald N. Gardner, Chief

Electrical Engineering Branch

Division of Reactor Safety

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

Background and Event Overview . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R21 Safety System Design and Performance Capability (71111.21) . . . . . . . . . . . . . . . . . . 6

Introduction . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

System Requirements . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

Inspection Scope . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

Observations and Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

Lack of a Design Basis Analysis for Containment Isolation Valve Backup Air

Supply Accumulators . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

Inadequate Blowdown Provisions for CAC Backup Air Accumulators . . . . . . . . 9

System Condition and Capability . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

Inspection Scope . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

Observations and Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

Failure to Perform Comprehensive Moderate Energy Line Break (MELB)

Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

Cracks in Other Moderate Energy Lines . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

Lifting of Service Water Relief Valves SW 3962 and SW 3963 . . . . . . . . . . . . 11

Inadequate Service Water Pump Room Temperature Analyses . . . . . . . . . . . 12

Service water Pump Room Steam Line Break . . . . . . . . . . . . . . . . . . . . . . . . . 13

Cable Ampacity . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

Identification and Resolution of Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

Inspection Scope . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

Observations and Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

Containment Air Coolers Nozzle Loading . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

SW Pump Curve Allowable Degradation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

Technical Specification Surveillance Requirement for High Pressure Injection

(HPI) Following Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

SW Relief Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

Non-Conservative Difference in Ultimate Heat Sink Temperature Measurements

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

System Walkdowns . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

Inspection Scope . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

Observations and Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

Inadequate Flooding Protection for The Service Water System . . . . . . . . . . . . 18

Design Review . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

1

Inspection Scope . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

Observations and Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

Non-Conservative TS Value for the 90 Percent Degraded Voltage Relay . . . . 21

Poor Quality Calculation for 90 Percent Degraded Voltage Relay . . . . . . . . . . 22

Non-Conservative Relay Setpoint Calculation for the 59 Percent Undervoltage

Relay . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

Inadequate Calculations for Control Room Operator Dose (GDC-19) and Off-Site

Dose (10 CFR Part 100) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25

HPI Pump Operation Under Long Term Minimum Flow . . . . . . . . . . . . . . . . . . 28

HPI Pumps Minimum Flow, Unanalyzed SBLOCA Sizes . . . . . . . . . . . . . . . . . 28

Inadequate Service Water System Flow Analyses . . . . . . . . . . . . . . . . . . . . . . 29

Definition of Passive Failure . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30

Inadequate Service Water System Thermal Analyses . . . . . . . . . . . . . . . . . . . 30

Inadequate Ultimate Heat Sink Inventory Analyses . . . . . . . . . . . . . . . . . . . . . 32

No Valid Service Water Pump Net Positive Suction Head Analysis . . . . . . . . . 33

Inadequate Service Water System (and Other Systems) Overpressure Protection

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

Service Water Source Temperature for Auxiliary Feedwater System . . . . . . . . 36

Short Circuit Calculations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 37

Inadequate Analytical Basis for the Setpoint to Swap Service Water System

Discharge Path . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 37

Safety System Inspection and Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 38

Inspection Scope . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 38

Observations and Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 38

HPI Quarterly Surveillance Test Instrumentation Issues . . . . . . . . . . . . . . . . . 38

SW Surveillance Test Does Not Use Worst Case Values . . . . . . . . . . . . . . . . 39

ECCS Sump Pump Test Acceptance Criteria . . . . . . . . . . . . . . . . . . . . . . . . . 39

Inadequate Service Water System Flow Balance Testing . . . . . . . . . . . . . . . . 40

Inadequate Corrective Actions for Service Water Pump Discharge Check Valves

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 40

4OA6 Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 41

Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 41

2

SUMMARY OF FINDINGS

IR 05000346-02-14; FirstEnergy Nuclear Operating Company; on 09/23-11/13/2002;

Davis-Besse Nuclear Power Station. Safety System Design and Performance Capability.

This was a special inspection of the design and performance capability of the service water

system, high pressure injection system, and the safety-related portions of the 4,160 volt

AC system. It was conducted by regional engineering specialists, resident inspectors and two

consultants. The inspection identified four NCVs, three of which had multiple examples, and

two unresolved items. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using IMC 0609 Significance Determination Process (SDP). Findings for

which the SDP does not apply are indicated by No Color or be assigned a severity level after

USNRC management review. The USNRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 3, dated July 2000.

A. Inspector Identified Findings

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a Non-Cited Violation (NCV) of Technical

Specification surveillance requirement 4.2.5.H, associated with failure to re-verify

High Pressure Injection pump flow following modifications that could alter system

flow characteristics.

This finding was determined to be more than minor because it affected the

mitigation systems cornerstone objective. This finding screened as Green in

the SDP phase 1, since this issue was not an actual loss of a safety function.

Because the finding was of very low safety significance, and was captured in

the licensees corrective action system this finding is being treated as an NCV

consistent with Section VI.A.1 of the NRC Enforcement Policy (Section 1R21.3).

  • Green. The inspectors identified an example of a Non-Cited Violation of 10 CFR

Part 50, Appendix B, Criterion III, associated with a non-conservative TS value

for the 90 percent degraded voltage relay.

This finding screened as Green in the SDP phase 1, since this issue was a

design deficiency that was confirmed not to result in loss of function in

accordance with Generic Letter 91-18 (Revision 1). Because the finding was of

very low safety significance, and was captured in the licensees corrective action

system this finding is being treated as an NCV consistent with Section VI.A.1 of

the NRC Enforcement Policy (Section 1R21.5).

Green. The inspectors identified an example of a Non-Cited Violation of 10 CFR

Part 50, Appendix B, Criterion III, associated with non-conservative relay setpoint

calculation for the 59 percent undervoltage relay.

3

This finding screened as Green in the SDP phase 1, since this issue does not

contribute to the likelihood of a Primary or Secondary system Loss of Coolant

Accident (LOCA) initiator, does not contribute to both the likelihood of a reactor

trip and the likelihood that mitigation equipment or functions will not be available,

and does not increase the likelihood of a fire or internal/external flood. Because

the finding was of very low safety significance, and was captured in the

licensees corrective action system, this finding is being treated as an NCV

consistent with Section VI.A.1 of the NRC Enforcement Policy (Section 1R21.5).

Green. The inspectors identified an example of a Non-Cited Violation of 10 CFR

Part 50, Appendix B, Criterion III, associated with an inadequate analytical basis

for the setpoint to swap service water system discharge path.

The inspectors considered this finding was more than minor because it could

affect the mitigating systems cornerstone objective of ensuring the capability of

systems that respond to initiating events to prevent undesirable consequences

attributable to design control. Using the significance determination process, the

safety significance was determined to be very low (Green) because the finding

did not screen as potentially risk significant due to a seismic, fire, flooding, or

severe weather event. Because the finding was of very low safety significance,

and was captured in the licensees corrective action system, this finding is being

treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy

(Section 1R21.5).

Appendix B, Criterion XI, associated with a service water surveillance test that

did not use worst case values.

This finding screened as Green in the SDP phase 1, since this issue was a

testing deficiency that was confirmed not to result in loss of function in

accordance with GL 91-18 (Revision 1). Because the finding was of very low

safety significance, and was captured in the licensees corrective action system

this finding is being treated as an NCV consistent with Section VI.A.1 of the NRC

Enforcement Policy (Section 1R21.6).

  • Green. The inspectors identified a Non-Cited Violation of 10 CFR 50,

Appendix B, Criterion XVI, associated with inadequate corrective actions for

service water pump discharge check valves test acceptance criteria.

This finding screened as Green in the SDP phase 1, since the finding did not

screen as risk significant due to a seismic, fire, flooding, or severe weather

event. Because the finding was of very low safety significance, and was

captured in the licensees corrective action system this finding is being treated

as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy

(Section 1R21.6).

4

Cornerstone: Barrier Integrity

  • Green. The inspectors identified an example of a Non-Cited Violation of 10 CFR

Part 50, Appendix B, Criterion III, associated with the lack of a design basis

analysis for containment isolation valve backup air supply accumulators.

This finding screened as Green in the SDP phase 1, since this issue did not

represent an actual open pathway in the physical integrity of reactor

containment. Because the finding was of very low safety significance, and was

captured in the licensees corrective action system this finding is being treated as

an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy

(Section 1R21.1).

  • Green. The inspectors identified an example of a Non-Cited Violation of 10 CFR

Part 50, Appendix B, Criterion III, associated with inadequate blowdown

provisions for Containment Air Cooler (CAC) backup air accumulators.

This finding screened as Green in the SDP phase 1, since this issue did not

represent an actual open pathway affecting the physical integrity of reactor

containment. Because the finding was of very low safety significance, and was

captured in the licensees corrective action system, this finding is being treated

as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy

(Section 1R21.1).

5

REPORT DETAILS

Background and Event Overview

On March 6, 2002, Davis-Besse personnel notified the NRC of degradation (corrosion) of the

reactor vessel head material adjacent to a control rod drive mechanism (CRDM) nozzle. This

condition was caused by coolant leakage and boric acid corrosion of the head material induced

by an undetected crack in the adjacent CRDM nozzle. The degraded area covered in excess of

20 square inches where the low-alloy structural steel was corroded away, leaving the thin

stainless steel cladding layer. This condition represented a loss of the reactor vessels

pressure retaining design function, since the cladding was not considered as pressure

boundary material in the structural design of the reactor pressure vessel. While the

cladding did provide a pressure retaining capability during reactor operations, the identified

degradation represented an unacceptable reduction in the margin of safety of one of the

three principal fission product barriers at the Davis-Besse Nuclear Power Station (reference

NRC report 50-346/02-03(DRS)).

As part of the licensees Return to Service plan and as corrective action for the circumstances

that led to the vessel head degradation, the licensee implemented the Davis-Besse System

Health Assurance Plan (DBSHAP). This plan described activities to review plant systems prior

to restart to ensure that plant systems were in a condition that would support safe and reliable

operation. To assess the quality of the licensees reviews, the NRC conducted an in-depth

design and performance capability inspection of three of the systems reviewed by the licensee.

Given the high public interest in this subject area at Davis-Besse, and therefore the need to

clearly communicate the rationale for NRC staff conclusions regarding the effectiveness of

licensee extent of condition inspections, this report documents the inspectors observations.

1. REACTOR SAFETY

Cornerstones: Mitigating Systems and Barrier Integrity

1R21 Safety System Design and Performance Capability (71111.21)

Introduction

Inspection of safety system design and performance verifies the initial design of the

Davis-Besse plant as well as subsequent modifications of the plant, and provides

monitoring of the capability of the selected systems to perform design bases functions.

As plants age, the design bases may be lost and important design features may be

altered or disabled. The plant risk assessment model is based on the capability of the

as-built safety system to perform the intended safety functions successfully. This

inspectable area will verify aspects of the mitigating systems and barrier integrity

cornerstones for which there are no indicators to measure performance.

The objective of the safety system design and performance capability inspection was to

assess the adequacy of calculations, analyses, other engineering documents, and

operational and testing practices that were used to support the performance of the

service water, high pressure injection, and the safety-related portions of the 4,160 volt

6

AC systems during normal, abnormal, and accident conditions. The inspection was

performed by a team of inspectors that consisted of a team leader, two Region III

inspectors, one Region IV inspector, and two consultants.

The service water, high pressure injection, and 4,160 volt AC systems were selected for

review during this inspection. This selection was based upon:

  • having a high probabilistic risk analysis ranking;
  • selecting one system from the licensees list of 5 systems receiving a Latent

Issues Review;

  • selecting two systems from the licensees list of 31 systems receiving System

Health Readiness Reviews and;

  • not having received recent NRC review.

The criteria used to determine the systems performance included:

  • applicable Technical Specifications;
  • the systems design documents.

.1 System Requirements

a. Inspection Scope

The team reviewed the following attributes for the service water (SW) system, high

pressure injection (HPI) system, and the safety-related portions of the 4,160 Vac

system: (1) process medium (water, steam, and air); (2) energy sources; (3) control

systems; and (4) equipment protection. The team verified that procedural instructions to

operators were consistent with the operator actions required to meet, prevent, and/or

mitigate design basis accidents. The teams review considered requirements and

commitments identified in the Updated Final Safety Analysis Report (UFSAR), Technical

Specifications (TS), design basis documents, and plant drawings. This review further

verified that the required support functions for the selected systems would be available.

The team verified that the system needs for the selected systems were met. The supply

of air, water, steam, and electrical power required by the TS were verified through a

review of the design of the selected systems, and those systems providing support

functions.

The team verified equipment for the selected systems required to operate and/or change

state during accidents and events would have control power available. The team further

reviewed the adequacy of alarm setpoints and verified that necessary instrumentation

and alarms were available to operators for making necessary decisions in coping with

postulated accident conditions. In addition, the team verified that the systems standby

alignments were consistent with assumptions in the operating procedures as well as

design and licensing basis assumptions.

7

b. Observations and Findings

Lack of a Design Basis Analysis for Containment Isolation Valve Backup Air Supply

Accumulators

The inspectors identified a Green finding that is an example of a Non-Cited Violation of

10 CFR Part 50, Appendix B, Criterion III, Design Control, associated with a failure to

assure that applicable regulatory requirements and the design basis for structures,

systems, and components were correctly translated into specifications, drawings,

procedures, and instructions. Service water (SW) system valves SW-1356, SW-1357,

and SW-1358 are the containment air cooler (CAC) outlet containment isolation valves.

They are air-operated valves that fail open on a loss of instrument air. Since the plants

instrument air system was nonsafety-related, the containment isolation valves were

provided with a safety-related backup air system with accumulators to assure that they

could be isolated and held closed for containment isolation under accident conditions.

However, no viable design basis description or analyses could be found for the backup

air system or for the size of the accumulators. Additionally, no acceptance criteria,

basis, or analysis could be found to support the surveillance test which leak-tested this

system. Therefore, the ability of the safety-related backup air supplies to perform their

safety-related functions of enabling the closure of these valves upon demand for

containment isolation could not be verified.

The procedures acceptance criterion was that the accumulators are capable of stroking

the valves and holding them shut for 30 minutes. Discussions with licensee engineers

determined that the 30-minute criterion was based on the expectation that instrument air

would be restored in this time and that the operators could manually shut the valves if

necessary. However, for design basis analysis credit should not be given for restoration

of the non-safety instrument air system. In addition, the ability of the plant operators to

manually close the air-operated containment isolation valves in an area that could have

very high post-accident radiation levels had not been demonstrated.

The licensee informed the inspectors that the lack of a design basis had been identified

prior the inspectors arrival on site. However, condition report (CR) 02-06546 only

identified that the basis for the 30-minute test acceptance time could not be located, and

this was deemed as only an administrative inadequacy.

The licensee missed at least two opportunities to have identified and corrected these

concerns. The first was when Generic Letter (GL) 88-14, Instrument Air Supply

Problems Affecting Safety-Related Equipment, dated August 8, 1988, was issued to

all licensees. The licensees docketed response letter stated, in part, Additionally,

safety-related accumulators were verified to be sized correctly and to perform as

required during a loss of instrument air and other design-basis events.

The second missed opportunity was when these service water valves and operators were

replaced with components of completely different design (Modification 99-0039-00, CAC

Temperature Control Valve Replacement, dated June 29, 1999). The modification effort

should have prompted a review of the backup air system design bases and capabilities to

verify that they were adequate for the new equipment.

8

10 CFR Part 50, Appendix B, Criterion III, Design Control, requires that Measures shall

be established to assure that applicable regulatory requirements and the design

basis...are correctly translated into specifications, drawings, procedures, and

instructions. Contrary to this requirement, the licensee failed to correctly translate the

design basis requirements for sizing of the safety-related backup air supplies for service

water containment isolation valves SW-1356, SW-1357, and SW-1358 into the design.

This finding was determined to be more than minor because it affected the barrier

integrity cornerstone objective. This finding screened as Green in the Significance

Determination Process (SDP) phase 1 because the issue did not represent an actual

open pathway in the physical integrity of reactor containment. Because the finding was

of very low safety significance, and was captured in the licensees corrective action

system as CR 02-07750, this finding is being treated as an example of a Non-Cited

Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, consistent with

Section VI.A.1 of the NRC Enforcement Policy (NCV 50-346/2002-014-01a).

Inadequate Blowdown Provisions for Containment Air Cooler Backup Air Accumulators

The inspectors identified a Green finding that is being treated as an additional example of

a Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control,

associated with a failure to assure that applicable regulatory requirements and the design

basis for structures, systems, and components were correctly translated into

specifications, drawings, procedures, and instructions. The inspectors determined that

the CAC containment isolation valve backup air accumulators were not equipped with

blowdown valves or other provisions to allow removal of condensation as described in

Updated Safety Analysis Report (USAR) Section 9.3.1.5, which stated, Regular

maintenance of the equipment is performed to ensure cleanliness. This includes regular

blowing down of receivers....

The failure to include blowdown provisions meant that any moisture intrusion into the

accumulator would not be identifiable and would not be removable. This would result in

the reduction in the amount of air available to maintain the containment isolation valves

closed and would result in rust and other debris in the accumulator.

10 CFR Part 50, Appendix B, Criterion III, Design Control, requires that Measures shall

be established to assure that applicable regulatory requirements and the design

basis...are correctly translated into specifications, drawings, procedures, and

instructions. Contrary to this requirement, the licensee failed to include blowdown

valves or other provisions to allow removal of condensation as described in Updated

Safety Analysis Report (USAR) Section 9.3.1.5.

This finding was determined to be more than minor because it affected the barrier

integrity cornerstone objective. This finding screened as Green in the SDP phase 1

since this issue did not represent an actual open pathway in the physical integrity of

reactor containment. Because the finding was of very low safety significance, and was

captured in the licensees corrective action system as CR 02-07750, this finding is being

treated as an additional example of a Non-Cited Violation of 10 CFR Part 50, Appendix

B, Criterion III, Design Control, consistent with Section VI.A.1 of the NRC Enforcement

Policy (NCV 50-346/2002-014-01b).

9

.2 System Condition and Capability

a. Inspection Scope

The team reviewed the periodic testing procedures for the selected systems to verify that

the design requirements were adequately demonstrated. The team reviewed the

environmental qualification of a sample of system components to verify the capability to

operate under design environmental conditions and the assumed operating parameters

including: voltage, speed, power, flow, temperature, and pressure. The team also

reviewed recent instrument setpoint changes to verify that the design basis or capability

for the selected systems had not been affected by the setpoint change process.

The team reviewed the systems operations by conducting system walkdowns; reviewing

normal, abnormal, and emergency operating procedures; and reviewing the Updated

Final Safety Analysis Report, technical specifications, design calculations, drawings, and

procedures. In addition, the team reviewed the list of active and closed standing orders

and operator work-arounds to ensure no design assumptions were invalidated by past or

current operator daily practices.

b. Observations and Findings

Failure to Perform Comprehensive Moderate Energy Line Break (MELB) Analysis

Pump Seal Leakage

The inspectors identified an unresolved item associated with a failure to evaluate the

environmental effects of a postulated Decay Heat Removal (DHR) pump seal failure.

Following a review of the USAR description of a postulated DHR pump seal failure

following a postulated Loss of Coolant Accident (LOCA) (Section 3.6.2.7.1.11), and

discussions with the licensee, the inspectors determined that only the effects of flooding

had been evaluated. The environmental effects of the assumed 120 gallons per minute

(gpm) seal failure on the equipment in the area, such as pressurization, increase of

humidity and temperature, jet impingement, etc, had not been evaluated.

Due to the interconnection of rooms in the Auxiliary Building, the environmental effects

could impact the other emergency core cooling system (ECCS) pump room and the

remaining ECCS train. The licensee issued CR 02-07757 to document the inspectors

finding.

The inspectors were unable to fully evaluate the effects of the assumed seal failure on

licensee equipment in order to assess whether the finding represented a design or

qualification deficiency that would result in a loss of function. At the close of the

inspection, the licensee was re-evaluating the effects of a postulated DHR pump seal

failure on the operation of plant equipment. This issue will remain as unresolved pending

the licensees evaluation and the NRCs review (URI 50-346/2002-014-01c).

10

Cracks in Other Moderate Energy Lines

The teams review of USAR Section 3.6.2.7, Protection Against Environmental Effects

Outside the Containment Vessel, and discussions with the licensee identified that critical

cracks at selected locations during normal plant shutdown cooling mode for the low

pressure injection/decay heat removal (DHR) system had not been evaluated. The

effects of those cracks on safety related Structures, Systems, or Components (SSCs)

(e.g., pressurization, increase of humidity and temperature, jet impingement) had not

been evaluated. Due to the interconnection of rooms in the Auxiliary Building, this

environment could potentially reach the other ECCS Pump Room and affect the

remaining DHR train. The licensee issued CR 02-07777 to document this teams finding.

Lifting of Service Water Relief Valves SW-3962 and SW-3963

The inspectors identified an unresolved item in that the service water supply header relief

valves, SW-3962 and SW-3963, had a history of lifting and not reseating after expected

plant transients. The resultant diversion of flow away from the systems safety-related

heat exchangers could have, under some conditions, prevented one or both trains of the

SW system from performing its safety function.

The service water system was protected against overpressure from the pumps by 6"x 8"

relief valves, SW-3962 and SW-3963, on each of the respective supply headers. Since

initial plant startup in 1977, a chronic problem existed with these valves lifting during

normal system transients that produced pressure pulses in the supply headers. These

included pump swaps, system lineup changes, load changes, and high system pressures

during winter months when system flows were restricted. Additionally, due to the

steady-state operating header pressure often being close to the valves reseat pressure,

they have frequently experienced chatter, resultant damage, and failure to fully reseat. In

this condition, the valves could divert substantial flow from the systems heat exchangers

that is not accounted for in the system analyses or flow balance tests. Therefore, for this

condition, the ability of the system to provide the required design basis flows to the

safety-related heat exchangers in both divisions could not be verified. This design also

did not meet the requirements of American Society of Mechanical Engineering (ASME)

Code,Section III, 1971, Article NB-7400, Paragraph NB-7614.1, Anti-Chattering and Life

Requirements, which stated, Safety valves shall be designed and constructed to

operate without chattering...

This has been a significant concern for the licensee as evidenced in CRs 00-2478 and

01-0350. One of the licensees responses has been to structure the system operating

procedure, DB-OP-06261, Service Water System Operating Procedure, with steps to

intentionally lower header pressure, such as by opening the strainer blowdown valves,

before performing any activities likely to cause the valves to lift. Although this allowed

the system to be operated with lowered potential for valve actuations, it did not

eliminate the problem, even for normal operations. More important, it did not address

the systems safety function and accident-induced pressure transients, such as the

automatic isolation of the non-safety portion of the system by the closing of either valve

SW-1395 or SW-1399, depending on which division was supporting the turbine building

loads at the time, which would produce a relatively large pressure transient. A single

failure on the opposite division would render the system unable to perform its safety

11

function. Other events alone, such as loss-of-offsite-power (LOOP) without an accident

could cause such a transient with pump restart after starting of the diesel generators.

Based on actual plant experience, these appeared to be high probability transient

responses.

Therefore, as a result of the systems supply header overpressure protection design,

there was a high potential that the SW system could not adequately perform its safety

function for design basis accidents and other design basis events. Although the licensee

formally identified this concern with respect to operations impact, the safety implications

were never formally recognized and documented.

The inspectors determined that the design of the SW system relief valves which could

result in a loss of flow to safety-related components was a performance deficiency

warranting a significance evaluation. At the close of the inspection, the licensee was

re-evaluating the effects of leaking SW relief valves on the operation of plant equipment.

The licensee entered the issue into its corrective action program as CR 02-07879. The

licensee screened the CR as requiring resolution prior to the mode in which SW was

required by plant TS (Mode 4). This item will remain unresolved pending the licensees

evaluation and the NRCs review (URI 50-346/2002-014-01d).

Inadequate Service Water Pump Room Temperature Analyses

The inspectors identified an unresolved item associated with assurance that applicable

regulatory requirements and the design basis for structures, systems, and components

were correctly translated into specifications, drawings, procedures, and instructions. The

inspectors questioned whether the licensee correctly translated the USAR commitments

regarding the service water pump room temperature limits into analyses that

demonstrated these limits would not be violated for design basis conditions.

USAR Section 9.4.5.1, Service Water Pump Room Ventilation System Design Bases,

stated, The system is designed to maintain the service water pump room and

diesel-driven fire pump room between 40EF and 104EF year-round for all modes of

operation including post-accident. Calculation 67.005, Service Water Pump Room

Ventilation System Capacity, analyzed the heat loads in the service water pump room

and the ability of the ventilation system to maintain the pump room temperatures within

this range. The inspectors determined that calculation 67.005 contained multiple

non-conservative attributes:

For summer, with an assumed 95EF outside design temperature:

  • The calculation did not fully consider accidents without a LOOP, in which case, all

of the non-1E-powered loads in the rooms, such as the two cooling tower makeup

(CTMU) pumps, could remain energized, adding to the heat load.

  • The calculation did not consider a seismic event that could start the diesel fire

pump as a result of fire system water losses, thereby adding this large heat load.

12

For winter, with an assumed -10EF outside design temperature:

  • The calculation modeled the room temperature as uniform. However, for worst

case conditions, the only significant heat source could be one operating service

water motor at one end of the room, with vulnerable components at the opposite

end. There is approximately 44 feet of separation and an intervening wall with an

opening in the approximate center, and there would be no ventilation fans

operating.

  • The calculation evaluated only heat transfer by conduction through the walls, roof,

and floor; it did not account for the fixed open ventilation roof inlets. Heated air

from the operating pump would rise and exit the room at the nearer opening and

be replaced by -10EF outside air entering the room at the farther opening.

At the close of the inspection, the licensee was re-evaluating the issue of correctly

translating the USAR commitments regarding the service water pump room

temperature limits into analyses that demonstrated these limits would not be violated

for design basis conditions. The licensee entered the issue into its corrective action

program as CR 02-07188. The licensee screened the CR as requiring resolution prior

to the mode in which SW was required by plant TS (Mode 4). This item will remain

as unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-01e).

Service Water Pump Room Steam Line Break

The inspectors identified an unresolved item associated with assurance that applicable

regulatory requirements and the design basis for structures, systems, and components

were correctly translated into specifications, drawings, procedures, and instructions. The

inspectors questioned whether the licensee correctly translated the USAR commitments

regarding the service water pump room environmental limits into analyses that

demonstrated these limits would not be violated for design basis conditions.

The inspectors reviewed Calculation C-NSA-085.00-002, Auxiliary Steam Blowdown in

the Intake Structure, that addressed a postulated auxiliary steam line break in the

service water pump room. The inspectors determined that the calculation failed to

account for any steam condensation in safety-related electrical equipment in the room.

Such condensation could render this equipment or equipment powered by or through

these components inoperable. Such equipment could include the service water pump

motors, the safety-related motor control centers, and pull/junction boxes in the room.

USAR Section 3.11.1.2, Environmental Conditions, stated, Environmental conditions

have been developed for all safety-related areas of the plant...The environmental

conditions include temperature, pressure, relative humidity...

This concern was also identified by the licensee in the Latent Issues Review and

documented in CR 02-05966; however, this CR only addressed pull/junction boxes. In

order to resolve the issue, the licensee will need to assess the impact of steam

condensation on the operation of the SW system.

13

At the close of the inspection, the licensee was re-evaluating the impact of steam

condensation following a postulated heating steam line break. The licensee entered the

issue into its corrective action program as CR 02-07475. The licensee screened the CR

as requiring resolution prior to the mode in which SW was required by plant TS (Mode 4).

This item will remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-01f).

Cable Ampacity

The inspectors identified an unresolved item associated with assurance that applicable

regulatory requirements and the design basis for structures, systems, and components

were correctly translated into specifications, drawings, procedures, and instructions. The

inspectors determined the licensee failed to correctly translate the USAR commitments

regarding the cable ampacity analysis for electrical cable passing through ECCS pump

room number 115.

ECCS pump room number 115 had an analysis for cable de-rating /ampacity for

temperatures up to 120EF, however; the peak calculated temperature in the room is now

124.2EF and the licensee has not performed a derate for the extra 4.2 degrees.

At the close of the inspection, the licensee was re-evaluating the impact of steam

condensation following a postulated heating steam line break. The licensee entered the

issue into its corrective action program as CR 02-06893. The licensee screened the CR

as requiring resolution prior to the mode in which this equipment was required by plant

TS (Mode 4). In order to resolve the item, the Licensee will need to assess the impact of

the revised temperature analysis on cable ampacity and its effect on safety-related

cables passing through room 115. This issue will remain unresolved pending the

licensees evaluation and the NRCs review (URI 50-346/2002-014-01g).

.3 Identification and Resolution of Issues

a. Inspection Scope

The team reviewed a sample of problems identified by the licensee in the corrective

action program to evaluate the effectiveness of corrective actions related to design

issues. The sample included open and closed condition reports going back three years

that identified issues related to or affecting the systems and safety-related setpoint

issues. The specific corrective action documents that were sampled and reviewed by

the team are listed in the attachment to this report. Inspection Procedure 71152,

Identification and Resolution of Problems, was used as guidance to perform this part of

the inspection.

The issues addressed by the condition reports reviewed included:

  • The disposition of technical specification interpretations to address system and

component operability;

  • The identification and correction of configuration control events and errors;
  • The identification and correction of issues related to testing failures;

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  • The identification and corrective action associated with personnel errors, primarily

in the operations area;

  • The identification and correction of safety-related setpoint issues; and
  • The identification and correction of apparently degraded equipment.

b. Observations and Findings

Containment Air Coolers Nozzle Loading

On September 5, 2002, the licensee identified a non-conservatism in their analysis of

CAC mechanical stresses. This analysis evaluated the connection of the service water

system to the CACs. During a LOCA, the service water piping will expand as the water

temperature increases. The amount of stress applied to the CAC nozzle is partially

determined by the flexibility of the nozzle. In the analysis, the licensee overestimated

nozzle flexibility by a factor of one thousand. As a result, the calculated stresses on the

nozzle were significantly lower than would actually be experienced during a postulated

LOCA or other transient. By reducing nozzle flexibility to more realistic values, the

licensee determined that the coolers could exceed code allowable values under either a

LOCA or water hammer event. In the case of a LOCA, this would be a common mode

failure that could render all three trains of containment air coolers inoperable. The

licensee had at least one prior opportunity to identify this error. In 1997, the licensee

performed a water hammer analysis to respond to Generic Letter 96-06. This analysis

included use of the CAC stress calculations as a base model for the analysis. During

development of this analysis, the licensee failed to identify the erroneous nozzle flexibility

assumption.

As of the close of this inspection, the licensee had yet to complete the re-analysis

using the proper nozzle flexibility. The licensee entered the issue into its corrective

action program as CR 02-05563. The licensee screened the CR as requiring

resolution prior to the mode in which SW was required by plant TS (Mode 4). This

item will remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-03e).

SW Pump Curve Allowable Degradation

The inspectors identified an unresolved item associated prompt corrective action to

resolve an identified condition where the allowable degradation of the SW pumps did

not match the design basis required flow rate from the SW pumps.

In the Latent Issues Review (LIR), the licensee re-identified a condition where the total

head across the SW pumps could degrade by as much as 7 percent before corrective

action was required under ASME Section XI. The flow balance procedures (DB-SP-3000

and DB-SP-3001) did not adjust the available SW pump head for the maximum possible

SW pump degradation.

This issue was documented in CR 02-05369. The teams review of this CR identified

that this CR was approved, yet it did not identify a need to evaluate possible generic

implications. When questioned about the extent of condition and applicability to other

systems, e.g., component cooling system, the licensee agreed that the extent of

15

condition should have been considered and issued CR 02-06863 to document a lack of

the extent of condition evaluation. The CR was noted as ...needs to be considered for

restart.

At the close of the inspection, the licensee had yet to determine if the SW pumps were

performing at a level that would supply the needs of the SW system during all required

accident conditions. The licensee entered the issue into its corrective action program as

CR 02-07468. The licensee screened the CR as requiring resolution prior to the mode in

which SW was required by plant TS (Mode 4). This item will remain unresolved pending

the licensees evaluation and the NRCs review (URI 50-346/2002-014-03a).

Technical Specification Surveillance Requirement for High Pressure Injection (HPI)

Following Modifications

The inspectors identified one Green finding that is being treated as a Non-Cited Violation

of TS 4.5.2.H which requires re-verification of HPI pump flow following modifications that

could alter system flow characteristics.

The inspectors review of the HPI pump surveillances, design basis calculation, and the

TS requirements determined that TS 4.5.2 H had not been implemented. The TS

required verification that the HPI pump is capable of delivering a total of 750 gpm at

400 pounds per square inch gage (psig) at the Reactor Coolant System (RCS) nozzle

...following completions of modifications to the HPI ... subsystems that alter the

subsystem flow characteristics... Calculations and surveillance test procedures address

flow rates of about 400 gpm (HPI pump flow test region). Thus, there were no tests or

calculations to demonstrate that the HPI pumps complied with TS requirements. The

inspectors questioned the licensee about this discrepancy. The licensee stated that the

HPI self-assessment conducted in parallel with the teams inspection also identified this

issue and was documented in CR 02-06996. The basis for closure of this CR stated:

The bottom line of all this is that T.S. 4.5.2 H and the calculations

that support it are not well aligned. However, it appears that past

testing and acceptance criteria was sufficient to support that the

implied requirement is met. This issue should be cleaned up prior

to restart to absolutely assure alignment and that testing is in full

compliance with requirements.

This CR failed to address that the HPI system was modified such that system flow

characteristics were altered. CR 02-06996 was the second CR issued by the licensee

to address this failure to comply with the TS requirements. The first CR which identified

the failure to comply with the TS requirements was CR 02-03331; however; this CR

was being tracked as an administrative issue. When questioned by the team if the

required TS 4.5.2 H verification was performed, the licensee was not able to verify the

TS required verification was done. Based on this question, the licensee issued

CR 02-07468.

The inspectors determined that flow testing was performed following replacement of the

HPI impellers and that this flow testing confirmed that the new impellers performed

similarly to the old impellers.

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This finding was determined to be more than minor because it affected the mitigation

systems cornerstone objective. This finding screened as Green in the SDP phase 1,

since this issue was not an actual loss of a safety function. Because the finding was of

very low safety significance, and was captured in the licensees corrective action system

as CR 02-07468, this finding is being treated as an NCV consistent with Section VI.A.1 of

the NRC Enforcement Policy (NCV 50-346/2002-014-04).

SW Relief Valves

The inspectors identified an unresolved item associated with safety-related service water

relief valves which failed and malfunctioned due to poor design, potentially preventing the

system from performing its safety function, and the licensee had not corrected this

condition.

At the close of the inspection, the licensee was re-evaluating the effects of leaking SW

relief valves on the operation of plant equipment. The licensee entered the issue into

its corrective action program as CR 02-07995 and screened the CR as requiring

resolution prior to the mode in which SW was required by plant TS (Mode 4). To

resolve this issue the Licensee will need to assess the ability of the licensees SW

system to withstand a loss of SW flow due to the partially open relief valves. This issue

will remain as unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-03b).

Non-Conservative Difference in Ultimate Heat Sink Temperature Measurements

The inspectors identified an unresolved item associated with plant staff awareness of the

non-conservative mismatch between the Ultimate Heat Sink (UHS) temperature, as

indicated by the difference between the TS temperature instrument readings, and the

2EF higher actual service water heat exchanger inlet temperatures, and the failure to

promptly correct this condition.

The licensee entered the issue into its corrective action program as CRs 02-05372,

02-06177, 02-06332, 02-06336, 02-06370, 02-07004, and 02-07716 and screened

the CRs as requiring resolution prior to the mode in which the SW system was

required by plant TS (Mode 4). In order to resolve this issue, the licensee and the

NRC will need to assess the service water system thermal requirements. This issue

will remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-03c).

.4 System Walkdowns

a. Inspection Scope

The team performed walkdowns of the accessible portions of the selected systems, as

well as the required support systems. The walkdowns focused on the installation and

configuration of power supplies, piping, components, and instruments. During the

walkdowns, the team assessed:

  • The placement of protective barriers and systems;

17

  • The susceptibility to flooding, fire, or environmental conditions;
  • The physical separation of trains and the provisions for seismic concerns;
  • Accessibility and lighting for any required local operator action; and
  • The materiel condition and preservation of systems and equipment.

Finally, the team assessed the conformance of the currently installed system

configurations to the current design and licensing bases.

b. Observations and Findings

Inadequate Flooding Protection for The Service Water System

The inspectors identified an unresolved item associated with correctly translating the

USAR commitments regarding flood protection for the service water pump room.

USAR Section 2.4.8.2 stated, The Probable Maximum Flood Water is elevation

583.7 feet... Section 9.2.1.3 stated, In the event of high water levels,...the

[service water] pump room is sealed to prevent flooding. Section 3D.1.4, [GDC]

Criterion 4 - Environmental and Missile Design Basis, stated, These [safety-related]

structures, systems, and components are appropriately protected against dynamic

effects...and discharging fluids, that may result from equipment failures and from events

and conditions outside the nuclear power unit.

Contrary to these commitments, the service water system was not adequately

protected against flooding effects that could result from high lake water levels, from

internal flooding, and from other threats to the system that could result from failure of

non-seismically qualified equipment as follows:

(1) The three service water pumps were located in a single sealed room in the

service water pump house. Also located in the same room, immediately adjacent

to and staggered between the service water pumps, were two cooling tower

makeup (CTMU) pumps, each capable of pumping up to about 15,000 gallons per

minute. Neither the CTMU pumps nor the associated piping and equipment were

seismically qualified or mounted. The inspectors determined that during a

seismic event, the pumps could be dislodged from their mountings. If this were to

occur then the CTMU pumps could impact the adjacent service water pump

columns and pump motors, resulting in their failure. Additionally, failure of a

CTMU pump casing or its associated piping could produce flooding rates which

could completely fill the room in approximately two minutes. The service water

pump motors would begin to flood at a water level of about five feet above the

floor in significantly less time, and the safety-related motor control centers

(MCCs) located in this room at approximately one foot off the floor in just

seconds. These MCCs provided power for service water system motor operated

valves, the safety-related room ventilation fans, the service water strainer motors,

and other equipment. Therefore, a seismic event that could cause structural

failure of the CTMU pumps or piping could result in rapid loss of both divisions of

service water due to mechanical impact or room flooding.

18

The concern with the seismic qualification of the CTMU piping was identified by

the licensee in the LIR and documented on CRs 02-06297 and 02-06139. The

issue of the seismic qualification of the CTMU pumps with respect to impact on

the adjacent service water pumps and the issue of flooding as a result of the

movement of the seismically non-qualified CTMU pumps causing their own casing

failure or the failure of the attached piping had not been identified or documented

by the licensees LIR.

(2) The CTMU pumps were equipped with a feature intended to provide protection for

the service water system components in the room in the event of cracks or breaks

in the CTMU components in the room. The feature was a pressure switch located

in the discharge piping of each CTMU pump that was designed to shut down the

pump whenever discharge pressure decreased to 20 psig from normal operating

pressure, about 50 psig. However, informal evaluations performed by the

inspectors and subsequently by the licensee, indicated that break flows of several

thousand gallons per minute would be required to reduce the pressure to the

shutdown setpoint. At this rate the vital equipment in the room would be flooded

in seconds. Therefore, the inspectors concluded that this device was incapable

of performing its intended purpose. Additionally, this feature was non-safety,

non-1E powered, non-environmentally qualified, and not designed for single

failure. Therefore, it did not meet the fundamental design requirements for

equipment required to perform a safety function.

(3) The diesel fire pump was located in a space adjacent to the service water pump

room but within the same sealed enclosure, and the spaces were connected by a

non-watertight door and a ventilation opening in the wall between the rooms. The

floor elevation of this enclosure was 576'. The fire pump room contained a drain

sump with two non-safety related sump pumps, each equipped with a single

non-safety related discharge check valve. A common four-inch discharge line

downstream of the check valves penetrated the west wall below the maximum

lake flood level (583.7') and was connected to the plant storm drains. These

valves were not in any test or inspection program; therefore, they could be

considered failed open. Therefore, a design basis flood from the lake could

cause backflooding of both rooms through these valves.

An extent-of-condition review, performed at the inspectors request, in the service

water valve room and pipe tunnel located just outside the sealed service water

pump room revealed a similar condition. This area, at a floor elevation of 566'-3",

was connected to an adjacent water treatment building by a non-watertight door

and another ventilation wall opening. This review identified three sumps

containing a total of seven sump pumps, each equipped with an unqualified,

untested check valve that connected with the storm drains. In this area and

below flood elevation, were the safety-related service water valves SW-1395 and

SW-1399, which were required to provide isolation of the non-safety related

portion of the system for accident conditions. Such flooding could also preclude

operator access to these valves for manual isolation.

flooded due to postulated failures of either water treatment structures and

19

systems or failure of Seismic Class II pipe within the tunnel. It goes on to say

that, The Seismic Class I systems within the tunnel are designed to remain

operational while flooded. As a result of questions by the inspectors, the

licensee identified several non-seismic pipes and components in the service water

pipe tunnel/valve room and the connected water treatment structure that had not

been evaluated in the flooding analyses; no documentation could be provided that

demonstrated the ability of the service water isolation valves SW-1395 and

SW-1399 to operate while flooded.

  • In response to inspector questions, the licensee performed a review of the service

water pump room penetrations that were below the external flood elevation. This

review revealed that conduits that terminated at junction boxes below the flood

level were not sealed against flooding; the sealing of these junction boxes had

been credited for flood protection. However, these boxes were not rated for flood

conditions (internal flooding of the box), and their seals could not be reliably

assured.

  • The inspectors walkdown of the service water system identified another potential

external flood source in the service water pump room. CTMU pump number

116-2 was out of service, and the two-inch drain valve from its strainer was

danger tagged open. This formed a direct communication between the room and

the intake bay through the pump column, the discharge piping, and the strainer.

For an external flood, this valve would have allowed the room to be flooded. The

Senior Reactor Operator accompanying the walkdown was asked what actions

with regard to valve lineup in the room would be required for an external flood,

and the response was none. The inspectors then reviewed the plants external

flood procedure, RA-EP-02830, Emergency Plan Off Normal Occurrence

Procedure, Flooding, Revision 00, and found that it had no guidance with respect

to verifying proper valve lineup for flood protection, and the licensees clearance

order tagging procedure also did not address this condition.

  • One of the documents provided to the inspectors in response to these concerns

was Safety Evaluation 96-0078, which addressed potential flooding of electrical

duct banks. This document addressed the fact that the then-current USAR

indicated that three of the duct banks were enveloped in a waterproof membrane

up to the 577'-10" elevation, but in fact, those three, along with the other plant

duct banks, were only protected up to 575'. However, the maximum lake flood

level was 583.7', and the safety evaluation addressed only the effect that such a

flood would have on groundwater table seepage. The safety evaluation

incorrectly concluded that groundwater would not exceed 574.5', and therefore,

the duct banks were protected. It also incorrectly appeared to assume that the

breakwater dike at elevation 591' would protect the general site from the static

lake level during such a flood, and therefore it did not address the potential for

direct flooding of the duct banks from this source.

The licensee entered the issue into its corrective action program as CRs 02-07714,

02-07782, 02-07760, 02-07569, 02-07746, 02-06297, 02-06139 and screened the CRs

as requiring resolution prior to the mode in which SW was required by plant TS (Mode 4).

In order to resolve the issue, the licensee will need to perform additional analyses to

20

assess the ability of the licensees SW pumphouse to withstand internal and external

flooding. This issue will remain unresolved pending the licensees evaluation and the

NRCs review (URI 50-346/2002-014-01h).

.5 Design Review

a. Inspection Scope

The team reviewed the current as-built instrument and control, electrical, and mechanical

design of the selected systems. These reviews included a review of design assumptions,

calculations, required system thermal-hydraulic performance, electrical power system

performance, protective relaying, and instrument setpoints and uncertainties. The team

also performed a single failure review of individual components to determine the effects

of such failures on the capability of the systems to perform their design safety functions.

The inspectors reviewed the selected systems including a review of calculations,

drawings, specifications, vendor documents, Updated Final Safety Analysis Report, TS,

emergency operating procedures, and temporary and permanent modifications.

b. Observations and Findings

Non-Conservative TS Value for the 90 Percent Degraded Voltage Relay

The inspectors identified a Green finding that is being treated as an additional example of

a Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control,

associated with assurance that applicable regulatory requirements and the design basis

for structures, systems, and components were correctly translated into specifications,

drawings, procedures, and instructions. Specifically, the inspectors determined that the

TS allowable value for the 4160 VAC, 90-percent Degraded Voltage function as stated in

TS Table 3.3-4 was non-conservative.

This table established an allowable setpoint value of $ 3558 Volts for the 90 percent

Degraded Voltage Relay at Davis-Besse Nuclear Plant. Licensee calculation

C-EE-004.01-049 established an allowable value for Degraded Voltage at 90 percent of

the nominal bus voltage of 4160 V, or 3744 V. The calculation determined this value

based upon the minimum voltage value that motor operated valves (MOVs) require to

successfully operate. Based upon voltage drop analysis of the Davis-Besse electrical

distribution system, the calculation determined that 88.5 percent (3682 V) was the

minimum acceptable short-term degraded voltage at the safety related 4160 V buses.

The calculation allowed for uncertainties and established additional margin for future

application against plant modifications and minor changes. Based upon the calculation,

the analytical limit was determined to be 3690 V and the resulting allowable value was

established as 3744 V.

While the value calculated appeared to be sufficiently conservative, the inspectors noted

that the licensee had not established administrative controls in relation to this issue.

While CR 02-06243, documenting the discrepancy between the TS allowable value and

the value determined by the calculation, had been issued four days prior to the inspection

team arriving on site, the CR concluded that no immediate action was required at that

21

time. Further, the CR recommended that the calculation procedure should be revised to

permit calculation preparers to place calculations that require an event to take place prior

to permitting use in Restricted-Hold status. To date, there is no mechanism that

permits a calculation to be performed and issued without approving it. This makes it part

of the design basis and could have severe ramifications if the calculation data were used

in the field. In lieu of having the requirements in the calculation procedure that permit

issuance of Restricted-Hold calculations, this calculation should be revised to reflect the

current licensing basis in the TS.

The inspectors communicated to the licensee that while they had identified the

discrepancy between the TS allowable value and the value determined by the calculation,

the actions that they had proposed in CR 02-06243 appeared to be inadequate. The

inspectors noted that since the value in the calculation was the correct value,

administrative actions should be taken to make the operations staff aware that the TS

allowable value was incorrect and non-conservative.

Without administrative controls in place to identify the non-conservative TS allowable

value for the 90 percent Degraded Voltage Relay, a condition could exist in which the

voltage setting for this relay could have been set non-conservatively and still declared

operable. With a lower setpoint, motor-operated-valves required for post-accident

operation may not have been able to operate when called upon.

10 CFR Part 50, Appendix B, Criterion III, Design Control, requires that Measures shall

be established to assure that applicable regulatory requirements and the design

basis...are correctly translated into specifications, drawings, procedures, and

instructions. Contrary to this requirement, the licensee failed to correctly establish the

TS allowable value for the 90 percent Degraded Voltage Relay setpoint.

This finding was determined to be more than minor because it affected the mitigation

systems cornerstone objective. This finding screened as Green in the SDP phase 1,

since this issue was a design deficiency that was confirmed not to result in loss of

function in accordance with GL 91-18 (Revision 1). Because the finding was of very low

safety significance, and was captured in the licensees corrective action system as

CR 02-07766, this finding is being treated as an NCV consistent with Section VI.A.1 of

the NRC Enforcement Policy (NCV 50-346/2002-014-01i).

Poor Quality Calculation for 90 Percent Degraded Voltage Relay

The inspectors identified an unresolved item associated with use of insufficiently justified,

non-conservative uncertainty values in the calculation for the 90 percent Undervoltage

Relays.

The inspectors questioned why the licensee did not use vendor-supplied numbers for

uncertainties for the 90 percent Undervoltage Relays. Instead, the licensee used

uncertainty values associated with a vendor test report for the relay. This test report,

however, only provided test data for one tested relay and not for a batch of relays. This

resulted in the licensee using smaller uncertainty values in their calculation. The use of

these smaller uncertainty values resulted in non-conservative results in the setpoint

calculation for the 90 percent Undervoltage Relays.

22

The licensee entered the issue into its corrective action program as CR 02-07633.

In order to resolve the issue, the licensee will need to perform additional analysis

to assess the impact of using non-conservative uncertainty values. This issue will

remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-01j).

Non-Conservative Relay Setpoint Calculation for the 59 Percent Undervoltage Relay

The inspectors identified a Green finding that is being treated as an additional example of

a Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control,

associated with assurance that applicable regulatory requirements and the design basis

for structures, systems, and components were correctly translated into specifications,

drawings, procedures, and instructions. Specifically, the inspectors identified that

uncertainties associated with the 59 percent Undervoltage Relay TS allowable setpoint

value were non-conservative. Based upon the as-left values and the tolerance band

used in the calibration procedures for the relays, this allowed the relays to be calibrated

to an upper band that, with the true uncertainties taken into account, allowed the TS

upper setpoint to be exceeded.

TS Table 3.3-4 established an allowable setpoint value of $ 2071 to # 2450 Volts for the

59 percent Undervoltage Relay at Davis-Besse Nuclear Plant. Therefore, the relays

should have been calibrated to a value that, with uncertainties factored in, was within the

allowable values band. Calculation C-EE-004.01-051 established a value for calibration.

In the calculation, uncertainty values for M&TE equipment, Potential Transformer (PT)

accuracy, drift, and tolerance (band allowed for technician setting the relay) were used to

determine the nominal setpoint for the relays.

Since electrical undervoltage relays operate at voltage levels much less than the voltage

seen at the 4160 VAC bus, the voltage is stepped down through a PT to allow relay

operation. The PT ratio used at Davis-Besse corresponds to a 35 to 1 primary to

secondary turns ratio. Thus, at 2450 Volts on the primary side of the PT, the relay would

experience a voltage of 70 Volts. With uncertainties taken into account, the relays would

need to have been set at a voltage less than 70 volts; however, the relay (type NGV)

used at Davis-Besse was not rated for operation below 70 volts. The NGV relay is rated

for operation within a band of 70 volts to 120 volts. Since the relay could be physically

set below 70 volts, the licensee still used the relay, with a lower setting. The inspectors

noted that it is uncertain how this would have affected the relays operation; however,

since operation below rated values could cause additional inaccuracies in the relay, the

inspectors determined that an evaluation would need to be performed to determine the

effects of operating below the relays established vendor ratings. This evaluation had not

been performed by the licensee.

Additionally, the drift value used by the licensee was based upon observed calibration

data performed on relays prior to 1992. The value that was established (+/- 0.5V) was

based upon monthly as-found values. Based upon review of monthly functional results

on the relays from the past three years, the inspectors discovered that the drift actually

exceeded the +/- 0.5V value used in the calculation. In fact, one as-left value showed a

drift of 0.9V in the positive direction. Based upon this, the inspectors determined that the

23

drift value that was used by the licensee was poorly established and resulted in the use

of a non-conservative drift. Condition Report 02-06737 documented this issue.

The inspectors also questioned the absence of a value for uncertainties associated with

temperature effects on the relay. Since temperature effects for the most part were also

in the positive direction, the absence of such a value again would be non-conservative.

The licensee acknowledged this concern in CR 02-07646.

Additionally, the vendor manual for the NGV relay established an accuracy value for

dropout of the relay on undervoltage. Vendor documentation stated, On any dropout

operation, the voltage range from the beginning of the action to its completion is about

one percent of rated voltage. The rated voltage for the NGV relays is 120 volts.

Consequently, the accuracy of these relays is 1.2 volts. This meant that if an

undervoltage condition were to occur, the relay was not guaranteed to dropout until

the voltage reached 1.2 volts below the relay setting. Calculation C-EE-004.01-051 did

not account for this accuracy. The absence of this value again resulted in a

non-conservative value for the 59 percent Undervoltage Relays.

In accordance with Davis-Besse maintenance/testing procedures for these relays, the

upper band for the 59 percent Undervoltage Relay was 68 volts. If the more conservative

values had been accounted for in the calculation, and the NGV relay vendor-provided

accuracy had been accounted for, this value would have been lower. Additionally, had

temperature effects and the operation of the relay outside of its rated band been taken

into account, the upper voltage value could have been even lower. By not accurately

factoring in all the uncertainties, the licensees upper voltage limit allowed the setpoint for

the 59 percent Undervoltage Relay to be above the allowable value of 70 volts.

In addition, the results in calculation C-EE-004.01-051 established a Dropout Setting

Range for the relay as 65 to 69 volts. The calculation also stated that for operability

purposes, an undervoltage relay whose as-found operating voltage if found to be

greater than (>) 69.64 volts (2437.4 volts primary) will be considered to be outside the

bound of the Technical Specification allowable values. These conclusions were clearly

incorrect.

Not exceeding the upper voltage limit is important, because the undervoltage relay

should actuate at a value low enough so that inadvertent power supply transfers can be

prevented. Since both divisional sets of undervoltage relays were affected, this could

have potentially led to a premature loss of offsite power. However, since each division

had four relays for each safety-related 4160-Volt bus, and since the likelihood of an

occurrence of the type of limited undervoltage transient that would cause the relays to

drop out prematurely is small, the risk significance of this issue is very low.

10 CFR Part 50, Appendix B, Criterion III, Design Control, requires that Measures shall

be established to assure that applicable regulatory requirements and the design

basis...are correctly translated into specifications, drawings, procedures, and

instructions. Contrary to this requirement, the licensee failed to correctly calculate the

59 percent Undervoltage Relay TS allowable setpoint value.

24

This finding was determined to be more than minor because it affected the initiating

events cornerstone objective. This finding screened as Green in the SDP phase 1, since

this issue does not contribute to the likelihood of a Primary or Secondary system LOCA

initiator, does not contribute to both the likelihood of a reactor trip and the likelihood that

mitigation equipment or functions will not be available, and does not increase the

likelihood of a fire or internal/external flood. Because the finding was of very low safety

significance, and was captured in the licensees corrective action system, this finding is

being treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy

(NCV 50-346/2002-014-01k).

Inadequate Calculations for Control Room Operator Dose (GDC-19) and Off-Site Dose

(10 CFR Part 100)

High Pressure Injection Pump Minimum Flow Valves HP31 and HP32

The inspectors identified an unresolved item associated with correctly translating the

USAR commitments regarding calculations for General Design Criteria (GDC)19 and

10 CFR Part 100 requirements. The design of the HPI system has a single isolation

valve on each of the minimum flow return isolation lines to the borated water storage tank

(BWST). The teams review identified inadequate analysis of a single failure of the

minimum flow valve return check valve HP31/32 to close during the recirculation phase of

a postulated LOCA.

Note 1 of USAR Table 6.3-6 entitled Single Failure Analysis - Emergency Core Cooling

System, stated the following: The dose rate at the site boundary due to shine from

the Borated Water Storage Tank (BWST) has been evaluated for this case and found to

be 300 mr/hr. This was based on a site boundary minimum distance of 737 meters. The

flow through the line to the BWST was assumed to be 500 gallons (expected flow rate is

35 gpm). The activity entering the BWST was the activity in the Containment Vessel

Emergency Sump water, containing 50 percent of the core saturation inventory

consistent with licensee specifications. This activity was based on an assumed decay for

90 minutes, the time at which the recirculation mode is initiated, based on the worst RCS

break (0.1 ft2) for which the piggyback mode may be required. The dose rate was

determined by considering the BWST as a point source conservatively neglecting

self-attenuation of the water in the tank and not taking any credit for dilution with water

already in the lower portion of the tank.

Assumption 5, Sheet 3 of calculation 35.25, Dose Rate from BWST, states the

following: The input of the CTMT sump water into the BWST starts at 90 min after the

LOCA and lasts 10 min. Input rate is 50 GPM... This assumption of the total release

based on the 500 gallons did not appear to be conservative for the following reasons:

  • Use of an assumed 10 minutes for operator action could not be supported

because the most limiting single active failure for this scenario is a spurious

reopening of one of the minimum flow valve return check valves after valve

closure. Due to the lack of a safety grade alarm which indicates mispositioned

valves, the basis for the 10-minute assumption could not be validated by the

licensee.

25

  • Review of surveillance test procedure DB-SP-03218/03219 showed that the

indicated flow was approximately 50 gpm. However, the test configuration is

different from the post-LOCA recirculation phase. The test configuration

simulated the injection phase, where the HPI pump suction was aligned to the

BWST tank. The release configuration takes place in the recirculation, piggyback

mode, where the HPI pump suction is aligned to the discharge of the low head

injection (LPI) pumps. The discharge head of the LPI/DHR pumps would add to

HPI pumps, greatly increasing the discharge pressure, resulting in a significantly

higher flow than 50 gpm.

  • The assumption of a 90-minute delay was also non-conservative. Emergency

procedure DB-OP-02000 stated that the piggyback mode would be used for all

LOCAs which result in LPI flows less than 1100 gpm. The 90-minute assumption

appears to be based on the no LPI flow time calculation. USAR Section 6.3.2.11,

Reliability Considerations, states: Since LPI injection is not flowing in this

situation, it will take at least 100 minutes to empty the BWST with both HPI and

Containment Spray pumps running at design capacity, which gives the operator

an ample amount of time to determine the need for, and to perform the required

actions. Motor operators on the valves and hand switches in the control room are

installed to allow alignment from the control room. Based on the usable BWST

volume of 360,000 gallons and combined LPI flow of 2,200 gpm, the time at

which recirculation will take place is estimated to be approximately 60 minutes or

less (depending on the level and LPI flow instrument accuracy, actual

containment spray flow vs. the design flow, etc). Thus, a 90-minute delay is not

conservative.

  • The miniflow return line is located near the top of the BWST. During the event of

interest, the BWST level is significantly below the point of the return pipe entry.

The jet of a high pressure liquid at the temperature of about 200EF exiting the

pipe nozzle inside the tank will have an appreciable fraction of its liquid flash to

vapor along with the entrained gases. The remaining liquid could have a large

surface area as it travels downwards, liberating the remaining gases which have

partial pressures below the tank atmosphere. Thus the USAR statement and

calculation assumptions of iodine coming out of solution are correct and not

overly conservative, contrary to the statement made in the calculation.

Therefore, the critical inputs used for dose calculation (the assumed volume and the

activity decay time) appear to be non-conservative.

The calculation was silent on the impact on the GDC 19 limits. Part B of the calculation

dealt with the gaseous release.

The licensee issued CR 02-06701 to document the teams concern. This CR noted that,

...this issue involves past operability issues and must be considered a restart issue.

The inspectors questioned the licensee if the site boundary release described in Note 1

of USAR Table 6.3-6 was incorporated in the 10 CFR 100 or the GDC 19 calculations.

Based on this question and other related team questions, the licensee issued

26

CRs 02-07701 & 02-07713, which identified problems related to GDC 19 and 10 CFR

Part 100 calculations (see discussion below).

The licensee screened the three CRs as requiring resolution prior to the mode in which

ECCS was required by plant TS (Mode 4). In order to resolve the issues, the NRC

will need to assess the licensees reevaluation and the impact of the calculational

deficiencies on the GDC-19 and 10 CFR Part 100 regulatory limits. This issue will

remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-01l).

Other GDC 19 and 10 CFR 100 Issues

The inspectors identified an unresolved item associated with correctly translating USAR

commitments regarding calculations for GDC-19 and 10 CFR Part 100 requirements.

The inspectors review of the surveillance test procedures, USAR, calculations and

discussions with the licensee determined that the USAR calculated offsite dose was

based on an ECCS leakage rate of 1.6 gallons per hour (gph) while the allowable

leakage rate was based on 40 gph.

USAR Section 3.6.2.7.1.11 discusses a pump seal failure 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after a LOCA with an

assumed leak rate of 120 gpm. However, offsite dose calculations and control room

dose calculations for this postulated passive failure were not calculated. Some of the

(iodine) releases from this postulated leak would be in the ECCS pump rooms, which

were ventilated through safety grade charcoal filters. However, the iodine remaining in

the solution could come out of the system after it has been pumped to the radwaste

system. A leak in this area would be through a path outside of the ECCS pump room

ventilation filters. Also, the radwaste storage tank is not seismic and releases from the

area would not be filtered. It should be noted that calculation 36.28, ECCS - Pump Seal

Failure, Revision 0, determined the maximum acceptable leakage rate through the pump

seal as 82.7 gpm based on the control room dose (GDC 19). In response to the teams

question as to whether this calculation was current or superceded, the licensee

responded that no calculation that superceded calculation 36.28 could be located.

In response to the teams concerns described above, the licensee issued CR 02-07713.

This CR documented the above concerns and also stated the following:

In general, the dose contributions expected from these sources is

not large compared to other accident dose. However, in a fairly

short review time, the above issues were all identified. Therefore,

as noted above, a thorough extent of condition review should be

performed to look for identification of all required accident dose

contributors and consistent treatment of accident dose

contributions.

Additionally, CR 02-07713 documented that the control room operator doses evaluated

in USAR Section 15.4.6 were based on only the containment leakage contribution. The

doses resulting from expected fluid leakage from the ECCS post-LOCA were not

addressed. NRC Regulatory Guide 0737 requires such an evaluation to be performed.

27

The licensee screened CR 02-07713 as requiring resolution prior to the mode in which

ECCS was required by plant TS (Mode 4). In order to resolve the issue, the licensee will

need to assess the impact of the calculational deficiencies on the GDC-19 and 10 CFR

Part 100 regulatory limits This issue will remain unresolved pending the licensees

evaluation and the NRCs review (URI 50-346/2002-014-01m).

HPI Pump Operation Under Long Term Minimum Flow

The inspectors identified an unresolved item associated with adequately assessing HPI

pump operation under long term minimum flow. The team reviewed the licensees

response to NRC Bulletin 88-04 which directed licensees to evaluate the capability of

safety related pumps to run at minimum recirculation flow rates. For the HPI pumps, the

licensee had concluded that the supplied minimum recirculation flow was adequate. The

licensee had contacted the HPI pump vendor for information and the vendor responded

that, while there was no definitive data that would raise doubts concerning the HPI pump

miniflow, they were unable to confirm that these flows were adequate to ensure that HPI

pumps would not experience degradation as a result of the impeller recirculation. The

vendor further recommended that a pump test to verify the endurance be conducted

under actual miniflow conditions.

The licensee subsequently performed a test, which indicated low vibration readings when

in the minimum recirculation mode. The teams review of the test determined that the

test conditions appeared to be non-conservative. The test had been performed at normal

ambient temperature using BWST water which simulated the injection phase of the

accident rather than the recirculation phase which would experience significantly higher

fluid temperatures and possibly debris. Additionally, this was a one-time-only test,

hence, the effects of degradation, wear, and tear were not addressed. The licensees

assessment also did not address the allowable duration of operation at a minimum flow

condition. Based on the teams questions, the licensee issued CR 02-07684. This CR

noted that ...due to the importance of the pumps to perform their functions, and the

potential for extended periods of operation on minimum recirculation mode, this issue

should be considered a mode 3 restart constraint.

The licensee screened CR 02-07684 as requiring resolution prior to the mode in which

ECCS was required by plant TS (Mode 4). In order to resolve the issue, the licensee will

need to assess the ability of the HPI pumps to perform as intended during extended

operation on minimum flow. This issue will remain unresolved pending the licensees

evaluation and the NRCs review (URI 50-346/2002-014-01n).

HPI Pumps Minimum Flow, Unanalyzed SBLOCA Sizes

The inspectors identified an unresolved item associated with analyzing some small break

LOCA (SBLOCA) sizes. The inspectors review of the USAR and discussions with the

licensee determined that the SBLOCA analysis covered a spectrum of breaks starting at

0.01 sq. ft. USAR Sections 15.3.1.1 states Depending on the break location and

imposed boundary conditions, a break area can be identified for which the HPI or normal

makeup system is capable of matching the leak rate ensuring an orderly shutdown. For

example, the leak rate resulting from the rupture of a 3/4" schedule 160 instrument line

(0.002 ft2) is matched by the normal makeup system about 1000 seconds into a

28

postulated accident without a complete loss of the pressurizer liquid level. The HPI

pump minimum flow recirculation valves are closed prior to transferring to the

containment emergency sump following a loss of coolant accident (LOCA). If the HPI

pumps are not assured of injecting sufficient water into the Reactor Coolant System, the

pump flow may not be adequate for thermal protection (reference NRC Bulletin 88-04

minimum flow issues).

An example condition where this could be problematic is for very small break LOCAs that

later repressurize the RCS above the HPI shut-off head. An additional issue involves

performance of the water lubricated outboard bearing when on containment sump

recirculation. The concern is that at low flow rates, the bearing load may be higher and

the bearing could be less tolerant of debris.

The licensee contacted the NSSS vendor for discussion of smaller break sizes, between

the capacity of the makeup system and up to the 0.005 ft2 range, which were not covered

by the existing SBLOCA analyses. For these breaks, the vendor could not discount the

possibility of intermittent repressurization that would challenge the minimum HPI pump

flow requirements for both HPI trains.

In summary, the spectrum of the SBLOCA breaks from 0.002 to 0.01 sq. ft. breaks was

not analyzed and the impact on the HPI pumps ability to perform their safety-related

function was unknown prior to the inspectors questions. This scenario could

simultaneously affect both HPI trains, without any additional postulated single failures.

This CR noted that This issue needs to be resolved prior to restart.

Based on the inspectors questions, the licensee issued CR 02-06702 and screened the

CR as requiring resolution prior to the mode in which ECCS was required by plant TS

(Mode 4). In order to resolve the issue, the licensee will need to assess the ability of the

HPI pumps to perform as intended during extended operation on minimum flow. This

issue will remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-01o).

Inadequate Service Water System Flow Analyses

The licensee and the inspectors identified an unresolved item associated the licensees

SW system flow analysis in properly accounting for a number of required conditions. The

latest service water system flow calculation of record that was intended to demonstrate

the ability of the system to deliver the design basis flows to the various service water

system safety-related loads was C-NSA-000.00-017, PROTO-FLO Service Water

System Model. The inspectors reviewed this calculation and found that it non-

conservatively did not account for the following:

  • The lowest acceptable service water pump performance (the calculation utilized

the original vendor performance curves with no degradation margin).

  • Single failure of the forebay return valve SW-2930 to open, which required

opening SW-2929 in order to use deicing return flowpath, which was the highest

resistance pathway.

  • Design basis strainer resistance.
  • Strainer blowdown losses.

29

acceptance criterion for these valves was that back flow would not cause idle

pump rotation which, in fact, would require flows of several hundred gpm).

  • Removal of various check valve internals (valves were modeled as straight pipe).

Therefore, the ability of the system to provide the required design basis flows to the

safety-related heat exchangers could not be verified.

All of these deficiencies except for the pump discharge check valve leakage were also

identified by the licensee in the LIR and documented in CR 02-06438. Some were also

re-identified in the licensees Safety System Design and Performance Capability (SSDPC)

self-assessment and documented in CRs 02-6333 and 02-07745.

The licensee screened the three CRs as requiring resolution prior to the mode in

which the SW system was required by plant TS (Mode 4). In order to resolve the issue,

the licensee will need to assess the service water system flow requirements against the

yet-to-be-performed analyses that demonstrate the ability of the system to provide the

required flows to safety-related loads under design basis conditions. This issue will

remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-01p).

Definition of Passive Failure

During the review of the single-failure effects in the SW system, the inspectors postulated

a passive failure in valve SW-82. The inspectors requested the licensees analysis for

assuming that valve SW-82 failed closed and could not be reopened; for example, if the

valve had a stem-to-disc separation. The licensee stated that other failures of valve

SW-82 had been assessed previously and documented in PCAQR 91-0611, but that they

did not consider a stem-to-disc separation as either credible or required to be assumed as

part of a passive failure analysis.

The inspectors disagreed with the licensees position that stem-to-disc separation was not

credible and also disagreed with the licensees position that stem-to-disc separation was

not required to be assumed as part of a passive failure analysis.

This matter will be referred to the Office of Nuclear Reactor Regulation. Pending the

results of that deferral this item will remain unresolved (URI 50-346/2002-014-05).

Inadequate Service Water System Thermal Analyses

The inspectors identified an unresolved item associated with the licensees SW system

thermal analysis properly accounting for a number of required conditions. The inspectors

reviewed several calculations that were intended to establish the design basis

temperature profile for the Ultimate Heat Sink (UHS). The UHS temperature profile

information generated in these calculations was required as an input to the SW heat

exchanger thermal performance calculations, which were intended to demonstrate their

30

ability to remove their design basis heat loads without exceeding their individual design

temperature limits.

The inspectors identified a number of non-conservatisms (listed below) in the UHS

calculations and in the measurement of service water temperatures. As a result, the

calculated time-dependent service water temperature profile, which was input to all of the

SW system heat exchanger performance analyses, was determined to be

non-conservative:

  • The UHS analyses did not consider a postulated single failure-to-open of the

forebay return valve, SW-2930. Failure of valve SW-2930 to open is the worst

case system lineup with respect to SW system temperature profile, since it would

redirect service water to the forebay through the deicing line. This flowpath

returned the heated service water directly in front of the service water pump house

trash bars rather than at the opposite end of the forebay, which was the normal

post-accident return discharge point. Therefore, the returned water had a much

lower heat rejection opportunity than from the normal return point.

  • The licensee had analyzed the deicing flowpath and determined a higher UHS

temperature profile would result. The forebay return path resulted in a peak of

112.6EF instead of 107.6EF for the normal accident flowpath; however; only the

lower value was used as input for all service water heat exchanger calculations.

An additional non-conservatism was that the calculation only considered the clean

pond condition, (i.e., with no silting).

  • Calculation 12501-M-00004, UHS Pond Performance Analysis - Max Evaporation

- Silting, addressed the UHS thermal performance and volume for 1.5 feet of

silting in the forebay; however, it did not consider the deicing return flowpath.

  • The design basis initial service water temperature used for all heat exchanger

analyses was 90EF. This was reflected by TS 3.7.5.1.b, which limited the UHS

temperature (not service water temperature) to an average of #90EF. A single

instrument was used for determining compliance with this TS. It was located in

front of the service water pump house trash bars, approximately two feet above

the pond bottom. However, as early as 1995, the service water system supply

header temperature had been measured with very accurate measurement and

testing instrumentation (M&TE) at approximately 1.5EF to 2EF warmer than the

readings from the TS instrument. This information indicated three non-

conservatisms with the service water heat exchanger analyses and the UHS

thermal analyses as follows:

- With the indicated UHS temperature at the TS 90EF limit, the actual

temperature entering the heat exchangers could be as much as 2EF higher

than the analyzed condition, significantly reducing their performance,

potentially below design basis values.

- All UHS pond analyses started with an assumed uniform pond temperature of

90EF. The observed temperature offset during normal operation between the

31

UHS pond temperature near the bottom and the service water header

temperature indicated that the service water delivered to the heat exchangers

was a mixture of warmer, upper-strata pond water with the cooler near-bottom

water. Therefore, the temperature as read from the TS instrument was also

not indicative of the average [UHS] water temperature as required by the TS.

Rather the true average UHS temperature was somewhat higher than the

monitored temperature at the TS instrument. Therefore, the UHS analyses

contained non-conservative initial temperatures with respect to the indicated

TS value.

- The UHS analyses were based on a time-dependent model that started with

uniform pond temperature at 90EF, and the hotter returning service water

entering the pond near the surface and displacing the uniform temperature

water downward toward the entrance to the intake structure. However, this

was a non-conservative model with respect to the actual stratification indicated

by the temperature observations. With stratification existing during normal

operation, hotter water would reach the service water intakes sooner than the

model predicted for accident conditions.

  • None of the UHS analyses accounted for the spent fuel pool (SFP) heat load

which is initially shed from the component cooling water (CCW) system (cooled by

service water) early in an accident, but must be restored by operator action at a

later time to prevent exceeding the SFP design temperature, 150EF. The design

basis analyses indicated that the fuel pool would not only exceed 150EF very

quickly, but would reach boiling within ten hours of loss-of-cooling (SFP heat load

was significantly increased with the high density fuel storage modifications). There

were no analyses that addressed the structural or leak-tight integrity of the SFP,

the thermal-hydraulic capability, e.g., restart capability of the SFP cooling system,

or the ability to provide makeup to the SFP for conditions beyond its design basis

temperature. The inspectors estimated this additional heat load at eight to ten

million BTUs per hour.

  • The inspectors also identified that the ECCS pump room temperature analyses,

Calculation 12501-M-003, ECCS Pump Room Temperature, did not consider the

probable worst-case heat loads from pump motors and piping that would be

associated with the high pressure injection (HPI) pumps operating in the piggyback

mode.

Therefore, the ability of the service water system to provide the required design

basis heat transfer thermal conditions for the safety-related heat exchangers could

not be verified.

The licensee entered the issue into its corrective action program as CRs 02-05372,

02-06177, 02-06332, 02-06336, 02-06370, 02-07004, and 02-07716 and screened the

CRs as requiring resolution prior to the mode in which the SW system was required by

plant TS (Mode 4). In order to resolve the issue, the licensee will need to assess the

service water system thermal requirements. This issue will remain unresolved pending

the licensees evaluation and the NRCs review (URI 50-346/2002-014-01q).

32

Inadequate Ultimate Heat Sink Inventory Analyses

The inspectors identified an unresolved item associated with the licensees UHS inventory

analysis properly accounting for a number of required conditions. USAR Section 9.2.5.1,

Loss of Intake Canal, stated, The water stored in the intake forebay below elevation

562 feet will provide sufficient cooling surface to continue cooling the station by

evaporation for at least 30 days. The inspectors determined that the plants UHS water

inventory analysis of record, Calculation 12501-M-00004, UHS Pond Performance

Analysis - Max Evaporation - Silt, did not adequately account for the following water loss

pathways:

  • During normal operation the service water system return water is routed through

valve SW-2931 to the plant cooling tower to provide its makeup (this routing does

not return the water to the UHS). In order to preserve UHS water inventory during

accident conditions, this valve is closed, and the water is returned to the UHS

(either through the forebay return valve SW-2930, or if it has failed to open,

through the deicing return valve SW-2929). However, the single failure of the

cooling tower return valve to close on demand would cause a substantial water

loss from the UHS through this pathway (30 inches diameter) that was not

accounted for in the calculation.

USAR Section 9.2.1.2 stated that for this condition, the operator could manually

close SW-2931 within three hours. However, this statement was valid only for an

electrical failure where the operator could manually close the valve, but would not

necessarily be valid for a mechanical failure. Additionally, the existing analyses did

not account for even this three-hour water loss.

the service water system. However, the licensee did not account for UHS water

loss through this pathway for events that would require AFW operation. For such

events, it was assumed that the non-seismically qualified condensate storage tank

(CST) would supply AFW, with no decay heat or reactor coolant system (RCS)

sensible heat rejected to the UHS for thirteen hours. This was a non-conservative

assumption; there would be more net inventory loss from the UHS with the AFW

supply from the service water system than from the CST.

  • Evaporation losses were based on the incorrect UHS temperatures described

earlier in the report. With higher actual UHS surface temperatures, evaporation

losses would be higher than calculated.

Therefore, the ability of the UHS to provide the required design basis inventory to support

operability of the service water system for the required 30 days could not be verified.

The licensee entered the issue into its corrective action program as CRs 02-05986,

02-06332, 02-06336, and 02-07692 and screened the CRs as requiring resolution prior

to the mode in which the SW system was required by plant TS (Mode 4). In order to

resolve the issue, the licensee will need to assess the impact of the calculational

deficiencies on the ability of the UHS to perform its intended function. This issue will

33

remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-01r).

No Valid Service Water Pump Net Positive Suction Head Analysis

The licensee identified an unresolved item associated with a lack of a valid net positive

suction head analysis for the SW pumps. USAR Section 9.2.5.1 contained a discussion

of the adequacy of the service water pumps net positive suction head (NPSH) for all

design basis conditions. However, the licensee could provide no valid design basis

analysis that demonstrated this adequacy and the adequacy of the pump submergence

with respect to vortex prevention. Additionally, even if such an analysis had been

available, it would have likely been rendered non-conservative by the previously described

issues related to non-conservative UHS water inventory and temperature analyses.

Therefore, the ability of the system to perform its design basis safety function for all

conditions of reduced available NPSH and pump submergence within the design bases

could not be verified.

This concern was also identified by the licensee in the LIR, documented on CR 02-05923,

and screened as requiring resolution prior to the mode in which the SW system was

required by plant TS (Mode 4). In order to resolve the issue, the licensee will need to

assess the impact of the licensees failure to correctly translate the USAR commitments

with respect to adequacy of service water pumps NPSH and vortex margin into analyses

demonstrating adequacy. This issue will remain unresolved pending the licensees

evaluation and the NRCs review (URI 50-346/2002-014-01s).

Inadequate Service Water System (and Other Systems) Overpressure Protection

The design of the service water system was performed under the requirements of

ASME Code,Section III, Article NB-7000, Protection Against Overpressure.

Paragraph NB-7155 required that Individual pressure-relief devices shall be installed

for the overpressure protection of components which are isolable from the normal system

overpressure protection. Contrary to this requirement, none of the service water system

individual heat exchangers and associated piping that were isolable from the system were

provided with individual overpressure protection. Other safety-related system heat

exchangers, such as the decay heat removal and diesel generator jacket water heat

exchangers, were also found to not be provided with individual overpressure protection

devices.

Paragraph NB-7153, Provisions When Stop Valves are Used, required, No stop valve or

other device shall be placed relative to a pressure-relief device so that it could reduce the

overpressure protection below that required by these rules, unless such stop valves are

constructed and installed with positive controls and interlocks so that the relieving-capacity

requirements of NB-7400 are met under all conditions of operation of both the system and

the stop valves. Contrary to this requirement, many of the safety-related components in

the plant that were provided with relief devices also had manual isolation valves between

the components and the relief devices.

These conditions were identified by the inspectors as a result of review of

Modification 94-0009, Service Water Thermal Relief Valve Replacement for

34

Containment Air Coolers [CACs], which removed these valves from the CACs and did

not replace them. These valves had been initially installed by Modification 88-0234,

Overpressure Protection for the Containment Air Coolers, when it was determined that

the coolers were not originally provided with relief valves and, therefore, did not meet

Code requirements, as documented in PCAQR Number 88-0737. Discussions with

licensee engineers determined that this condition extended to other plant systems and

also that some of the relief valves that were installed had the prohibited isolation valves.

The licensee maintained that these conditions were acceptable based on their

interpretations of the Code. These interpretations and the inspectors responses follow:

On the concern of relief protection not provided:

  • The licensee maintained that the heat exchangers in question were not designed

to the Code. However, the attached non-isolable piping was; therefore, by default,

in the inspectors view, they were required to meet Code requirements.

  • The licensee stated that heat exchangers in operation were not isolated and thus

could not be thermally overpressurized; therefore, they were not required to be

protected. The licensee also stated that heat exchangers not in operation, i.e.,

not performing their cooling function but still filled with water, were not required by

the Code to be protected. Therefore, per these interpretations, relief protection

was never required for heat exchangers and associated piping under any

condition, whether in operation or not. The only other condition that could exist

was - not in operation and not filled with water, in which case, relief protection was

not required. Therefore, there was no condition - in operation, out of operation, or

completely disabled - for which the Code was applicable, which defied the obvious

intent of the Code. As reflected in Paragraph NB-7155, a heat exchanger is in

operation when it is completely filled with water, regardless of whether it is in

service or not, or isolated or not. The Codes only concern is whether the

component is isolable, because that was the only condition when the potential

to be overpressurized by isolation exists.

The conditions of concern for which the Code requirements were created were

for when heat exchangers and associated piping were filled with liquid

(incompressible), when they were isolated or could be required to be isolated, for

instance, as part of their operational mission, and therefore, when they could be

subjected to heating that could cause overpressurization. Many safety-related

heat exchangers and associated piping fell into these categories because they

could be in standby and fully isolated during normal operation, or partially isolated

and could be required by accident conditions to become fully isolated, such as the

CACs, which may be required to be fully isolated for containment isolation.

Additionally, isolation of the CACs for maintenance could subject them to

undetected overpressure that could compromise their leak tightness, which is one

of their safety functions as a containment barrier.

  • The licensee maintained that heat exchangers were protected from overpressure

by plant procedures that prevented them from being isolated when they were filled.

However, the Code made no allowances for such administrative controls. The

35

licensee, however, stated that Paragraph NB-7153's allowance of positive

controls permitted the use of administrative controls in lieu of protection devices.

The inspectors disagreed for two reasons: first, that paragraph was applicable only

to the use of stop valves between relief devices and the components being

protected (which is addressed with the next concern), not valves that isolate the

components from the system. Second, in the context of that paragraph and all of

Article NB-7000, controls clearly refers to instrumented control devices, not

administrative controls. For example, the last sentence in this Code paragraph

discussed verification testing of such controls, which could not be appropriately

applied to administrative controls.

  • The licensee stated that not having such devices could, at worst, result in slight

yielding of the components. Such yielding is not allowed by the Code for design

conditions for such components.

  • The licensee stated that isolated heat exchangers other than the CACs could not

be subjected to temperatures nearly as high as the CACs, and therefore, would

not experience high stresses. Contrary to this, industry experience has shown that

heat exchangers filled solid with water can be subjected to very high stresses and

failure with relatively small temperature changes.

Regarding the concern of isolation valves between the protected components and the

relief devices:

  • The licensee stated that isolation valves were allowed between the relief devices

and the components being protected by Paragraph NB-7153, as long as they were

administratively controlled. However, as discussed above, the only controls

allowed by this paragraph were control devices that were constructed and

installed. In common parlance, administrative controls cannot be constructed

and installed and their operability cannot be verified by test, as also required

by this paragraph.

In response to the inspectors concerns, the licensee generated CR 02-06860.

The licensee disagreed with the inspectors observations and stated that to their

knowledge they were in compliance with all code requirements. This matter will be

referred to the Office of Nuclear Reactor Regulation. Pending the results of that deferral

this item will remain unresolved (URI 50-346/2002-014-06).

Service Water Source Temperature for Auxiliary Feedwater System

The inspectors identified an unresolved item associated with the licensees analysis for

the elevated temperature effects on the AFW system. Section 9.2.1.1, of the USAR

[Service Water System] Design Basis, states that, The service water system also

provides a backup source of water to the auxiliary feedwater [AFW] system... Although

the condensate storage tank was the preferred water source because of its high water

quality, this tank was not seismically qualified. The service water system, therefore,

provided the seismically-qualified, safety-related backup water source. The inspectors

determined that the service water source for AFW had not been analyzed with respect to

36

its potentially higher temperature condition for various design basis events and the

possible impact on the ability of the AFW system to perform its safety function. Such

effects could include reduced heat absorption capability for AFW injected into the steam

generators and inadequate cooling of AFW lubricating oil. Therefore, the ability of the

AFW system to perform its safety function using the service water source for all design

basis events for which it may be required could not be verified.

Elements of this concern were identified by the licensees LIR in CR 02-06107. The

licensee entered the entire issue into its corrective action program as CR 02-05923 and

screened the CR as requiring resolution prior to the mode in which the SW system was

required by plant TS (Mode 4). In order to resolve the issue, the licensee will need to

assess the impact of the increased SW temperature on the operability of the AFW pumps.

This issue will remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-01t).

Short Circuit Calculations

The inspectors identified an unresolved item associated with the licensees analysis for

postulated short circuits. During the performance of the original calculations the licensee

used normal operating voltages instead of maximum voltages. At the higher voltages

some results may no longer be acceptable (e.g., if rated for 25,000 amps (25 kva) it may

now see 26 kva). This could result in some breakers not tripping and causing the fault to

propagate upwards to the 13.8 kv buses. The licensee had identified this issue about a

year ago, but the observation was being treated as an administrative issue only. In fact, if

a fault propagated upward, the fault could end up resulting in a loss of both normal power

supplies.

The licensee entered the issue into its corrective action program as CRs 02-06837

and 02-06302 and screened the CRs as requiring resolution prior to the mode in which

the 4160VAC was required by plant TS (Mode 4). In order to resolve the issue, the

licensee will need to assess the impact of the higher voltages on the licensees short

circuit calculations and the effect upon the safety-related 4160VAC buses. This issue

will remain unresolved pending the licensees evaluation and the NRCs review

(URI 50-346/2002-014-01u).

Inadequate Analytical Basis for the Setpoint to Swap Service Water System Discharge

Path

The inspectors identified a Green finding that is being treated as an additional example

of a Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control,

associated with assurance that applicable regulatory requirements and the design basis

for structures, systems, and components were correctly translated into specifications,

drawings, procedures, and instructions when licensee personnel could not find an

analytical basis for the setpoint to swap service water system discharge path.

The service water system discharges into one of four paths. Two of these paths (cooling

tower makeup and the collection box) were not seismically qualified and provisions were

made in the design of the system to automatically divert flow to the seismically qualified

discharge lines (intake forebay and intake structure) in the event of obstruction of one of

37

the non-seismic lines. The setpoint for the swapover is 50 psig. The inspectors asked

licensee personnel for the calculational bases for this setpoint. Licensee personnel could

not locate an analysis.

Not having an analytical basis is of concern for two reasons. First, the plant could have

experienced a seismic event which did not fully obstruct the discharge path for service

water such that pressure would have been slightly less than the 50 psig setpoint and flow

would have been choked down. This extent of flow reduction should have previously been

evaluated to demonstrate the ability of the service water system to provide sufficient

cooling capability to survive a safe shutdown earthquake. Second, a passive failure

causing a similar flow reduction as above could have gone undetected during an event

which required design service water flow and design service water flow would not have

been demonstrated to be available. A suitable analysis which demonstrates acceptability

in these conditions was needed. The inspectors determined that the failure to have an

analysis which demonstrates acceptability of conditions with service water discharge

header pressure elevated higher than normal and up to the swapover setpoint could affect

the design function of the service water system.

10 CFR Part 50, Appendix B, Criterion III, Design Control, requires that Measures shall

be established to assure that applicable regulatory requirements and the design

basis...are correctly translated into specifications, drawings, procedures, and instructions.

Contrary to this requirement, the licensee failed to provide a basis for the setpoint to swap

the service water system discharge path.

The inspectors considered this finding more than minor because it could affect the

mitigating systems cornerstone objective of ensuring the capability of systems that

respond to initiating events to prevent undesirable consequences attributable to design

control. Using the significance determination process, the safety significance was

determined to be very low (Green) because the finding did not screen as potentially risk

significant due to a seismic, fire, flooding, or severe weather event. This violation is being

treated as a Non-Cited Violation (NCV 05000346/2002-014-01v) because of the very low

safety significance of this condition and because licensee personnel entered this finding in

the corrective action program as CR 02-07802. This condition report documents licensee

personnels intentions to check the adequacy of the setpoint.

.6 Safety System Inspection and Testing

a. Inspection Scope

The team reviewed the program and procedures for testing and inspecting designated

components of the selected systems. The review included the results of TS required

surveillance tests and ASME Code required quarterly in service tests conducted since

1994.

38

b. Observations and Findings

HPI Quarterly Surveillance Test Instrumentation Issues

The inspectors identified a minor Violation of 10 CFR 50, Appendix B, Criterion XI, Test

Control. Specifically, the inspectors review of the HPI pump quarterly tests identified that

the procedures specified M&TE instrumentation to be installed to improve the accuracy

of the test. The procedures specified three allowable instrument ranges for HPI pump

discharge pressure; however, two of the three specified instrument ranges (0-2500 psig,

0-3000 psig) were non-conservative when compared to the instrumentation range

(0-2000 psig) and readability specified in calculation C-NSA-052.01-003, HPI Pump

Acceptance Criteria, prepared in support of the above test procedures. Based on this

discrepancy, the licensee issued CR 02-07466.

10 CFR 50, Appendix B, Criterion XI, requires, in part, that adequate test

instrumentation is available and used. Contrary to this requirement, the licensee

specified non-conservative instrumentation ranges in the HPI quarterly surveillance test

procedure.

This finding screened as minor because the impact of the non-conservative test

instruments upon the readings was minimal. Although the failure to specify the

appropriate test instrumentation will be corrected, it constitutes a violation of minor

significance that is not subject to enforcement action in accordance with Section IV of the

USNRCs Enforcement Policy.

SW Surveillance Test Does Not Use Worst Case Values

The inspectors identified a Green finding that is being treated as a Non-Cited Violation of

10 CFR Part 50, Appendix B, Criterion XI, Test Control. Specifically, the inspectors

identified that the service water train valve test did not appear to demonstrate that worst-

case post-accident conditions were bounded. Based on the teams questions, the

licensee issued CR 02-07781 which provided a detailed discussion of the shortcomings of

the procedure which included lack of trending, failure to declare the valve(s) inoperable,

etc.

10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part, that testing be

performed in accordance with written test procedures which incorporate the requirements

and acceptance limits contained in applicable design documents. Contrary to this

requirement, the service water train valve test did not appear to demonstrate that worst-

case post-accident conditions in design documents were bounded.

This finding was determined to be more than minor because it affected the mitigation

systems cornerstone objective. This finding screened as Green in the SDP phase 1,

since this issue was a testing deficiency that was confirmed not to result in loss of function

in accordance with GL 91-18 (Rev. 1). Because the finding was of very low safety

significance, and was captured in the licensees corrective action system as CR 02-07781,

this finding is being treated as an NCV consistent with Section VI.A.1 of the NRC

Enforcement Policy (Section 1R05.02) (NCV 50-346/2002-014-02a).

39

ECCS Sump Pump Test Acceptance Criteria

The inspectors identified a minor violation of 10 CFR Part 50, Appendix B, Criterion XI,

Test Control. USAR Section 3.6.2.7.1.14 states that the capacity of each ECCS room

sump pump is approximately 75 gpm. USAR Sections 3.6.2.7.1.8 and 3.6.2.7.1.10 state

that the submersible duplex sump pumps in rooms number 105, 113, and 115 have a total

capacity of approximately 150 gpm (75 gpm per pump). This is greater than the assumed

120 gpm DHR seal leakage. The teams review of the ECCS Sump Pump Flow Check,

DB-SP-04162 identified that its acceptance criterion was 50 gpm per pump. In addition,

the test does not verify whether water is pumped from sump to sump (via leaking check

valves) or to the intended tank. Based on the teams questions the licensee issued

CR 02-07741, which stated that this issue should be considered a restart issue.

10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part, that testing be

performed in accordance with written test procedures which incorporate the requirements

and acceptance limits contained in applicable design documents. Contrary to this

requirement, the acceptance criteria for the ECCS Sump Pump Flow Check was incorrect.

This finding screened as minor because the actual ECCS sump pump performance was

determined to be approximately 75 gpm. This was greater than the largest assumed

ECCS leakage in the drainage area. Although the failure to utilize an appropriate test

acceptance criterion will be corrected, it constitutes a violation of minor significance that is

not subject to enforcement action in accordance with Section IV of the USNRCs

Enforcement Policy.

Inadequate Service Water System Flow Balance Testing

The inspectors identified an unresolved item associated with the licensees SW system

flow balance testing procedure properly accounting for a number of required conditions.

Surveillance Procedures DB-SP-03000 and 03001, Service Water Integrated Train I(II)

Flow Balance Procedure, were performed every refueling outage to balance the system

flows. The inspectors identified that this procedure did not establish flows to the safety-

related heat exchangers based on worst-case design basis conditions, such as degraded

service water pumps, lowest UHS level, highest resistance SW system lineup, system

resistance degradation, etc. Further, no analyses existed that established the test

acceptance criteria for design basis conditions. Therefore, the flow balance procedure did

not verify that the system was capable of providing the required flows to its safety-related

heat exchangers under design basis conditions.

Additionally, the inspectors noted that standard plant practice was to inspect the system at

the beginning of each refueling outage and to perform maintenance as required to remove

sediment, clean heat exchangers, and other system performance-improvement

maintenance activities prior to performing the flow balance. No analyses had been

performed of the as-found conditions. Therefore, the flow balances demonstrated the

systems operability only in the newly cleaned, groomed condition.

The licensee entered the issue into its corrective action program as CR 02-06064 and

screened the CR as requiring resolution prior to the mode in which the SW system was

required by plant TS (Mode 4). In order to resolve the issue, the licensee will need to

40

assess the impact of the as-found SW flow balance against the revised analysis being

performed by the licensee. This issue will remain unresolved pending the licensees

evaluation and the NRCs review (URI 50-346/2002-014-02b).

Inadequate Corrective Actions for Service Water Pump Discharge Check Valves

The inspectors identified a Green, Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion XVI when licensee personnel failed to take proper corrective action to correctly

change the acceptance criterion for the inservice full flow test for the service water pump

discharge check valves to a proper value when it was determined to be non-conservative.

The ASME Code requires check valves to be tested to either the full open position or to

the position required to perform their safety function. Prior to 2002, licensee personnel

were testing the service water pump discharge check valves for their inservice test for the

forward flow direction with an acceptance criterion which required system flow to exceed

9300 gpm to pass the test. An internal audit by Quality Assurance personnel noted that

this acceptance criterion was non-conservative. As a result, the acceptance criterion was

changed to 10,000 gpm in February 2002.

The inspectors questioned licensee personnel about the basis for the acceptance criterion

since in the USAR a design flow of 10,250 gpm was specified. Licensee personnel

acknowledged the discrepancy and initiated condition report CR 02-07657 to address it.

The explanation was that when licensee personnel made the initial change to the

acceptance criterion for flow, they had not taken all available information into account

when choosing the new setpoint. The inspectors determined that the failure to choose a

proper acceptance criterion for the inservice full flow test for the service water pump

discharge check valves could lead licensee personnel to accept test results which would

not ensure that the check valve was capable of passing its safety function flow.

10 CFR Part 50, Appendix B, Criterion XVI requires in part that measures shall be

established to ensure that conditions adverse to quality, such as non-conformances were

promptly identified and corrected. Contrary to the above, in February 2002, licensee

personnel did not properly correct the acceptance criterion for the service water pump

discharge check valves inservice full flow test when they first recognized it was not

correct.

This finding was more than minor because it could affect the mitigating systems

cornerstone objective of ensuring the capability of systems that respond to initiating

events to prevent undesirable consequences attributable to poor maintenance procedure

quality. Using the significance determination process, the safety significance was

determined to be very low (Green) because the finding did not screen as risk significant

due to a seismic, fire, flooding, or severe weather event. This violation is being treated as

a Non-Cited Violation (NCV 05000346/2002-014-03d) because of the very low safety

significance of this condition and because licensee personnel entered this finding in the

corrective action program as CR 02-07657.

41

4OA6 Meetings

Exit Meeting Summary

The NRC inspectors presented the results of this inspection during exit meetings with

Mr. L. Myers and other members of licensee management on November 13, 2002. The

licensee acknowledged the findings presented. Inspectors asked the licensee whether

any materials examined during the inspection should be considered proprietary. No

proprietary information was identified.

42

KEY POINTS OF CONTACT

Davis-Besse

L. Myers, Chief Operating Officer

R. Fast, Plant Manager

T. Chambers, Work Week Manager

J. Powers, Engineering Director

P. Roberts, Maintenance Manager

M. Roder, Operations Manager

J. Rogers, Plant Engineering Manager

R. Slyker, Licensing Staff Engineer

H. Stevens, Quality Assurance Manager

G. Wolf, Licensing Staff Engineer

Nuclear Regulatory Commission

J. Grobe, Chairman, Davis-Besse Oversight Panel

C. Lipa, Chief, Reactor Projects Branch 4

S. Thomas, Senior Resident Inspector

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-346/02-14-01a NCV Lack of a design basis analysis for containment isolation

valve backup air supplies

50-346/02-14-01b NCV Inadequate blowdown provisions for CAC backup air

accumulators

50-346/02-14-01c URI Failure to perform comprehensive Moderate Energy Line

Break analysis

50-346/02-14-01d URI Lifting of Service Water Relief Valves

50-346/02-14-01e URI Inadequate SW pump room temperature analysis

50-346/02-14-01f URI Inadequate SW pump room steam line break analysis

50-346/02-14-01g URI Inadequate cable ampacity analysis

50-346/02-14-01h URI Inadequate flooding protection for the SW pump house

50-346/02-14-01i NCV Non-conservative TS value for 90 percent undervoltage

relays

43

50-346/02-14-01j URI Poor quality calculation for 90 percent undervoltage relays

50-346/02-14-01k NCV Non-conservative relay setpoint calculation for the 59

percent undervoltage relays

50-346/02-14-01l URI Inadequate calculations for control room operator dose

(GDC-19) and offsite dose (10 CFR Part 100) related to HPI

pump minimum flow valves

50-346/02-14-01m URI Other GDC-19 and 10 CFR Part 100 issues

50-346/02-14-01n URI HPI Pump Operation Under Long Term Minimum Flow

50-346/02-14-01o URI Some small break LOCA sizes not analyzed

50-346/02-14-01p URI Inadequate SW flow analysis

50-346/02-14-01q URI Inadequate SW thermal analysis

50-346/02-14-01r URI Inadequate UHS inventory analysis

50-346/02-14-01s URI No Valid Service Water Pump Net Positive Suction Head

Analysis

50-346/02-14-01t URI SW source temperature analysis for AFW

50-346/02-14-01u URI Inadequate short circuit calculations

50-346/02-14-01v NCV No analytical basis for the setpoint to swap service water

system discharge path

50-346/02-14-02a NCV SW surveillance test did not use worst case values

50-346/02-14-02b URI Inadequate SW system flow balance testing

50-346/02-14-03a URI Inappropriate SW pump curve allowable degradation

50-346/02-14-03b URI Repetitive failures of SW relief valves

50-346/02-14-03c URI Non-Conservative Difference in UHS Temperature

Measurements

50-346/02-14-03d NCV Inadequate corrective actions related to SW pump discharge

check valve acceptance criteria

50-346/02-14-03e URI Non-conservative containment air cooler mechanical stress

analysis

44

50-346/02-14-04 NCV Failure to perform TS surveillance requirement for HPI pump

following maintenance

50-346/02-14-05 URI Question regarding the definition of a passive failure

50-346/02-14-06 URI Question regarding licensee compliance with code relief

valve requirements

Closed

None

Discussed

None

45

LIST OF ACRONYMS USED

AC Alternating Current

ASME American Society of Mechanical Engineers

AFW Auxiliary Feedwater

B&W Babcock and Wilcox

BWST Borated Water Storage Tank

CAC Containment Air Cooler

CFR Code of Federal Regulations

CR Condition Report

CST Condensate Storage Tank

CTMU Cooling Tower Makeup

DHR Decay Heat Removal

ECCS Emergency Core Cooling System

GDC General Design Criteria

GL Generic Letter

gpm Gallon Per Minute

HPI High Pressure Injection

LER Licensee Event Report

LIR Latent Issues Review

LOCA Loss of Coolant Accident

LOOP Loss of Off-Site Power

LPI Low Pressure Injection

MCC Motor Control Center

MELB Moderate Energy Line Break

M&TE Measurement and Testing Instrumentation

MOV Motor Operated Valve

NCV Non-Cited Violation

NRC Nuclear Regulatory Commission

PCAQR Potential Conditions Adverse to Quality Report

PDR Public Document Room

psig pounds per square inch gage

PT Potential Transformer

RCS Reactor Coolant System

RPV Reactor Pressure Vessel

SBLOCA Small Break Loss of Coolant Accident

SDP Significance Determination Process

SSCs Systems, Structures and Components

SSDPC Safety System Design and Performance Capability

SFP Spent Fuel Pool

SW Service Water

TS Technical Specifications

UFSAR Updated Final Safety Analysis Report

UHS Ultimate Heat Sink

URI Unresolved Item

USNRC United States Nuclear Regulatory Commission

VAC Volts Alternating Current

VDC Volts Direct Current

46

LIST OF DOCUMENTS REVIEWED

The following is a list of licensee documents reviewed during the inspection, including documents

prepared by others for the licensee. Inclusion on this list does not imply that NRC inspectors

reviewed the documents in their entirety, but that selected sections or portions of the documents

were evaluated as part of the overall inspection effort. Inclusion on this list does not imply NRC

acceptance of the document, unless specifically stated in the inspection report.

Calculations

C-EE-003.02-012 Protective Relay Setpoint for Transformer BD (Bkr Revision 2

HBBD)

C-EE-004.01-001 Protective Relay Setpoint for Service Water Pump Revision 4

Motor 1-1 (AC107)

C-EE-004.01-002 Protective Relay Setpoint for Service Water Pump Revision 4

Motor 1-2 (AD107)

C-EE-004.01-003 Protective Relay Setpoint for Service Water Pump Revision 2

Motor 1-3 (AC 109)

C-EE-004.01-004 Protective Relay Setpoint for Service Water Pump Revision 2

Motor 1-3 (AD109)

C-EE-004.01-009 Protective Relay Setpoint Calculation for High Pressure Revision 2

Injection Pump Motor 1-1 (AC111)

C-EE-004.01-010 Protective Relay Setpoint Calculation for High Pressure Revision 1

Injection Pump Motor 1-2 (AD111)

C-EE-004.01-030 Protective Relay Setpoint Calculation for 4.16 kV Revision 3

Feeder Ground Relays

C-EE-004.01-031 Protective Relay Setpoint Calculation for Ground Fault Revision 3

Protection - 4.16 kV Buses C1 & C2

C-EE-004.01-032 Protective Relay Setpoint for Incoming to Transformer Revision 2

DF1-1 (Bkr AD1DF11)

C-EE-004.01-033 Protective Relay Setpoint for Incoming to Transformer Revision 4

DF1-2 (Bkr AD1DF12)

C-EE-004.01-038 Protective Relay Setpoint Calculation for Incoming Revision 4

Transformer CE1-1

C-EE-004.01-039 Protective Relay Setpoint Calculation for Incoming to Revision 2

Transformer CE1-2 (Bkr AC1CE12)

C-EE-004.01-043 Protective Relay Setpoints for Ground Fault Protection Revision 3

- 4.16 kV Buses D1 & D2

47

C-EE-004.01-046 4.16 kV Short Circuit Calculations July 8, 1991

C-EE-004.01-047 Protective Relay Setpoint Calculation for Phase Fault Revision 2

Protection - 4.16 kV Buses C1 & C2

C-EE-004.01-048 Protective Relay Setpoint Calculation for Phase Fault Revision 3

Protection - 4.16 kV Buses D1 & D2

C-EE-004.01-049 4.16 Kv Bus Degraded Voltage (90 percent November 7,

Undervoltage) Relay Setpoint 2001

C-EE-004.01-050 4.16 kV Bus Motor Residual Voltage Calculation Revision 0

C-EE-004.01-051 59 percent Undervoltage (Loss of Station Power) Revision 3

Setpoint Calculation

C-EE-004.01-055 Motor Damage Data Extrapolation for Schulz HPI Pump Revision 0

Motor

C-EE-006.01-026 Voltage Drop for GL 89-10 Valve Operators November 9,

1992

C-EE-015.03-003 Steady State Analysis - Electrical Load Management Revision 23

System ELMS

C-EE-015.7-001 Power Cable Ampacity May 7, 1992

Calculation No. Calculate Temperature -vs- Time for Loss of Ventilation Revision 1

24.001 in Room 323, 324, and 325

C-NSA-011.01- Allowable Service Water Flow Diversion During Cold Revision 1

003 Weather

C-NSA-016.04- Allowed CCW System Essential Header Integrated Revision 0

007 Leakage

67.005 Service Water Pump Room Ventilation System Revision 2

Capacity

67.004 Service Water Pump Maximum Allowable Outside Air Revision 1

Temperature to Dissipate Entire Room Heat Load with

One Ventilation Fan C99 1, 2, 3, or 4 Operable

Calculation Maximum Allowable Service Water Temperature w/ Revision 4

C-NSA-032.02- Inoperable ECCS Room Cooler

003

Calculation HPI Pump Acceptance Criteria Revision 4

C-NSA-52.01-003

Calculation Maximum Allowable Leak Rate through HP31/32 or Revision 0

C-NSA-52.01-012 ECCS Systems

48

Calculation 25.006 ECCS Rooms - Cooling System Revision 1

Calculation 35.25 Dose Rate from BWST Revision 0

Calculation 36.28 ECCS - Pump Seal Failure Revision 0

C-NSA-011.01- Service Water Pump Startup/Coastdown Time for CAC Revision 0

004 Water Hammer Input

C-NSA-011.01- Replacement of SW1356, SW1357 and SW1358 Revision 0

008

SAROS/92-02 Identification of Flood Initiating Events for the Davis-

Besse Individual Plant Examination

C-NSA-011.01- Service Water Discharge Through SW 2929 February 6,

007 2001

C-CSS-011.01- Service Water Return Line to Forebay from SW 2929 December 19,

170 2000

C-NSA-085.00- Auxiliary Steam Blowdown in the Intake Structure October 30,

002 1993

12501-M-001 UHS Thermal Performance for Pond Water Area and July 14, 1998

Volume to Station 10+00

H&H-1 Thermal Performance Analysis for Ultimate Heat Sink December 26,

(UHS) Pond 1995

NOPS99-464 UHS Silting Study October 20,

1999

C-NSA 011.01-010 Maximum Service Water Pressure to AFW System April 2, 2002

C-NSA-60.05-008 Containment Post LOCA Response with Variable SW October 20,

Temperature 2001

C-NSA-000.00- PROTO-FLO Service Water System Model December 19,

017 2001

C-NSA-011.01- Allowable Service Water Flow Diversion During Cold March 21,

003 Weather 1997

C-CSS-011.01- Seismic Evaluation For Control Appurtenances On

172 Valves SW 1356, SW 1357, and SW 1358

C-ICE-011-01-001 Service Water Pump Discharge Pressure Switches September 2,

1986

C-NSA-60.05-007 CAC Heat Duty At Elevated SW Inlet Temperatures August 10,

1998

12501-M-003 ECCS Room Temperatures with Initial 90F Forebay May 27, 1999

49

67.005 Service Water Pump Room Ventilation System August 30,

Capacity 2002

67.007 Service Water Pump Room Ventilation System - August 30,

Pressure Drop 2002

C-CSS-11.01-169 Containment Air Cooler Evaluation For Generic Letter October 1,

96-06 1997

C-CSS-011.01- Structural Analysis of Service Water Strainer Internals November 30,

171 2000

12501-M-00004 UHS Pond Performance Analysis - Max Evaporation - March 15,

Silt 2001

Condition Reports Reviewed

CR 02-02658 Inadequate Ventilation for Rooms 323, 324, 325 June 18, 2002

CR 02-06120 SHRR - Testing Review - Maintenance Burden September 18,

Associated with Undervoltage Relays 2002

CR 02-06243 SSDPC Issue - Calculation Approved Prior to Receipt September 19,

of LAR 2002

CR 02-06428 SSDPC - Review of Calculation C-EE-004.01-051, 59 September 22,

percent Undervoltage, Revision 3 2002

CR 02-06430 SSDPC - Review of Calculation C-EE-004.01-049, September 21,

Revision 10, 90 percent Degraded Voltage 2002

CR 2000-2428 No title October 9,

2000

CR 01-0005 SW2930 Stroke Time Increase January 1,

2001

CR 01-0053 Screenwash to Circ. Water Pump Chlorine Diffuser January 8,

Pipe Rupture 2001

CR 01-0059 Water Treatment Building Sump Pumps Removed January 9,

2001

CR 01-0340 Degrading Trend of Service Water Butterfly Manual February 5,

Isolation Valves 2001

CR 01-0350 Inadequate Design of Service Water Header Relief February 5,

Valves 2001

CR 01-0429 Service Water Pump 1 has Rain Water Leaking on Its February 14,

Motor 2001

50

CR 01-0459 HPI Pump 1 D/P Trending Down February 16,

2001

CR 01-0512 Traveling Screen #3- Failed to Start February 21,

2001

CR 01-0676 Tubing Configuration on Instrumentation March 8, 2001

CR 01-0679 SW 2945 Bent Position Indicator March 8, 2001

CR 01-0842 DB-SC-4146, Quarterly Functional of RE8434 Failed March 24,

Low Flow Alarm Function 2001

CR 01-0871 HPI 2 AC Oil Pump Motor Bearing Degradation March 17,

2001

CR 01-0934 Missing P111-B Fastener April 2, 2001

CR 01-1002 Unexpected Service Water Motor Temperature April 9, 2001

Increase

CR 01-1267 ECCS Cooler Operability Justification May 14, 2001

CR 01-1716 Lack of Service Water Chlorination July 10, 2001

CR 01-1724 Service Water Pump 3 Test Data Problems July 10, 2001

CR 01-1787 M&TE Accuracies in Six I&C Data Packages Outside July 18, 2001

Calculation Allowed Accuracies

CR 01-1788 M&TE Used in Two Calibrations Did not Meet July 18, 2001

Applicable Accuracy Requirements

CR 01-1789 Design Database Errors for Service Water Pump July 18, 2001

Discharge Pressure Switches

CR 01-2532 Testing of Service Water Pump Cables September 26,

2001

CR 01-2763 P58-1 & P58-2 Bolting Non-Compliance with ASME October 18,

Code 2001

CR 01-3115 HPI Recirc Flow November 20,

2001

CR 01-3261 Service Water Pump 1 Motor Identified Problems December 6,

2001

CR 01-3292 SW-1356 Closing Stroke Time Increase December 10,

2001

CR 02-00754 Scheduling Conflict on HPI Pumps 1 and 2 February 23,

2002

51

CR 02-00899 Improvements Required in DB-OP-06904 February 25,

2002

CR 02-01058 Mod 99-0039 Calc Basis Determination Concerns March 5, 2002

CR 02-01419 Chlorination of the Service Water System March 29,

2002

CR 02-01450 Modification 99-0039 Does not Adequately Address April 3, 2002

New Valve Design

CR 02-01589 Some Floor Drains on East Side of CTMT 565 Level April 18, 2002

are Plugged

CR 02-01848 Inspection Plan IP-M-029 Extent of Condition Area 565- May 2, 2002

3P

CR 02-01937 Inspection Plan IP-M-029 Containment Area Inspection May 6, 2002

Findings

CR 02-01998 Inspection Plan IP-M-029 Area 565-1P, Room 216-East May 13, 2002

D-ring, Interior Findings

CR 02-02016 Pipe Support 33A-HCB-2-H13 Removal/Reinstallation May 13, 2002

CR 02-02038 Inspection Plan IP-M-028 Findings Component HP57 May 14, 2002

CR 02-02040 Inspection Plan IP-M-028 Findings Component HP56 May 14, 2002

CR 02-02041 Inspection Plan IP-M-028 Findings Component HP48 May 14, 2002

CR 02-02056 Post Loca Boron Precipitation Design Issues May 15, 2002

CR 02-02088 Inspection Plan IP-M-029 Area 585-5E Findings May 15, 2002

CR 02-02294 Degradation of Containment Air Cooler #1 Due to Boric May 28, 2002

Acid Corrosion

CR 02-02391 Intake Chlorine Pump Will Not Maintain Its Prime June 2, 2002

CR 02-02394 Degradation of Service Water Piping in Containment June 3, 2002

CR 02-02432 SW Pump 3 Flowrate Limited by Strainer Blowdown June 5, 2002

CR 02-02478 PR/PSA: Improvements in the CCW System Need to June 7, 2002

be Considered

CR 02-02749 Boric Acid on Equipment in the Aux Building June 24, 2002

CR 02-02764 Service Water Piping Inside Containment Unqualified June 24, 2002

Paint

CR 02-02943 Containment Air Cooler Boric Acid Corrosion July 2, 2002

52

CR 02-03028 HPI Stop Check Valves May Not be Oriented Correctly July 8, 2002

CR 02-03224 Boric Acid on HP4BB Due to Body to Bonnet Leak July 15, 2002

CR 02-03235 SW1434 Did Not Respond as Expected During Post July 15, 2002

Maintenance Testing

CR 02-03256 Degradation of Circulation Water Chlorination Supply July 16, 2002

Lines

CR 02-03383 Problems with HP 48 July 22, 2002

CR 02-03655 High Pressure Injection Boron Corrosion August 8, 2002

CR 02-03972 Degradation of Service Water Supply Piping to August 10,

Auxiliary Feed Water Pumps 2002

CR 02-04173 SHRR Walkdown of HPI Train 1, Corrosion Issues August 10,

2002

CR 02-04419 Biofouling of Containment Air Cooler E37-3 August 16,

2002

CR 02-04697 MCC Bucket for BF1281 August 21,

2002

CR 02-04760 BF 1281 Loose Terminal August 21,

2002

CR 02-05011 SHRR Walkdown of HPI Train 2: Insulation Issues August 16,

2002

CR 02-05528 LIR-SW:ECCS Room Cooler Material Deficiencies August 14,

2002

CR 02-05563 Nozzle Flexibility Assumed in Calculation 65A/B (Part September 5,

II) is Non-Conservative 2002

CR 00-1779 No test to verify flow from Service Water System to July 13, 2000

Component Cooling Water System for Makeup

CR 01-2928 Intake Structure Flooding Issue with Pumps Removed November 1,

2001

CR 02-04514 Inadequate Interface Between the IST Program and August 19,

Design Basis Information 2002

CR 02-05784 Service Water Strainer Design Flow

CR 02-06370 SSDPC: ECCS Pump Room Heat Load Calculation is September 20,

Non-conservative 2002

CR 02-06388 SSDPC: Issues with DB-OP-06261 Guidance for September 20,

Inoperable ECCS Room Coolers 2002

53

CR 02-07232 LIR CCW - Non-conservative CCW Leakage October 2,

Calculation 2002

CR 02-07378 LIR CCW - Service Water to CCW Makeup Line Flow October 3,

Verification Test Discrepancies 2002

CR 00-0096 Failure to Perform Off-site AC Sources Line Up as January 17,

Required by Tech Spec 2000

CR 00-4035 Closing Springs Failed to Charge December 18,

2000

CR 00-4113 ACD2 Would Not Close When Placing #3 CCW in December 24,

Service As 1 2000

CR 00-4116 ACD3 Breaker Closed When the Springs Discharged December 24,

While Racking Out 2000

CR 01-0043 Maintenance Rule (a)(1) Corrective Action Plan for February 4,

Breakers may Need Re-evaluating 2001

CR 01-0138 Some Inhouse Refurb Breakers Have Different Stock January 2,

Code Arcing Contact Mt 2001

CR 01-0413 Circuit Breaker ACD3 Did Not Pass Post-Maintenance February 12,

Checks 2001

CR 01-0823 AC113 Failed Resistance Checks per Standing Order March 22,

99-09 2001

CR 01-1049 Breaker Could Not Be Tested per DB-OP-01000 April 21, 2001

CR 01-1104 C1 Low Voltage Alarms April 22, 2001

CR 01-1721 DC Bus 1 Ground July 10, 2001

CR 01-2120 AC113 Thermography Noted Warm Relay Not Noted in August 16,

Other Breakers 2001

CR 01-2158 High Voltage Switchgear Room Temperature Concerns August 21,

2001

CR 02-00817 Inadequate Clearance on AD 111 Trip Plunger February 26,

2002

CR 02-01161 59 percent UV Relay Failure May 9, 2002

CR 02-01526 Unexpected AC Transformer Lockout April 11, 2002

CR 02-01550 Unexpected AC Transformer Lockout April 15, 2002

CR 02-02658 Inadequate Ventilation for Rooms 323, 324, 325 June 18, 2002

CR 02-03845 Loose Termination in AC 113 August 8, 2002

54

CR 02-04999 SHRR - Testing Review for 4.16 kV System August 26,

2002

CR 02-05000 SHRR - Testing Review for 4.16 kV System August 26,

2002

CR 02-03331 Noteworthy Items from Test Control Program Self July 19, 2002

Assessment

CR 02-04514 Inadequate Interface Between the IST Program and August 19,

Design Basis Information 2002

CR 02-05369 LIR of Inadequate Service Water System Flow Balance September 2,

Procedure 2002

CR 00-2478 Service Water Relief Valves Lifted and Failed to Reseat October 13,

2000

CR 01-2182 Bench Testing SW 3963 Relief Valve During 13RFO August 23,

2001

CR 01-2407 #1 Service Water Pump Strainer Leak September 18,

2001

CR 01-0350 Inadequate Design Of Service Water Header Relief February 5,

Valves 2001

CR 02-04514 Inadequate Interface Between The IST Program And August 19,

Design Basis Information 2002

CR 02-05372 LIR of Service Water System Design Flow Rates to the September 2,

ECCS Room Coolers 2002

CR 02-05640 No Design Basis/Flow verification Testing of SW Flow September 7,

to AFW System 2002

CR 02-05923 No Design Basis For Service Water Pump NPSH September 13,

Available 2002

CR 02-05966 LIR-SW-EQ Walkdown August 30,

2002

CR 02-06139 SSDPC Self Assessment Identified Seismic II/I September 18,

Concern for CTMU Pumps 2002

CR 02-06177 CREVS Calculation Not Updated To Address 90F September 18,

Temperature Increase 2002

CR 02-06297 Cooling Tower Makeup and Service Water Pumps September 19,

2002

CR 02-06436 Collective Significance of Issues From SW Self September 21,

Assessment and LIR 2002

55

CR 02-06438 Evaluate Worst Case (Highest Flow) for the Service September 21,

Water System 2002

CR 02-06546 Design Basis Validation Open Items - Containment Air September 23,

Coolers 2002

CR 02-06791 ECCS Room Cooler Common Outlet Isolation Valve September 26,

2002

CR 02-07004 Heat Added by SW Pumps Not Accounted For In September 29,

Containment Response Analysis 2002

Condition Reports Written As a Result of Inspection

CR 02-06571 Calculation Inadequacy September 24,

2002

CR 02-06737 SSDPC - Calc C-EE-004.01-051 Uncertainty Treatment September 25,

2002

CR 02-06837 Inadequate Supervisors Review of CR 02-06302 September 27,

2002

CR 02-06893 Unevaluated Temperature Increase Because of LAR September 24,96-008 2002

CR 02-07633 SSDPC/Uncertainties Treatment in C-EE-004.01-049 October 8,

R10 Is Non-Conservative 2002

CR 02-07646 SSDPC - Calc C-EE-004.01-051 Temperature Variation October 8,

Not Considered 2002

CR 02-07766 Non-Conservative Value for 90 percent Volt in Table October 9,

3.3-4 2002

CR 02-06618 Appendix R Disconnect Switch Cabinet Found Open September 24,

During NRC Walkdown 2002

CR 02-06674 HP 209 Was Found Out of Expected Position September 24,

2002

CR 02-06726 Leakage Collection Devices and Their Usage in RRA September 25,

Clarification 2002

CR 02-06749 NRC Inspection of Top of BWST Tank September 26,

2002

CR 02-06750 NRC Walkdown of the BWST September 26,

2002

56

CR 02-06571 Calculation Inadequacy September 24,

2002

CR 02-06855 NRC Walkdown of HPI in Containment September 27,

2002

CR 02-06801 Corrosion in Room 115 September 26,

2002

CR 02-07611 NRC Walkdown of HPI October 7,

2002

CR 02-07643 Improvements to DB-OP-02003, For HPI Flow Alarm October 8,

Response 2002

CR 02-07753 Failure to Require TS 4.5.2.H HPI Flow Testing September 9,

Following Maintenance 2002

CR 02-07779 Cable Seal for CCW Rad Monitor September 24,

2002

CR 02-07791 NRC Question On HPI System Modifications October 10,

2002

CR 02-07475 Instrument Inaccuracy for Air Temperature Not October 4,

Considered in Service Water Ventilation Calculation 2002

CR 02-07657 Service Water Pump Design Flow Rate in Question October 8,

2002

CR 02-07762 Questions on Mounting for CCW Heat Exchangers October 9,

2002

CR 02-07764 Calculation/Test May Not Consider Actual Plant October 9,

Conditions 2002

CR 02-07770 Security Equipment October 9,

2002

CR 02-07802 Calculational Basis for PSH 2929 and PSH 2930 October 10,

setpoint could not be found 2002

CR 02-07820 Bent Anchor Bolt on the CCW Ht Exchanger #1 Sliding October 10,

Connection 2002

CR 02-06615 Work Area in MPR #1 Unsatisfactory September 24,

2002

CR 02-06701 Post Loca Dose from BWST with Inadvertent September 25,

HP31/HP32 Failure 2002

CR 02-06702 Potential for Inadequate HPI Pump Minimum September 25,

Recirculation Following LOCA 2002

57

CR 02-06571 Calculation Inadequacy September 24,

2002

CR 02-06863 Extent of Condition of CR 02-05369 September 26,

2002

CR 02-06996 HPI Flow Test Acceptance Criteria Versus T.S. 4.5.2.h September 28,

2002

CR 02-07338 High Pressure Injection System Description (SD-038) October 2,

2002

CR 02-07466 HPI Pumps Test Procedures Deficiency with Required October 4,

Test Instrumentation Accuracy 2002

CR 02-07468 SSDP: Unverified Calculations in SW Qtrly Tests October 4,

DB-PF-03017, -03023, -03030 2002

CR 02-07684 HPI Pump Capability to Run at Minimum Flow October 8,

2002

CR 02-07701 Control Room Operator Dose Due to ECCS Leakage October 9,

Post-LOCA 2002

CR 02-07713 Post Accident Control Room Dose Calculations October 9,

2002

CR 02-07741 Acceptance Criteria of ECCS Sump Test below USAR October 9,

Assumption 2002

CR 02-07757 Environmental Conditions for Decay Heat Pump Seal October 4,

Leak Not Evaluated 2002

CR 02-07777 DHR System Needs Critical Crack Evaluation October 9,

2002

CR 02-07781 Weaknesses in Testing SW Outlet Valves to CAC October 9,

Coolers (SW - 1356, 1357, 1358) 2002

CR 02-05986 UHS Water Inventory Analysis Does Not Consider All September 14,

Water Losses 2002

CR 02-06064 SW Flow Balance Margins and Need For Additional September 15,

Recorded Data 2002

CR 02-06332 Potential Weaknesses Service Water Single Failure September 20,

Analysis 2002

CR 02-06333 Concerns With Calculation C-NSA-011.01-001 September 20,

2002

CR 02-06336 UHS Analyses Do Not Document That Worst-Case September 20,

Conditions are Enveloped 1992

58

CR 02-06571 Calculation Inadequacy September 24,

2002

CR 02-06344 Design Basis Concerns Regarding Service Water September 20,

Strainer Backwash Function 2002

CR 02-06370 ECCS Pump Room Heat Load Calculation Is Non- September 20,

Conservative 2002

CR 02-06379 ECCS Pump Room Heat Load Calculation Is Non- September 20,

Conservative 2002

CR 02-06860 Review of the Need for Relief Valves for Several Heat September 27,

Exchangers 2002

CR 02-07188 Non-Conservative Assumptions in Calc 76.005, SW October 2,

Ventilation Capacity 2002

CR 02-07286 Enhance RA-EP-02880, Internal Flooding Procedure October 2,

2002

CR 02-07569 Station Sump Pump Check Valves Not Tested October 7,

2002

CR 02-07427 Drainage Systems - Aux Building Dwg 173, Note 8 October 4,

Requires Clarification 2002

CR 02-07692 USAR Section 9.2.5.1 Concerning Placing SWP(s) Into October 8,

Operation After 13 Hours 2002

CR 02-07714 Lack of Procedures to Isolate SWP Room Equipment October 8,

During Flooding 2002

CR 02-07716 Wrong instrument May Be Used To Verify Ultimate October 9,

Heat Sink Temperature 2002

CR 02-07745 No Allowance for Flow Diversion in Calc C-NSA-00.00- October 9,

17 2002

CR 02-07746 Building Drainage Failure Criteria Question October 9,

2002

CR 02-07750 Basis For Air Operated Containment Isolation Valve Air October 9,

Volume Tanks 2002

CR 02-07752 NRC Inspection of SW, Transient Spikes in CTMT SW October 9,

Pressure Lines 2002

CR 02-07760 Flood Analysis Discrepancies in the Service Water Pipe October 9,

Tunnel and Valve Rooms 2002

CR 02-06108 AFW Pumps and H2 Dilution Blower Not Evaluated for September 17,

Maximum SW Temperature 2002

59

CR 02-06571 Calculation Inadequacy September 24,

2002

CR 02-07781 Weaknesses In Testing SW Outlet Valves to CAC October 9,

Coolers 2002

Drawings

E-1 SH. 1, 2, 3 AC Electrical System One Line Diagrams Revisions 21,

31, 2

E-3 4.16 kV Metering and Relaying One Line Diagram Revision 30

E-39 B SH. 11 Misc Control Schemes - Medium Voltage SWGR Revision 3

Rooms Lighting

E-52B SH. 63 HPI Pump AC Lube Oil Pump Revision 3

E-52B SH. 64 HPI Pump DC Lube Oil Pump Revision 5

DWG 033A High Pressure Injection Revision 3

DWG 041A Service Water Pumps and Secondary Service Water Revision 23

DWG 041B Service Water Pumps and Secondary Service Water Revision 54

DWG 041C Service Water Pumps and Secondary Service Water Revision 25

DWG OS-020 Operational Schematic Service Water System Revision 55

DWG 030A Reactor Coolant System Revision 52

DWG 363 Sprinkler System SW Pump Rm 52 Intake Structure Revision 2

Elev. 576'-0"

Operational High Pressure Injection System Revision 19

Schematic OS-003

P&ID M-033A High Pressure Injection Revision 30

Goulds Pumps Backup Service Water Pump, October 6,

Drawing Q307249 1981

Goulds Pumps Service Water Pumps September 18,

Drawing 1992

N300214401

Goulds Pumps Dilution Pump P180 November 1,

Drawing 301231 1973

Goulds Pumps Dilution Pump August 9, 1973

Drawing D-1375

60

P&ID M-041A Service Water Pumps and Secondary Service Water Revision 23

System

P&ID M-041B Primary Service Water System Revision 54

P&ID M-041C Service Water System for Containment Air Coolers Revision 25

P&ID M-006D Auxiliary Feedwater System Revision 47

Piping System Intake Structure Revision 17

Composite M-

251F

Goulds Pumps Service Water Pump P3-1 Pump Curves March 15,

Drawing T74-082 1974

Goulds Pumps Service Water Pump P3-2 Pump Curves March 15,

Drawing T74-084 1974

Goulds Pumps Service Water Pump P3-3 Pump Curves March 2, 1974

Drawing T74-090

C-1595 Penetration Schedule Revision 7

Equipment Intake Structure & Water Treatment Building Plans Revision 29

Locations Dwg

135

M-473-A Low Density Silicone Foam Penetration Seal Typical Revision 1

Details

M-473-B High Density Silicone Elastomer Penetration Seal Revision 0

Typical Details

M-473-C Grout or Ceramic Fiber and Caulk Penetration Seal Revision 1

Typical Details

A-2110 Barrier Penetration Drawing Barrier Identification Plan Revision 0

Rm 52 Intake Structure Elev. 576'-0"

A-2112 Barrier Penetration Drawing Barrier Identification Plan Revision 1

Rm 53 Intake Structure Elev. 566'-0"

A-2111 Barrier Penetration Drawing Barrier Identification Plan Revision 0

Rm 52-E Intake Structure

C-1594 Barrier Functional List Revision 2

Procedures

DB-OP-02001 Electrical Distribution Alarm Panel 1 Alarm Procedure Revision 3

61

DB-OP-02103 Transformer AC Alarm Panel 103 Annunciators Revision 1

DB-OP-02104 Transformer BD Alarm Panel 104 Annunciators Revision 1

DB-OP-02521 Loss of AC Bus Power Sources Revision 2

DB-OP-06315 4160 Volt Switching Procedure Revision 2

DB-OP-06316 Diesel Generator Operating Procedure Revision 2

DB-OP-06334 Station Blackout Diesel Generator Operating Procedure Revision 3

DB-OP-06904 Shutdown Operations Revision 6

DB-OP-02000 RPS, SFAS, SFRCS Trip, or SG Tube Rupture Revision 6

DB-OP-00008 Operation and Control of Locked Valves Revision 1

DB-OP-02511 Loss of Service Water Pumps/Systems Revision 2

DB-OP-03007 Miscellaneous Instruments Daily Check Revision 3

DB-OP-06016 Containment Air Cooling System Procedure Revision 4

DB-OP-06261 Service Water System Operating Procedure Revision 2

DB-OP-06262 Component Cooling Water System Operating Revision 2

Procedure

DB-OP-06904 Shutdown Operations Revision 6

DB-OP-06913 Seasonal Plant Preparation Checklist Revision 4

DB-MM-03006 Inspection of Tech Spec Hydraulic Snubbers Revision 1

DB-PF-03017 Service Water Pump 1 Quarterly Test Revision 2

DB-PF-03020 Service Water Train 1 Quarterly Valve Test Revision 4

DB-PF-03023 Service Water Pump 2 Quarterly Test Revision 2

DB-PF-03026 Service Water Manual Valve Test Revision 0

DB-PF-03027 Service Water Train 2 Quarterly Valve Test Revision 4

DB-PF-03100 Component Cooling Water Valve Test Revision 4

DB-PF-03154 AFW Train 1 Valve Testing Revision 4

DB-PF-03163 AFW Train 2 Valve Testing Revision 4

DB-PF-03205 ECCS Train 1 Valve Test Revision 4

DB-PF-03206 ECCS Train 2 Valve Test Revision 3

DB-PF-03811 Miscellaneous Valves Test Revision 6

62

DB-PF-03812 Miscellaneous Valves Cold Shutdown and Refueling Revision 6

Test

DB-PF-03813 Miscellaneous Augmented Valve Test Revision 0

DB-PF-04704 Performance Test - Component Cooling Water Heat Revision 4

Exchanger 1

DB-PF-04705 Performance Test - Component Cooling Water Heat Revision 3

Exchanger 2

DB-PF-04706 Performance Test - Component Cooling Water Heat Revision 3

Exchanger 3

DB-PF-04729 Containment Air Cooler Monitoring Test Revision 6

DB-PF-04736 ECCS Room Cooler Monitoring Test Revision 0

DB-SC-03114 SFAS Integrated Time Response Test Revision 1

DB-SC-03122 SFAS Components Test Revision 1

DB-SP-03018 Service Water Pump 1 Refueling Test Revision 2

DB-SP-03019 Service Water Valve Verification Monthly Test Train 1 Revision 1

DB-SP-03024 Service Water Pump 2 Refueling Test Revision 2

DB-SP-03026 Service Water Valve Verification Monthly Test Train 2 Revision 1

DB-SP-03032 Service Water Pump 3 Refueling Test Revision 2

DB-SS-03041 Control Room Emergency Ventilation System Train 1 Revision 3

Monthly Test

DB-SS-03042 Control Room Emergency Ventilation System Train 2 Revision 3

Monthly Test

DB-SS-04021 Backup Service Water Pump Quarterly Test Revision 2

DB-SC-03020 13.8 KV System Bus A & B Transfer Test Revision 3

DB-SC-03022 Off-site AC Sources Bus Transfer Test Revision 2

DB-SC-03023 Off-site AC Sources Lined Up and Available Revision 3

DB-SC-03041 On-site AC Bus Sources Lined Up, Available and Revision 2

Isolated (Modes 1, 2, 3, and 4)

DB-SC-03042 On-site AC Bus Sources Lined Up and Available Revision 2

(Modes 5 and 6)

DB-SC-04052 4160V System Transfer and Lockout Test - Buses D1 Revision 1

and D2

63

DB-SC-04053 4160V System Transfer and Lockout Test - Buses C1 Revision 1

and C2

DB-SC-10000 Main Transformer Backfeed Test Revision 0

Emergency RPS, SFAS, SFRCS Trip, OR SG Tube Rupture Revision 06

Procedure

DB-OP-02000

Systems ECCS Sump Pump Flow Check Revision 01

Procedure

DB-SP-04162

Surveillance Test ECCS Integrated Train 1 Leakage Rate Test Revision 00

Procedure

DB-PF-03011

Surveillance Test ECCS Integrated Train 2 Leakage Rate Test Revision 00

Procedure

DB-PF-03012

Surveillance Test Service Water Pump 1 Testing Revision 03

Procedure

DB-PF-03017

Surveillance Test HPI Train 1 Pump and Valve Test Revision 04

Procedure

DB-SP-03218

Surveillance Test HPI Train 2 Pump and Valve Test Revision 05

Procedure

DB-SP-03219

Surveillance Test Service Water Train 1 Valve Test Revision 04

Procedure

DB-PF-03020

Surveillance Test Service Water Train 2 Valve Test Revision 04

Procedure

DB-PF-03027

Periodic Test HPI Pump 1 Baseline Test Revision 00

Procedure

DB-PF-04207

Mechanical Torquing Revision4

Maintenance

Procedure DB-

MM-09266

RA-EP-02880 Internal Flooding October 14,

1998

64

DB-OP-02011 Heat Sink Alarm Panel 11 Annunciators September 16,

2002

DB-OP-06261 Service Water System Operating Procedure June 6, 2002

DB-PF-03272 Post Maintenance Valve Test Revision 2

DB-SP-03152 AFW Train 1 Level Control, Interlock and Flow Revision 6

Transmitter Test

DB-SP-03161 AFW Train 2 Level Control, Interlock and Flow Revision 6

Transmitter Tes

DB-OP-02000 Emergency Procedure Bases and Derivation Document Revision 11

DB-OP-02000 Emergency Procedure May 14, 2001

RA-EP-02830 Emergency Plan Off Normal Occurrence Procedure, Revision 00

Flooding

Surveillances and Tests

DB-MM-03006 Inspection of Tech Spec Hydraulic Snubbers January 28,

2002

DB-PF-03017 Service Water Pump 1 Quarterly Test February 8,

2000

Service Water Pump 1 Quarterly Test May 8, 2000

Service Water Pump 1 Quarterly Test September 8,

2000

Service Water Pump 1 Quarterly Test February 23,

2001

Service Water Pump 1 Quarterly Test April 29, 2001

Service Water Pump 1 Quarterly Test August 7, 2001

Service Water Pump 1 Quarterly Test October 30,

2001

Service Water Pump 1 Quarterly Test January 23,

2002

DB-PF-03020 Service Water Train 1 Quarterly Valve Test January 26,

2000

Service Water Train 1 Quarterly Valve Test July 11, 2000

Service Water Train 1 Quarterly Valve Test March 7, 2001

65

Service Water Train 1 Quarterly Valve Test December 27,

2001

Service Water Train 1 Quarterly Valve Test January 23,

2002

DB-PF-03023 Service Water Pump 2 Quarterly Test October 19,

2000

Service Water Pump 2 Quarterly Test January 8,

2001

Service Water Pump 2 Quarterly Test April 6, 2001

Service Water Pump 2 Quarterly Test June 29, 2001

Service Water Pump 2 Quarterly Test September 17,

2001

Service Water Pump 2 Quarterly Test November 11,

2001

DB-PF-03027 Service Water Train 2 Quarterly Valve Test November 13,

2001

Service Water Train 2 Quarterly Valve Test December 11,

2001

Service Water Train 2 Quarterly Valve Test January 9,

2002

DB-PF-04704 Performance Test - Component Cooling Water Heat September 16,

Exchanger 1 1999

Performance Test - Component Cooling Water Heat June 19, 2001

Exchanger 1

DB-PF-04705 Performance Test - Component Cooling Water Heat September 29,

Exchanger 2 1999

Performance Test - Component Cooling Water Heat August 2, 2000

Exchanger 2

DB-PF-04706 Performance Test - Component Cooling Water Heat September 29,

Exchanger 3 1999

Performance Test - Component Cooling Water Heat August 29,

Exchanger 3 2000

DB-PF-04729 Containment Air Cooler Monitoring Test March 15,

1999

Containment Air Cooler Monitoring Test March 9, 2000

66

Containment Air Cooler Monitoring Test June 8, 2000

Containment Air Cooler Monitoring Test June 9, 2000

Containment Air Cooler Monitoring Test March 20,

2001

Containment Air Cooler Monitoring Test June 13, 2001

Containment Air Cooler Monitoring Test June 20, 2001

Containment Air Cooler Monitoring Test August 8, 2001

Containment Air Cooler Monitoring Test August 14,

2001

Containment Air Cooler Monitoring Test November 1,

2001

Containment Air Cooler Monitoring Test November 6,

2001

Containment Air Cooler Monitoring Test January 22,

2002

Containment Air Cooler Monitoring Test January 29,

2002

DB-PF-04736 ECCS Room Cooler Monitoring Test July 21, 2000

ECCS Room Cooler Monitoring Test October 13,

2000

ECCS Room Cooler Monitoring Test April 11, 2001

ECCS Room Cooler Monitoring Test January 15,

2001

DB-SC-03114 SFAS Integrated Time Response Test May 6, 1998

SFAS Integrated Time Response Test May 4, 2000

DB-SC-03122 SFAS Components Test May 13, 1998

SFAS Components Test May 7, 2000

DB-SP-03032 Service Water Pump 3 Refueling Test May 9, 2000

Service Water Pump 3 Refueling Test June 26, 2000

DB-SS-04021 Backup Service Water Pump Quarterly Test April 18, 2002

Backup Service Water Pump Quarterly Test July 11, 2002

67

Other Documents

ISA-S67.04 Setpoints for Nuclear Safety-Related Instrumentation September

1994

DB-ME-03045 R00 C1 Bus Undervoltage Units Monthly Functional Test Revision 00

DB-ME-05319 GE NGV13B Voltage Relay Maintenance and Revision 00

Calibration

RFM 89-0011 Obsolete M-2 Valve Actuator January 17,

1989

SCR 92-5013 Increase the Upper Bound of the Allowable Setpoint June 16, 1992

Range for the 59 percent Relays from 67 Volts to 69

Volts

FCR 83-063 Replace HPI Pump 1-2 AC Lube Oil Pump May 2, 1983

Operability Operability Justification 01-0015 for Condition Report August 22,

Justification 01- 01-2158, High Voltage Switchgear Room Temperature 2001

0015 Concerns

E-005-00154-4 Instr Man-I-T-E Single Phase Voltage Relays 35891

USAR Change Safety Evaluations Associated with LAR 89-0017 and January 8,

Notice (UCN) 90- MOD 88-0234 1990

001

Davis-Besse Letter Response to NRC Regarding Davis-Besse Unit No. 1 July 18, 1977

- Serial No. 293 Grid Stability

Davis-Besse Letter License Amendment Application to Clarify that Decay June 13, 1989

- Serial No. 1667 Heat Removal Valve DH23 Is not Subject to Type C

Test Requirements (TAC Number 73244)

Davis-Besse Letter License Amendment Application to Remove Technical December 22,

- Serial No. 1737 Specification Table 3.6-2, Containment Isolation Valves 1989

(TAC Number 75235)

Davis-Besse Letter Revision 11 to the Updated Safety Analysis Report May 31, 1990

- Serial No. 1794

Davis-Besse Letter Withdrawal of License Amendment Applications to June 1, 1990

- Serial No. 1812 Revise Technical Specification 3/4.6.3.1, Containment

Isolation Valves (TAC Numbers 66008 and 73244)

License Amendment No. 147 to Facility Operating License No. April 13, 1990

Amendment No. NPF-3 (TAC No. 75235)

147

68

EPRI TR-103335 Guidelines for Instrument Calibration March 1994

Extension/Reduction Programs

DB-OP-02000 RPS, SFAS, SFRCS or SG Tube Rupture Revision 06

Basis and Deviation Document for DB-OP-02000 Revision 11

Design Report for Modification 99-0039-00 Replace Revision 0

Valves SW 1356, SW 1357, and SW1358

Spec. 7749-M-319 Design Specification for Nuclear Ball and Butterfly Revision 4

Control Valves for The Toledo Edison Company and

the Cleveland Electric Illuminating Company Davis-

Besse Nuclear Power Station Unit No. 1

Spec. M-319CQ Technical Specification for Operational Phase Service Revision 0

Water Nuclear Ball Control Valves SW 1356, SW 1357,

and Sw 1358 for Davis-Besse Nuclear Power Station

SD-038 System Description for High Pressure Injection System Revision 2

SD-003A System Description for the 4160 volt Auxiliary System Revision 3

SD-018 System Description for Service Water System Revision 2

High Pressure Injection Pump 1 Inservice Testing Data October 8,

2002

High Pressure Injection Pump 2 Inservice Testing Data October 8,

2002

High Pressure Injection Valve Inservice Testing Data October 8,

2002

DB-OP-06011 High Pressure Injection System Revision 02

DB-OP-02003 ECCS Alarm Panel 3 Annunciators Revision 02

DB-PF-03205 ECCS Train 1 Valve Test Revision 04

DB-OP-06331 Freeze Protection and Electrical Heat Trace Revision 03

DB-PF-03207 HPI Pump Comprehensive and Check Valve Forward Revision 02

Flow Tests

EN-DP-01080 Calculations Revision 01

DB-PF-03969 HPI System Pressure Isolation Integrity test Back-to Revision 04

Back Check Valves

DB-PF-03069 Check Valve reverse Flow Tests Revision 04

Calc 67A Pipe Stress Analysis Revision 05

69

50-346/89-201 Interfacing System LOCA Inspection December 22,

1989

50-346/92010 Announced Safety Inspection of the Licensees August 20,

Response to Generic Letter 89-10 1992

SN 1793 Response to Inspection Report 50-346/89-201- April 27, 2002

Interfacing System Loss of Coolant Accident

UCN 98-022 U Seismic Qualification of Valves SW-1424, SW-1429, February 18,

and SW-1434 2002

PCAQR 95-0681 T413 May Read Low August 17,

1995

PCAQR 97-1174 Decay Heat Exchangers Overstressed September 4,

1997

USAR 6.3 Emergency Core Cooling Systems Revision 22

TS 3/4.5 Emergency Core Cooling Systems

SD003A System Description for the 4160 Volt Auxiliary System Revision 3

Standing Order Interim Guidance on High Voltage Switchgear Room July 13, 2002

02-005 Ventilation

4160 VAC Maintenance Rule Scoping Documents

Davis-Besse Materiel Condition Report - Essential and 4th Quarter

Miscellaneous AC 1999

Davis-Besse Materiel Condition Report - Essential and 2nd Quarter

Miscellaneous AC 2000

Davis-Besse Materiel Condition Report - Essential and 3rd Quarter

Miscellaneous AC 2000

Davis-Besse Materiel Condition Report - Essential and 4th Quarter

Miscellaneous AC 2000

Davis-Besse Materiel Condition Report - Essential and 1st Quarter

Miscellaneous AC 2001

Davis-Besse Materiel Condition Report - Essential and 2nd Quarter

Miscellaneous AC 2001

Davis-Besse Materiel Condition Report - Essential and 3rd Quarter

Miscellaneous AC 2001

Davis-Besse Materiel Condition Report - Essential and 4th Quarter

Miscellaneous AC 2001

70

Davis-Besse Materiel Condition Report - Medium 1st Quarter

Voltage AC 2002

Davis-Besse Weekly Maintenance Risk Summary February 12,

2002

M-45-18-4 Goulds Pumps Service Water Pumps Vendor Manual October 30,

1987

MPR-876 Davis-Besse Auxiliary Feed Pumps Evaluation of October 1985

Automatic Transfer of Suction to the Service Water

System

OS-020 SH 1 Service Water System Operational Schematic - Sheet 1 Revision 55

OS-020 SH 2 Service Water System Operational Schematic - Sheet 2 Revision 24

PFP-IS-52 Protected Area Pre-fire Plan for Service Water Pump Revision 2

Room, Room 52, Fire Area BF

SD-018 System Description for Service Water System Revision 2

TM 02-0019 Temporary Modification - Install temporary flood barrier August 27,

in place of Cooling Tower Makeup Pump #1 2002

Service Water Pump 1 IST Trend Data September

2000 - present

Service Water Valve Test Data January 1992 -

present

Letter Serial No. 1- Response to Generic Letter 89-13, Service Water January 30,

904 System Problems Affecting Safety-Related Equipment 1990

Letter Serial No. 1- Final Response to Generic Letter 89-13, Service Water December 23,

966 System Problems Affecting Safety-Related Equipment 1991

Letter Serial No. 1- Supplemental Response to Generic Letter 89-13, September 9,

1022 Service Water System Problems Affecting Safety- 1993

Related Equipment

Letter Serial No. Commitment Change Summary Report November 20,

2575 1998

NRC Bulletin No. Potential Safety Related Pump Loss May 5, 1988

88-04

Toledo Edison Subject: Response to NRC Bulletin No. 88-04: Potential September 8,

Letter Serial No. 1- Safety Related Pump Loss 1988

823

71

Toledo Edison Subject: Final Response to Nuclear Regulatory April 14, 1989

Letter Serial No. 1- Commission (NRC) Bulletin No. 88-04: Potential Safety

871 Related Pump Loss (TAC 69906)

Toledo Edison Subject: Update on Activities Relating to NRC Bulletin December 16,

Letter Serial No. 1- No. 88-04: Potential Safety Related Pump Loss 1988

849

Mod 94-0009 Service Water Thermal Relief Valve Replacement for April 1995

Containment Air Coolers

SCR 93-5016 Change PSL 1377, Service Water Strainer Discharge January 12,

Pressure Switch to 55 PSIG 1994

Mod 87-1076 Remove ECCS Room Coolers Service Water Return January 12,

Check Valves Internals 1988

Mod 87-1290 Remove Internal of Valve SW-329 July 6, 1990

Mod 88-0234 Overpressure Protection for the Containment Air November 11,

Coolers 1988

FCR 84-0147 Service Water Pump Room Ventilation Upgrade November 23,

1985

Mod 99-0039-00 CAC Temperature Control Valve Replacement June 29, 1999

FCR 78-039 Change Setpoints on SW-PSH-2917 and SW-PSH- January 23,

2917A 1978

SE 87-0366 Remove Internals of Check Valves SW - 217 & SW - January 12,

218 1988

SE 95-0056 Remove Relief Valves SW - 10210, SW - 10211, & SW September 9,

-10212 From Containment Air Coolers 1995

SE 84-147 Service Water Pump Room Ventilation Upgrade November 23,

1985

SE 01-0008 CAC Temperature Control Valve Replacement June 2, 2001

72

List of Documents Requested by USNRC

Document Request (Bob Daley)

Please provide a copy of the following documents (Items in Bold should be higher priority):

SCR 92-5028 Revise Setting 4.16 KV Bus 2/23/95

SCR 92-5029 Rev Trip Timer for 4.16 KV Loads 6/2/95

MOD 89-0011-00 Obsolete Type M-2 Vlv Actuators 8/23/01

MOD 97-0002-00 LM-Replace PDS 3886 7/17/98

C-EE-004.01-001 Protective Relay Setpoints for Service Water 5/12/98

Pump Motor 1-1 (AC107)

C-EE-004.01-003 Protective Relay Setpoints for Service Water 10/27/92

Pump Motor 1-3 (AC109)

C-EE-004.01-009 Protective Relay Setpoints High Pressure 1/22/02

Injection Pump Motor 1-1 (AC111)

C-EE-004.01-010 Protective Relay Setpoints High Pressure 6/21/91

Injection Pump Motor 1-2 (AD111)

C-EE-004.01-046 4.16 KV Short Circuit Calculations 7/8/91

C-EE-004.01-049 4.16 KV Bus Degraded Voltage (90 percent 6/27/02

Undervoltage) Relay Setpoint

C-EE-004.01-051 59 percent Undervoltage (Loss of Station Power) 8/23/93

Setpoint Calculation

C-EE-006.01-026 Voltage Drop for GL 89-13 Valve Operators 5/21/02

C-EE-006.01-027 SFAS Control Ckt Voltage Drop 5/4/92

C-EE-015.07-001 4.16 & 13.8 KV Cable Ampacity 5/7/92

C-ICE-048.01-002 SFAS Reactor Coolant Pressure Actuation 10/14/97

Setpoints

C-ICE-011.01-001 Service Water Pump Discharge Pressure 4/19/01

Switches

Op Eval 2000-0012 HPI Flow Indicating Switches

of CR 2000-2382

73

Op eval 2001-0003 4160 Breakers

of CR 01-0138

Op eval 2001-0015 HV SWGR Room HVAC

of CR 01-2158

Op eval 2001-0025 SFAS Sequencer

of CR 01-2919

Please provide one line electrical schematics for the following:

13. Service Water Pumps

14. HPI Pumps

15. MOVs SW 1382, SW 1383, SW 5421, SW 5422, SW 5423, SW 5424, SW 5425, SW 2927,

SW 2928

16. FCVs SW 5896, SW 5897

Please provide the nameplate data for the following pumps:

1. Service Water Pumps

2. HPI Pumps

Please provide the coordination calculations for all loads and feeder breakers for Buses AC and

BD.

Please have available:

1. NEC Code

2. IEEE Std 242, IEEE Recommended Practice for Protection and Coordination of Industrial

and Commercial Power Systems. (IEEE Buff Book)

3. IEEE Std 141, IEEE Recommended Practice for Electric Power Distribution for Industrial

Plants. (IEEE Red Book)

4. Nuclear IEEE Standards, Volume 1 and 2

74

DOCUMENTS REQUEST FOR D. C. PREVATTE, 9/17/02

Please provide the latest revisions of the following documents.

In order to minimize unnecessary copying, for modification packages that are very large, please

provide only the basic package front-end materials that describe the modification, its bases,

etc., the 10CFR50.59 safety evaluation and/or screening, and the post modification testing

documents, but not the detailed construction and installation documents. Likewise, for

calculations that are very large, please provide only the basic front-end portions of the

calculations, e.g., the purpose, assumptions, inputs, references, and results and conclusions

sections, but not the large appendices.

Thank you for your support.

Modifications:

Modification # Modification Title/Subject

For Service Water System:

FCR 78-0039-2917 Change setpoints on PSH-2917

FCR 80-0225-00 Delete auto close SW 1395, 1399

FCR 80-0252-00 Replace valve bodies

FCR 80-0054-00 Back-up service water capability

FCR 84-0151-00 SWS valve & anchor modification

FCR 84-0111-00 Setpoint change - SW pump

FCR 84-0115-00 Changed SW valves locked position

FCR 84-0147-00 SW pump room ventilation upgrade

MOD 87-1072-00 Service water check valve

MOD 87-1075-00 Remove check valves SW-130, 134

MOD 87-1076-00 Remove check valves SW-217, 218

MOD 87-1290-00 Remove internals of SW-329

SCR 93-5016 Change PSL 1377 setpoint

FCR 80-0221-00 Piping change/service water

MOD 88-0234-00 Containment air coolers

MOD 94-0009-00 SW thermal relief valve replacement

For HPSI System:

FCR 78-0414-00 Change Tech Spec 4.5.2.6

FCR 78-0498-00 Correct determination of FSAR

FCR 86-0291-00 Mod high pressure injection line

75

Calculations:

(Please note that some of these calculations appear from the title to address the same subject. If

any of these are more current versions of the same analysis, or if any of these have been

superceded by calculations not listed here, please provide only the most current calculations that

address the subject.):

Calculation # Calculation Title/Subject

For Service Water System:

Mech 11.036 Traveling water screens

Struct 59 SW pipe stress analysis w/supports

Nucl 12501-M-001 UHS pond thermal performance analysis...

Nucl 12501-M-003 ECCS room temperature with initial 90 degree F forebay

Nucl 12501-M-004 UHS heat sink analysis of maximum evaporation period

Mech 59.001 UHS input

Mech 59-009 Davis Besse UHS

Mech 59-011 UHS analysis

Mech 59-016 UHS - Loss of intake canal - cooling pond calc

Mech 67.004 SW pump room - max allowable outside air temp to...

Mech 67.005 SW pump room ventilation capacity

Mech 67.006 SW pump room fan flow requirements

Mech 67.007 SW pump room ventilation system - pressure drop

Mech 67.008 SW pump room ventilation system - new penthouse...

Struct C-CSS-11.01-169 Containment air cooler eval for GL 96-06

Struct C-CSS-11.01-171 SW strainer internals analysis

Mech C-ME-011.01-130 SW system hydraulic calculation

Mech C-ME-011.06-003 Cont. cooler control valve travel

Nucl C-NSA-000.00-017 Service water system model

Nucl C-NSA-011.01-003 Allowable SW flow diversion during cold weather

Nucl C-NSA-011.01-004 SW pump start/coastdown time, CAC water hammer input

Nucl C-NSA-011.01-007 SW discharge through valve located at the intake struct.

Nucl C-NSA-001.01-008 Replacement of CAC flow control valves

Nucl C-NSA-001.01-010 Maximum SW pressure to AFW system

Nucl C-NSA-060.05-006 Revised containment response with 90 degree F SW

Nucl C-NSA-060.05-007 CAC duty at elevated SW inlet temperatures

Nucl C-NSA-060.05-008 Cont post-LOCA response w/variable SW temperature

Nucl ESM-99-002 Effect of UHS pond siltation on SW intake temperature

For HPSI System:

Mech 25.006 ECCS Rooms - Cooling System

Mech 25.013 ECCS Pump Room Heat Load

Mech 25.014 ECCS Pump Room Heat Load

Mech 32-1106901 MU/HP flow rates vs. reactor pressure...

Nucl 32-1159853 HPI flow vs. RCS pressure

Mech 36.010 LPI, HPI, CS pump NPSH from BWST

76

Mech 36.028 ECCS seal failure

Mech 36.031 HPI pump NPSH at a possible 1020 gpm

Mech 36.032 HPI pump test flow line

Mech 58.020 Flooding of ECCS pump rooms due to FW line break

Nucl 86-5006232 LOCA summary report

Mech C-ME-052.01-110 Reverse engineer HPI pump casing studs & casing nuts

Nucl C-NSA-032-02-003 Max allowable SW temp with inop ECCS room cooler

Nucl C-NSA-049.01-002 Adequacy of BWST for feed and bleed

Nucl C-NSA-049.01-004 Vortex formation with ECCS pump suction from the BWST

Nucl C-NSA-052.01-003 HPI pump acceptance testing

Nucl C-NSA-052.01-004 HPI system resistance curves

Nucl C-NSA-052.01-011 HPI NPSH on containment emergence sump recirc

Nucl C-NSA-052.01-012 Max. allowable leak rate through HP31/32

Nucl C-NSA-052.01-014 HPSI flow vs. RCS pressure for LOCA analysis input

Nucl C-NSA-052.01-016 Add T to HPI pump 2 discharge line

Nucl C-NSA-052.01-015 HPI pump curve based on system curve in LOCA analysis

Nucl C-NSA-063.01-008 Verification of HPI system performance during a SGTR

Nucl C-NSA-065.01-008 Makeup and HPI NPSH

77

Request for Documents Part III

Service Water Strainer

a. Drawings

b. Procedures, (surveillance, PMs, operating, abnormal, )

c. Maintenance history

d. Operational history (clogging events, identification of debris making it past the strainers,

damage to the strainers, etc)

e. Last time opened for inspection, inspection results

f. Vendor Manual

g. Ultimate heat sink inspections, inspection results, maintenance and operational history,

h. Lay out drawing for the Service Water intake building (where the SW pumps are located)

i. For HPI pump #1 and SW pump #1 need the breaker relay vendor technical manual, the

motor start curves and for HPI #1 motor need the name plate data

j. Do you have copies of the TS and UFSAR available on CDs?

Backup air supplies to the Containment Air Cooler (CAC) valves

k. Calculations for sizing

l. Basis calculation for the test acceptance criteria

m. Last two completed surveillance tests

78

Request for Documents Part IV

a. List of all work orders (preventive, corrective, troubleshooting, etc) for 4160 for the last

two years.

b. Same as above except for service water system

c. Copy of Tech Spec Basis

d. Copy of annunciator response procedures for local and control room annunciators for

service water and 4160

e. SBO D/G operating procedure DB-OP-06334

f. Implementing procedures for the following Tech Spec surveillance requirements:

a. 4.8.2.1 - Onsite power dist systems

b. 4.8.2.2 - Onsite power dist systems

c. 4.6.3.1.2.a - containment iso valves

d. 4.6.3.1.3 - containment iso valves

e. 4.7.4.1.a - Service water system

f. 4.7.4.1.b - Service water system

g. 4.7.5.1 - UHS

h. 4.8.1.1.1.a - Elect Power Systems

i. 4.8.1.1.1.b - Elect Power Systems

g. The procedure performing and the last results for any snubbers in the service water

system governed by SR 4.7.7

h. All IST procedures for the Service Water system components

i. One additional set of P&IDs for SW (sheets A, B, C)

j. Operability justifications and their associated CRS

a. 2001 - 0003 01-0138

b. 2001 - 0015 01-2158

c. 2002 - 0009 02-01157

d. 2002 - 0023 02-02658

k. Description of operability justification 2002 - 0027

79

l. EWR 02-0247-00 and CR 02-1459 and CR 02-2372 all dealing with operator work-around

for intake chlorination

m. Copies of all other surveillance procedures preventive maintenance procedures and

operator logs for SW and 4160.

80