Information Notice 2008-13, Main Feedwater System Issues and Related 2007 Reactor Trip Data

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Main Feedwater System Issues and Related 2007 Reactor Trip Data
ML080880115
Person / Time
Site: Perry 
Issue date: 07/30/2008
From: Michael Case
NRC/NRR/ADRA/DPR
To:
King Mark, DIRS/IOEB, 301-415-1150
References
IN-08-013
Download: ML080880115 (5)


ML080880115 UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, DC 20555-0001

July 30, 2008

NRC INFORMATION NOTICE 2008-13:

MAIN FEEDWATER SYSTEM ISSUES AND

RELATED 2007 REACTOR TRIP DATA

ADDRESSEES

All holders of operating licenses for nuclear power reactors, except those who have

permanently ceased operations and who have certified that fuel has been permanently removed

from the reactor vessel.

PURPOSE

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform

addressees of a reactor trip event involving a loss of the main feedwater (FW) system that

occurred at Perry Nuclear Power Plant, Unit 1. This IN also discusses the NRC review of

reactor trip data for 2007, which showed that FW system issues caused an unusually high

proportion of reactor trips. The NRC expects that recipients will review the information for

applicability to their facilities and consider actions, as appropriate, to avoid similar problems.

Suggestions contained in this IN are not NRC requirements; therefore, no specific action or

written response is required.

DESCRIPTION OF CIRCUMSTANCES

Perry Nuclear Power Plant, Unit 1

On November 28, 2007, an unplanned automatic reactor trip occurred at Perry, a boiling-water

reactor (BWR), in response to a turbine control valve fast closure signal caused by failure of the

digital FW control system (DFWCS). Recovery from the reactor trip was complicated because

several means of supplying water to the reactor vessel were lost, including both of the turbine- driven FW pumps, the motor-driven FW pump, and the reactor core isolation cooling (RCIC)

pump. Reactor vessel water level was maintained using the high pressure core spray (HPCS)

system by cycling the HPCS injection valve. The HPCS system injected water to the reactor

vessel nine times over the next 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.

Both turbine-driven FW pumps tripped because of DFWCS power supply failures. Operator

attempts to recover one of these pumps were unsuccessful. The motor-driven FW pump, which

was in standby readiness, did not start because of DFWCS failures. Operators attempted to

start the motor-driven FW pump and use it to control reactor vessel water level but the minimum

flow valve could not be verified as opened because of the loss of the DFWCS power supplies. As the reactor vessel water level decreased, the RCIC pump automatically started but tripped

after 13 seconds on low RCIC pump suction pressure. The RCIC system tripped again when an

operator manually started the RCIC pump and attempted to supply water to the reactor vessel

with the flow controller in automatic. Operators eventually recovered the RCIC system when

they started the pump with the flow controller in manual.

The licensee performed a root cause analysis of the reactor trip event. The failure analysis of

the DFWCS power supplies found that a transformer on the 24-volt direct current converter

board of both the primary and secondary power supplies contained a defect. The investigation

identified that on November 28, 2007, the primary power supply was in a degraded condition

and the secondary power supply was completely failed. This configuration resulted in erratic

performance of the input and output modules.

The licensee took the following corrective actions:

replaced the DFWCS power supplies with a newer model from the same manufacturer

and connected a voltage status alarm to the process alarm for DFWCS (although, the

load carrying capacity of the power supplies still cannot be directly monitored)

added an additional power supply, using a different model for diversity and defense-in- depth, to each redundant pair of power supplies in the DFWCS, and to the digital reactor

feedpump turbine speed control system

established preventive maintenance tasks for load testing and line regulation for the

DFWCS power supplies.

Before the event, the licensee had two precursor alarms pointing to possible problems with the

digital power supplies; however, no troubleshooting took place. Industry guidance and

operating experience suggest it is important to conduct timely investigation, troubleshooting and

analysis of power supply and communications alarms.

The failure of the RCIC system to start and run was the result of improper tuning of the flow

controller in January 2006, with the implementation of incorrect RCIC flow controller tuning

parameters. This error stemmed from a change in 1987 that removed the controller settings

from the configuration control process, since they were considered operational adjustments, without also changing the tuning procedure to specify adjustment limits. Insufficient procedural

guidance then resulted in subsequent flow controller adjustments outside of the ranges that

would support stable response on a system actuation.

Licensee corrective actions included revising the RCIC flow controller tuning procedure to

specify adjustment limits that appropriately consider vendor manual guidance, as well as

industry operating experience reports.

The Perry Nuclear Power Plant NRC Special Inspection Report 05000440/2007010, dated

January 25, 2008, contains additional information on this event. The inspection report is

available on the NRCs public website in the Agencywide Documents Access and Management

System (ADAMS) under Accession No. ML080280499. This event is also the subject of

Licensee Event Report (LER) 07-004-001, dated February 15, 2008 (ADAMS Accession No.

ML080530390). NRC Review of Reactor Trip Data for 2007

The NRC Operating Experience Branch reviewed the reactor trip data for 2007 and noted that

although the total number of reactor trips fleet wide was typical, the proportion of reactor trips

caused by the FW system (or the condensate system) in 2007 was 37 percent, which is higher

than the typical 10 to 25 percent. The FW system problems often involved (1) insufficient

preventive and corrective maintenance, and (2) instrumentation and control malfunctions, particularly associated with the FW regulating valves. The NRC staff has also noted several

instances where station knowledge of digital systems was lacking, which resulted in a high

reliance on vendors for engineering, equipment recommendations, troubleshooting and

maintenance.

Actions that licensees have taken to improve overall FW system performance and reduce

operator challenges caused by FW system transients and the related reactor scrams include the

following:

Benchmark similar plants and evaluate actions to address single-point vulnerabilities that

have resulted in scrams caused by the FW system

Develop or improve long-term strategies to anticipate and prevent FW equipment problems

caused by aging and obsolescence

Review and take corrective actions resulting from FW-related operating experience

Ensure that FW system design improvements and major corrective actions are completed as

scheduled to improve overall main FW system reliability

Ensure that main FW system digital modifications are fully understood and properly

implemented, and that operators are trained on the modified system and abnormal operating

procedures regarding FW system responses to failures

Ensure that operators are trained in the monitoring of important parameters such as power

supply voltage to provide for early identification and correction of problems.

When the main FW system is lost, licensees rely on other systems to provide feedwater such as

the RCIC system at BWRs and the auxiliary feedwater (AFW) system at pressurized-water

reactors (PWRs). Since the NRC implemented the revised Reactor Oversight Process in 2000,

NRC inspection reports have documented more than 500 findings involving the main FW, AFW,

or RCIC systems. More than half of these findings involved maintenance errors and/or

corrective action issues. These findings also show that the AFW pumps were the primary

contributor in 14 of 17 greater than green FW-related inspection findings at PWR plants.

BACKGROUND

NRC IN 2000-01, Operational Issues Identified in Boiling Water Reactor Trip and Transient

(ADAMS Accession Number ML003682692), discussed an event at Hatch Unit 1 that involved

an automatic reactor trip on low reactor water level after one of two main FW lines was isolated

when a valve unexpectedly closed in the FW flow path to the reactor.

DISCUSSION

This IN describes FW system performance issues and actions that licensees have taken to

improve overall FW system performance and reduce operator challenges caused by FW system

transients and the related reactor trips. The reactor trip event at Perry began with the failure of

power supplies in the DFWCS, a non-safety related control system. Although there are no

specific NRC requirements related to DFWCS, its failure led to a loss of main FW and revealed

that the RCIC system was inoperable which necessitated the use of the HPCS system to

restore and maintain the reactor vessel level.

The RCIC system at BWRs and the AFW system at PWRs are systems important to safety that

are designed to provide feedwater upon a loss of the main FW system. The AFW systems are

safety-related and required to be operable as described in technical specifications and are

subject to the NRC requirements for Quality Assurance Criteria for Nuclear Power Plants and

Fuel Reprocessing Plants, covered in Title 10 of the Code of Federal Regulations (10 CFR)

Part 50, Appendix B, which also includes corrective action requirements. While the main FW

system is generally non-safety related, it is scoped under the Maintenance Rule (10 CFR 50.65)

and a loss of main FW may be subject to NRC review under the reactive inspection process, event follow-up, or the Reactor Oversight Process performance indicator (PI) for Scrams or the

PI for Unplanned Scrams with Complications.

Reducing initiating events caused by the main FW systems and ensuring the availability and

operability of the mitigating systems for response to loss of FW events will help enhance overall

reactor safety.

CONTACT

S

This IN requires no specific action or written response. Please direct any questions about this

matter to the technical contacts listed below or the appropriate Office of Nuclear Reactor

Regulation (NRR) project manager.

/RA by MMaxin for/

Michael J. Case, Director

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Technical Contacts: Mark King, NRR/DIRS/IOEB

Geoffrey Wright, Region III, DRP

Operating Experience Branch

Perry Special Inspection Team Lead

301-415-1150

601-829-9602 E-mail: Mark.King@nrc.gov

E-mail: Geoffrey.Wright@nrc.gov

Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.

DISCUSSION

This IN describes FW system performance issues and actions that licensees have taken to

improve overall FW system performance and reduce operator challenges caused by FW system

transients and the related reactor trips. The reactor trip event at Perry began with the failure of

power supplies in the DFWCS, a non-safety related control system. Although there are no

specific NRC requirements related to DFWCS, its failure led to a loss of main FW and revealed

that the RCIC system was inoperable which necessitated the use of the HPCS system to

restore and maintain the reactor vessel level.

The RCIC system at BWRs and the AFW system at PWRs are systems important to safety that

are designed to provide feedwater upon a loss of the main FW system. The AFW systems are

safety-related and required to be operable as described in technical specifications and are

subject to the NRC requirements for Quality Assurance Criteria for Nuclear Power Plants and

Fuel Reprocessing Plants, covered in Title 10 of the Code of Federal Regulations (10 CFR)

Part 50, Appendix B, which also includes corrective action requirements. While the main FW

system is generally non-safety related, it is scoped under the Maintenance Rule (10 CFR 50.65)

and a loss of main FW may be subject to NRC review under the reactive inspection process, event follow-up, or the Reactor Oversight Process performance indicator (PI) for Scrams or the

PI for Unplanned Scrams with Complications.

Reducing initiating events caused by the main FW systems and ensuring the availability and

operability of the mitigating systems for response to loss of FW events will help enhance overall

reactor safety.

CONTACT

S

This IN requires no specific action or written response. Please direct any questions about this

matter to the technical contacts listed below or the appropriate Office of Nuclear Reactor

Regulation (NRR) project manager.

/RA by MMaxin for/

Michael J. Case, Director

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Technical Contacts: Mark King, NRR/DIRS/IOEB

Geoffrey Wright, Region III, DRP

Operating Experience Branch

Perry Special Inspection Team Lead

301-415-1150

601-829-9602 E-mail: Mark.King@nrc.gov

E-mail: Geoffrey.Wright@nrc.gov

Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.

DISTRIBUTION:

IN r/f

  • Concurred via email

ADAMS Accession Number: ML080880115 OFFICE

DIRS/IOEB

RIII/BRP*

Tech Editor*

TL/DIRS/IOEB

ABC/DIRS/IOEB

NAME

MKing

GWright

HChang

LFields

BWhite

DATE

07/15/08

07/16/08

05/27/08

07/24/08

07/24/08 OFFICE

NRR/DIRS

DPR/PGCB

DPR/PGCB

BC/PGCB

D/NRR/DPR

NAME

FBrown

DBeaulieu

CHawes

MMurphy

MCase

DATE

07/28/08

07/28/08

07/29/08

07/30/08

07/30/08 OFFICIAL RECORD COPY