L-02-056, April 2002 Monthly Operating Report for Beaver Valley Power Station

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April 2002 Monthly Operating Report for Beaver Valley Power Station
ML021440220
Person / Time
Site: Beaver Valley
Issue date: 05/07/2002
From: Pearce L
FirstEnergy Nuclear Operating Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
GL-97-002, L-02-056
Download: ML021440220 (6)


Text

FENOC Beaver Valley Power Station P. 0. Box 4 Shippingport,PA 15077 L-02-056 May 7, 2002 Beaver Valley Power Station Unit 1 - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operating Report U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

In accordance with NRC Generic Letter 97-02, "Revised Contents of the Monthly Operating Operating Report", and Unit 1 and 2 Technical Specification 6.9.4, the "Monthly Report" is submitted for Unit 1 and Unit 2 for the month of April 2002.

Respectfully, W. Pearce Acting Site Vice-President DTJ/caj Enclosures cc: NRC Regional Office King of Prussia, PA "U, q)

UNIT SHUTDOWNS DOCKET NO. 50-334 UNIT NAME BVPS Unit #1 DATE May 2,2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD: April 2002 No. Date Type Duration Reason Method of Cause / Corrective Actions (YIM/D) F: Forced (Hours) (1) Shutting S: Scheduled Down (2) Comments NONE.

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip / Scram C - Refueling 3 - Automatic Trip I Scram D - Regulatory Restriction 4- Continuation E - Operator Training / License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

done in The Unit began the report period operating at approximately 95% output. This was being Feedwater Pump order to maintain reduced loading on the outboard motor bearings of the "A" Main until a planned power reduction to replace the motor bearings could be started on 4/2/02. Outboard 4/2/02, motor bearing temperatures had been running higher in the previous month. At 0052 hours6.018519e-4 days <br />0.0144 hours <br />8.597884e-5 weeks <br />1.9786e-5 months <br /> on the Unit began a power reduction to approximately 63% output in order to replace the motor bearings on on the "A" Main Feedwater Pump. An output of approximately 63% was achieved at 0353 hours0.00409 days <br />0.0981 hours <br />5.83664e-4 weeks <br />1.343165e-4 months <br /> during this 4/2/02. Cleaning of the "C" and "D" Main Unit Condenser Waterboxes was also performed 0446 planned reduction. Upon completion of repairs, the Unit commenced a return to full power at hours on 4/5/02. A nominal value of 100% output was achieved at 1100 hours on 4/5/02.

when a The Unit continued to operate at a nominal value of 100% output until 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br /> on 4/12/02 to clean the "A" and "B" planned power reduction to approximately 90% output was begun in order on Main Unit Condenser Waterboxes. An output of approximately 90% was achieved at 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br /> vacuum 4/12/02. However, with the "A" Condenser Waterbox isolated and degrading Condenser incremental load reductions between 0750 conditions indicated, the Unit performed several unplanned and 1247 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.744835e-4 months <br /> on 4/13/02 as a conservative action based on available Condenser vacuum operating at indications, until the "A" Condenser Waterbox was returned to service. With the Unit hours on approximately 80% output, a return to approximately 90% output was commenced at 1532 "B"

4/13/02. An output of approximately 90% was achieved at 1656 hours0.0192 days <br />0.46 hours <br />0.00274 weeks <br />6.30108e-4 months <br /> on 4/13/02. The any degrading Condenser Condenser Waterbox was removed from service and cleaned without full power.

vacuum conditions occurring. At 1331 hours0.0154 days <br />0.37 hours <br />0.0022 weeks <br />5.064455e-4 months <br /> on 4/14/02, the Unit commenced a return to to A nominal value of 100% output was achieved at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on 4/14/02. The Unit continued operate at a nominal value of 100% output for the remainder of the report period.

OPERATING DATA REPORT DOCKET NO.: 50-334 UNIT NAME: BVPS UNIT #1 REPORT DATE: 05/02/02 COMPLETED BY: DAVID T. JONES TELEPHONE: (724) 682-4962

  • Notes: Rated thermal power at
  • la. REPORTING PERIOD: APRIL 2002
  • BVPS-1 was uprated from 2652 MWt*

to 2689 MWt on 10/20/01. Net *

1. DESIGN ELECTRICAL RATING (Net MWe): 835
  • uprated from
  • 810 MWe to 821 MWe.
  • 821
2. MAX. DEPENDABLE CAPACITY (Net MWe): * * * * * * * * ** * * * * * * *
  • THIS MONTH YEAR TO DATE CUMULATIVE 719.0 2879.0 227903.0 3a. HOURS IN REPORTING PERIOD:

2879.0 154960.5 719.0

3. NO. OF ERS. REACTOR WAS CRITICAL:

2879.0 152500.9 719.0

4. SERVICE HOURS GENERATOR ON LINE:

0.0 0.0 0.0

5. UNIT RESERVE SHUTDOWN HOURS:

2367910.0 114034053.0 567550.0

6. NET ELECTRICAL ENERGY GEN. (MWH):

601370.0 2505980.0 121772766.0

7. GROSS ELECT. ENERGY GEN. (MWH):

7619403.0 375254208.5 (KWH): 1837779.0

8. GROSS THERMAL ENERGY GEN.

100.0 68.4 100.0

9. UNIT AVAILABILITY FACTOR (M):

100.2 63.7 96.1

10. UNIT CAPACITY FACTOR (MDC) (M):

0.0 16.2 0.0

11. UNIT FORCED OUTAGE RATE (M):

UNIT SHUTDOWNS DOCKET NO. 50-412 UNIT NAME BVPS Unit #2 DATE May 2, 2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD: April 2002 No. Date Type Duration Reason Method of Cause / Corrective Actions (Y/M/D) F: Forced (Hours) (1) Shutting S: Scheduled Down (2) Comments 3 020405 F 17.9 A I The Unit was shut down to Mode 2 (Reactor remained critical) due to degraded chemistry conditions in the Steam Generators caused by a tube leak in the *C"Waterbox of the Main Unit Condenser. The tube leak was repaired, and once chemistry conditions in the Steam Generators improved, the Unit was returned to full power.

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip Scram C - Refueling 3 - Automatic Trip I Scram D - Regulatory Restriction 4 - Continuation E - Operator Training t License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

The Unit began the report period operating at a nominal value of 100% output until 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on 4/4/02 when a planned power reduction to approximately 90% output was begun in order to remove the "C" Main Unit Condenser Waterbox from service for cleaning. An output of approximately 90%

was achieved at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> on 4/4/02. With the "C" Condenser Waterbox isolated, the Unit commenced to return to full power at 0358 hours0.00414 days <br />0.0994 hours <br />5.919312e-4 weeks <br />1.36219e-4 months <br /> on 4/4/02. A nominal value of 100% output was achieved at 0455 hours0.00527 days <br />0.126 hours <br />7.523148e-4 weeks <br />1.731275e-4 months <br /> on 4/4/02.

The Unit continued to operate at a nominal value of 100% output until 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on 4/5/02 when a planned power reduction to approximately 90% output was begun in order to remove the "B" Main Unit Condenser Waterbox from service for cleaning. An output of approximately 90% was achieved at 0150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br /> on 4/5/02. With the "B" Condenser Waterbox isolated, the Unit commenced a return to full power at 0236 hours0.00273 days <br />0.0656 hours <br />3.902116e-4 weeks <br />8.9798e-5 months <br /> on 4/5/02. A nominal value of 100% output was achieved at 0347 hours0.00402 days <br />0.0964 hours <br />5.737434e-4 weeks <br />1.320335e-4 months <br /> on 4/5/02.

However, with degrading chemistry conditions occurring in the Steam Generators, an unplanned power reduction to approximately 90% output was begun at 0623 hours0.00721 days <br />0.173 hours <br />0.00103 weeks <br />2.370515e-4 months <br /> on 4/5/02 in order to investigate a potential tube leak in the "C"Waterbox of the Main Unit Condenser. At 0758 hours0.00877 days <br />0.211 hours <br />0.00125 weeks <br />2.88419e-4 months <br /> on 4/5/02, the Unit commenced a shut down due to degraded chemistry conditions in the Steam Generators. The Unit was taken off-line at 1424 hours0.0165 days <br />0.396 hours <br />0.00235 weeks <br />5.41832e-4 months <br /> on 4/5/02 and entered Mode 2 at 1443 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.490615e-4 months <br /> on 4/5/02 with the Reactor remaining critical. Once the tube leak in the "C" Condenser Waterbox was

UNIT SHUTDOWNS DOCKET NO. 50-412 UNIT NAME BVPS Unit #2 DATE May 2, 2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD: April 2002

SUMMARY

(continued):

repaired and chemistry conditions in the Steam Generators improved, the Unit commenced to startup, 0817 entering Mode I at 0603 hours0.00698 days <br />0.168 hours <br />9.970238e-4 weeks <br />2.294415e-4 months <br /> on 4/6/02. The Unit was synchronized to the electrical grid at full power. A nominal value of 100% output was hours on 4/6/02 and commenced to return to achieved at 2400 hours0.0278 days <br />0.667 hours <br />0.00397 weeks <br />9.132e-4 months <br /> on 4/6/02.

The Unit continued to operate at a nominal value of 100% output until 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> on 4/20/02 when a Unit planned power reduction to approximately 75% output was begun in order to clean the "B" Main Condenser Waterbox. An output of approximately 75% was achieved at 0017 hours on 4/21/02.

Upon completion of cleaning the "B" Condenser Waterbox, the Unit commenced to return to full power at 1650 hours0.0191 days <br />0.458 hours <br />0.00273 weeks <br />6.27825e-4 months <br /> on 4/21/02. A nominal value of 100% output was achieved at 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br /> on 4/21/02.

The Unit continued to operate at a nominal value of 100% output for the remainder of the report period.

OPERATING DATA REPORT DOCKET NO.: 50-412 UNIT NAME: BVPS UNIT #2 REPORT DATE: 05/02/02 COMPLETED BY: DAVID T. JONES TELEPHONE: (724) 682-4962 Notes: Rated thermal power at

  • la. REPORTING PERIOD: APRIL 2002
  • BVPS-2 was uprated from 2652 MWt*
  • to 2689 Mwt on 10/30/01. Net *
1. DESIGN ELECTRICAL RATING (Net MWe): 836
  • m)C was also uprated from *
  • 831 MWe.
  • 831 820 MWe to
2. MAX. DEPENDABLE CAPACITY (Net MWe): * * * * * * * * * * * * * * ** *
  • THIS MONTH YEAR TO DATE CUMULATIVE 719.0 2879.0 126686.0 3a. HOURS IN REPORTING PERIOD:

719.0 2319.6 103674.1

3. NO. OF RRS. REACTOR WAS CRITICAL:

701.1 2287.8 102980.4

4. SERVICE HOURS GENERATOR ON LINE:

0.0 0.0 0.0

5. UNIT RESERVE SHUTDOWN HOURS:

577393.0 1789764.0 80367856.0

6. NET ELECTRICAL ENERGY GEN. (MWH):

1891744.0 84966487.0 (MWH): 608248.0

7. GROSS ELECT. ENERGY GEN.

1842917.0 5727455.0 259135036.0

8. GROSS THERMAL ENERGY GEN. (MWH):

79.5 81.3 97.5

9. UNIT AVAILABILITY FACTOR (%):

74.8 76.9 96.6

10. UNIT CAPACITY FACTOR (MDC) (M):

0.8 10.3 (M): 2.5

11. UNIT FORCED OUTAGE RATE

Text

FENOC Beaver Valley Power Station P. 0. Box 4 Shippingport,PA 15077 L-02-056 May 7, 2002 Beaver Valley Power Station Unit 1 - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 Monthly Operating Report U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

In accordance with NRC Generic Letter 97-02, "Revised Contents of the Monthly Operating Operating Report", and Unit 1 and 2 Technical Specification 6.9.4, the "Monthly Report" is submitted for Unit 1 and Unit 2 for the month of April 2002.

Respectfully, W. Pearce Acting Site Vice-President DTJ/caj Enclosures cc: NRC Regional Office King of Prussia, PA "U, q)

UNIT SHUTDOWNS DOCKET NO. 50-334 UNIT NAME BVPS Unit #1 DATE May 2,2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD: April 2002 No. Date Type Duration Reason Method of Cause / Corrective Actions (YIM/D) F: Forced (Hours) (1) Shutting S: Scheduled Down (2) Comments NONE.

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip / Scram C - Refueling 3 - Automatic Trip I Scram D - Regulatory Restriction 4- Continuation E - Operator Training / License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

done in The Unit began the report period operating at approximately 95% output. This was being Feedwater Pump order to maintain reduced loading on the outboard motor bearings of the "A" Main until a planned power reduction to replace the motor bearings could be started on 4/2/02. Outboard 4/2/02, motor bearing temperatures had been running higher in the previous month. At 0052 hours6.018519e-4 days <br />0.0144 hours <br />8.597884e-5 weeks <br />1.9786e-5 months <br /> on the Unit began a power reduction to approximately 63% output in order to replace the motor bearings on on the "A" Main Feedwater Pump. An output of approximately 63% was achieved at 0353 hours0.00409 days <br />0.0981 hours <br />5.83664e-4 weeks <br />1.343165e-4 months <br /> during this 4/2/02. Cleaning of the "C" and "D" Main Unit Condenser Waterboxes was also performed 0446 planned reduction. Upon completion of repairs, the Unit commenced a return to full power at hours on 4/5/02. A nominal value of 100% output was achieved at 1100 hours on 4/5/02.

when a The Unit continued to operate at a nominal value of 100% output until 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br /> on 4/12/02 to clean the "A" and "B" planned power reduction to approximately 90% output was begun in order on Main Unit Condenser Waterboxes. An output of approximately 90% was achieved at 2215 hours0.0256 days <br />0.615 hours <br />0.00366 weeks <br />8.428075e-4 months <br /> vacuum 4/12/02. However, with the "A" Condenser Waterbox isolated and degrading Condenser incremental load reductions between 0750 conditions indicated, the Unit performed several unplanned and 1247 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.744835e-4 months <br /> on 4/13/02 as a conservative action based on available Condenser vacuum operating at indications, until the "A" Condenser Waterbox was returned to service. With the Unit hours on approximately 80% output, a return to approximately 90% output was commenced at 1532 "B"

4/13/02. An output of approximately 90% was achieved at 1656 hours0.0192 days <br />0.46 hours <br />0.00274 weeks <br />6.30108e-4 months <br /> on 4/13/02. The any degrading Condenser Condenser Waterbox was removed from service and cleaned without full power.

vacuum conditions occurring. At 1331 hours0.0154 days <br />0.37 hours <br />0.0022 weeks <br />5.064455e-4 months <br /> on 4/14/02, the Unit commenced a return to to A nominal value of 100% output was achieved at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on 4/14/02. The Unit continued operate at a nominal value of 100% output for the remainder of the report period.

OPERATING DATA REPORT DOCKET NO.: 50-334 UNIT NAME: BVPS UNIT #1 REPORT DATE: 05/02/02 COMPLETED BY: DAVID T. JONES TELEPHONE: (724) 682-4962

  • Notes: Rated thermal power at
  • la. REPORTING PERIOD: APRIL 2002
  • BVPS-1 was uprated from 2652 MWt*

to 2689 MWt on 10/20/01. Net *

1. DESIGN ELECTRICAL RATING (Net MWe): 835
  • uprated from
  • 810 MWe to 821 MWe.
  • 821
2. MAX. DEPENDABLE CAPACITY (Net MWe): * * * * * * * * ** * * * * * * *
  • THIS MONTH YEAR TO DATE CUMULATIVE 719.0 2879.0 227903.0 3a. HOURS IN REPORTING PERIOD:

2879.0 154960.5 719.0

3. NO. OF ERS. REACTOR WAS CRITICAL:

2879.0 152500.9 719.0

4. SERVICE HOURS GENERATOR ON LINE:

0.0 0.0 0.0

5. UNIT RESERVE SHUTDOWN HOURS:

2367910.0 114034053.0 567550.0

6. NET ELECTRICAL ENERGY GEN. (MWH):

601370.0 2505980.0 121772766.0

7. GROSS ELECT. ENERGY GEN. (MWH):

7619403.0 375254208.5 (KWH): 1837779.0

8. GROSS THERMAL ENERGY GEN.

100.0 68.4 100.0

9. UNIT AVAILABILITY FACTOR (M):

100.2 63.7 96.1

10. UNIT CAPACITY FACTOR (MDC) (M):

0.0 16.2 0.0

11. UNIT FORCED OUTAGE RATE (M):

UNIT SHUTDOWNS DOCKET NO. 50-412 UNIT NAME BVPS Unit #2 DATE May 2, 2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD: April 2002 No. Date Type Duration Reason Method of Cause / Corrective Actions (Y/M/D) F: Forced (Hours) (1) Shutting S: Scheduled Down (2) Comments 3 020405 F 17.9 A I The Unit was shut down to Mode 2 (Reactor remained critical) due to degraded chemistry conditions in the Steam Generators caused by a tube leak in the *C"Waterbox of the Main Unit Condenser. The tube leak was repaired, and once chemistry conditions in the Steam Generators improved, the Unit was returned to full power.

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip Scram C - Refueling 3 - Automatic Trip I Scram D - Regulatory Restriction 4 - Continuation E - Operator Training t License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other (Explain)

SUMMARY

The Unit began the report period operating at a nominal value of 100% output until 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on 4/4/02 when a planned power reduction to approximately 90% output was begun in order to remove the "C" Main Unit Condenser Waterbox from service for cleaning. An output of approximately 90%

was achieved at 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> on 4/4/02. With the "C" Condenser Waterbox isolated, the Unit commenced to return to full power at 0358 hours0.00414 days <br />0.0994 hours <br />5.919312e-4 weeks <br />1.36219e-4 months <br /> on 4/4/02. A nominal value of 100% output was achieved at 0455 hours0.00527 days <br />0.126 hours <br />7.523148e-4 weeks <br />1.731275e-4 months <br /> on 4/4/02.

The Unit continued to operate at a nominal value of 100% output until 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on 4/5/02 when a planned power reduction to approximately 90% output was begun in order to remove the "B" Main Unit Condenser Waterbox from service for cleaning. An output of approximately 90% was achieved at 0150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br /> on 4/5/02. With the "B" Condenser Waterbox isolated, the Unit commenced a return to full power at 0236 hours0.00273 days <br />0.0656 hours <br />3.902116e-4 weeks <br />8.9798e-5 months <br /> on 4/5/02. A nominal value of 100% output was achieved at 0347 hours0.00402 days <br />0.0964 hours <br />5.737434e-4 weeks <br />1.320335e-4 months <br /> on 4/5/02.

However, with degrading chemistry conditions occurring in the Steam Generators, an unplanned power reduction to approximately 90% output was begun at 0623 hours0.00721 days <br />0.173 hours <br />0.00103 weeks <br />2.370515e-4 months <br /> on 4/5/02 in order to investigate a potential tube leak in the "C"Waterbox of the Main Unit Condenser. At 0758 hours0.00877 days <br />0.211 hours <br />0.00125 weeks <br />2.88419e-4 months <br /> on 4/5/02, the Unit commenced a shut down due to degraded chemistry conditions in the Steam Generators. The Unit was taken off-line at 1424 hours0.0165 days <br />0.396 hours <br />0.00235 weeks <br />5.41832e-4 months <br /> on 4/5/02 and entered Mode 2 at 1443 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.490615e-4 months <br /> on 4/5/02 with the Reactor remaining critical. Once the tube leak in the "C" Condenser Waterbox was

UNIT SHUTDOWNS DOCKET NO. 50-412 UNIT NAME BVPS Unit #2 DATE May 2, 2002 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD: April 2002

SUMMARY

(continued):

repaired and chemistry conditions in the Steam Generators improved, the Unit commenced to startup, 0817 entering Mode I at 0603 hours0.00698 days <br />0.168 hours <br />9.970238e-4 weeks <br />2.294415e-4 months <br /> on 4/6/02. The Unit was synchronized to the electrical grid at full power. A nominal value of 100% output was hours on 4/6/02 and commenced to return to achieved at 2400 hours0.0278 days <br />0.667 hours <br />0.00397 weeks <br />9.132e-4 months <br /> on 4/6/02.

The Unit continued to operate at a nominal value of 100% output until 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> on 4/20/02 when a Unit planned power reduction to approximately 75% output was begun in order to clean the "B" Main Condenser Waterbox. An output of approximately 75% was achieved at 0017 hours on 4/21/02.

Upon completion of cleaning the "B" Condenser Waterbox, the Unit commenced to return to full power at 1650 hours0.0191 days <br />0.458 hours <br />0.00273 weeks <br />6.27825e-4 months <br /> on 4/21/02. A nominal value of 100% output was achieved at 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br /> on 4/21/02.

The Unit continued to operate at a nominal value of 100% output for the remainder of the report period.

OPERATING DATA REPORT DOCKET NO.: 50-412 UNIT NAME: BVPS UNIT #2 REPORT DATE: 05/02/02 COMPLETED BY: DAVID T. JONES TELEPHONE: (724) 682-4962 Notes: Rated thermal power at

  • la. REPORTING PERIOD: APRIL 2002
  • BVPS-2 was uprated from 2652 MWt*
  • to 2689 Mwt on 10/30/01. Net *
1. DESIGN ELECTRICAL RATING (Net MWe): 836
  • m)C was also uprated from *
  • 831 MWe.
  • 831 820 MWe to
2. MAX. DEPENDABLE CAPACITY (Net MWe): * * * * * * * * * * * * * * ** *
  • THIS MONTH YEAR TO DATE CUMULATIVE 719.0 2879.0 126686.0 3a. HOURS IN REPORTING PERIOD:

719.0 2319.6 103674.1

3. NO. OF RRS. REACTOR WAS CRITICAL:

701.1 2287.8 102980.4

4. SERVICE HOURS GENERATOR ON LINE:

0.0 0.0 0.0

5. UNIT RESERVE SHUTDOWN HOURS:

577393.0 1789764.0 80367856.0

6. NET ELECTRICAL ENERGY GEN. (MWH):

1891744.0 84966487.0 (MWH): 608248.0

7. GROSS ELECT. ENERGY GEN.

1842917.0 5727455.0 259135036.0

8. GROSS THERMAL ENERGY GEN. (MWH):

79.5 81.3 97.5

9. UNIT AVAILABILITY FACTOR (%):

74.8 76.9 96.6

10. UNIT CAPACITY FACTOR (MDC) (M):

0.8 10.3 (M): 2.5

11. UNIT FORCED OUTAGE RATE