ML020780234

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IR 05000456/2002-003 & 05000457/2002-003 (Drp), Braidwood Station Units 1 & 2, Inspection on 02/04/2002 - 02/22/2002 Related to Identification & Resolution of Problems. One Noncited Violation Noted
ML020780234
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 03/18/2002
From: Ann Marie Stone
Division Reactor Projects III
To: Skolds J
Exelon Generation Co, Exelon Nuclear
References
FOIA/PA-2006-0115 IR-02-003
Download: ML020780234 (45)


See also: IR 05000456/2002003

Text

March 18, 2002

Mr. John L. Skolds, President

Exelon Nuclear

Exelon Generation Company, LLC

4300 Winfield Road

Warrenville, IL 60555

SUBJECT:

BRAIDWOOD STATION, UNITS 1 AND 2

NRC INSPECTION REPORT 50-456/02-03(DRP); 50-457/02-03(DRP)

Dear Mr. Skolds:

On February 22, 2002, the NRC completed an inspection at your Braidwood Station Units 1

and 2. The enclosed report documents the inspection findings which were discussed on

February 22, 2002, with Mr. J. von Suskil and other members of your staff.

The inspection examined activities conducted under your license as they relate to identification

and resolution of problems, and compliance with the Commissions rules and regulations and

with the conditions of your license. Within these areas, the inspection involved selected

examination of procedures and representative records, observations of activities, and interviews

with personnel.

On the basis of the sample selected for review, the inspectors concluded that your corrective

action program adequately identified, evaluated, and resolved conditions adverse to quality.

One finding of very low safety significance (Green) was identified (self-revealed). This finding

was associated with the failure to follow procedure which caused the Unit 1 Train B of the

containment spray system to be inoperable. The finding was determined to involve a violation

of NRC requirements. However, because of its very low safety significance and because the

finding was entered into your corrective action program, the NRC is treating the issue as Non-

Cited Violations, consistent with Section VI.A.1, of the NRCs Enforcement Policy. If you deny

this Non-Cited Violation, you should provide a response with the basis for your denial, within

30 days of the date of this inspection report, to the Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region III; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Resident Inspectors at the Braidwood

Station.

In addition, the inspectors identified an apparent violation of 10 CFR 50, Appendix B,

Criterion XVI, "Corrective Action," for the failure to identify the cause and take action to prevent

recurrence for recurring failures of the check valves between the instrument air system and the

accumulators for the Unit 1 pressurizer power operated relief valves. However, the staffs

significance determination of this issue was not complete at the time this report was issued;

therefore, this issue is considered an unresolved item.

J. Skolds

-2-

During this inspection, several examples of poor quality apparent cause evaluations were

identified. A variety of deficiencies were noted; however, the most significant involved

evaluations where potential common mode failure mechanisms were mentioned but not

addressed in the documented corrective actions. In some cases, it was unclear whether the

common mode failure aspect was evaluated as evident in the apparent violation described

above. In addition, these deficiencies were not identified by your staff in the review and

approval process.

In accordance with 10 CFR 2.790 of the NRCs Rules of Practice, a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRCs document

system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/NRC/ADAMS/index.html (the Public Electronic Reading Room).

Sincerely,

/RA/Ann Marie Stone

Ann Marie Stone, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-456; 50-457

License Nos. NPF-72; NPF-77

Enclosure:

Inspection Report 50-456/02-03(DRP);

50-457/02-03(DRP)

See Attached Distribution

DOCUMENT NAME: G:\\BRAI\\bra 2002-03.wpd

To receive a copy of this document, indicate in the box:"C" = Copy without enclosure "E"= Copy with enclosure"N"= No copy

OFFICE

RIII

NAME

AMStone:dtp

DATE

03/18/02

OFFICIAL RECORD COPY

J. Skolds

-3-

cc w/encl:

Site Vice President - Braidwood

Braidwood Station Plant Manager

Regulatory Assurance Manager - Braidwood

Chief Operating Officer

Senior Vice President - Nuclear Services

Senior Vice President - Mid-West Regional

Operating Group

Vice President - Mid-West Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing - Mid-West Regional

Operating Group

Manager Licensing - Braidwood and Byron

Senior Counsel, Nuclear, Mid-West Regional

Operating Group

Document Control Desk - Licensing

M. Aguilar, Assistant Attorney General

Illinois Department of Nuclear Safety

State Liaison Officer

Chairman, Illinois Commerce Commission

J. Skolds

-3-

cc w/encl:

Site Vice President - Braidwood

Braidwood Station Plant Manager

Regulatory Assurance Manager - Braidwood

Chief Operating Officer

Senior Vice President - Nuclear Services

Senior Vice President - Mid-West Regional

Operating Group

Vice President - Mid-West Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing - Mid-West Regional

Operating Group

Manager Licensing - Braidwood and Byron

Senior Counsel, Nuclear, Mid-West Regional

Operating Group

Document Control Desk - Licensing

M. Aguilar, Assistant Attorney General

Illinois Department of Nuclear Safety

State Liaison Officer

Chairman, Illinois Commerce Commission

ADAMS Distribution:

AJM

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MLC

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HBC

CJP3

C. Ariano (hard copy)

DRPIII

DRSIII

PLB1

JRK1

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-456; 50-457

License Nos:

NPF-72; NPF-77

Report Nos:

50-456/02-03(DRP); 50-457/02-03(DRP)

Licensee:

Exelon Generation Company, LLC

Facility:

Braidwood Station, Units 1 and 2

Location:

35100 S. Route 53

Suite 84

Braceville, IL 60407-9617

Dates:

February 4 through February 22, 2002

Inspectors:

R. Skokowski, Senior Resident Inspector, Team Leader

D. Schrum, Reactor Engineer

N. Shah, Resident Inspector

Observer:

N. Valos, Reactor Inspector (Trainee)

Approved by:

Ann Marie Stone, Chief

Branch 3

Division of Reactor Projects

2

SUMMARY OF FINDINGS

IR 05000456-02-03(DRP), 05000457-02-03(DRP); on 02/04-02/22/2002, Exelon Generation

Company, LLC; Braidwood Station; Units 1 & 2. Identification and Resolution of Problems.

The inspection was conducted by one senior resident inspector, one region-based reactor

engineer and one resident inspector. This inspection identified one Green finding which

involved Non-Cited Violations. In addition, the inspectors identified an apparent violation of

NRC requirements. The staffs significance determination of this issue was not complete at the

time this report was issued; therefore, this issue was considered an unresolved item. The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using NRC

Inspection Manual Chapter 0609 Significance Determination Process (SDP). The NRCs

program for overseeing the safe operation of commercial nuclear power reactors is described at

its Reactor Oversight Process website at http://www.nrc.gov/NRR/OVERSIGHT/index.html.

Findings for which the SDP does not apply are indicated by No Color or by the severity level of

the applicable violation.

Identification and Resolution of Problems

The inspectors concluded that the licensee adequately identified, evaluated, and resolved

problems within the requirements of the corrective action program (CAP). In general, the

significance threshold for entering issues into the corrective action program appeared

appropriate. However, the inspectors noted several examples where apparent cause

evaluations (ACEs) were of poor quality. These deficiencies were not identified by line

management during the licensee's review and approval process. The types of deficiencies

varied but included the following:

New information that could impact the original operability and reportability evaluations

was not re-evaluated by shift management.

Other apparent problems were mentioned but were not fully addressed in the evaluation.

For example, potential common cause failure mechanisms were included as possible

apparent causes; however, the impact on like-equipment was not resolved or evaluated.

The extent of the evaluations and corrective actions were not always well documented.

In addition, the inspectors noted that equipment problems identified during outages were not

always evaluated for operability or reportability. In addition, causes for significant equipment

problems were not always addressed prior to plant startup.

The licensee was effective in correcting broke/fix type issues such as equipment problems,

procedure deficiencies, and calculational errors. However, the licensee was less effective in

correcting recurring human performance problems. This was evidenced by recurring problems

associated with configuration control, contractor control, foreign material exclusion control, fire

protection control, and rework issues.

Through interviews and observations, the inspectors concluded that Braidwood established a

safety-conscious work environment where people were not reluctant to raise issues. However,

the inspectors noted that recent changes to the CAP made it somewhat burdensome to enter

3

items into the corrective action program computerized process. Additionally, the inspectors

ascertained that the recent changes to the CAP also made the trending condition report-related

data burdensome by making the manipulation of the data difficult.

A.

Inspector Identified Findings

Cornerstone: Mitigating Systems

(TBD). The inspectors identified an apparent violation of 10 CFR 50, Appendix B,

Criterion XVI, "Corrective Action," for the licensees failure to identify the cause and take

action to prevent recurrence for failures of the check valves between the instrument air

system and the accumulators for the Unit 1 pressurizer power operated relief valves

(PORVs). Specifically, following the October 1998 failures of all the Unit 1 pressurizer

PORV accumulator check valves, a significant condition adverse to quality, the licensee

did not determine the cause of the back leakage and take actions to preclude repetition

as evidenced by the similar failures of the same valves in September 2001.

The staffs significance determination of this finding was not complete at the time of

issuance of this report; therefore, this issue is considered an unresolved item. The safety

significance of this issue has been characterized as "To Be Determined (TBD)" pending

the completion of additional risk analysis. (Section 4OA2 a).

Cornerstone: Barrier Integrity

Green. Following a trip of the circuit breaker during surveillance testing, the licensee

determined that 14 months earlier, technicians failed to reset the instantaneous

overcurrent trip setpoint for the 1CS009B circuit break as prescribed in the station

procedure resulting in the instantaneous overcurrent being left at a nonconservatively

low value. This event was considered self-revealing.

The inspectors determined that this issue had a credible impact on safety because

under certain voltage conditions the 1B train of the containment spray would not have

been capable of fulfilling the design safety function. The inspectors concluded that this

issue could have affected the capability of controlling containment pressure; however,

because no actual reduction of the containment pressure control function occurred, this

issue was of very low safety significance. The failure to follow the maintenance

procedure for the inspection and testing of the 1B containment spray suction valve from

the containment sump circuit breaker was a violation of Technical Specification 5.4.1 a.

However, since this finding is of very low safety significance and it was captured in the

licensees corrective action program, this finding is being treated as a Non-Cited

Violation consistent with Section V1.A.1 of the NRC Enforcement Policy

(Section 40A2 b).

4

Report Details

4.

OTHER ACTIVITIES (OA)

40A2

Identification and Resolution of Problems (71152)

a.

Effectiveness of Problem Identification

(1)

Inspection Scope

The inspectors conducted a review of the Braidwood process for identifying and

correcting problems in the plant. The inspectors reviewed previous licensee and

inspector-identified issues related to the seven safety cornerstones in the Reactor

Safety, Radiation Safety, and Safeguards strategic performance areas to determine if

problems were appropriately identified, characterized, and entered into the corrective

action program. Specifically, the inspectors reviewed selected plant procedures and

program description handbooks, interviewed selected plant personnel, and attended

various station meetings to understand the stations process for implementing the

corrective action program (CAP) and related activities.

The inspectors selected several condition reports generated since the last Problem

Identification and Resolution (PI&R) inspection. Also, the inspectors selected areas that

looked like potential trends and assessed whether the licensees had appropriately

identified and captured these trends within the corrective action program. In addition,

from a list of work request generated since the last PI&R inspection, the inspectors

selected 25 work requests to verify that CRs were generated when appropriate in

accordance with the thresholds established by the CAP.

To assess trending, maintenance rule implementation and to identify items that were

missed by the licensee, the inspectors reviewed the past performance of three systems.

The systems selected were the centrifugal charge system (CV), essential service water

system (SX) and instrument air system. These systems were selected because they

appeared together in several accident scenarios in the Significance Determination

Process (SDP). In addition, the inspectors selected the 4160/480 volt circuit breakers

for a similar review to assess how the licensee evaluated component issues related to

several systems. As part of this assessment, the inspectors interviewed the respective

system engineers, and reviewed system health reports, and system monitoring

programs and completed partial system walkdowns.

From a list of station and departmental self-assessments and audits, the inspectors

conducted a review to determine whether the audit and self-assessment programs were

effectively managed, and adequately covered the subject areas. In addition, the

inspectors interviewed licensee staff regarding the audit and self-assessment programs.

The inspectors also evaluated the licensees operator work around (OWA) process. The

evaluation included a review of the governing procedure and the licensees list of

identified OWAs. In order to assess the licensees performance with respect to

identifying OWAs, the inspectors evaluated issues described in various licensee CAP

5

documents to determine whether issues that met the threshold to be considered an

OWA were appropriately dispositioned. In addition, the inspectors compared a list of

OWAs from another station to assess whether similar OWA existed at Braidwood.

The specific documents reviewed are listed in Attachment 1 of this report.

(2)

Issues

The inspectors identified an apparent violation of 10 CFR 50, Appendix B, Criterion XVI,

"Corrective Action," for the licensees failure to identify the cause and take action to

prevent recurrence for failures of the check valves between the instrument air system

and the accumulators for the Unit 1 pressurizer power operated relief valves (PORVs).

The safety significance of this issue has been characterized as "To Be Determined

(TBD)" pending the completion of additional risk analysis.

In general, station personnel effectively identified at a low threshold and entered

problems as CRs into the corrective action program. Although thousands of CRs were

initiated this past year, the inspectors identified two examples where the licensee failed

to recognize and address issues at the identification phase of the corrective actions

process. The first example was the apparent violation described above, and the second

example dealt with the failure to provide operators additional guidance regarding

alternative means of determining valve position after the normal local position indicator

for an SX valve was found degraded.

In addition, based on interviews with plant personnel, the inspectors ascertained that

some employees found the CAP computer program complex and difficult to navigate and

some individuals routinely relied on their supervisors for entering items into the CAP.

Additionally, the inspectors identified that a new assigned chemistry supervisor was not

provided the management training on the CAP process. The inspectors concluded that

no significant issues were missed based on the lack of training. The corrective action

program coordinator stated that the other supervisors received the applicable CAP

training and that the chemistry supervisor would be trained in the very near future.

Pressurizer PORV Accumulator Check Valve Failures

During the Fall 2001 Unit 1 refueling outage, all four check valves that separate the non

safety-related instrument air system from the safety-related pressurizer PORV control air

accumulators were found to have excessive back leakage. In the event of a loss of

instrument air pressure, these check valves ensure sufficient air pressure is available to

operate the PORVs, and therefore, allowing a means to depressurize the reactor coolant

system in response to certain transients.

On September 29, 2001, the licensee initiated CR 00076349, During Performance of

1BwOSR 3.4.11.3.3 Check Valves Failed, to document this issue. The licensee

generated work orders to repair and retest the valves. On October 15, 2001, the

licensee generated CR 00078892, Maintenance Rule Criteria RY2 Exceeds Reliability

Criteria, and an apparent cause evaluation (ACE) was written to determine the cause of

the failures. Within this ACE, the licensee stated that all four valves failed due to a

dislodged O-ring on the valve disc, which prevented the disc from fully engaging with the

6

seat. The licensee also stated in the ACE that all four of these valves failed for the same

reason back in 1998, and, at that time, the valves were rebuilt and successfully tested;

however no CR was generated to evaluate the cause. After additional review and

discussions with system engineering staff, the inspectors ascertained that in 1998, these

valves had passed their as-found surveillance test; however, during the scheduled

rebuild of the valves, the O-rings were found dislodged. Furthermore, the inspectors

determined that since 1991, these valves on Unit 1 have had similar failures.

The inspectors concluded that the licensee did not identify and correct the cause

for Unit 1 pressurizer PORV accumulator check valve failures following the

October 1998, and September 2001 failures. This was based on ineffectiveness of

the 1998 corrective actions to address the O-rings becoming dislodged as evidenced

by the similar failure in September 2001. Furthermore, the corrective actions taken to

address the September 2001 failures were the same as the ineffective actions taken in

October 1998, specifically rebuilding the valves. Based on the apparent common mode

failure mechanism that could impact both pressurizer PORVs on both units, the

inspectors considered this to be a significant condition adverse to quality.

The inspectors discussed with the Braidwood Station Management, the impact of the

issue with respect to the current operability of the pressurizer PORVs for both units and

with respect to the past operability of the pressurizer PORVs in Unit 1. The licensee

stated historical data showed that the valves operated satisfactorily for greater than one

operating cycle after rebuild, and since the valves were just rebuilt in September 2001,

the licensee concluded the Unit 1 valves were currently operable. In addition, the

licensees review of the Unit 2 operating history of the same valves revealed very few

failures; therefore, the licensee concluded that the Unit 2 valves were also operable.

The inspectors could not dispute the licensees conclusion regarding current operability.

With respect to past operability, the inspectors concluded that both Unit 1 pressurizer

PORVs were inoperable for some period prior to the as-found test failure. This

conclusion was reached because the cause of the failures was unknown and the

accumulator check valves failed the as-found surveillance test.

10 CFR Part 50, Appendix B, Criteria XVI, Corrective Action, requires, in part,

that measures shall be established to assure that conditions adverse to quality,

such as failures, are promptly identified and corrected. In the case of significant

conditions adverse to quality, the measure shall assure that the cause of the

condition is determined and corrective actions taken to preclude repetition. Following

the October 1998 failures of all the Unit 1 pressurizer PORV accumulator check valves

to maintain pressure, a significant condition adverse to quality, the licensee failed to

determine the cause of the condition and take actions to preclude repetition as

evidenced by the similar failures of the same valves in September 2001. This issue is

considered an apparent violation of 10 CFR 50 Appendix B, Criterion XVI. This issue

was entered into the licensees corrective action program as Condition

Report 00095245.

The inspectors determined that this issue had a credible impact on safety because the

Unit 1 pressurizer PORVs could not be relied upon to mitigate a steam generator tube

rupture event. The staffs significance determination of this finding was not complete at

the time of issuance of this report; therefore, this issue is considered an Unresolved Item

7

(50-456/02-03-01(DRP)). The safety significance has been characterized as TBD

pending the completion of additional risk analysis.

Alternate valve position indication

The inspectors the reviewed CR A2000-03490, Failed Surveillance -

0BwOSR 3.7.8.3-1 for 0SX147, which was written after an operator was unable

to determine the position of the Unit 0 component cooling water heat exchanger outlet

valve (0SX147) during a surveillance test. The inspectors noted that since 1997, there

has been an open work order to repair the 0SX147 local valve position indication.

When the work order was initiated, the licensee did not provide formal guidance to the

operators regarding how to alternatively determine the valve position. Subsequently,

operators continued to complete this surveillance on a quarterly basis using alternative

methods, based on institutional knowledge, to determine the valve position. After

discussions with members of the Braidwood operations and engineering departments,

the inspectors concluded that the operators were adequately determining the valve

position. However, the licensees informal approach that relied on institutional

knowledge was less than effective as evident by the operator's need to generate

CR A2000-03490. Additionally, the licensee closed this CR without taking action to

repair the valve or to sanction the other methods being used by the operators. The

licensee acknowledged these shortcomings and issued CR 00094403 to address the

concerns.

Trending of Issues

The inspectors determined that the licensees trending of issues was adequate. Station

personnel identified individual specific deficiencies and entered those deficiencies into

the CAP database. Although the Station's Coding and Trending Manual provided

detailed guidance on trending CR-related information, the inspectors found that the

trending of CR-related data was inconsistent with some departments informally trending

CR-related information. Additionally, the inspectors ascertained that trending CR-related

data became burdensome due to recent changes to the Exelon-wide CAP database that

made manipulating the data difficult. The inspectors noted that the licensee was aware

of this issue as evidenced by CR 00093520. However, the inspectors also noted that

the quality of CR-related trending had been on ongoing issue at Braidwood even before

the change to the CAP-database.

b.

Prioritization and Evaluation of Issues

(1)

Inspection Scope

The inspectors reviewed previous inspection reports and corrective action documents

generated since September 2000. In particular the inspectors reviewed selected ACEs,

root cause reviews, prompt investigations, operability determinations and common

cause analysis to verify that identified issues were appropriately prioritized and

evaluated when entered into the licensees corrective action program. During this

review, the inspectors focused on the technical adequacy of the cause determinations,

extent of condition reviews including evaluations of potential common cause or generic

8

concerns, and the appropriateness of the corrective actions. In addition, the inspectors

also focused on the operability and reportability determinations.

The inspectors selected several items to ensure proper implementation of the

Maintenance Rule. This included verifying that the functional failures and unavailability

time were properly counted and tracked.

The inspectors attended management meetings to observe the assignment of

CR categories for current issues including the initial operability and reportability

evaluations. In addition, during some of these meetings, the inspectors observed station

managements review of root cause analyses and corrective actions for existing CRs.

The inspectors also evaluated the licensees process for reviewing industry operating

experience (OPEX). Documents reviewed included the licensees procedure, and their

assessment of selected industry operating event reports, NRC, and vendor generic

notices recorded since September 2000. Additionally, the inspectors discussed the

process with the Braidwood OPEX coordinator.

A listing of the specific documents reviewed is attached to the report.

(2)

Issues

The inspectors identified one finding of very low safety significance that was determined

to be a Non-Cited Violation (NCV). This finding involved the failure to follow procedure

resulting in the inoperability of one division of the Unit 1 the containment spray system.

Specifically, during a maintenance activity on the circuit breaker for the suction valve

from the containment sump (1CS009B) to the 1B containment spray pump, a technician

left the instantaneous overcurrent setting nonconservatively low.

Furthermore, during the review, the inspectors noted several examples where ACEs

were of poor quality. The inspectors noted that these poor quality ACEs were reviewed

and approved by a first line manager or above. The types of deficiencies varied but

included the following:

New information that could impact the original operability and reportability

evaluations was not re-evaluated by shift management.

Other apparent problems were mentioned but were not fully addressed in the

evaluation. For example, potential common cause failure mechanisms were

included as possible apparent causes; however, the impact on like-equipment

was not resolved or evaluated.

Examples where the apparent cause, extent of the evaluations and corrective

actions were not well documented.

These problems were more apparent for ACEs generated early in the assessment

period, but a few examples of similar problems were noted with more recent ACEs. In

most cases, after discussions with the responsible individuals, the inspectors concluded

9

that the causes were truly determined, that the corrective actions were appropriate, and

other issues, including operability and potential common cause issues were addressed.

In addition, the inspectors noted that equipment problems identified during outages were

not always evaluated for operability or reportability. In addition, causes for significant

equipment problems were not always addressed prior to plant startup.

Specific examples include:

CR A2001-01170 Potential Rework - 1CS009B trips breaker during votes

testing after maintenance. This CR described a condition where the

containment spray recirculation suction valved tripped on instantaneous over

current during motor-operated valve testing. During the ACE for this CR, the

licensee discovered that 14 months earlier, a technician dialed down the

instantaneous over current setting to the minimum value during circuit breaker

testing and did not return the setting to the normal value as required by

Procedure MA-BR-EM-1-3.8.a.3-1, Surveillance for Inspection and Testing of

480 Volt Motor Control Center (MCC) Draw-Out Units. Furthermore, in the ACE,

the licensee documented that if the valve was called upon to operate during the

14 months while the instantaneous overcurrent trip setpoint was set

nonconservatively low, the breaker would have probably tripped and the valve

would not have opened and could have possibly resulted in eventual pump

damage. The inspectors determined that this information was not provided back

to the shift manager for operability and reportability reviews. When the

inspectors questioned the operability of the valve, the licensee re-evaluated the

operability of the breaker and determined that under the normal voltage

conditions experienced during the 14 months in question, the breaker would not

have tripped prematurely. However, under worst case design conditions, the

breaker would have tripped prematurely if it had been called upon to operate.

The inspectors determined that the failure to reset the instantaneous overcurrent

trip setpoint for the 1CS009B circuit break as prescribed in the station procedure

had a credible impact on safety because under certain voltage conditions the

1B train of containment spray would not have been capable of fulfilling the design

safety function. The inspectors concluded that this issue could have affected the

capability of controlling containment pressure. The inspectors evaluated this

issue through the SDP and determined that since the other train of containment

spray was not affected, there was no actual reduction of the atmospheric

pressure control function of the reactor containment, and therefore this issue was

of very low safety significance (Green).

Technical Specification 5.4.1, states, in part, that written procedures shall be

established, implemented, and maintained covering the following activities: The

applicable procedures recommended in Regulatory Guide 1.33, Revision 2,

Appendix A, February 1978. Paragraph 9.a. of this Regulatory Guide states, in

part, that procedures for performing maintenance that can affect the performance

of safety-related equipment shall be prepared and activities shall be performed in

accordance with these procedures. The licensee established Procedure MA-BR-

EM-1-3.8.a.3-1, Surveillance for Inspection and Testing of 480 Volt Motor

10

Control Center (MCC) Draw-Out Units, as the implementing procedure for

inspecting and testing 480 Volt circuit breakers. Contrary to the above, on

February 29, 2000, the technicians failed to return the adjustable magnetic

element (instantaneous overcurrent setpoint) to the setting position recorded

earlier in Procedure MA-BR-EM-1-3.8.a.3-1. This is considered a violation of

Technical Specification 5.4.1. However, because this violation was of very low

risk significance, was non-repetitive, and was captured in the licensees

corrective action program (CR 00094420), this violation is being treated as a

Non-Cited Violation in accordance with Section V1.A.1 of the NRC Enforcement

Policy (NCV 50-456-02-03-02 (DRP)).

CR A2000-04475, Unplanned Limiting Condition for Operations entry for

the 2B AF pump during surveillance run. This CR described an instance

when Unit 2 diesel driven auxiliary feedwater (AFW) pump room cooler failed to

automatically start as designed. Specifically, on December 1, 2000, during a test

start of the diesel driven AFW pump, the SX outlet valve for the room cooler

failed to open and resulted in the inoperability of the 2B AFW pump. The room

cooler was designed such that on a AFW pump start the SX inlet valve opens

and upon reaching a full open position, a limit switch on the valve stem makes-up

a permissive contact in the control circuit to allow the room cooler outlet valve to

open.

The ACE associated with this CR described the cause as three physical

deficiencies with the limit switch on the inlet valve. However, no discussion was

provided on how these deficiencies were caused. The corrective actions merely

corrected the deficiencies, not the cause, and provided additional clarification to

a maintenance procedure associated with the inlet valve limit switch. Based on

the review of the ACE, the inspectors were unable to determine the cause of the

event, and therefore, were unable to determine whether or not the corrective

actions were appropriate to prevent recurrence. Furthermore, the inspectors

noted that the licensee reviewer for this ACE did not identify the same problems.

In fact, the completed apparent cause evaluation quality checklist was marked

"yes" for the following questions:

Does the Apparent Cause Section clearly describe why the problem

occurred and is the Apparent Cause(s) clearly stated?

Are the corrective actions linked to the apparent cause(s) stated?

After a discussion with the engineers responsible for reviewing this event, the

inspectors ascertained that the cause of the limit switch deficiencies was a failure

to adequately tighten the limit switch jam nut. Therefore, the inspectors

concluded that the cause was appropriately determined and the corrective

actions were acceptable; however, the documentation of the evaluation was

poor. Furthermore, the inspectors concluded that tightening the jam nut, was a

skill of the craft activity and the failure to adequately tighten the jam nut was not a

violation of NRC requirements. The licensee acknowledged the shortcomings

with the ACE documentation and issued CR 00094186 to address this concern.

11

ACE for A2001-02003, Inadequate ACE performed per CR A2001-01168."

This ACE was written to re-evaluate the cause of the April 20, 2001 1B AFW

pump room cooler outlet valve (1SX178) failure. The original ACE was re-

evaluated because the NRC resident inspectors determined that the cause was

not well supported. (The technical issues related to this event were described in

NRC Inspection Report 50-456-01-07.) In the ACE for CR A2001-02003, the

licensee concluded that dust, oil, and moisture in the air controlling this valve

caused the failure. Although this cause would appear to be a potential common

mode failure mechanism to other components that require instrument air to

operate, no discussion was provided within the ACE indicating that this common

mode failure mechanism was addressed. After discussing this concern with

station engineering personnel, the inspectors ascertained that, based on reviews

of the instrument air quality and other component performance histories, an

actual common mode failure problem with the instrument air system did not exist.

Again, the licensee reviewer of this ACE did not identify the potential common

cause failure mechanism. Additional information regarding this failure is provided

in NRC Inspection Report 50-456-02-04, the supplemental inspection for the

WHITE performance indicator for Unit 1 AFW functional failures.

Evaluating Equipment Problems During Outages. As discussed in

Section 4OA2 a(2), during the Fall 2001 Unit 1 refueling outage, all four check

valves that separate the non safety-related instrument air system from the safety-

related pressurizer PORV control air accumulators were found to have excessive

back leakage. On September 29, 2001, the licensee initiated CR 00076349 to

document this issue and generated work orders to repair and retest the valves.

The inspectors noted that shift management did not review the initial failure of

these valves for potential operability or reportability issues. Likewise, shift

management did not review CR 00078892 and associated ACE which described

a potential common mode failure mechanism that could have impacted both

units.

Based on discussions with the Shift Operations Supervisor, the inspectors

ascertained that during outages, operability and reportability issues routinely do

not go to the shift management review. This practice was based on the

philosophy that the items are normally not required to be operable during

outages, and that the equipment is repaired and tested prior to be returned to

service. As a result of this practice, it was unclear to the inspectors how

Braidwood ensured that past operability was reviewed and evaluated with

respect the reportability requirements.

The inspectors selected three additional CRs generated during the

September 2001 Unit 1 refueling outage to confirm that the causes of the

equipment problems were appropriately evaluated prior to returning the

equipment to service. The inspectors noted the following comment in

CR 0076146, 1PS9357B Failed Local Leak Rate Test (LLRT) per

1BwOSR 3.6.1.1-8 Section 4, When the valve was made available to work,

there was pressure from Work Control to work the valve and solenoid and not to

return the valve to service to perform troubleshooting. During the ACE

associated with the CR, the licensee identified the potential problem with not

12

troubleshooting similar equipment problems and had established corrective

actions to re-enforce station managements expectations to identify the cause of

equipment failures.

The licensee acknowledged these two shortcomings and issued CR 0009537 to

address the concerns.

c.

Effectiveness of Corrective Action

(1)

Inspection Scope

The inspectors reviewed selected CRs and associated corrective actions to evaluate

the effectiveness of corrective actions. The inspectors reviewed CRs, operability

determinations, ACEs, and root cause reports to verify that corrective actions,

commensurate with the safety significance of the issues, were identified and

implemented in a timely manner, including corrective actions to address common cause

or generic concerns. The inspectors also verified the implementation of a sample of

corrective actions. In addition, the inspectors reviewed a sample of corrective action

effectiveness reviews completed by the licensee. The samples were selected based on

their importance in reducing operational risks and recurring problems. The inspectors

reviewed information recorded since September 2000.

Since the licensees CAP allowed for the closing of corrective action tracking items

once the work control process was initiated, the inspectors reviewed the status of all

work request created as corrective actions for the period October 1, 2000, though

December 31, 2000, to ensure items that these were not subsequently canceled or

excessively postponed.

A listing of the specific documents reviewed is attached to the report.

(2)

Issues

During the review, the inspectors noted that the licensee was effective in correcting

broke/fix type issues such as equipment problems, procedure deficiencies, calculational

errors. However, the licensee was less effective in correcting recurring human

performance problems. This was evidenced by recurring problems associated with

configuration control, contractor control, foreign material exclusion (FME) control, fire

protection control, and rework issues.

Regarding configuration controls, the licensee's July 2001 human performance root

cause review recognized that past corrective actions were less than effective and new

corrective actions were established to address the problem from a different perspective.

In the areas of FME, fire protection, contractor controls and rework issues, the licensee

repeatedly identified trends in these areas; however, the corrective actions have not

effectively reduced the trends. Often the corrective actions had been used repeatedly

even though these actions had not substantially reduced the trends in the past. For

example, departmental meetings to discuss the problems were routinely used as a

corrective action even though it was evident that these meetings were not effective in the

13

past. The licensee was aware that these trends have been continuing and they planned

additional corrective actions to be taken during the next refueling outage. The

inspectors reviewed the proposed actions, but it was too early to assess the

effectiveness of the corrective actions.

During review of the corrective actions associated with the Root Cause Review,

2B residual heat removal (RH) pump Tripped on Phase C Overcurrent (AR 00081944),

the inspectors noted that a procedure change made to address this problem did not

provide clear guidance to the operators. Specifically, in order to address concerns with

potential binding of the RH pump, a change was made to Braidwood Operating

Procedure BwOP RH-06 Placing the RH System in Shutdown Cooling, to monitoring

and limit the heatup rate of the pump prior to placing shutdown cooling in service.

Although the 10 CFR 50.59 safety evaluation for this change adequately supported the

change, it specified that there was only a limited time to establish shutdown cooling due

the available condensate storage volume, and assumed that heatup rate monitoring of

the RH system would not start until 260oF. However, this was not clearly stated in the

procedure and there was the potential that operators could have inappropriately

monitored the heatup rate of the system from ambient temperatures, which could have

delayed placing shutdown cooling in service. Based on discussions with the Operations

Manager, the inspectors ascertained that the operators were trained on the new

procedure and during the training, RH system heatup monitoring was started at the

appropriate temperatures. Furthermore, the inspectors ascertained that the licensee

had not yet had the need to perform this procedure in the plant. However, the Operation

Manager acknowledged that the procedure could be enhanced to provide clearer

direction and CR 00094181 was generated to address the issue.

The inspectors review of licensee event reports identified no significant concerns.

Additionally, the inspectors reviewed corrective actions created to address NCVs and

concluded that the licensees proposed actions were completed in a timely manner and

that the actions appeared appropriate as evidenced by the lack of repeat problems.

d.

Assessment of Safety-Conscious Work Environment

(1)

Inspection Scope

The inspectors interviewed plant staff to assess the establishment of a safety conscious

work environment.

During the conduct of interviews, document reviews and observations of activities, the

inspectors looked for evidence that suggested plant employees may be reluctant to raise

safety concerns. Most of the individuals interviewed were asked questions similar to

those listed in Appendix 1 to NRC Inspection Procedure 71152, Suggested Questions

for Use in Discussions with Licensee Individuals Concerning PI&R Issues. The

inspectors also reviewed the stations procedures related to the Employee Concerns

Program, and discussed the implementation of this program with the stations program

coordinator.

14

(2). Issues

No significant findings were identified. The inspectors noted no indications of

unwillingness to raise safety issues. However, during some of the interviews, the

inspectors were informed that the August 2001 change to the CAP made it somewhat

burdensome to enter items into the corrective action program computerized process.

4OA6 Meetings

Exit Meeting

The inspectors presented the inspection results to Mr. J. von Suskil and other members

of licensee management on February 22, 2002. The licensee acknowledged the

findings presented. The inspectors confirmed with the licensee that proprietary

information was examined during the inspection; however, this was not specifically

discussed in this report.

15

KEY POINTS OF CONTACT

Licensee

J. von Suskil, Site Vice President

K. Schwartz, Plant Manager

J. Bailey, Regulatory Assurance - NRC Coordinator

G. Baker, Security Manager

G. Dudek, Operations Manager

C. Dunn, Engineering Director

A. Ferko, Regulatory Assurance Manager

R. Graham, Work Management Director

L. Guthrie, Maintenance Director

F. Lentine, Design Engineering Manager

K. Schwartz, Plant Manager

Nuclear Regulatory Commission

G. Grant, Director, Division of Reactor Projects

A. Stone, Chief, Reactor Projects Branch 3

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-456/02-03-01

URI

Apparent violation of 10 CFR Appendix B, Criterion XVI, for

the licensees failure to identify the cause and take action to

prevent recurrence for failures Unit 1 pressurizer PORV

accumulator check valves

50-456/02-03-02

NCV

Failure to follow procedure resulted in the inoperability of the

1B containment spray suction valve from the containment

sump

Closed

50-456/02-03-02

NCV

Failure to follow procedure resulted in the inoperability of the

1B containment spray suction valve from the containment

sump

16

LIST OF ACRONYMS AND INITIALISMS USED

ACE

Apparent Cause Evaluation

AFW

Auxiliary Feedwater System

AR

Action Request

CAP

Corrective Action Program

CCA

Common Cause Analysis

CFR

Code of Federal Regulations

CR

Condition Report

CV

Centrifugal Charge System

DRP

Division of Reactor Projects

ESF

Engineered Safety Feature

FME

Foreign Material Exclusion

IA

Instrument Air System

LCO

Limiting Condition for Operations

LCOAR

Limiting Condition for Operations Action Requirement

LER

Licensee Event Report

LLRT

Local Leak Rate Test

MCC

Motor Control Center

NCV

Non-Cited Violation

NO

Nuclear Oversight

NRC

Nuclear Regulatory Commission

OOS

Out-Of-Service

OPEX

Operating Experience

OWA

Operator Work Around

PI&R

Problem Identification and Resolution

PORV

Power Operated Relief Valve

RCR

Root Cause Report

RH

Residual Heat Removal

SDP

Significance Determination Process

SSPS

Solid State Protection System

SX

Essential Service Water System

TBD

To Be Determined

TRM

Technical Requirements Manual

TS

Technical Specification

U1

Unit 1

U2

Unit 2

UFSAR

Updated Final Safety Analysis Report

WR

Work Request 17

LIST OF INFORMATION REQUESTED

1.

Copy of the Administrative procedure(s) governing the identification and resolution of

problems.

2.

Copies of any Quality Assurance audit (self-assessment) of the corrective action

program completed since September 1, 2000.

3.

List of Maintenance Rule (a)(1) systems and components, and the associated system

health reports since September 1, 2000.

4.

List of all significant conditions adverse to quality Condition Reports since September 1,

2000.

5.

List of all Condition Reports involving human performance or corrective action problems

since September 1, 2000.

6.

List of Operator Work Arounds and Temporary Modifications since September 1, 2000.

7.

Copies of Root Cause evaluations since September 1, 2000.

8.

List of Condition Reports since September 1, 2000.

9.

Copies of Prompt Investigations since September 1, 2000.

10.

List of Work Orders and Action Requests since September 1, 2000.

11.

List of Apparent Root Causes completed since September 1, 2000.

12.

Copies of Operability Evaluations performed since September 1, 2000.

13.

List of Quality Assurance audits and self assessments performed since September 1,

2000.

14.

List of top 10 risk significant systems and components.

15.

(NRC identified issues) Copies of NCVs since September 1, 2000, and copies of the

licensees actions for issues related to NCVs by cornerstones.

16.

List of issues identified through employee concerns program.

17.

Copies of latest outage critiques for each unit.

18.

Copies of Common Cause Evaluations completed since September 1, 2000.

19.

Copies of Effectiveness Reviews completed since September 1, 2000.

20.

Copy of administrative procedure for the employee concerns program.

18

21.

Copy of administrative procedure for incorporating industry operating experience

(OPEX).

22.

Copies of trend analysis reports for condition reports (Station and Department level).

23.

List of the corrective action backlog; work order backlog risk significance assessment.

24.

Copies of the corrective action system program reports submitted to management since

September 1, 2000.

25.

Copies of procedures governing Operator Work Arounds, Temporary Modifications,

Operability Evaluations, Root Cause Evaluations, and Prompt Investigations.

26.

List of times and locations of site meetings, particularly those associated with the

corrective action process.

27.

Copy of Site Organization Charts.

28.

List or rework items and repeat failures since September 1, 2000.

Documents requested to be available during the inspection:

a.

Updated Final Safety Analysis Report,

b.

Technical Specifications,

c.

Procedures,

d.

Copies of any self-assessments and associated condition reports generated in

preparation for the inspection.

19

LIST OF DOCUMENTS REVIEWED

Action Requests (AR) and Condition Reports (CR)

AR 00034620

A2000-03509: Nuclear Oversight (NO)

Identifies Operator Work Around Program

Deficiencies/Weakness

September 8, 2000

AR 00036951

Assignment Detail for A2000-03928;

Report of the Site Self Assessment

Indicates

January 12, 2001

AR 00038869

AR Assignment/Sub Assignment Summary

Report (CAP010) for A2000-04348;

Potential trend - Foreign Material Exclusion

- FH

November 17, 2000

AR 00073928

Minute Oil Leak and Water Leaks on 1A

and 2A Centrifugal Charge System (CV)

Pumps

AR 00075347

2CV8519 Found Open

September 15, 2001

AR 00076754

Siemens - Westinghouse Individual Was

Injured

September 27, 2001

AR 00077005

No Timer Signal for OB WO Signal During

1BwVSR 3.8.1.11-2

September 29, 2001

AR 00077716

Radiological Series of Events Requires

Common Cause Analysis

January 11, 2002

AR 00078651

Operator Workaround Procedure Has

Confusing Examples

October 11, 2001

AR 00079272

Potential Trend - Increasing Amount of

Foreign Material Exclusion (FME) Issues &

Events

October 17, 2001;

October 19, 2001;

October 24, 2001

AR 00079519

Potential Trend - Contractor Control Issues

in A1R09

October 23, 2001;

October 24, 2001

AR 00079525

NRC Identified Need to Revise Procedure

October 18, 2001

AR 00079728

Potential Trend - Increasing Amount of

Rework Issues

December 14, 2001

AR 00081972

Reactor Coolant System Cooldown

Surveillance Acceptance Criteria Conflict

November 7, 2001

20

AR 00082135

Inappropriate Shutdown Safety

Classification on 2B Residual Heat

Removal (RH) Pump Failure

November 7, 2001

AR 00082711

Disposition of 1B RH Pump Running

Clearances

November 12, 2001

AR 00082907

Ambiguous Terms Used in Procedures

November 8, 2001

AR 00085786

Braidwood SME Review - Non BY-01-097

January 8, 2002

AR 00087834

Recommendation for RH Demonstration

During AR09

November 15, 2001

AR 00091960

Secondary Plant Transient During

Instrument Maintenance Department

Calibration of 2F-CB001

January 23, 2002

AR 00092217

Evaluate Unit 2 (U2) Cond Overflow for

Potential Operator Work Around

January 24, 2002

AR 00093733

Trend - Preventive Maintenance Exceed

Late Date Prior to Deferral Approval

February 4, 2002

AR 00093792

No Service Air or Caustic Isolation on OA

Radwaste Demin Clearance Order

February 4, 2002

CR A2000-00268

Potential Trend - Increased Frequency of

Human Performance Errors in Fuel

Handling

January 18, 2000

CR A2000-00968

2A CV Pump Seal Leakage

March 5, 2000

CR A2000-01988

2CV206 Leakage Has Increased

April 23, 2000

CR A2000-03478

Rework - Air Deflector on Unit 0 Station Air

Compressor Was Not Installed Correctly

September 1, 2000

CR A2000-03484

Potential Functional Failures for

Maintenance Rule Criteria PS3

September 1, 2000

CR A2000-03490

Failed Surveillance -0BwOSR 3.7.8.3-1 for

0SX147

September 3, 2000

CR A2000-03491

Unplanned GW004 Technical

Requirements Manual (TRM) Entry

September 3, 2000

CR A2000-03495

Poor Sequencing of 2B RH Train Work

Due to Procedure Inadequacies

September 5, 2000

CR A2000-03498

NO Identified Action Item Not Created for

Root Cause Corrective Action

September 5, 2000

21

CR A2000-03504

NO Identified: Design Deficiency Rework

Items Not Driven to Closure

September 5, 2000

CR A2000-03505

NO Identified Poor Quality of Apparent

Cause Evaluations (ACEs)

September 5, 2000

CR A2000-03512

NO Identifies Enhancement

Recommendation for System Engineering

September 5, 2000

CR A2000-03539

6.9 KiloVolt Breaker Sent to Wrong

Location

September 6, 2000

CR A2000-03545

Form Looks Like an Approved Procedure

September 5, 2000

CR A2000-03567

Unplanned Entry Into TRM 3.3.1 Due to

1FI-AF014A Main Control Room Flow

Indicator Pegged Low

September 8, 2000

CR A2000-03584

Conflicting Acceptance Criteria in Local

Leak Rate Test Procedures

September 13, 2000

CR A2000-03596

Unplanned Entry Into Fire Protection

GOCAR For Zone 2D-49

September 13, 2000

CR A2000-03606

A2R08 Procedure(s) Identified After Freeze

Date

September 13, 2000

CR A2000-03623

Special Plant Procedure 98-014 is Not

Available in Procedure Files or Entered

Into Controlled Documents

September 14, 2000

CR A2000-03632

2A CV Pump Inboard Leakage

September 18, 2000

CR A2000-03659

1A CV Pump Outboard Seal Leak Has

Increased

September 18, 2000

CR A2000-03668

4KV Breaker Motor Cutout Switch Failed

Surveillance

September 16, 2000

CR A2000-03672

Superceded Procedure Form Found in

D20-1-99-370-003

September 19, 2000

CR A2000-03686

50.59 Missing Tracking No. and Site

Procedure Not Detected for Safety Nuclear

Station Procedure

September 19, 2000

CR A2000-03712

Focus Area Self-Assessment Identified

Mechanical Maintenance Field

Observations Are Not Sufficiently

Objective/Critical

September 26, 2000

CR A2000-03719

2CV206 Leakage Discrepancies

September 25, 2000

22

CR A2000-03746

Adverse Trend Identified: Foreign Material

Exclusion Work Practices in Maintenance

September 27, 2000

CR A2000-03749

Procedure Revisions Needed as a Result

of Diesel Generator Modifications

September 27, 2000

CR A2000-03767

Unnecessary Diesel Unavailability Due to

Fire Protection CO2 Testing

September 28, 2000

CR A2000-03783

Radwaste Rounds Could Not Be

Performed on the Husky

October 1, 2000

CR A2000-03792

1MS018A Trouble Alarm/Unplanned

Limiting Condition for Operation Action

Requirement (LCOAR) Entry

October 3, 2000

CR A2000-03799

Incorrect Application of Procedural

Guidance, RS-AA-122-117

October 3, 2000

CR A2000-03819

Latch Check Switch on 6.9KiloVolt Breaker

Out of Adjustment

September 29, 2000

CR A2000-03825

Review Byron CR (B2000-02760)

Regarding Debris in the Safety Injection

system for Applicability to Braidwood

October 10, 2000

CR A2000-03843

Minimum Wall Thickness on Line

2SXB1AB-3"

October 9, 2000

CR A2000-03845

Maintenance Rule Functional Failure

Monthly Review for July and August 2000

October 9, 2000

CR A2000-03885

Work Performed Without Shift

Authorization

October 12, 2000

CR A2000-03893

2SX046B Was Not Leakage By

October 13, 2000

CR A2000-03909

Contingency Actions for Spent Fuel Pool

Level Loss Not Communicated to All Shift

Personnel

October 16, 2000

CR A2000-03909

Contingency Actions for Spent Fuel Pool

Level Loss Not Communicated to All Shift

Personnel

October 16, 2000

CR A2000-03921

1WX036B Found Open

October 17, 2000

CR A2000-03925

Supply Management Focus Area Self-

Assessment Deficiencies (MS-AA-402

Procedure)

October 18, 2000

23

CR A2000-03926

Report of the site Self Assessment

Indicates an Area for Improvement in

Industrial Safety

October 18, 2000

CR A2000-03927

Report of the Site Self Assessment

Indicates the Area for Improvement MA.2-1

Requires Further Action

October 20, 2000

CR A2000-03928

Report of the site Self Assessment

Indicates Area for Improvement MA.2-2

Requires Further Action

October 18, 2000

CR A2000-03929

Report of the Site Self Assessment

Indicates an Area for Improvement in

Operations

October 18, 2000

CR A2000-03948

Safety System Unavailability & YELLOW

Online Risk Extended by Unscheduled

Activity

October 19, 2000

CR A2000-04397

1B Essential Service Water System (SX)

Strainer Corrosion - NRC Concern

November 17, 2000

CR A2000-04475

Unplanned Limiting Condition for

Operations (LCO) Entry for the 2B Auxiliary

Feedwater System Pump During

Surveillance Run

December 1, 2000

CR A2000-04675

Potential Rework - Damage to Pump

Casing Caused by Incorrect Maintenance

Practices

December 21, 2000

CR A2001-00131

Adverse Trend Identified in Fire Protection

January 16, 2001

CR A2001-00371

Emergency Diesel Fuel Calculation

Discrepancies

February 5, 2001

CR A2001-00495

Instrument Inverter 213 Temperature

Qualification

February 15, 2001

CR A2001-00569

Inadequate Contingency Preparations

When Spent Fuel Pool Cooling Pump Not

Available

February 22, 2001

CR A2001-00795

Supply Management Identified - Ineffective

Corrective Actions

March 16, 2001

CR A2001-00844

1BwGP 100-1 Errors Identified by NRC

March 21, 2001

CR A2001-01192

Ultrasonic Inspection Results on 1B SX

Pump Strainer Drain Line

April 23, 2001

24

CR A2001-01291

Pipe Penetrations Not Protected - Safety

Issue

May 1, 2001

CR A2001-01331

NRC Question Regarding Floor Openings -

Safety Issue

May 4, 2001

CR A2001-01451

Essential Service Water Pump Weight

Increase

May 15, 2001

CR A2001-01802

2A CV Pump Has Excessive Inboard Seal

Leakage

June 17, 2001

CR A2001-02013

Ineffective Corrective Action - Pre-define is

Still Not Properly Scheduled

July 9, 2001

CR A2001-02030

Validation of Trend in Human Performance

Warrants Root Cause Analysis

July 11, 2001

CR A2001-02102

NO Identified Corrective Actions Not

Initiated in Action Tracking per Corrective

Action Program

July 18, 2001

CR A2001-02152

1VA06SB - Isolation Valves

July 20, 2001

CR 00076349

During Performance of 1BwOSR 3.4.11.3.3

Check Valves Failed

September 24, 2001

CR 00077005

No Timer Signal for 0B WO signal during

BwVSR 3.8.1.11-2

September 29, 2001

CR 00078892

Maintenance Rule Criteria RY2 Exceeds

Reliability Criteria

October 15, 2001

CR 00091925

Unit 2 Train of Instrument Air Exceeded

Maintenance Rule Unavailability Goal

CR 00093520

Weaknesses in Trending Noted in CAP

Self-Assessment

February 1, 2002

CR 00094181 1

Potential Misinterpretation in BwOP RH-6

Heatup Limits

February 6, 2002

CR 00094403 1

0SX147 Valve Stroke Issue/Potential

Operator Workaround

February 8, 2002

CR 00094420 1

Operability Concern with Valve 1CS009B

for 14 Month Period

February 8, 2002

CR 00094527 1

New Corrective Action Not Created From

ACE

February 9, 2002

CR 00095373 1

Process Issue with Investigation and

Potential Inoperability

February 14, 2002

25

LS-AA-105-1001

CR 82711 - Supporting Operability

Documentation

July 9, 2001

Effectiveness Reviews

AR 00003185

Effectiveness Review of A1998-02989;

Four 480V Motor Control Center (MCC)

Feed Breakers Would Not Close on

Effectiveness Review

March 12, 2001

AR 00003191

Effectiveness Review of A1998-04252;

Train A Reactor Vessel Level Indication

System Unplanned LCOAR Entry

January 1, 2001

AR 00003625

Effectiveness Review of SOER 91-01,

conduct of Infrequently Tests or Evolutions

September 28, 2001

AR 00003630

Effectiveness Review of SOER 95-01:

Reducing Events

November 15, 2001

AR 00003633

INPO SOER 97-1 - Potential Loss of High

Pressure Injection

December 13, 2000

AR 00003665

Effectiveness Review of A1997-04982;

2SI8851 Relief Valve Lift - Corrective

Actions

March 20, 2001

AR 00007716

Effectiveness Review of A1999-01229

Accident in Containment

March 8, 2001

AR 00011381

Effectiveness Review of A1999-01692;

Unit 2 Reactor Trip on 1R High Flux

December 8, 2000

AR 00016833

Effectiveness Review of A1999-02929;

Solid State Protection System (SSPS)

Slave Relays Response Time Untested

November 17, 2000

AR 00019885

Effectiveness Review of A1999-03710;

Trend Problem Identification Form-Out-of-

Service (OOS) Issue Within Maintenance

June 29, 2001

AR 00023629

A2000-00691: Potential Trend-Wrong

Lubricants Being Used

December 15, 2000

AR 00023792

A2000-00729: Excessive Unit 2 Reactor

Coolant System Leakage

March 27, 2001

AR 00024390

Effectiveness Review of A2000-00883;

Trend-Incorrect/Uncontrolled Procedures

in Radiation Protection

March 30, 2001

26

AR 00024710

A2000-00661: Lack of Rigor in Handling

Increased Radiation Indication on Control

Room Heating, Ventilation and Air

Conditioning System

August 31, 2001

AR 00027323

Effectiveness Review of A2000-01910;

2FW079A/B Graphoil Seal Found

Extruded

November 16, 2001

AR 00024246

Effectiveness Review of A2000-00855;

Potential Trend - Missed Fire Watches

February 28, 2001

AR 00025270

A2000-01121: Loss of Unit 1 (U1) and U2

SG Blowdown

May 4, 2001

AR 00030935

Effectiveness Review of A2000-02626;

Bad Wire Replacement in Security

Multiplexer 2

February 28, 2001

AR 00031642

Effectiveness Review of A2000-03032;

Rework - 1CB01PD Outboard Bearing

Failure Due to Lubrication

June 27, 2002

AR 00033390

Effectiveness Review of A2000-03203;

Adverse Trend-Plant Personnel Dont

Understand

October 18, 2001

AR 00042593

Effectiveness Review of A2001-00131;

Adverse Trend Identified in Fire Protection

February 25, 2002

CR A2001-00582

Corrective Actions for CR A1999-03530,

OOS Error Not Effective

November 15, 1999

CR A2001-00712

Corrective Action to Prevent Recurrence

for Effectiveness Review Determined to Be

Collectively Ineffective

March 7, 2001

Root Cause Reports

AR 00038237

A2000-04281 Failed Circulation Water

Blowdown Vacuum Breaker Flooding

May 30, 2002

AR 00041352

A2000-04707 Number of Out-of-Service

Errors is Increasing

February 1, 2001

AR 00042593

A2001-00131 Adverse Trend Identified in

Fire Protection

February 25, 2002

AR 00042593-02-00

AR Assignment/Sub Assignment Summary

Report (CAP010) -Completed and Open

Actions from A2001-00131

February 6, 2001

27

AR 00056777

A2001-02014 Steam Dump Valves

1MS004 C and G Made Inoperable

June 3, 2002

AR 00075897

Root Cause Analysis for 1MS016B,

1MS017B, and 1MS014D Exceeds 3%

Technical Specification Criteria

November 7, 2001

AR 00076608

Root Cause Analysis for Main Steam Line

Isolation Valves Not Stroke Timed in Mode

3 as Required

November 9, 2001

AR 00081944

Root Cause Analysis for 2B RH Pump

Tripped on Phase C Overcurrent

December 13, 2001

AR 00085836

Adverse Trend Observed During Rework

Common Cause Analysis (CCA) (AR

79728)

February 8, 2002

CR A2000-03746

Adverse Trend of Foreign Material

Exclusion Events and Issues Caused by a

Lack of Procedural Understanding and

Inadequate Training

October 20, 2000

CR A2000-04494

Adverse Trend - Contractors Fail to

Adequately Follow the Hot Work

Procedure (OP-AA-201-004) Due to Lack

of Reinforcement of Procedural

Requirements During Pre-Job Briefings

December 3, 2000

CR A2000-04587

Root Cause Evaluation for Erroneous

Feedwater Temperature Input into the

Calorimetric Program due to a Modification

Installation Error

January 23, 2000

CR A2000-04707

Number of Out-of-Service Errors is

Increasing

December 19, 2000

CR A2001-00131

Root Cause Evaluation Report for Lack of

Sensitivity and Awareness by Supervision

and Work Force to Engage Fire Protection

Standards Pertaining to Combustible

Storage (Transient Fire Loading) and

Blockage of Fire Protection Equipment

January 16, 2001

CR A2001-00815

Unintentional Rotation of Unit 1 C/D

Traveling Screens During Maintenance

March 19, 2001

ATI 00056776-02

Root Cause Investigation Report for

Procedural Noncompliance at Braidwood

Station Due to a Lack of Management

Oversight and Failure to Enforce

Management Standards and Expectations

July 23, 2001

28

Abstract from Root Cause Report Titled

Adverse Trend - contractors Fail to

Adequately Follow the Hot work Procedure

(OP-AA-201-004) Due to Lack of

Reinforcement of Procedural

Requirements During Pre-Job Briefs (ATI

42593-02)

Non-Cited Violations (NCVs)

50-456/2000011-01

Equipment Alignment of 1A Safety

Injection Pump

September 13, 2000

50-456/457/2001002-01

Violation of Criterion III Due to Failure to

Correctly Translate Tank Weight Into a

Seismic Calculation

March 12, 2001

50-456/2001005-01

Inadequate Post Maintenance Testing

Associated with Preventive Maintenance

on the OA Hydrogen Recombiner

April 27, 2001

50-456/457/2002007-01

Inadequate Procedure for Performing

Maintenance on the 1AOV-SX178 Valve

July 26, 2001

50-457/2002009-02

Failure to Follow Procedures Lead to Unit

2 Reactor Trip

September 17, 2001

50-456/2001010-01

Failure to Follow Procedure Resulting in a

Water Spill

October 26, 2001

50-456/457/2001010-02

Failure to Have Procedure Appropriate to

Circumstances

October 26, 2001

50-456/457/2001011-01

Failure to Follow Procedure during Startup

December 12, 2001

50-456/457/2001011-03

Failure to Follow Technical Specification 5.7.2(d)

December 12, 2001

50-456/457/2001013-02

Failure to Perform RH Pump Maintenance

in Accordance with Procedure

November 7, 2001

Apparent Cause Evaluation (ACE)

PIF A1998-02003

Inappropriate Temp Lift

June 2, 1998

PIF A2000-02112

Potential Trend - Contractor Control

Issues During Refuel Outage

May 3, 2000

AR 00034943

ACE for CR A2000-3576; Potential

Weakness Exists for Identifying

Maintenance Rule Functional Failure

November 30, 2001

29

AR 00071357

Procedure Adherence Determined to be

Common Cause During CCA

August 8, 2001

AR 00072949

Missed Firewatch on U1 Cable Tunnel

August 22, 2001

AR 00072983

Reliability Criteria for Function SX1 Has

Been Exceeded

August 23, 2001

AR 00074717

1SI8804B Trips Breaker When Trying to

Stroke - Unplanned LCO

September 10, 2001

AR 00075330

Testing of 1CV03P, Letdown Booster PP,

Configuration Control

September 14, 2001

AR 00076106

Unit 1 6.9KV Bus 156 and 157 Problems

With Breaker Rosettes

September 22, 2001

AR 00076146

1PS9357B Failed Local Leak Rate Test

(LLRT) per 1BwOSR 3.6.1.1-8 Section 4

September 24, 2001

AR 00076349

During Performance of 1BwOSR

3.4.11.3.3 Check Valves Failed

September 24, 2001

AR 00076372

1CV8396A Found Open During LLRT

Subsequent Leak in Containment CWA

September 25, 2001

AR 00076399

LLRT Failure of 1RY8047

September 25, 2001

AR 00076572

Hydrolazing SX Cooling in 1B AF Water

Room, Water Spray

September 26, 2001

AR 00079302

Potential Trend - Fire Protection/Hot Work

Issues in A1R09

October 18, 2001

AR 00083778

Cardon Dioxide Restored to Unit 2 Cable

Tunnel Improperly

November 13, 2001

AR 00085601

2CV460 Did Not Close While Establishing

Excess Letdown

December 7, 2001

AR 00094186 1

ACE on 2SX178 Failure to Open (39827-

02) Requires Updating

February 6, 2002

CR A2000-03499

NO Identified Examples of Inadequate

Dispositioning of Operating Experience

(OPEX)

September 5, 2000

CR A2000-03532

Loss of Refueling Water Storage Tank

Level

September 6, 2000

CR A2000-03576

The Potential Exists That Maintenance

Rule Functional Failures Are Not Being

Identified

September 12, 2000

30

CR A2000-03615

Corrective Actions from CAP ACE Not

Performed or Tracked

September 14, 2000

CR A2000-03621

Preventive Maintenance Scheduled Past

Due Dates

September 14, 2000

CR A2000-03681

Incorrect Parts Issued for 2CV01PB Work

September 14, 2000

CR A2000-03706

0GW073 (Analyzer Outlet Isolation Valve)

Found Closed During Set Up for Monthly

Calibration

September 21, 2000

CR A2000-03727

Potential Rework - 1PR06J configuration

Incorrect

September 25, 2000

CR A2000-03739

LSH Sump Pump Breaker Trips

September 26, 2000

CR A2000-03897

FME Issue - Lock Tube Lost in Fuel Pool

During Top Nozzle Reconstitution

October 15, 2000

CR A2000-03958

Entry Into LCOAR 3.4.5

October 21, 2000

CR A2000-03960

2PS5552A Fount Out of Position

October 21, 2000

CR A2000-03976

2B CW Pump Found Running

October 22, 2000

CR A2000-04111

Potential Rework - Reactor Trip Bypass

Breaker Replacement Contact Blocks

Installed in Incorrect Position

October 26, 2000

CR A2000-04153

A Train Engineered Safety Feature (ESF)

Sequence Timer Wired Wrong

October 30, 2000

CR A2000-04156

Loss of Seal Injection Flow to 2D Reactor

Coolant Pump

October 21, 2000

CR A2000-04170

OOS Not Properly Hung for 2CV8153A

October 30, 2000

CR A2000-04197

Rework - 2CV121 Valve Sticking

October 29, 2000

CR A2000-04246

Rework - Pressurizer Spray Valve

Temporary Modification Not Removed

November 8, 2000

CR A2000-04284

Incorrect Delta-I Target Leads to Unit 2

Ramp Down

November 8, 2000

CR A2000-04317

Potential Trend - Contractor Control

Issues During Refuel Outage

November 9, 2000

CR A2000-04554

480V ESF Switchgear 231X Breakers

Found in REMOVED Position

December 10, 2000

CR A2000-04679

Failure to Follow Written

Procedure/Program

December 22, 2000

31

CR A2001-00006

Engineering Self Assessment Identifies

NRC Commitment Not Met

January 2, 2001

CR A2001-00028

Poor Quality ACEs Being Completed by

Maintenance

January 4, 2001

CR A2001-00059

Performance Indicator OM.1, Unplanned

Entries Into LCOs, is in Variance

January 8, 2001

CR A2001-00208

Potential FME - 2SX052B Seat Ring and

Plate Missing

January 22, 2001

CR A2001-00379

Admin Procedure Not Adhered to

Resulting in NEP Inadvertent Deletion

February 6, 2001

CR A2001-00515

1CF5000B Found Out of Position

February 18, 2001

CR A2001-00608

Required Work for Temporary Modification

Removal Not Completed as Scheduled

February 28, 2001

CR A2001-00633

Unit 1 Station Air Compressor Found with

Low Oil Level

March 2, 2001

CR A2001-00714

Entry Into LCO 3.6.5 for U2 High

Containment Temperature

March 6, 2001

CR A2001-00916

Ambiguous Work Task Instructions Can

Result in OOS Error and Personal Injury

March 26, 2001

CR A2001-00930

NO Identified an Inadequate Corrective

Action

March 28, 2001

CR A2001-01168

Potential Rework - 1SX178 Failed to Open

on 1B Auxiliary Feedwater Pump Diesel

Start

April 20, 2001

CR A2001-01170

Potential Rework - 1CS009B Trips

Breaker During Votes Testing after

Maintenance

April 20, 2001

CR A2001-01187

Unplanned Entry Into LCO 3.7.8 Due to 1B

SX Train Declared Inoperable

April 23, 2001

CR A2001-01337

Isolation of Secondary Pot Fuses for 4.16

and 6.9 KiloVolt Busses

May 6, 2001

CR A2001-01421

Unplanned Entry into TRM Technical LCO

Due to OOS

May 13, 2001

CR A2001-01535

Received Over Temperature Delta

Temperature High Reactor Trip Alert

Annunciator & Bistable Due to

Misperformed Procedure

May 21, 2001

32

CR A2001-01588

2SI080A Valve Found Out of Position

During Operator Rounds

May 28, 2001

CR A2001-01645

2RE1003 Failure to Open - Unplanned

LCOAR Entry

June 2, 2001

CR A2001-01735

2PR030J Failing Checksource, Unplanned

TRM Technical LCO Entry

June 10, 2001

CR A2001-01768

Work Delayed by Confined Space

Procedure Revision

June 11, 2001

CR A2001-01808

OPR10J Purge Inlet Valve Found Out of

Position

June 18, 2001

CR A2001-01893

Procedure Deficiency Associated with

Breath Alcohol Testing

June 25, 2001

CR A2001-02123

NRC Comments Associated with

Performance of 1BwOSR 3.5.2.2-2

July 20, 2001

CR A2001-02174

Unit 0 Service Air Compressor Unloader

Valve Malfunction

July 26, 2001

CR A2001-02271

Bus 159 Blew Secondary Pot Fuse

August 5, 2001

CR A2001-02304

Repair in Switchyard Without Proper

Procedure

August 8, 2001

CR A2000-03499

No Identified Examples of Inadequate

Dispositioning of OPEX

September 5, 2000

Work Requests (WRs)

WR 00009258

Wall Thinning Replace Pipe

July 11, 2001

WR 00012700

Cut Fire Retardant Door Wedges for

6.9/4 KiloVolt Breaker Doors

August 5, 2001

WR 00017854

Aftercooler Cu Discharge Line is Cracked.

Please Replace

September 20, 2001

WR 00018809

Pipe Break Upstream of Valve

September 28, 2001

WR 00018989

Open End Limit Switch is Broken and

Requires Replacement

September 29, 2001

WR 00019023

Instrument Air System (IA) Isolation Valve

to 1PS9354B is Broken Off

September 29, 2001

WR 00019095

Air Line Upstream of IA Isolation Valve to

1WS106 Broke

September 30, 2001

33

WR 00019385

Change Hand Switch Design to Dual

Action

October 4, 2001

WR 00019389

Change Hand Switch Design to Dual

Action

October 4, 2001

WR 00019503

Valve Wont Open, May be Bound, Need

Assist to Open

October 2, 2001

WR 00019668

Internal of OWX248 Installed Backward.

Install it Correctly.

October 18, 2001

WR 00019711

Valve May be Mechanically Binding,

Adjust Limits

October 4, 2001

WR 00019881

Found IA Line Disconnected

October 4, 2001

WR 00021134

Several Concerns With Steam Dumps

Discovered

October 12, 2001

WR 00021827

Stem Separated From Diaphragm

October 18, 2001

WR 00022576

Grease Fitting on Pipe Support Painted:

Prevents Lubrication

October 25, 2001

WR 00022583

Grease Fitting on Pipe Support Painted:

Prevents Lubrication

October 25, 2001

WR 00022584

Grease Fitting on Pipe Support Painted:

Prevents Lubrication

October 25, 2001

WR 00022598

Grease Fitting on Pipe Support Painted:

Prevents Lubrication

October 25, 2001

WR 00023689

Replace Cylinder #9R Kiene Valve

(Binding, Wont Open Fully)

October 31, 2001

WR 00026488

Valve Will Not cycle During Performance

of 2BwOS SX-Q1

November 24, 2001

WR 00357926-01

1 SI8840B Breaker Trips When Trying To

Open the Valve

September 10, 2001

WR 97081669

Reverse Threaded Valve Installed

October 30, 1997

WR 99052492

Disassemble, Inspect, and Preventive

Maintenance Recondition per NSP-ER-

3017

October 12, 1999

WR 9980095908

1CS009B MCC Thermal Overload

Protection Surveillance (132X1-G1)

1AP23E-G!

February 29, 2000

34

WR 99078723

Outboard Seal is Leaking Approximately 2

Drops/Minute. Repair/Replace Pump, 2A

Centrifugal Charging Assembly

March 5, 2000

WR 99088228

Remove Pipe Cap, Clean and chase

Threads, Install New Pipe

April 24, 2000

WR 99095065

Valve Stem Twisted-Replace. Discovered

While Trying to Achieve

June 9, 2000

WR 99107345

Replace Relay K0913, Contact

Discrepancy Noted During SSPS

September 8, 2000

WR 99109392

Pipe Wall has Significant Thinning.

Correct Per Engineering Request 9801093

September 22, 2000

WR 99114474

IA Line Separated from I/A Isolation Valve

October 19, 2000

WR 99115148

Valve Does Not Completely Isolate on

Close Signal

October 24, 2000

WR 99116225

2CV121, Stuck 10% Open Will Not Move

Either Direction

October 30, 2000

WR 99116652

2RY8028 Valve Will Not Stay Open When

Stroked. Troubleshoot

October 31, 2000

WR 99125319

Water Seeping Into Room Thru East Wall

and to Floor

December 31, 2000

WR 99135361

Erosion/Replace 8" 90el AND 16" OF Pipe

Downstream W/P22

February 28, 2001

WR 99136759

High Speed Breaker Fails to Close When

Attempted

March 8, 2001

WR 99137981-01

MM Leaks By

December 27, 2001

WR 99140898

High Pressure Turbine #1 Governor Valve

Failed Closed

April 3, 2001

WR 9914659

Pinhole Leak in Elbow Located at 418oF

10 + 11 FT.

April 9, 2001

WR 990172455

1CS009B; Molded Case Circuit Breaker

Trip Test Surveillance

April 18, 2001

WR 990130116 01

SX Crosstie Valve Stroke & Indication

Quarterly Surveillance Test

March 16, 2000

WR 990155110 01

SX Crosstie Valve Stroke & Indication

Quarterly Surveillance Test

June 10, 2000

35

WR 990184343 01

SX Crosstie Valve Stroke & Indication

Quarterly Surveillance Test

September 2, 2000

WR 99106670

Valve Will Not Fully Close, Troubleshoot

Repair as Necessary

September 3, 2000

WR 99277806 01

Essential Service Water Indication 18

Month Surveillance Test

November 21, 2001

WR A56570

Power Operated Relief Valve (PORV)

Accumulator Check Valve

October 6, 1992

WR A56571

PORV Accumulator Check Valve

October 6, 1992

WR A56572

PORV Accumulator Check Valve

October 6, 1992

WR A56573

PORV Accumulator Check Valve

October 6, 1992

WR 970072753

1RY085A Inspection

October 9, 1998

WR 970072754

1RY085B Inspection

October 9, 1998

WR 970072755

1RY086A Inspection

October 9, 1998

WR 970072757

1RY086B Inspection

October 9, 1998

WR 970051161 01

Unit 1 Pressurizer PORV Instrument Air

Accumulator Check Valve Test

October 17, 1998

WR 970114258 01

Unit 2 Pressurizer PORV Instrument Air

Accumulator Check Valve Test

May 3, 1999

WR 9800112231 01

Unit 1 Pressurizer PORV Instrument Air

Accumulator Check Valve Test

March 22, 2000

WR 990050256 01

Unit 2 Pressurizer PORV Instrument Air

Accumulator Check Valve Test

October 24, 2000

WR 990224847 01

Unit 2 Pressurizer PORV Instrument Air

Accumulator Check Valve Test

October 28, 2000

WR 99159828 01

Unit 1 Pressurizer PORV Instrument Air

Accumulator Check Valve Test

September 24, 2001

Common Cause Analysis

AR 00031900

A2000-02557: A Review of CAPSYS

Indicates 23 PIFs Initiated This Year

Identifying Incorrect or Non-Conforming

Parts Received at Braidwood A2000-

02557)

August 4, 2000

AR 00034295

A2000-03442: Potential Trend-Foreign

Material Events and Issues

September 29, 2000

36

AR 00034609

A2000-03505: Nuclear Oversight Identified

Poor Quality of ACEs

October 4, 2000

AR 00035394

A2000-03675: 7 of 7 Trend Reports

Reviewed Found Unsatisfactory by

Downers Grove Office

November 17, 2000

AR 00038455

A2000-04317: Potential Trend-Contractor

Control Issue-Outage

June 29, 2001

AR 00038589

A2000-04329: A2R08 Outage Reactivity

Management

December 15, 2000

AR 00038869

A2000-04348: Potential Trend: Foreign

Material Exclusion

April 2, 2001

AR 00039981

A2000-04494: Procedural Non-

Compliance of OP-AA-201-004

January 19, 2001

AR 00040371

A2000-04560: Administrative Directors Not

Contacted During August Drill

February 21, 2001

AR 00040707

A2000-04610: Common Cause Related to

A2R08-Overconfidence

December 3, 2001

AR 00043451

A2001-00271: Potential Adverse Trend

Related Electrical Maintenance

Department

December 31, 2001

AR 00044640

A2001-00381: Potential Increase Trend of

Errors - Design Change Document

March 20, 2001

AR 00044926

A2001-00440: Safety System Design

Inspection Items-Drawings

April 6, 2001

AR 00055823

A2001-01917: Potential Adverse Trend-

Rework Issues Relating

August 21, 2001

AR 00074457

NO Identified Problems with Administrative

Procedure Adherence

October 16, 2001

AR 00079302

Potential Trend - Fire Protection/Hot Work

Issues in A2R09

December 14, 2001

AR 00079519

Potential Trend - Contractor Control

Issues in A1R09

January 18, 2001

AR 00079728

Potential Trend - Increasing Amount of

Rework Issues

December 14, 2001

AR 0032989-02

Ineffective Corrective Actions to Prevent

Recurrence Associated with Work

Package Quality

October 31, 2000

37

CR A2000-03675

7 of 7 Trend Reports Reviewed Found

Unsatisfactory by Downers Grove

September 19, 2000

CR A2000-04610

Common Cause Related to A2R08 -

Overconfidence

December 15, 2000

AIT 57124-02

An Investigation Into the High Number of

Chiller Related CRs Generated in 2001

August 16, 2001

AIT 79302-03

Perform a Review of the 23 Condition

Reports Identified Under CR# 79302 to

Determine if an Adverse Trend Exists in

the Area of Fire Protection/Hot Work

Issues in A1R09

December 16, 2001

AIT 79519-03

Perform a Review of Approximately 88

Condition Reports Identified Under CR#

79519 to Determine if an Adverse Trend

Exists in the Area of Contractor Control

January 10, 2001

NF-AA-200-1530

Reactivity Management Controls During

Plant Operations

Revision 0

NF-AP-230

Pressure Water Reactor Reactivity

Management Controls During Operations

Revision 0

Self-Assessments

AR 00035774

Braidwood Plant Support 4Q 2000

Observations

October 22, 2000

AR 00036195

Maintenance FOs for NOA-BW-00-4Q

Assessment AR 36187

October 30, 2000

AR 00036196

Plant Support FOs for NOA BW-00-4Q

Assessment AR 36187

January 3, 2001

AR 00041556

Plant Support FOs for NOA BW-01-1Q

Assessment AR 41552

February 6, 2001

AR 00048679

Operations FOs for NOA BW-01-2Q

Assessment AR 48227

July 28, 2001

AR 00048679

Operations FOs for NOA BW-01-2Q

Assessment AR 48227

August 28, 2001

AR 00048682

Maintenance FOs for NOA BW-01-2Q

Assessment AR 48227

June 22, 2001

AR 00048684

Plant Support FOs for NOA BW-01-2Q

Assessment AR 48227

May 10, 2001

38

AR 00048684

Plant Support FOs for NOA BW-01-2Q

Assessment AR 48227

June 30, 2001

AR 00054548

Operations FOs for NOA BW-01-3Q

Assessment AR 48228

August 28, 2001

AR 00054548

Operations FOs for NOA BW-01-3Q

Assessment AR 48228

August 29, 2001

AR 00054548

Operations FOs for NOA BW-01-3Q

Assessment AR 48228

September 20, 2001

AR 00054550

Maintenance FOs for NOA BW-01-3Q

Assessment AR 48228

August 21, 2001

AR 00054550

Maintenance FOs for NOA BW-01-3Q

Assessment AR 48228

August 28, 2001

AR 00054550

Maintenance FOs for NOA BW-01-3Q

Assessment AR 48228

September 7, 2001

AR 00054550

Maintenance FOs for NOA BW-01-3Q

Assessment AR 48228

September 12, 2001

AR 00054550

Maintenance FOs for NOA BW-01-3Q

Assessment AR 48228

September 20, 2001

AR 00054550

Maintenance FOs for NOA BW-01-3Q

Assessment AR 48228

September 21, 2001

AR 00054550

Maintenance FOs for NOA BW-01-3Q

Assessment AR 48228

September 30, 2001

AR 00075249

Braidwood A1R09 Outage Field

Observations

September 18, 2001

AR 00075249

Braidwood A1R09 Outage Field

Observations

September 24, 2001

AR 00076567

Braidwood A1R09 Outage Field

Observations

September 29, 2001

AR 00076871

Operations FOs for NOA-BW-01-4Q

Assessment AR 76870

December 1, 2001

AR 00076871

Operations FOs for NOA-BW-01-4Q

Assessment AR 76870

December 17, 2001

AR 00076871

Operations FOs for NOA-BW-01-4Q

Assessment AR 76870

December 30, 2001

AR 00076874

Maintenance FOs for NOA-BW-01-4Q

Assessment AR 76870

November 21, 2001

39

AR 00076874

Maintenance FOs for NOA-BW-01-4Q

Assessment AR 76870

November 30, 2001

AR 00076875

Plant Support FOs for NOA-BW-01-4Q

Assessment AR 76870

December 20, 2001

AR 00077971

Braidwood A1R09 Outage Field

Observations

October 9, 2001

AR 00077971

Braidwood A1R09 Outage Field

Observations

October 21, 2001

AR 00081706

Braidwood A2F35 Outage Field

Observations

November 10, 2001

Braidwood Station Chemistry, Radwaste &

Environmental Areas - 4th Quarter 2000

Braidwood Station Chemistry, Radwaste &

Environmental Areas - 1st Quarter 2001

Braidwood Station Chemistry, Radwaste &

Environmental Areas - 2nd Quarter 2001

Braidwood Station Chemistry, Radwaste &

Environmental Areas - 3rd Quarter 2001

NOL 20-01-034

Braidwood Station Nuclear Oversight

Post-Outage Performance Assessment for

A1R09

November 16, 2001

NOL 20-01-035

Braidwood Station Nuclear Oversight

Post-Outage Performance Assessment for

A2F35

November 30, 2001

NOA-BW-00-4Q

Nuclear Oversight Continuous

Assessment Report Braidwood Generating

Station October - December 2000

January 31, 2001

NOA-BW-01-1Q

Nuclear Oversight Continuous

Assessment Report Braidwood Generating

Station January - March 2001

April 30, 2001

NOA-BW-01-2Q

Nuclear Oversight Continuous

Assessment Report Braidwood Generating

Station April - June 2001

July 30, 2001

NOA-BW-01-3Q

Nuclear Oversight Continuous

Assessment Report Braidwood Generating

Station July - September 2001

October 31, 2001

40

NOA-BW-01-4Q

Nuclear Oversight Continuous

Assessment Report Braidwood Generating

Station October - December 2001

January 29, 2002

Nuclear Oversight Self-Assessment

Report 4th Quarter 2000

Nuclear Oversight Self-Assessment

Report 1st Quarter 2001

Nuclear Oversight Self-Assessment

Report 2nd Quarter 2001

Nuclear Oversight Self-Assessment

Report 3rd Quarter 2001

Radiation Protection Self-Assessment

Report - 3rd Quarter 2001

Self Assessment Report - 3rd Quarter 2001

Site-wide CAP Focused Area Self-

Assessment Report ( Follow-up Report)

February 1, 2001

Regulatory Assurance Self-Assessment 1st

Quarter 2001

Regulatory Assurance Self-Assessment 1st

Quarter 2001

Regulatory Assurance Self-Assessment

2nd Quarter 2001

Regulatory Assurance Self-Assessment

3rd Quarter 2001

Maintenance Quarterly Assessment

Report 3rd Quarter 2001

System Health Indicator Program

Braidwood Station SHIP Report for

September 2000

Procedures

BwOP RH-6

Placing the RH System in Shutdown

Cooling

Revision 2

0Bw0A PRI - 8

Auxiliary Building Flooding

Revision 1

1Bw0A PRI - 8

Essential Service Water Malfunction

Revision 100

41

1BwOSR 0.1-1,2,3

U1 Modes 1,2, and 2 3 Shiftly and Daily

Operating Surveillance

Revision 14

1BwOSR 3.3.1.2-1

U1 Power Range High Flux Setpoint Daily

Channel Calibration (Computer

Calorimetric)

Revision 7

1BwOSR 3.4.11.3

Pressurizer PORV Instrument Air

Accumulator Check Valve Test

Revision 1

1BwOSR 3.4.11.3

Pressurizer PORV Instrument Air

Accumulator Check Valve Test

Revision 2

1BwOSR 3.4.11.3

Pressurizer PORV Instrument Air

Accumulator Check Valve Test

Revision 3

1BwOSR 3.7.8.1

U2 Essential Service Water Monthly

Surveillance Data Sheet

Revision 4

2BwOSR 5.5.8.SX-1B

Essential Service Water Train B Valve

Stroke Quarterly Surveillance

Revision 3

1BwOS SX-Q1

U2 Essential Service Water System

Manual Ball Valve Cycle Quarterly

Surveillance

Revision 2

BwVS 800-2

Instrument Air Sampling Requirements

Revision 4E2

MA-BR-EM-1-3.8.a.3-1

Surveillance for Inspection and Testing of

480 Volt Motor Control Center (MCC)

Draw-Out Units

Revision 1

MA-BR-EM-1-3.8.a.3-1

Surveillance for Inspection and Testing of

480 Volt Motor Control Center (MCC)

Draw-Out Units

Revision 2

WC-AA-101

Work Screening and Classification

Revision 5

OP-AA-102-103

Operator Work-Around Program

Revision 0

LS-AA-125

Corrective Action Program (CAP)

Procedure

Revision 1

LS-AA-125-1002

Common Cause Analysis Manual

Revision 1

LS-AA-125-1003

Apparent Cause Evaluation Manual

Revision 0

LS-AA-125-1004

Effectiveness Review Manual

Revision 0

LS-AA-125-1005

Coding and Trending Manual

Revision 1

LS-AA-125-1006

CAP Process Expectations Manual

Revision 0

ER-AA-10

Equipment Reliability Process Description

Revision 0

42

ER-AA-310

Implementation of the Maintenance Rule

Revision 1

EI-AA-10

Exelon Nuclear Employee Concerns

Program Process Description

Revision 0

EI-AA-1

Nuclear Policy Employee Issues

June 25, 2001

OU-AA-103

Shutdown Safety Management Program

Revision 1

RS-AA-115

Operating Experience (OPEX)

Revision 2

Q1 2001 Procedure Use and Compliance

Prompt Investigations

AR 00056777

A2001-02014: Steam Dump Valves

1MS004 C and G Made Inoperable

June 3, 2002

Prompt Investigation Into the Motor

Rotation Issues With the 1D

Condensate/Condensate Booster Pump

Motor

June 8, 2001

Prompt Investigation of 1WG01FB Circuit

Found Energized with Clearance Order

Placed (CR 82702)

November 13, 2001

Miscellaneous

Operator Work Around Status Update

February 11, 2001

Operator Workaround Minutes

October 5, 2000

ER 99-029

1B Charging Pump (1CV01PB) Seal

Leakage

December 22, 1999

UFSAR 9-058

Increase the Maximum Allowed ESF

Recirculation Loop Leakage External to

Containment

Braidwood Chronic Problem List

PIF A1997-04845

Incorrect Valve Installed as 2SX124B

October 30, 1997

Braidwood Maintenance Rule (a)(1)

Systems Since 09/01/2000

System Health Overview Instrument Air 4th

Quarter 2001

43

Drawing. M55

Diagram of Instrument Air Lake/River

Screen House and Make-up Demin. Bldg.

Units 1 & 2

Revision AA

System Monitoring Plan

Instrument Air System

April 30, 2001

AIT 79728

Potential Adverse Trend - Increasing

Rework Issues

December 12, 2001

00042593-05-00

Completed and Open Actions from A2001-

00131: AR Assignment/Sub Assignment

Summary Report (CAP010)

February 26, 2001

Instrument Air Sample Data 1/2000-

12/2001

NUREG-1275 Vol. 2

Operating Experience Feedback Report -

Air Systems Problems

December 1987

ANSI/ISA-S7.3-1975

Quality Standard for Instrument Air

November 16, 1981

Instrument Air System Maintenance Rule -

Evaluation History

AR 00054375

Perform OPEX Review of NRC

Information Notice 2001-09

June 12, 2001

IN 2001-09

Main Feedwater system Degradation in

Safety-Related ASME Code class 2 Piping

Inside the Containment of a Pressurized

Water Reactor

June 2, 2001

IN 2002-05

Foreign Material in Standby Liquid Control

Storage Tanks

January 17, 2002

NON BY-01-097

Planning and Human Performance Errors

Delay 2B Diesel Generator Return to

Service

December 3, 2001

NSAL-01-004

Westinghouse

May 2, 2001

ESBU-TB-96-03-RO

RH Pump Operating Recommendations

June 20, 1996

TS 3.76

Condensate Storage Tank

Licensee Event Report

(LER) 456/01-001-00

Three Main Steam Safety Valves

Exceeded the Technical specification Limit

by Greater Than 3%

November 19, 2001

44

LER 457/01-001-00

Braidwood U2 Reactor Trip and

Subsequent Loss of Non-Safety Related

Offsite Power Due to Failure to Perform

Concurrent Verification and Improper

Command and Control

July 17, 2001

LER 457/01-002-00

Main Steam Isolation Valves Not Stroke

Timed in Mode 3 as Required

November 26, 2001

CQD-003676

Review of the Sulzer Qualification Report

(E12.5.785, Rev. 0) for the Essential

Service Water Pumps (1,2SX01PA & PB)

for the Braidwood and Byron Stations

Revision 1

AP System Notebook, Section 4,

Performance Monitoring Failures (DHP

Breaker Significant events)

September 12, 2001

AP System Notebook, Section 6,

Performance Monitoring Failures (MCC

Significant Events)

February 6, 2002

AP System Notebook, Section 6,

Performance Monitoring Failures (DS

Breaker significant Events)

Braidwood Inservice Inspection Program

Plan

September 1, 2001

01823-TR-001

Evaluation of Dresser 3700 Series Safety

Valve Inconel X-750 Disc

Revision 0

EC 0000332797 000

Change Breaker Setting for 1SI8804B

September 11, 2001

ComEd Corrective Action Program - NRC

Presentation

June 15, 2000

Nuclear Safety Review Board - Braidwood

Station

February 1, 2002

Braidwood Pressurizer PORV

Accumulator Instrument Air Isolation

Check Valve Performance

February 20, 2002