ML023120116

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IR 05000443-02-005 North Atlantic Energy Service Corporation (FPL Energy Seabrook, LLC as of November 1, 2002); on 06/30-09/28/2002; Seabrook Station, Unit 1. Surveillance Testing and Response to Contingency Events
ML023120116
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 11/07/2002
From: Brian Mcdermott
NRC/RGN-I/DRP/PB6
To: Warner M
North Atlantic Energy Service Corp
References
IR-02-005
Download: ML023120116 (37)


See also: IR 05000443/2002005

Text

November 7, 2002

Mr. Mark E. Warner

Site Vice President

c/o Mr. James M. Peschel

Seabrook Station

P.O. Box 300

Seabrook, NH 03874

SUBJECT: SEABROOK STATION - NRC INSPECTION REPORT 50-443/02-05

Dear Mr. Warner:

On September 28, 2002, the NRC completed an inspection at the Seabrook Station. The

enclosed report documents the inspection findings which were discussed on October 7, 2002,

with Mr. J. Vargas and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the inspectors identified two issues of very low safety

significance (Green). The findings were determined to be violations of NRC requirements

involving inadequate corrective actions and security personnel readiness. However, because of

their low safety significance and because they have been entered into your corrective action

program, the NRC is treating these issues as Non-Cited violations, in accordance with Section

VI.A.1 of the NRCs Enforcement Policy. If you deny these Non-Cited violations, you should

provide a response with the basis for your denial, within 30 days of the date of this inspection

report, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington,

D.C. 20555-0001, with copies to the Regional Administrator, Region I, and the Director, Office

of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-001,

and the NRC Resident Inspector at the Seabrook Station.

The NRC has increased security requirements at Seabrook Station in response to terrorist acts

on September 11, 2001. Although the NRC is not aware of any specific threat against nuclear

facilities, the NRC has issued an Order and several threat advisories to commercial power

reactors to strengthen licensees' capabilities and readiness to respond to a potential attack.

The NRC continues to inspect the licensee's security controls and its compliance with the Order

and current security regulations.

Mr. Mark E. Warner 2

In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRCs document system

(ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html.

Sincerely,

/RA/

Brian J. McDermott, Chief

Projects Branch 6

Division of Reactor Projects

Docket No. 50-443

License No: NPF-86

Enclosure: NRC Inspection Report No. 50-443/02-05

Attachment 1: Supplemental Information

cc w/encl:

J. A. Stall, FPL Senior Vice President, Nuclear & CNO

J. M. Peschel, Manager - Regulatory Programs

G. F. St. Pierre, Station Director - Seabrook Station

R. S. Kundalkar, FPL Vice President - Nuclear Engineering

D. G. Roy, Nuclear Training Manager - Seabrook Station

D. Bliss, Director, New Hampshire Office of Emergency Management

D. McElhinney, RAC Chairman, FEMA RI, Boston, Massachusetts

R. Backus, Esquire, Backus, Meyer and Solomon, New Hampshire

D. Brown-Couture, Director, Nuclear Safety, Massachusetts Emergency Management Agency

S. McGrail, Director, Massachusetts Emergency Management Agency

R. Hallisey, Director, Dept. of Public Health, Commonwealth of Massachusetts

M. Metcalf, Seacoast Anti-Pollution League

D. Tefft, Administrator, Bureau of Radiological Health, State of New Hampshire

S. Comley, Executive Director, We the People of the United States

W. Meinert, Nuclear Engineer, Massachusetts Municipal Wholesale Electric Company

R. Shadis, New England Coalition Staff

P. Brann, Assistant Attorney General

M. S. Ross, Attorney, Florida Power and Light Company

Office of the Attorney General

Town of Exeter

Board of Selectmen

Mr. Mark E. Warner 3

Distribution w/encl: (VIA E-MAIL)

H. Miller, RA

J. Wiggins, DRA

H. Nieh, EDO Coordinator

S. Richards, NRR (ridsnrrdlpmlpdi)

D. Starkey, PM, NRR

V. Nerses, Backup PM, NRR

B. McDermott, DRP

K. Jenison, DRP

G. Dental, SRI - Seabrook

J. R. White, DRS

D. C. Lew, DRS

J. C. Linville, DRS

L. T. Doerflein, DRS

R. J. Conte, DRS

T. Moslak, DRS

P. Frechette, DRS

N. McNamara, DRS

Region I Docket Room (with concurrences)

DOCUMENT NAME: C:\ORPCheckout\FileNET\ML023120116.wpd

After declaring this document An Official Agency Record it will be released to the Public.

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with

attachment/enclosure "N" = No copy

OFFICE RI/DRP RI/DRP E RI/DRP

NAME GDentel/KMJ for/ K Jenison B McDermott

DATE 11/07/02 11/07/02 11/07/02

OFFICIAL RECORD COPY

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No.: 50-443

License No.: NPF-86

Report No.: 50-443/2002-05

Licensee: North Atlantic Energy Service Corporation

Facility: Seabrook Station, Unit 1

Location: Post Office Box 300

Seabrook, New Hampshire 03874

Dates: June 30, 2002 to September 28, 2002

Inspectors: Glenn Dentel, Senior Resident Inspector

Javier Brand, Resident Inspector

David Kern, Senior Resident Inspector, Beaver Valley

Kenneth Jenison, Senior Project Engineer

Antone Cerne, Senior Resident Inspector, Millstone Unit 3

Thomas Moslak, Health Physicist

Paul Frechette, Security Specialist

Gregory Smith, Senior Security Specialist

Martha Barillas, Reactor Engineer

Approved by: Brian J. McDermott, Chief

Projects Branch 6

Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000443-02-05; North Atlantic Energy Service Corporation (FPL Energy Seabrook, LLC as

of November 1, 2002); on 06/30-09/28/2002; Seabrook Station, Unit 1. Surveillance Testing

and Response to Contingency Events.

The inspection was conducted by resident inspectors, a reactor engineer, a senior project

engineer, a health physics inspector, and security specialists. The inspectors identified two

Green findings that were also determined to involve non-cited violations. The significance of

most findings is indicated by their color (Green, White, Yellow, Red) using IMC 0609,

Significance Determination Process (SDP). Findings for which the SDP does not apply may

be Green or be assigned a severity level after NRC management review. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspector Identified Findings

Cornerstone: Mitigating Systems

C Green. The inspectors identified a Non-Cited Violation of 10 CFR 50, Appendix B,

Criterion XVI Corrective Action, in that corrective actions were not adequate for

degraded electrical connections found on rectifier bank #1 for the B Emergency Diesel

Generator (EDG) in October 2001. The degraded rectifier bank connections were

characterized as serious by industry standards for thermography and required prompt

corrective maintenance. The licensees corrective actions did not adequately evaluate

whether the cause was applicable to rectifier bank #2. In July 2002, during

troubleshooting efforts for problems with the B EDG, two additional serious hot

connections were discovered on rectifier bank #2.

The finding was considered more than minor because if the finding was left uncorrected,

the degraded connections could have degraded further and impacted the reliability of

the EDG. The finding was determined to be of very low safety significance (Green)

since the hot connections did not result in an actual failure of the EDG. Because the

finding is of very low safety significance and the finding was captured in the licensees

corrective action program, this finding is being treated as a Non-Cited Violations,

consistent with Section VI.A.1 of the NRC Enforcement Policy. (Section 1R22)

Cornerstone: Physical Protection

C Green. An in-office review by Region I security specialists identified a non-cited

violation of 10 CFR 73.55(b.1.i) and the requirements of Seabrook Physical Security

Plan. On July 25, 2002, a member of the Security Response Force failed to respond to

an intrusion alarm and was subsequently found inattentive while on duty.

Failure of the response force member to respond to the intrusion alarm in a manner to

assure conformance with the requirements of the Seabrook Station Physical Security

Plan and Procedures was determined to have very low safety significance using the

Interim Physical Significance Determination Process. The finding involved a

ii

vulnerability of Safeguards Systems or Plans, but no actual intrusion occurred and there

have not been more than two similar findings in the past four quarters. (Section 3PP3)

B. Licensee Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been

reviewed by the inspector. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and its

corrective action tracking number are listed in Section 4OA7 of this report.

iii

TABLE OF CONTENTS

Page

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii

TABLE OF CONTENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

1. REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R11 Licensed Operator Requalification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R12 Maintenance Rule Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R13 Maintenance Risk Assessments and Emergent Work Evaluation . . . . . . . . . . 6

1R14 Personnel Performance During Non-routine Plant Evolutions . . . . . . . . . . . . . 7

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R19 Post-Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

2. RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

2PS2 Radioactive Material Processing and Transportation . . . . . . . . . . . . . . . . . . . 17

3. SAFEGUARDS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

3PP3 Response to Contingency Events . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

3PP4 Security Plan Changes . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4. OTHER ACTIVITIES [OA] . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA3 Event Follow-Up . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

4OA6 Meetings, including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

4OA7 Licensee Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

ATTACHMENT 1

SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

iv

Report Details

SUMMARY OF PLANT STATUS:

The plant operated at approximately 100% power for the duration of the inspection period.

1. REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity [R]

1R01 Adverse Weather Protection

.1 Hurricane/Severe Weather Preparations

a. Inspection Scope

The inspectors reviewed Seabrooks preparations for weather related risks associated

with tornados, hurricanes, and high winds. The inspectors performed walkdowns of

systems including the service water building and the emergency feedwater pump house

to evaluate the material condition of tornado dampers, doors, and seals. On August 9,

2002, the inspectors observed testing of tornado dampers. The inspectors reviewed the

following Seabrook Station documents:

C OS1200.03, Severe Weather Conditions, Rev. 10

C NM 11800, Hazardous Condition Response Plan, Rev. 9

C CR 01-12479, Testing of Tornado Dampers

C WO 01B9987, CBA Tornado Damper Testing and Cleaning

C USFAR Section 1.2, 2.3, 2.4

The inspectors also verified that the NRC Regulatory Issue Summary 2000-15,

Recommendations for Ensuring Continued Safe Plant Operation and Minimizing

Requests for Enforcement Discretion during Extreme Weather Conditions was properly

evaluated and procedures were updated.

b. Findings

No findings of significance were identified.

.2 Effects of Hot Weather

a. Inspection Scope

The inspectors reviewed the effects on plant equipment and the stations response to

increased ambient temperatures during June through August 18, 2002. The inspectors

reviewed CR 02-12420 and CR 02-12419, which documented several alarms caused by

the increased ambient temperature, and verified that the effect on the plant was of minor

significance and properly captured in the corrective action program.

The inspectors reviewed applicable data documenting repeated high temperature

alarms and performed partial walkdowns of the affected areas and the control room. In

2

addition, the inspectors interviewed control room operators and the instrumentation and

control supervisor to assess their understanding of the effect of the heat wave on plant

equipment and associated alarms. The following challenges were documented and

evaluated by the station.

  • Battery rooms A, B, and D high temperature alarms
  • Emergency feedwater pump house high temperature

In addition, the inspectors reviewed CR 02-12987, which documented potential

vulnerabilities introduced by the large error band (+/- 10 degrees Fahrenheit) of the local

area temperature indicators. These indicators are used to confirm compliance with area

temperature requirements specified in Technical Specification (TS) 4.7.10. The

inspectors verified that the TS limits were not exceeded based on other, independent

instruments.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Full System Walkdown - Service Water System

a. Inspection Scope

The inspectors performed a full system walkdown of the service water (SW) system,

involving equipment in both trains, associated main control room valve position

indication, and associated piping and in-line components.

The inspectors used the piping and instrumentation drawings for the SW system, the

system health report, the system design bases document, and a list of system related

condition reports and open work orders, to verify the material condition of the inspected

equipment. In addition, the inspectors used the following completed valve lineup

procedures to verify the position of a sample of selected system valves.

  • OX1416.01 Service Water System Fill and Vent, Forms A, B, and C, Rev. 7.

b. Findings

No findings of significance were identified.

3

.2 Full System Walkdown - A Emergency Diesel Generator and Support Systems

a. Inspection Scope

The inspectors performed a full system walkdown of the A Emergency Diesel

Generator (EDG) and partial system walkdowns of several support systems including

the equipment associated with the main control room EDG indicators and associated

piping and in-line components.

The inspectors referenced Seabrook Piping and Instrumentation Drawings for the EDG

fuel oil system, EDG air start system, service water system, and electrical distribution

system. In addition, the inspectors reviewed a list of EDG related condition reports and

a selection of automated work orders to verify the material condition of the inspected

equipment.

b. Findings

No findings of significance were identified.

.3 Partial System Walkdown - Instrument Air System

a. Inspection Scope

The inspectors performed a partial system walkdown of the instrument air system to

verify system alignment during installation and testing of Design Change Request (DCR)

00-0014, Instrument Air Dryer Replacement, (see Section 1R17). Installation of the

DCR involved configuration changes which connected the new dryer (SKD-18B) and a

temporary air dryer to the instrument air system. This system was selected for

alignment verification due to the increased likelihood for a reactor trip initiating event

during DCR installation.

The inspectors reviewed the following documents to determine proper equipment

alignments.

C Procedure ON1042.01, Operation of the Compressed Air System, Rev. 8

  • Procedure ON1242.01, Loss of Instrument Air, Rev. 7
  • Drawing 1-IA-20636, Instrument Air, Rev. 2

C Drawing 1-IA-20637, Instrument Air, Rev. 12

C Drawing 1-IA-20638, Instrument Air, Rev. 11

  • Drawing 1-IA-20639, Instrument Air, Rev. 10
  • Drawing 1-SA-20650, Service Air, Rev. 20

C Temporary Modification 01-0007, Temporary Air Dryer, Rev. 1

Additionally, the inspectors reviewed and evaluated impact on instrument air system

operation for selected open work orders, design change packages, engineering

evaluations, and corrective action program condition reports. The system health report

was reviewed and open issues were discussed with the system engineer.

b. Findings

4

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors examined several areas of the plant to assess: 1) the control of transient

combustibles and ignition sources; 2) the operational status and material condition of

the fire detection, fire suppression, and manual fire fighting equipment; 3) the material

condition of the passive fire protection features (fire doors, fire dampers, fire penetration

seals, etc.); and 4) the compensatory measures for out-of-service or degraded fire

protection equipment. The following areas were inspected:

C B Essential Switchgear Room-Control Building, 21'6" elevation

C A Emergency Diesel Generator Building, all elevations - multiple occasions

C B Emergency Diesel Generator Building, all elevations - multiple occasions

C A High Head Safety Injection Pump Room-Primary Auxiliary Building, 7'0" elevation

C B High Head Safety Injection Pump Room-Primary Auxiliary Building, 7'0" elevation

C A and C Battery Rooms-Control Building, 21'6" elevation

C B and D Battery Rooms-Control Building, 21'6" elevation

C Cable Spreading Room-Control Building, 50'0" elevation

The inspectors reviewed the following documents:

C Fire Protection Pre-Fire Strategies

C FP2.1 Control of Ignition Sources, Rev. 5

C FP2.2 Control of Combustible Materials, Rev. 6

C OX0443.12 Fire Protection Dry Pipe Spray and Sprinkler Systems 18 Month

Inspection, Rev. 6

C Compensatory List of Fire Protection Equipment out-of-service

C Fire Protection Equipment Layout Drawings.

C Technical Requirements Manual Sections 2.7 to 2.12

C Selected CRs and Work Orders

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

a. Inspection Scope

On August 15, 2002, the inspectors observed operator training focusing on human

performance of time critical tasks. The inspectors reviewed the operators ability to

correctly evaluate the training scenario and implement the emergency plan. The

inspectors also evaluated whether or not deficiencies were identified and discussed

during critiques.

b. Findings

5

No findings of significance were identified

1R12 Maintenance Rule Implementation

.1 Enclosure Air Handling (EAH) Damper Failure

a. Inspection Scope

The inspectors evaluated Maintenance Rule (MR) implementation pertaining to an

enclosure air handling (EAH) ventilation damper (EAH-DP-30B) failure that occurred on

August 29, 2002. The damper failed to open as required upon starting its associated

fan for monthly surveillance testing. The damper failure was due to failure of its

normally energized solenoid valve (EAH-FY-30B). The inspectors verified that system

performance was monitored and evaluated as required by 10 Code of Federal

Regulations (CFR) 50.65, Requirements for Monitoring the Effectiveness of

Maintenance of Nuclear Power Plants. The inspectors performed field walkdowns and

a review of historical EAH damper related CRs. The inspectors also performed a review

of historical data documenting solenoid valves failures to access the general

performance of these valves including the effects of aging. In addition, the inspectors

interviewed various licensee personnel including the several system engineers and

evaluated the licensees operability and reportability evaluation documented in CR 02-

12902. The following documents were reviewed:

C CR 02-12902, EAH-DP-30B failed to open upon starting fan EAH-FN-4B;

C IS0603.005, Equipment qualification for ASCO Solenoid Valves, Rev. 4;

C Work Order 0227324 issued to investigate damper EAH-DP-30B failure;

C NUREG-1275, Vol.6, Operating Experience Feedback Report Solenoid-Operated

Valve Problems;

C List of historical CRs documenting solenoid valves and ventilation dampers failures.

b. Findings

No findings of significance were identified.

.2 Instrument Air System

a. Inspection Scope

The inspectors evaluated MR implementation for the instrument air system. The system

was placed in MR category (a)(1) on March 7, 2002, due to unreliable air dryer

performance. Specific attributes reviewed included MR scoping, characterization of

failed structures, systems, and components (SSCs), MR risk categorization of SSCs,

SSC performance criteria or goals, and appropriateness of corrective actions. The

inspectors verified that system performance was monitored and evaluated as required

by 10 Code of Federal Regulations (CFR) 50.65, Requirements for Monitoring the

Effectiveness of Maintenance of Nuclear Power Plants. The inspectors interviewed

engineers, observed system testing, and reviewed various documents including:

C Instrument Air System Performance Report dated July 2002;

6

C MR (a)(1) Improvement Plan for Instrument Air Dryer IA-SKD-18B, Rev. 0;

C Instrument Air System MR Performance and Scope Report, Rev. 1;

C CR 01-07313, 01-13574, 01-12718, 01-11776, 01-10564, 02-03059, and 02-11619.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed the scheduling and control of maintenance activities in order to

evaluate the effect on plant risk. The inspectors reviewed the routine planned

maintenance and emergent work for the following equipment removed from service.

C On July 18, 2002, the inspectors reviewed the risk associated with restoration of the

A battery following discharge testing. The inspectors attended the pre-evolution

briefing, observed the work activity, and verified the proper use of procedures. When

the normal battery supply breaker did not close as expected (CR 02-11408), the

inspectors verified that operators minimized the risk associated with a battery

configuration.

C On August 6, 2002, the inspectors reviewed the risk assessment for the days work

activities. The equipment removed from service included the A cooling tower fan,

two switch yard breakers, the A EDG and the A residual heat removal (RHR)

pump. The inspectors evaluated the controls placed on the risk significant activities

and active measures taken to reduce the risk. For example, the inspectors verified

the surveillance test, which resulted in inoperability of the EDG and RHR pump, was

not performed at the same time as active work in the switch yard (risk for loss of

offsite power).

C On August 13, 2002, the inspectors reviewed the risk associated with spurious trips

of the Tewksbury offsite power line on August 10 and 13. The inspectors examined

the operators actions to evaluate risk and actions taken by maintenance technicians

to prevent further trips. The inspectors reviewed CRs 02-12194, 02-12279 and 01-

00507, interviewed maintenance technicians and the system engineer, and reviewed

various electrical prints.

C On August 19, 2002, the inspectors reviewed the risk associated with inspections of

vendor supplied electrical wire terminations on the A EDG panels (CP-75A and B).

The inspectors observed the work activity, interviewed field personnel, verified the

proper use of procedures, and reviewed the associated work order (WO 0225256).

The inspectors also reviewed the engineering evaluation documented under CR 02-

12142 and associated corrective actions for some broken strands and loose wires

identified during the inspection of both EDG cabinets.

C On August 30, 2002, the inspectors reviewed the risk associated with emergent work

to investigate the failure of EAH damper (EAH-DP-30B) and to implement repairs.

7

The inspectors performed field walkdowns, reviewed the associated work order (WO)

0227324, and verified the proper use of procedures.

C On September 17, 2002, the inspectors reviewed the risk associated with inspections

and actions to correct deficiencies in the B and C secondary component cooling

water pumps oil bubblers. The inspectors performed field walkdowns, interviewed the

pump specialist, and reviewed CR 02-13505. In addition, the inspectors verified that

the evaluation of this issue included an adequate extent of condition review and

assessment of generic implications.

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-routine Plant Evolutions

.1 Spent Fuel Pool Dive and Strainer Gasket Replacement

a. Inspection Scope

On September 11 to 16, 2002 the inspectors reviewed the activities associated with the

gasket replacement for the spent fuel pool skimmers. The replacement required the

use of qualified divers and the installation of a temporary platform for the divers. The

inspectors examined the controls placed on the divers by reviewing procedure

HN0960.01, Radiological Safety Requirements for Diving Operations, Rev. 23, and by

interviewing the divers, operators, the job supervisor, maintenance engineers and

technicians, and radiation protection personnel. In addition, the inspectors attended

several pre-job briefs, reviewed the WO 00C5355, and assessed the controls of foreign

material and temporary equipment.

b. Findings

No findings of significance were identified.

8

.2 Control Room Annunciator Power Failure

a. Inspection Scope

On September 9, the inspectors reviewed the operators activities associated with the

unexpected loss of power to hard wired annunciator panel UA-51 documented under CR

02-13247. The inspectors performed field walkdowns, interviewed operators, and

examined the Seabrook Station Alarm Response Procedures associated with this panel

to assess the effect on plant safety. The inspectors also reviewed the Emergency

Response Manual, Section 1.1 to confirm the determination that the loss of the

annunciators did not require an entry into an emergency action level.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

.1 Incorrectly Installed Electrical Connection on the Emergency Diesel Generator Control

Panel

a. Inspection Scope

The inspectors reviewed CR 02-11097, which evaluated the effects of a shorted

connection in the A EDG, in order to determine that the identified condition did not

adversely affect safety system operability or plant safety. The shorted connection,

which the licensee attributed to a human performance error, occurred on July 10, while

the "A" EDG was out of service for scheduled maintenance activities. The inspectors

verified the TS limiting condition for operation implications were properly addressed, and

that an adequate extent of condition review was performed. Seabrook Station

Administrative Procedure OE 4.5, "Operability Determination," and NRC Generic Letter 91-18, "Resolution of Degraded and Nonconforming Conditions" were used to evaluate

the licensees operability determination.

b. Findings

No findings of significance were identified.

.2 Emergency Power Sequencer Switch Found in the Test Position

a. Inspection Scope

The inspectors reviewed the Operability Determination (OD) prepared on August 1,

2002 to address the degraded equipment conditions documented in two condition

reports, (CRs) 02-11857, which discusses the trip of battery charger 1-EDE-BC-1B, and

CR 02-11865, which identifies a condition where the test switches in the emergency

power sequencer (EPS) on both safety trains were found to be in an abnormal position

(the TEST mode). The CRs are related by the facts discovered during the investigation

of the loss of the battery charger, which noted that an EPS output relay had spuriously

9

energized, causing the battery chargers power supply input breaker to trip open. Since

the EPS test switches were determined to have been out of position since May 2002,

the OD was initiated to evaluate this condition with respect to the functionality of each

EPS, the possibility of a causal relationship between the mis-positioned switches and

the failed relay, and the potential for either the energized relay or a relay driver card

malfunction to adversely affect the EPS function.

The inspectors reviewed the WOs 0224585 and 0224586 issued to conduct the

troubleshooting activities to determine the cause of the loss of battery charger 1-EDE-

BC-1B and subsequently witnessed testing and repair activities in the train B EPS to

establish that the problem was caused by an intermittent failure of a relay driver card.

The inspectors also reviewed the record for the operational surveillance (OX1426.20) for

the testing in May 2002 of one EDG and its associated EPS. The inspectors verified

consistency between the surveillance test logic and details in the OD regarding the EPS

design features that allow proper sequencing of the EDG loads with the sequencer

switch position in TEST. The applicable electrical schematic diagrams (e.g., FP 31427)

for the battery charger supply power, related EPS relays and wiring were reviewed and

discussed with the cognizant licensee instrumentation, and control personnel involved in

the troubleshooting and repair activities.

The inspectors evaluated the Seabrooks justification for continued operation,

addressing the problems identified in both CRs that necessitated the required operability

determination. The inspectors verified that the post-maintenance test and operational

surveillance (OX1426.03) of the train B EPS validated the troubleshooting results,

corrective actions, and overall determination regarding operability of the EPS function.

b. Findings

No findings of significance were identified.

.3 Emergency Diesel Generator Issues

a. Inspection Scope

The inspectors reviewed the following conditions in order to determine that the

conditions did not adversely affect safety system operability or plant safety. In addition,

where a component was determined to be inoperable, the inspectors verified the TS

limiting condition for operation implications were properly addressed. Seabrook Station

Administrative Procedure OE 4.5, Operability Determination, and NRC Generic Letter 91-18, Resolution of Degraded and Nonconforming Conditions were used to evaluate

the licensees operability determinations. The inspectors performed field walkdowns,

interviewed personnel, and reviewed the following items:

inspectors reviewed the evaluation, interviewed the system engineer, evaluated the

impact of a small jacket water leak, and examined the effects of a sustained leak for

a 24-hour period. The inspectors also evaluated the expected accident loading for

the EDG since the size of the leak appeared load dependent. In addition, the

10

inspectors reviewed the available indications of a jacket leak and prescribed operator

actions in response to those indications.

  • CR 02-12412, Loose wires in the B EDG rectifier selector switch. During

determination of the rectifier selector switch, maintenance technicians identified wires

that separated from a lug. Subsequent inspections of the A and B EDGs identified

other loose or not optimal connections. The inspectors reviewed the past operability

evaluation concentrating on the seismic qualification, the extent of condition review

evaluation, and actions taken to correct the deficiencies.

b. Findings

No findings of significance were identified.

.4 Unit Substation Electrical Breaker Found in Incorrect Position

a. Inspection Scope

The inspectors reviewed CR 02-10945, which discusses the incorrect racked out

position of unit substation breaker 61, to determine if the as found condition had any

adverse effect on any of the offsite electrical power supplies to Seabrook Station. The

inspectors reviewed the licensees evaluation to determine the cause of the breaker

being found in the incorrect position.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed DCR 00-0014, Instrument Air Dryer Replacement, design

change notice (DCN) number two to verify that system design bases, licensing bases,

and performance capability were not degraded by the DCR. The inspectors observed

selected instrument air dryer SKD-18B testing activities to ensure operability of the

instrument air system and to verify that plant risk was not adversely impacted. The

inspectors monitored installation of a temporary air dryer as a contingency for continued

system operation during SKD-18D installation and testing. The inspectors observed

pre-evolution briefings, interviewed various station personnel, witnessed a portion of the

post-installation testing, and reviewed selected design documents including those listed

below. The DCR incorporated changes to address a recent industry loss of an

instrument air event and met the requirements of North Atlantic Design Control (NADC)

Manual, Rev. 19.

C DCR 00-0014, Instrument Air Dryer Replacement, DCN 2

C DCR 00-0014 installation schedule

C Work Order 01C0451, Post-Installation Testing of Instrument Air Dryer Skid SKD-

18B, Rev. 0

11

C NADC Manual, Rev. 19

C North Atlantic Work Management Program, Rev. 17

C Seabrook Updated Final Safety Analysis Report Sections 8.3.1.4, 9.3.1.2.a, 9.3.1.5,

and 10.4.10.2, Rev. 7

C Calculation SBC-565, Diesel Generator Fuel Oil Tank Vortexing Evaluation dated

April 1, 1993

C Calculation 760-11, Diesel Generator Fuel Oil Storage System Capacity dated

December 21, 1984

C Calculation C-S-1-E-0161, Diesel Generator Maximum Allowable Fuel Oil

Consumption Rate, Rev. 11

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the on-line maintenance assessment forms, and several post-

maintenance testing (PMTs) activities to ensure: 1) the PMT was appropriate for the

scope of the maintenance work completed; 2) the acceptance criteria were clear and

demonstrated operability of the component; and 3) the PMT was performed in

accordance with procedures. The following PMTs were reviewed:

  • On July 10, LSO563.58, Trip Check Procedure for The Diesel Generator Switchgear

Breakers, Rev. 1, following the preventive maintenance replacement of several

safety-related relays associated with the A EDG. The inspectors also reviewed

condition reports, CR 02-11114 and CR 01-11160, which documented minor

deficiencies identified during the testing.

  • On July 16, the function stroke of the C atmospheric dump valve following corrective

maintenance on the valve positioner completed per WO 0222395. The inspectors

also reviewed several condition reports, which documented minor deficiencies

identified during the testing.

  • On July 26 through July 29, numerous tests of the B EDG were conducted using

various combinations of installed rectifier banks and the operability surveillance

OX1426.05, DG 1B Monthly Operability Surveillance, following the performance of

several associated work orders that addressed rectifier bank condition, synchronizing

relay operability and other supporting maintenance activities.

  • On August 9, emergency starts of the B EDG using the #1 and #2 rectifier banks

and the operability surveillance OX1426.05, DG 1B Monthly Operability

Surveillance, Rev. 8 following replacement of the #1 rectifier bank (WO 0223733)

and the rectifier selector switch (WO 0223721) in the B EDG control panel.

  • On September 25 and 26, OX1412.02, PCCW Train B Quarterly Operability, 18

Month Position Indication, And Comprehensive Pump Testing, Rev. 8, following

12

corrective maintenance inspection and leak repair of the D primary component

cooling water pump seal water piping. The inspectors also reviewed the applicable

on-line maintenance assessment evaluation.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

.1 Miscellaneous Surveillance Tests

a. Inspection Scope

The inspectors observed portions of several surveillance tests for safety-related systems

to verify that the system and components were capable of performing their intended

safety function, to verify operational readiness, and to ensure compliance with required

TSs and surveillance procedures.

The inspectors attended some of the pre-evolution briefings, performed system and

control room walkdowns, observed operators and technicians perform test evolutions,

reviewed system parameters, and interviewed the system engineers and field operators.

The following surveillance procedures were reviewed:

C On July 9, IX1668.341, SI-P-937 Containment Pressure Protection Channel I

Operational Test, Rev. 6;

C On July 12, LS0563.68, Diesel Generator Bus Undervoltage Relay Inspection,

Testing and PM, Rev. 1;

C On July 23, IX1680.922, Solid State Protection System Train B Actuation Logic

Test, Rev. 8;

C On July 25, LX0563.01, Reactor Coolant Pump Undervoltage Quarterly

Surveillance, Rev. 3;

C On September 17, CS0910.01, Primary Systems Sampling at SS-CP-166A, Rev. 9

and CX0901.02, Determination of Dose Equivalent I-131, Rev. 10.

13

b. Findings

No findings of significance were identified.

.2 Emergency Diesel Generator Surveillance Testing

a. Inspection Scope

The inspectors reviewed licensee performance related to the following surveillance

tests, involving periodic operability verification of the EDGs:

C OX1426.01, DG 1A Monthly Operability Surveillance

C OX1426.18, Aligning DG 1A Controls for Auto Start

C OX1426.20, Diesel Generator 1A 18 Month Operability Surveillance

C OX1426.21, Diesel Generator 1B 18 Month Operability Surveillance

The test records for the 18-month operability surveillance of the A and B EDGs,

conducted in May 2002, were reviewed. The surveillance records were checked for

evidence of the satisfactory performance testing of both trains of EDG equipment, when

subjected to postulated accident signals, and EDG design events consistent with the TS 4.8.1.1.2f requirements. The inspectors examined the sequence of the test

performance and the system lineup for the conduct of each successive test event. The

inspectors verified that the surveillance records included proper notation of the test

equipment used, documentation of the required procedural step performance, and

evidence of the resolution of test exceptions.

The inspectors also reviewed and evaluated the operational preparations for

surveillance testing of the A EDG on July 30 and 31, 2002. The surveillance was

conducted based upon questions raised regarding common mode concerns relating to

recent problems with the B EDG surveillance test performance. [Note: the results of an

NRC Special Inspection of the problems observed, and resulting period of inoperability

for the B EDG was documented in NRC Inspection Report 50-443/02-10.] Work

Orders associated with the A EDG surveillance run were reviewed and the records of

the successful completion of surveillance procedures OX1426.01 and OX1426.18 were

verified to provide adequate documentation of the TS 4.8.1.1.2 a.5, 6, and 7

requirements. The inspectors discussed the performance results of the A EDG

operational test with the cognizant operations and engineering personnel to confirm

consideration of the test data in the continuing review of the impact of the B EDG

surveillance problems and to verify appropriate Seabrook management attention to the

EDG TS compliance ramifications (reference: Condition Report 02-11795).

b. Findings

No findings of significance were identified.

14

.3 Emergency Diesel Generators - Hot Connections

a. Inspection Scope

On July 26, 2002, during a maintenance run of the B EDG following problems with

reactive load fluctuations, engineers identified two unusual hot connections through the

use of thermography. NRC Inspection Report 50-443/02-10 documented the special

inspection team review of the reactive load swings. The inspectors reviewed the results

from a previous surveillance test on the B EDG conducted on October 17, 2001, which

also identified two hot connections. The inspectors reviewed the corrective actions for

the October 2001 event and their relation to the identified hot connection in July 2002

through interviewing various system engineers and examining the following documents:

C CR 01-10979 Two hot connections in control cabinet 1-DG-CP-76A (B EDG) -

October 2001

C CR 01-12362 Thermography Program Issues

C CR 02-11735 Two hot connections in control cabinet 1- DG-CP-76A (B EDG) - July

2002

C ES1807.016, Thermography Program, Rev. 2

C OX1426.05, DG 1B Monthly Operability Surveillance, Rev. 8

C WO 0223733 Replace/Repair Rectifier #1 for 10DG-1-B

C WO 0223721 Replace Rectifier Selector Switch

b. Findings

Introduction

The inspectors identified that Seabrooks corrective actions and extent of condition

reviews were not adequate for two hot connections found in the B EDG control panel

in October 2001. Failure to have adequate corrective actions contributed to not

identifying two additional hot connections that were discovered following problems with

the B EDG control panel in July 2002. This issue was assessed as having very low

safety significance (Green) and was determined to be a non-cited violation of 10 CFR

50, Appendix B, Criterion XVI Corrective Action.

Description

On October 17, 2001, Seabrook identified two hot connections associated with rectifier

bank #1 in the B EDG control panel. This was the first full thermography performed on

the B EDG control panel. The two hot connections were classified as serious based

on the temperature deviation from normal per the program guidance documents. The

issue was captured in the corrective action system (CR 01-10979) and immediate

actions were taken to correct the condition. The evaluation identified original

construction deficiencies that caused the hot connection and corrective actions included

some checks of the wiring.

The inspectors identified the corrective actions did not include a full review of B EDG

with rectifier bank #2 in-service. The local control panel for each EDG has two rectifier

banks, with only one bank in service at a time. The rectifier bank in service is typically

15

alternated on a monthly basis. Although it was the first full thermography, Seabrook did

not recognize that rectifier bank #2 potentially also had the same condition, which could

degrade and affect the reliability of the EDG. In addition, one of the two rectifier banks

on the A EDG had also not been analyzed with thermography.

On July 26, 2002, engineers identified two additional serious hot connections as part of

a troubleshooting effort following problems with reactive load fluctuations on the B

EDG. The hot connections were associated with rectifier bank #2 and located on a

termination (crimp lug barrel) of cable F1A near diode CR4 and on a termination of

cable P2A near the rectifier bank selector switch SW1. Engineers later determined that

the hot connections were not the most probable cause of the reactive load swings.

Although the serious hot connections were not identified as the most probable cause,

the hot connections could have affected the reliability of the EDG.

Analysis

Seabrooks failure to have adequate corrective actions for degraded electrical

connections found on rectifier bank #1 for the B EDG is considered a performance

deficiency since the corrective action program is required to assure the cause of

significant conditions is determined and corrective action taken to preclude repetition.

The licensees corrective actions did not adequately evaluate whether the cause was

applicable to rectifier bank #2. In July 2002, during troubleshooting efforts for problems

with the B EDG, two additional serious hot connections were discovered on rectifier

bank #2.

The finding was considered more than minor because if the finding was left uncorrected,

the degraded connections could have degraded further and impacted the reliability of

the EDG. Using Appendix A, Phase 1 of Manual Chapter MC 0609, the finding was

determined to be of very low safety significance (Green) since the hot connections did

not result in actual failure of the EDG. This analysis was based on the assumption that

the hot connections did not cause the B EDG reactive load fluctuation observed in July

2002 and described in NRC Inspection Report 50-443/02-10.

The failure to have adequate corrective actions and extent of condition reviews is an

item affecting the problem identification and resolution cross cutting area. (Section

4OA2)

Enforcement

Traditional enforcement does not apply because the issue did not have any actual safety

consequence or potential for impacting the NRCs regulatory function and was not the

result of any willful violation of NRC requirements or Seabrooks procedures.

10 CFR 50, Appendix B, Criterion XVI Corrective Action requires for a significant

condition adverse to quality, measures shall assure the cause of the condition is

determined and corrective action taken to preclude repetition. The hot connections on

the EDG control panel were considered significant since they could affect the EDG

controls and therefore the reliability of the EDG. Contrary to this requirement, Seabrook

failed to have adequate corrective actions to preclude recurrence of the deficiency.

16

Because this violation was of very low safety significance and Seabrook entered this

finding into its corrective action program (CR 02-14103), this violation is being treated as

a Non-Cited Violation consistent with section VI.A.1 of the NRC Enforcement Policy

(NCV 50-443/02-05-01).

1R23 Temporary Plant Modifications

a. Inspection Scope

On September 20, the inspectors reviewed temporary alteration 02-003 associated with

the installation of a temporary pneumatic gag to hold a charging and volume control

system valve (1-CS-V-521) in the open position to allow testing of a system circuit

breaker. The inspectors reviewed associated implementing documents including CR

02-13501 and loop diagram 1-NHY-506275, Rev. 17, to verify the design basis and that

the affected system/component operability was maintained.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness (EP)

1EP6 Drill Evaluation

a. Inspection Scope

On August 21, the inspectors observed portions of the Combined Functional Emergency

Preparedness Drill, 02-02, to evaluate the conduct of the drill and adequacy of the

Seabrooks critique. The inspectors verified that event classification and notification

were properly conducted and priorities were communicated in the technical support

center. The inspectors also verified that identified problems were entered into the

corrective action program through observation of the critique, review of the drill

evaluation report, and review of the list of CRs initiated.

The inspectors reviewed CR 02-13215, which documented a condition identified by the

inspectors, regarding the proper level of involvement by coaches and controllers during

critical evolutions. In addition, the inspectors reviewed CR 02-13203, which

documented a condition identified by the inspectors regarding the procedural

requirement to use data provided by the off-site emergency operations facility software

rather than the control room software when determining the projected off-site dose

calculation.

17

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Public Radiation Safety (PS)

2PS2 Radioactive Material Processing and Transportation

.1 System Walkdown

a. Inspection Scope

The inspectors walked down accessible portions of the radioactive liquid and solid waste

collection/processing systems, and radwaste storage locations, with a Nuclear Systems

Operator and the Health Physics Technical Supervisor, respectively, to determine if:

systems and facilities were consistent with descriptions contained in the Updated Final

Safety Analysis Report (UFSAR); to evaluate general material conditions; and to identify

changes to the systems. Systems visually inspected included portions of the Asphalt

Solidification System, Boron Recovery System, and Steam Generator Blowdown

System. Radwaste storage locations visually inspected included the Waste

Concentrates Tank Room, Spent Resin Sluice Filter Room, Resin Centrifuge Room,

Unit-2 Cooling Tower, and Radioactive Materials Storage Building.

During the walkdowns, the inspectors also reviewed the following:

C the status of any non-operational waste process equipment and the adequacy of

administrative and physical controls for those systems;

C changes made to radioactive waste processing systems and the potential radiological

impact, including safety evaluations, of these changes;

C current processes for transferring radioactive waste resin and sludge to shipping

containers and the mixing and sampling of the waste;

C radioactive waste/material storage and handling practices;

C sources of radioactive waste at the station; and,

C the general condition of facilities and equipment.

The review was against the criteria contained in the UFSAR, Technical Specifications,

the Process Control Plan (PCP), 10 CFR Parts 20, 61, 71, applicable Branch Technical

Positions, and the Seabrook procedures.

b. Findings

No findings of significance were identified.

18

.2 Waste Characterization and Classification

a. Inspection Scope

The inspectors reviewed the following matters:

C radio-chemical sample analysis results for the radioactive waste streams;

C the development of scaling factors for difficult to detect and measure radio nuclides;

C methods and practices to detect changes in waste streams;

C classification and characterization of waste relative to 10 CFR 61.55 and 10 CFR

61.56;

C implementation of applicable Branch Technical Positions on waste classification;

concentration averaging, waste stream determination, and sampling frequency;

C current waste streams and their processing relative to descriptions contained in the

UFSAR and the stations PCP; and

C current processes for transferring radioactive waste resin and sludge discharges into

shipping/disposal containers to determine the adequacy of sampling.

The review was against the criteria contained in the UFSAR, PCP, applicable Branch

Technical Positions, 10 CFR Parts 20, 61, 71, and licensee procedures.

b. Findings

No findings of significance were identified.

.3 Shipment Records and Documentation

a. Inspection Scope

The inspectors selected and reviewed records associated with five (5) non-excepted

shipments of radioactive material made since the previous inspection of this area. The

shipments were Nos.01-006, 01-009,02-003, 02-010, and 02-036. The following

aspects of the radioactive waste packaging and shipping activities were reviewed:

C Implementation of applicable shipping requirements including completion of waste

manifests;

C Implementation of the specifications in applicable Certificates of Compliance, for the

approved shipping casks including limits on package contents;

C Classification and characterization of waste relative to 10 CFR 61.55 and 61.56;

C Implementation of 10 CFR 20, Appendix G;

C Labeling of containers;

C Placarding of transport vehicles;

C Conduct of vehicle checks;

C Providing of driver emergency instructions;

C Completion of shipping paper/disposal manifest;

The review was against criteria contained in 10 CFR Parts 20, 61, 71, applicable

Department of Transportation requirements, as contained in 49 CFR Parts 170-189;

station procedures; and applicable disposal site licenses and related correspondence.

19

b. Findings

No findings of significance were identified.

3. SAFEGUARDS

Cornerstone: Physical Protection [PP]

3PP3 Response to Contingency Events

.1 Response Force Member Inattentive to Duty

a. Inspection Scope

The inspectors conducted an in-office review of the circumstances involving a failure of

a Response Force Member to respond to an Intrusion Alarm, as a result of being

inattentive to duty, on July 25, 2002. The following documents were reviewed:

C Seabrook Station Physical Security Plan, Revision 29, December 18, 2001

C Seabrook Station Contingency Plan, Revision 13, January 11, 2002

C Condition Report 02-05891, April 30, 2002, NRC perceived inattentive to duty

C Condition Report 02-10104, June 14, 2002, Security Officer inattentive to duty

C Condition Report 02-10541, June 25, 2002, Explore negative trends in Security

Officers being inattentive to duty

C Condition Report 02-11729, July 25, 2002, Security Officer inattentive to duty

The review was against applicable requirements contained in 10 CFR 73.55,

Requirements for physical protection of licensed activities in nuclear power reactors

against radiological sabotage, and the Seabrook Physical Security Plan, Revision 29,

dated December 18, 2001.

b. Findings

Introduction

The inspectors identified a finding having very low safety significance (Green) involving

the failure of a Seabrook Station armed response force member to respond to an

intrusion alarm, as a result of being inattentive while on duty on July 25, 2002. This

finding was considered a non-cited violation of the NRC-approved Physical Security

Plan for the Seabrook facility as required by 10 CFR 73.55, Requirements for physical

protection of licensed activities in nuclear power reactors against radiological sabotage.

20

Description

At approximately 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />, on July 25, 2002, Central Alarm Station (CAS) operator

attempted to contact a security response officer (an armed responder) by radio to direct

the individual to respond to a vital area door alarm, which is a possible indication of

intrusion. The security officer did not answer the radio call, and did not respond to the

vital area door alarm. A security supervisor who heard the radio transmission

responded to the indicated vital area door, and appropriately resolved the alarm

condition. The supervisor subsequently went to the ready room and found the response

force member inattentive to duty.

On the basis of radio communications, the inspectors determined that this condition

existed for no more than thirty minutes.

Analysis

The security response officers failure to meet specific conditions of the NRC-approved

Physical Security Plan, relative to being alert and immediately available for response,

constitutes a performance deficiency. The cause of this matter was reasonably within

Seabrooks ability to foresee and correct; and should have been prevented. However,

the occurrence did not represent an immediate safety concern since an alternate

responder properly assessed the alarm and appropriately resolved the alarm condition.

No actual intrusion occurred.

Traditional enforcement does not apply because the issue did not have any actual safety

consequence or potential for impacting the NRCs regulatory function. While the matter

does not currently appear to be the result of any willful violation of NRC requirements or

Seabrook Stations procedures, this finding will be re-evaluated in accordance with

NRCs Enforcement Policy if deliberateness is later determined.

The finding involved an occurrence relative to the licensees Physical Security program

that was contrary to NRC regulations and the NRC approved Physical Security Plan.

The matter is more than minor in that the issue is associated with the Response to

Contingency Events attribute of the Safeguards cornerstone; and affected the objective

of this cornerstone since failure to comply with the requirements of the Physical Security

Plan may compromise the licensees ability to provide high assurance that the physical

protection system can protect against the design basis threat of radiological sabotage.

The response force officers failure to maintain alertness and be immediately available

for response in accordance with the Physical Security Plan, was determined to have

very low safety significance (Green) using the Interim Physical Protection Significance

Determination Process (Appendix E, Manual Chapter 0609). Specifically, the finding

involved a Vulnerability of Safeguards Systems or Plans. However, in this case, no

actual intrusion occurred; and there have not been greater than two similar findings in

the last four quarters. A second similar licensee identified violation is described in

Section 4OA7.

Enforcement

21

10 CFR 73.55(b)(1)(i) requires all licensees to maintain safeguards in accordance with

Commission regulations and the licensees security plan. Seabrook Station License

Condition 2.E, Physical Security, requires in part, the licensee to fully implement and

maintain in effect all provisions of the physical security plan previously approved by the

Commission, and all amendments and revisions to such plans. Section 10.1 of the

Seabrook Physical Security Plan, Revision 29, dated December 18, 2001, states that

armed responders will be immediately available for response. The Physical Security

Plan also states, in Section 2.6.7, that specific duties of security personnel are

described in Seabrook Station Administrative Procedures. Section 4.1.3 of the

Seabrook Station Security Department Instruction SDI 0042, Security Posts and Recall

of Security Personnel, requires security personnel to remain alert and prevent

unauthorized entry to protected and vital areas.

Contrary to the above, a response force officer was inattentive to duty in the ready room

at approximately 2130, on July 25, 2002 and consequently, failed to remain alert and

immediately available for response. Specifically, the security response officer failed to

respond to a vital area door alarm, a possible indication of intrusion; and was

subsequently observed to be inattentive to duty, by a security supervisor.

Seabrook documented this issue in its corrective action program as Condition Report

02-11729, and initiated immediate actions to preclude recurrence, including initiation of

a formal root cause assessment. This finding is considered a non-cited violation having

very low safety significance (Green). (NCV 50-443/02-05-02)

.2 Periodic Inspection of Response to Contingency Events

a. Inspection Scope

The following activities were conducted to determine the effectiveness of Seabrook

Stations Response to Contingency Events, as measured against the requirements of

10 CFR 73.55 and the Seabrook Station Safeguards Contingency Plan:

C On September 12, 2002, a review of documentation associated with the licensees

force-on-force exercise program was conducted. The review included documentation

and critiques for exercises conducted since the first quarter of 2002 when the

exercises were resumed post September 11, 2001.

C On September 11, 2002, performance testing of the Seabrook Station intrusion

detection systems was conducted. This testing was accomplished by touring the

entire perimeter and selected areas of potential vulnerability in the intrusion detection

system. During the walkdown of the intrusion detection system, nine specific

locations were selected for testing. Observations were made of a Seabrook Station

Security Force Member performing crawl, jump and run testing at these nine

locations.

C On September 10, 2002, a review was conducted of the Seabrook Station defensive

strategy, response time lines, target sets and relevant implementing procedures.

22

C On September 10, 2002, three tabletop exercises were conducted. The mock

adversary was provided entry location and target set information by the inspector.

The response force was directed by a Central Alarm Station Operator. A senior

member of the Seabrook Station Operations staff provided relevant operations

information during the evolution of the exercises.

b. Findings

No findings of significance were identified.

.3 Response to Contingency Events

The Office of Homeland Security (OHS) developed a Homeland Security Advisory

System (HSAS) to disseminate information regarding the risk of terrorist attacks. The

HSAS implements five color-coded threat conditions with a description of corresponding

actions at each level. NRC Regulatory Information Summary (RIS) 2002-12a, dated

August 19, 2002, "NRC Threat Advisory and Protective Measures System," discusses

the HSAS and provides additional information on protective measures to licensees.

a. Inspection Scope

On September 10, 2002, the NRC issued a Safeguards Advisory to reactor licensees to

implement the protective measures described in RIS 2002-12a in response to the

Federal government declaration of threat level "orange." Subsequently, on

September 24, 2002, the OHS downgraded the national security threat condition to

"yellow" and a corresponding reduction in the risk of a terrorist threat.

The inspector interviewed licensee personnel and security staff, observed the conduct of

security operations, and assessed licensee implementation of the threat level "orange"

protective measures. Inspection results were communicated to the region and

headquarters security staff for further evaluation.

b. Findings

No findings of significance were identified.

3PP4 Security Plan Changes

a. Inspection Scope

An in-office review was conducted of changes to the Physical Security Plan (Revisions

28 and 29), Safeguards Contingency Plan (Revisions 12 and 13) and Training and

Qualification Plan (Revisions 12, 13, and 14) submitted to the NRC on April 5, 2001,

January 11, 2002, and March 22, 2002 in accordance with the provisions of

10 CFR 50.54(p). The review was conducted to confirm that the changes were made in

accordance with 10 CFR 50.54(p), and did not decrease the effectiveness of the plan.

b. Findings

23

No findings of significance were identified.

4. OTHER ACTIVITIES [OA]

4OA1 Performance Indicator Verification

.1 (Closed) URI 50-443/01-08-03: Emergency Preparedness Performance Indication -

Evaluating Exceeding the 15 Minutes for Classifications

In NRC Inspection Report 50-443/01-08, the inspectors identified Seabrook guidance

that potentially would consider classification of events greater than 15 minutes

acceptable for the emergency preparedness performance indicator. Seabrook

submitted a frequently asked question (FAQ) to resolve the issue. Seabrook has since

withdrawn the FAQ and revised their internal performance indicator guidance in

accordance with Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment

Performance Indicator Guideline, Rev. 2.

The inspectors reviewed the procedure Emergency Preparedness Performance

Indicators (EPDP-03), Rev. 9 and concluded that the corrective actions addressed the

issue. The inspectors determined based on a review of a sample of the 2002

performance indicator (PI) data that the actual guidance was not utilized to accept

greater than 15 minute classifications. Therefore, the data submitted to the NRC was

unchanged and no violation of NRC requirements was identified.

.2 Safety System Functional Failures

a. Inspection Scope

The inspectors reviewed the PI data for safety system functional failures to determine

whether NEI 99-02 was properly implemented. The inspectors reviewed the data

collected, PI definitions, and 10 CFR 50.73 requirements described in detail in NUREG

1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73, Rev. 2. The inspectors

verified the accuracy of the reported data through reviews of the Licensee Event

Reports submitted during the period of September 2001 to August 2002.

b. Findings

No findings of significance were identified.

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.3 Reactor Coolant System Activity

a. Inspection Scope

The inspectors reviewed the PI data for reactor coolant system activity to determine

whether NEI 99-02 was properly implemented during the period of June 2001 to June

2002. The inspectors verified the calculations and observed the reactor coolant system

sample and analysis using CS0910.01 and CX0901.02 (See Section 1R22). The

inspectors reviewed the following documents in the evaluation of the PI data:

C UFSAR Section 1.8 Conformance to NRC Regulatory Guides;

C Regulatory Guide 1.109, Calculation of Annual Doses to Man from Routine Releases

of Reactor Effluents for the Purpose of Evaluating Compliance with 10 CFR Part 50,

Appendix I, Rev. 1;

C JD0999.910, Reporting Key Performance Indicators Per NEI 99-02, Rev. 0;

C RCS sample results given in iodine 131 to 135 and as dose equivalent iodine;

C TS 3.4.8, Specific Activity

b. Findings

No findings of significance were identified.

.4 Reactor Coolant System Leakage

a. Inspection Scope

The inspectors reviewed the PI data for reactor coolant system leakage to determine

whether NEI 99-02 was properly implemented during the period of June 2001 to June

2002. The inspectors reviewed a sample (April, May, and June data) of the data used to

determine the maximum monthly leakage. The inspectors reviewed and observed

operator use of procedure OX1401.02, RCS Steady State Leak Rate Calculation,

Rev. 6. The inspectors also reviewed the RCS leakage TS requirements and verified

the PI calculation.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Processing and Shipping of Radioactive Material

a. Inspection Scope

The inspectors reviewed Nuclear Oversight Department (Quality Assurance)

audits/surveillance reports, and Health Physics Department self-assessments relating to

the radioactive waste handling, processing, storage, and shipping programs, including

the Process Control Plan. The inspectors also reviewed twenty (20) Condition Reports

(CRs) related to the control of radioactive material initiated between January 2001 and

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August 2002 to evaluated Seabrooks threshold for identifying, evaluating, and resolving

problems in implementing these programs. This review was conducted against the

criteria contained in 10 CFR Parts 20 and 71.101. The following documents were

reviewed:

QUALITY ASSURANCE SURVEILLANCE REPORTS/AUDITS:

C QASR 01-0171 Assessment of Mixed Waste

C QASR 02-0019 Assessment of Radiological Waste Services move of a

High Integrity Container to a Transfer Cask

C QASR 02-0095 Health Physics Activities during OR08

C Audit No. 00-A07-01 Radwaste/Process Control Program

C Audit No. 98-A07-01 Radwaste/Process Control Program

HEALTH PHYSICS DEPARTMENT SELF-ASSESSMENTS:

C SA 01-0045 Processing of Green-Is-Clean Trash

C SA 02-0074 HP/Radwaste Biannual Condition Report Trend Analysis

b. Findings

No findings of significance were identified.

.2 October 2001 Reactor Trip due to Control Rod Drop - Problem Identification and

Resolution Sample

a. Inspection Scope

The reactor trip and past issues leading to the trip were discussed in NRC Inspection

Reports 50-443/01-010,01-011, and 02-03. The inspectors had previously reviewed the

root cause and corrective actions identified in the CR 01-10868. During this review, the

inspectors examined the additional corrective actions completed under CR 01-12250.

The inspectors verified that remote inspections of the control rod drive mechanisms

were conducted, reviewed the videotape, and interviewed the engineers that conducted

the examination. Additionally, the inspectors independently reviewed chemistry

sampling data to determine if any trend was identified to further substantiate the root

cause of the reactor trip.

b. Findings

No findings of significance were identified.

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.3 Emergency Diesel Generators - Hot Connections

The inspectors identified a finding related to inadequate corrective actions and extent of

condition reviews. The finding is documented in Section 1R22.

4OA3 Event Follow-Up

.1 Reactive Load Fluctuation on the B Emergency Diesel Generator

a. Inspection Scope

On July 24, Seabrook experienced reactive load fluctuation on the B EDG during

normal monthly surveillance testing. Operators declared the EDG inoperable. The

inspectors observed troubleshooting activities through: 1) attendance at various

planning meeting; 2) interviews with engineers and maintenance technicians; 3)

walkdowns of the EDG system; and 4) observations of several EDG maintenance runs.

The overall evaluation of the event was completed by a special inspection team and

documented in NRC Inspection Report 50-443/02-010.

b. Findings

No findings of significance were identified.

4OA5 Other Activities

.1 License Transfer

On October 25, 2002, the NRC approved the transfer of the operating licensee for

Seabrook Station from North Atlantic Energy Service Corporation to FPL Energy

Seabrook, LLC. On November 1, the transfer was completed. Although this inspection

was performed while North Atlantic Energy Service Corporation was the license holder,

this report was issued and addressed to the new licensee holder, FPL Energy Seabrook,

LLC.

4OA6 Meetings, including Exit

.1 Exit Meeting Summary

The inspectors presented the inspection results to Mr. J. Vargas on October 7, 2002,

following the conclusion of the period. The licensee acknowledged the findings

presented. The licensee did not indicate that any of the information presented at the

exit meeting was proprietary.

.2 Site Management Visit

On September 26 and 27, Mr. Hubert Miller, Regional Administrator, Region I and

Mr. R. Crlenjak, Deputy Division Director, Division of Reactor Safety, toured the site and

met with Mr. Ted Feigenbaum and other members of Seabrooks management.

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Mr. Brian McDermott, Branch Chief, Division of Reactor Projects, Branch 6 visited the

site September 24 to 27 and accompanied Mr. Miller and Mr. Crlenjak.

On July 22 to 24, Mr. Douglas Starkey, Project Manager, Nuclear Reactor Regulation

toured the site and met with members of the Seabrooks staff.

4OA7 Licensee Identified Violations

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements which meets the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as NCV.

with Commission regulations and the licensees security plan. Section 10.1 of the

Seabrook Physical Security Plan, Revision 29, dated December 18, 2001, states that

armed responders will be immediately available for response. On June 14, 2002, an

armed responder was inattentive to duty, as described in the licensees corrective

action program Condition Report 02-10104. Though this matter involved a

vulnerability of Safeguards Systems or Plans, in this case no actual intrusion

occurred, and there have not been greater than two similar findings in the last four

quarters. Accordingly, this matter is being treated as a non-cited violation.

ATTACHMENT 1

SUPPLEMENTAL INFORMATION

a. Key Points of Contact

Licensee:

B. Plummer, Operations Manager

T. Nichols, Technical Support Manager

D. Sherwin, Maintenance Manager

J. Pandolfo, Security Manager

R. Hickok, NRC Coordinator

M. OKeefe, Regulatory Compliance Supervisor

C. Berry, Corrective Action/Human Performance Program Manager

M. Bianco, Radwaste Supervisor

W. Cash, Health Physics Department Manager

F. Hannify, Radwaste Technical Supervisor

W. Leland, Chemistry/Health Physics Group Manager

E. Metcalf, Plant Engineering Assistant Manager

J. More, Nuclear Systems Operator

R. Thurlow, Health Physics Technical Supervisor

D. Robinson, Chemistry Supervisor

T. Smith, Rad Technical Specialist (Training)

A. Stall, President Nuclear Production, Florida Power and Light

G. St. Pierre, Station Director

E. Moore, Security Supervisor

J. Peschel, Manager, Regulatory Programs

J. Sobotka, Manager, Oversight

P. Ryan, Supervisor, Security Operations

b. Items Opened, Closed, and Discussed

Opened and Closed:

50-443/02-05-01 NCV Inadequate corrective actions and extent of condition

reviews for two hot connections found in the EDG control

panel (Section 1R22).

50-443/02-05-02 NCV Failure to maintain safeguards in accordance with 10 CFR

73.55(b.1.i) and the licensees security plan (Section

3PP3).

Closed:

50-443/01-08-03 URI Emergency Preparedness Performance Indication -

Evaluating Exceeding the 15 Minutes for Classifications

(Section 4OA1.1)

Attachment 1 (Cont.)

c. List of Acronyms

ADAMS Agencywide Documents Access and Management System

CR Condition Report

DCN Design Change Notice

DCR Design Change Request

DG Diesel Generator

EDG Emergency Diesel Generator

EPS Emergency Power Sequencer

FAQ Frequently Asked Question

MR Maintenance Rule

NEI Nuclear Energy Institute

OD Operability Determination

PARS Publicly Available Records

PCP Process Control Plan

PI Performance Indicator

PMT Post-maintenance Testing

RHR Residual Heat Removal

SDP Significance Determination Process

SSC Structure, System, and Component

SW Service Water

TS Technical Specifications

UFSAR Updated Final Safety Analysis Report

d. Partial List of Documents Reviewed

PROCEDURES:

ES0825.01, Rev. 0 Abandoned and Infrequently Used Equipment

RP 13.1, Rev. 18 Radiological Controls for Material

WN0598.072, Rev. 3 Shipment of Radioactive Material

HD0958.32, Rev. 14 Release of Material From Radiological Controls

HD0963.41, Rev. 8 Calibration of Nuclear Enterprises SAM-9

CP 5.1, Rev. 15 Isotopic Characterization of Radwaste

CS0918.02, Rev. 5 Radwaste Analysis Methods

WD0598.069, Rev. 0 Storage of Radioactive Material/Waste Controlled by the Waste

Services Department

HD0958.38, Rev. 23 Evaluation of Isotopic Mix

SELF-ASSESSMENTS:

SA 01-0045 Processing of Green-Is-Clean Trash

SA 02-0074 HP/Radwaste Biannual Condition Report Trend Analysis

QUALITY ASSURANCE SURVEILLANCE REPORTS/AUDITS:

QASR 01-0171 Assessment of Mixed Waste

QASR 02-0019 Assessment of Radiological Waste Services move of a High

Integrity Container to a Transfer Cask

QASR 02-0095 Health Physics Activities during OR08

Audit No. 00-A07-01 Radwaste/Process Control Program

Audit No. 98-A07-01 Radwaste/Process Control Program

Attachment 1 (Cont.)

CONDITION REPORTS:

02-11981, 02-11875, 02-11874, 02-11873, 02-11797, 02-11796, 02-11627, 02-11616,

02-09445, 02-08226, 02-06973, 02-05600, 02-02716, 02-01917, 01-12722, 02-01135,

01-12423, 01-11716, 01-01973, 01-01588,

02-05891, April 30, 2002, NRC perceived inattentive to duty

02-10104, June 14, 2002, Security Officer inattentive to duty

02-10541, June 25, 2002, Explore negative trend in Security Officers being inattentive to

duty

02-11729, July 25, 2002, Security Officer inattentive to duty

SHIPPING MANIFESTS:

Ship No.01-006, Dewatered Filter Cartridges, 98 Ci, LSA II, Class C

Ship No.01-009, Dewatered Resin, 41 Ci, LSA II, Class B

Ship No.02-003, Dewatered Resin, 35 Ci, LSA II, Class B

Ship No.02-010, Dewatered Resin, 36 Ci, LSA II, Class B

Ship No.02-036, Dewatered Filter Cartridges, 39 Ci, LSA II, Class C

HEALTH PHYSICS STUDY/TECHNICAL INFORMATION DOCUMENT:

HPSTID 93-008 Radiological and Safety Evaluation for Storage of Spent Resin in

Water in the Waste Processing Building

HPSTID 91-003 Use of the Nuclear Enterprise Small Article Monitor for

Determining Compliance with Seabrook Station Contamination

Release Limits

HPSTID 90-005 NEA Small Article Monitor Evaluation and Set-Up

OTHER:

Change Management Plan - Waste Liquid Processing Vendor System Replacement

Engineering Evaluation EE-02-001, Rev. 0 - Comparison of the Duratek and Nukem

Liquid Processing Systems

Process Control Plan, Rev. 31

Radwaste Training Qualification Matrix

Seabrook Station Physical Security Plan, Rev. 29, December 18, 2001

Seabrook Station Contingency Plan, Revision 13, January 11, 2002

SECURITY DOCUMENTS:

Safeguards Event Reports for the last three quarters of 2002

Seabrook Station Contingency Plan

Seabrook Station Physical Security Plan

Drill and Exercise documentation for first three quarters of 2002