Information Notice 2002-05, Foreign Material in Standby Liquid Control Storage Tanks
| ML013530020 | |
| Person / Time | |
|---|---|
| Site: | River Bend |
| Issue date: | 01/17/2002 |
| From: | Beckner W Division of Regulatory Improvement Programs |
| To: | |
| Fields E N 301-415-1173 | |
| References | |
| TAC MB0371 IN-02-005 | |
| Download: ML013530020 (5) | |
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D. C. 20555-0001
January 17, 2002
NRC INFORMATION NOTICE 2002-05:
FOREIGN MATERIAL IN STANDBY LIQUID
CONTROL STORAGE TANKS
Addressees
All holders of licenses for nuclear power reactors.
Purpose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to inform
addressees of equipment and design issues identified recently at the River Bend Nuclear
Power Plant concerning debris found in the standby liquid control system storage tank. It is
expected that recipients will review the information for applicability to their facilities and consider
actions, as appropriate, to avoid similar problems. The aspect of this event considered of
particular interest is the evident potential for systems initially filled with a combination of dry
chemicals and water to have the wrapper material for the chemicals left in the system and to
remain there undetected for an extended period. However, suggestions contained in this
information notice are not NRC requirements; therefore, no specific actions or written response
is required.
Description of Circumstances
During monthly sampling of the standby liquid control (SLC) system storage tank in September
2000, part of a plastic bag was found in the SLC tank. Both trains of SLC were declared
inoperable while the licensee inspected the tank, removed several pieces of plastic, and
performed an evaluation. This event was discussed in NRC Inspection Report 50-458/00-14, ADAMS Accession No. ML003774888 and Licensee Event Report 50-458/00-013-00, ADAMS
Accession No. ML003769869.
Discussion
On September 14, 2000, while drawing a routine monthly sample from the SLC tank at River
Bend, Unit 1, chemistry personnel retrieved a 10-inch square piece of plastic along with the
sampling equipment. The SLC tank manway cover was removed and several additional pieces
of plastic were observed floating on the surface. Approximately 20 pieces of plastic which
ranged in size from 2 square feet to one-half square inch were identified and removed. Further
inspection of the tank with an underwater camera identified additional pieces of plastic on the
sparger supports and the mixing heater located at the bottom of the SLC tank.
Because of the potential for the plastic to be sucked into the SLC pump suction piping, both
SLC subsystems were declared inoperable. The plastic material was removed and further
inspections of the SLC tank were performed with an underwater camera. No additional foreign
material was identified. Additionally, a boroscope inspection of the horizontal suction piping
from the tank outlet to the downward elbow was performed. No material was identified during
the inspection. Based on the inspection and the buoyancy of the plastic material, the licensee
concluded that the remaining SLC pump suction piping would not contain any significant
amount of plastic material.
The licensee evaluated the effect that 1 square inch pieces of plastic would have on system
performance. The evaluation determined that pieces of plastic less than 1 square inch which
might be introduced into the SLC pump suction would not preclude the system from injecting
sodium pentaborate into the reactor. The licensee believed that any remaining plastic material
would be less than 1 square inch. At 8:59 p.m. that same day, both SLC subsystems were
declared operable due to the inspections of the SLC system, the removal of the plastic material, and the engineering evaluation.
The licensee established a significant event review team to investigate the event and evaluate
the safety significance of the plastic material in the SLC tank. The licensee determined that the
incremental risk from this event, assuming that the SLC system was out of service for a one
year time frame, was 3.0E-8. Since the upper limit for non risk-significant changes in
conditional core damage probability was 1.0E-6, the licensee concluded the event was not risk
significant.
Due to low flow velocities and the buoyancy of the plastic, the licensee believed that the SLC
system would have been able to perform its function even with the plastic in the tank, provided
the SLC storage tank was in a steady state condition. The only time the licensee believed that
the SLC systems behavior could not be predicted and operability demonstrated was during the
10-minute air agitation before the monthly chemistry sampling of the SLC tank contents. During
and immediately following the air sparger, the location of the plastic material in the SLC tank
could not be predicted. Therefore, the licensee concluded that the SLC system may not have
been able to provide its intended safety function during periods in which the tank was being
agitated with air.
On September 25, 2000, NRC inspectors conducted a walkdown of the alternate SLC injection
emergency operating procedure. They determined that the sodium borate and boric acid
chemicals to be used were not available in the warehouse or onsite for alternate SLC. The
inspectors notified the licensee and replacement chemicals were shipped from the Grand Gulf
Nuclear Station and arrived onsite at approximately 4 a.m., on September 26, 2000.
Further investigation by the licensee revealed that the alternate SLC injection chemicals had
been removed from the site. On March 3, 1999, a quality assurance chemistry audit had
identified chemical storage discrepancies (i.e., deteriorated packaging) with chemicals stored in
the onsite warehouse. On July 14, 1999, warehouse personnel removed the identified
chemicals from inventory as a corrective action for the deteriorated packaging problems
identified during the quality assurance audit. On July 28, 1999, the chemicals that had been
removed from inventory were transported to the environmental storage yard and subsequently shipped offsite. Warehouse personnel had not recognized that these chemicals were required
for an emergency operating procedure and adequate controls were not in place to identify them
as such. As a result, the chemicals were never replaced.
The licensees guidance document on procedural control, Authors Guide/Control and Use of
Emergency Operating and Severe Accident Procedures, required that operations personnel
perform yearly walkdowns of each emergency operating procedure enclosure. On October 2,
2000, in response to the inspectors identification of the missing chemicals, operations
personnel completed a review of their documentation of emergency operating procedure
enclosure audits and yearly walkdowns. The review determined that the yearly walkdowns of
each emergency operating procedure enclosure had not been performed since November 26,
1996.
As a result of this event, the Cooper Nuclear Station, also identified plastic material in their SLC
storage tank in the fall of 2001. Because of the small quantity of plastic found, the system was
not considered to be rendered inoperable.
This event points out the importance of effective foreign material exclusion controls to prevent
the introduction into the SLC storage tank or other similar systems of wrapper material which
could impair the system's operability. In this instance, the buoyancy of the plastic material
reduced the potential consequences. The event also pointed out the need for effective
periodic walkdowns of emergency operating procedure attachments to ensure that all required
equipment and materials are available to perform the emergency procedures.
This information notice requires no specific action or written response. If you have any
questions about the information in this notice, please contact one of the technical contacts
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
/RA/
William D. Beckner, Program Director
Operating Reactor Improvements Program
Division of Regulatory Improvement Programs
Office of Nuclear Reactor Regulation
Technical contacts: Stephen Max Schneider, Region IV
Ron Kopriva, Region IV
225-635-3193
817-860-8104 E-mail: sms2@nrc.gov
E-mail: rak1@nrc.gov
Attachment: List of Recently Issued NRC Information Notices shipped offsite. Warehouse personnel had not recognized that these chemicals were required
for an emergency operating procedure and adequate controls were not in place to identify them
as such. As a result, the chemicals were never replaced.
The licensees guidance document on procedural control, Authors Guide/Control and Use of
Emergency Operating and Severe Accident Procedures, required that operations personnel
perform yearly walkdowns of each emergency operating procedure enclosure. On October 2,
2000, in response to the inspectors identification of the missing chemicals, operations
personnel completed a review of their documentation of emergency operating procedure
enclosure audits and yearly walkdowns. The review determined that the yearly walkdowns of
each emergency operating procedure enclosure had not been performed since November 26,
1996.
As a result of this event, the Cooper Nuclear Station, also identified plastic material in their SLC
storage tank in the fall of 2001. Because of the small quantity of plastic found, the system was
not considered to be rendered inoperable.
This event points out the importance of effective foreign material exclusion controls to prevent
the introduction into the SLC storage tank or other similar systems of wrapper material which
could impair the system's operability. In this instance, the buoyancy of the plastic material
reduced the potential consequences. The event also pointed out the need for effective
periodic walkdowns of emergency operating procedure attachments to ensure that all required
equipment and materials are available to perform the emergency procedures.
This information notice requires no specific action or written response. If you have any
questions about the information in this notice, please contact one of the technical contacts
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
/RA/
William D. Beckner, Program Director
Operating Reactor Improvements Program
Division of Regulatory Improvement Programs
Office of Nuclear Reactor Regulation
Technical contacts: Stephen Max Schneider, Region IV
Ron Kopriva, Region IV
225-635-3193
817-860-8104 E-mail: sms2@nrc.gov
E-mail: rak1@nrc.gov
Attachment: List of Recently Issued NRC Information Notices
Accession No.: ML013530020
Template No.: 052 Distribution:
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Non-Publicly Available
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Non-Sensitive
OFFICE
RSE:RORP:DRIP
Tech Editor
BC:SRXB:DSSA
(A)SC:RORP:DRIP
PD:RORP:DRIP
NAME
NFields*
PKleene*
JSWermiel*
TKoshy*
WDBeckner*
DATE
01/15/2002
09/10/2001
01/16/2002
01/17/2002
01/17/2002 OFFICE
RIV
RIV
NAME
SMSchneider*
RKopriva*
DATE
01/15/2002
01/15/2002
OFFICIAL RECORD COPY
______________________________________________________________________________________
OL = Operating License
CP = Construction Permit
Attachment 1 LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
_____________________________________________________________________________________
Information
Date of
Notice No.
Subject
Issuance
Issued to
_____________________________________________________________________________________
2002-04
Wire Degradation at Breaker
Cubicle Door Hinges
1/10/02
All holders of operating licenses
for nuclear power reactors.
2002-03
Highly Radioactive Particle
Control Problems During Spent
Fuel Pool Cleanout
1/10/2002
All holders of operating licenses
for nuclear power reactors, holders of licenses for
permanently shutdown facilities
with fuel onsite, and holders of
licenses for non-power reactors.
2002-02
Recent Experience with
Plugged Steam Generator
Tubes
01/08/2002
All holders of operating licenses
for pressurized-water reactors
(PWRs), except those who have
permanently ceased operations
and have certified that fuel has
been permanently removed from
the reactor.
2002-01
Metalclad Switchgear Failures
and Consequent Losses of
Offsite Power
01/08/2002
All holders of licenses for nuclear
power reactors.
2001-19
Improper Maintenance and
Reassembly of Automatic Oil
Bubblers
12/17/2001
All holders of operating licenses
for nuclear power reactors, except those who have
permanently ceased operations
and have certified that fuel has
been permanently removed from
the reactor vessel.
2001-18
Degraded or Failed Automated
Electronic Monitoring, Control,
Alarming, Response, and
Communications Needed for
Safety and/or Safeguards
12/14/2001 All uranium fuel conversion, enrichment, and fabrication
licensees and certificate holders
authorized to receive safeguards
information. Information notice is
not available to the public
because it contains safeguards
information.