Information Notice 2008-13, Main Feedwater System Issues and Related 2007 Reactor Trip Data
| ML080880115 | |
| Person / Time | |
|---|---|
| Site: | Perry |
| Issue date: | 07/30/2008 |
| From: | Michael Case NRC/NRR/ADRA/DPR |
| To: | |
| King Mark, DIRS/IOEB, 301-415-1150 | |
| References | |
| IN-08-013 | |
| Download: ML080880115 (5) | |
ML080880115 UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, DC 20555-0001
July 30, 2008
NRC INFORMATION NOTICE 2008-13:
MAIN FEEDWATER SYSTEM ISSUES AND
RELATED 2007 REACTOR TRIP DATA
ADDRESSEES
All holders of operating licenses for nuclear power reactors, except those who have
permanently ceased operations and who have certified that fuel has been permanently removed
from the reactor vessel.
PURPOSE
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform
addressees of a reactor trip event involving a loss of the main feedwater (FW) system that
occurred at Perry Nuclear Power Plant, Unit 1. This IN also discusses the NRC review of
reactor trip data for 2007, which showed that FW system issues caused an unusually high
proportion of reactor trips. The NRC expects that recipients will review the information for
applicability to their facilities and consider actions, as appropriate, to avoid similar problems.
Suggestions contained in this IN are not NRC requirements; therefore, no specific action or
written response is required.
DESCRIPTION OF CIRCUMSTANCES
Perry Nuclear Power Plant, Unit 1
On November 28, 2007, an unplanned automatic reactor trip occurred at Perry, a boiling-water
reactor (BWR), in response to a turbine control valve fast closure signal caused by failure of the
digital FW control system (DFWCS). Recovery from the reactor trip was complicated because
several means of supplying water to the reactor vessel were lost, including both of the turbine- driven FW pumps, the motor-driven FW pump, and the reactor core isolation cooling (RCIC)
pump. Reactor vessel water level was maintained using the high pressure core spray (HPCS)
system by cycling the HPCS injection valve. The HPCS system injected water to the reactor
vessel nine times over the next 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
Both turbine-driven FW pumps tripped because of DFWCS power supply failures. Operator
attempts to recover one of these pumps were unsuccessful. The motor-driven FW pump, which
was in standby readiness, did not start because of DFWCS failures. Operators attempted to
start the motor-driven FW pump and use it to control reactor vessel water level but the minimum
flow valve could not be verified as opened because of the loss of the DFWCS power supplies. As the reactor vessel water level decreased, the RCIC pump automatically started but tripped
after 13 seconds on low RCIC pump suction pressure. The RCIC system tripped again when an
operator manually started the RCIC pump and attempted to supply water to the reactor vessel
with the flow controller in automatic. Operators eventually recovered the RCIC system when
they started the pump with the flow controller in manual.
The licensee performed a root cause analysis of the reactor trip event. The failure analysis of
the DFWCS power supplies found that a transformer on the 24-volt direct current converter
board of both the primary and secondary power supplies contained a defect. The investigation
identified that on November 28, 2007, the primary power supply was in a degraded condition
and the secondary power supply was completely failed. This configuration resulted in erratic
performance of the input and output modules.
The licensee took the following corrective actions:
replaced the DFWCS power supplies with a newer model from the same manufacturer
and connected a voltage status alarm to the process alarm for DFWCS (although, the
load carrying capacity of the power supplies still cannot be directly monitored)
added an additional power supply, using a different model for diversity and defense-in- depth, to each redundant pair of power supplies in the DFWCS, and to the digital reactor
feedpump turbine speed control system
established preventive maintenance tasks for load testing and line regulation for the
DFWCS power supplies.
Before the event, the licensee had two precursor alarms pointing to possible problems with the
digital power supplies; however, no troubleshooting took place. Industry guidance and
operating experience suggest it is important to conduct timely investigation, troubleshooting and
analysis of power supply and communications alarms.
The failure of the RCIC system to start and run was the result of improper tuning of the flow
controller in January 2006, with the implementation of incorrect RCIC flow controller tuning
parameters. This error stemmed from a change in 1987 that removed the controller settings
from the configuration control process, since they were considered operational adjustments, without also changing the tuning procedure to specify adjustment limits. Insufficient procedural
guidance then resulted in subsequent flow controller adjustments outside of the ranges that
would support stable response on a system actuation.
Licensee corrective actions included revising the RCIC flow controller tuning procedure to
specify adjustment limits that appropriately consider vendor manual guidance, as well as
industry operating experience reports.
The Perry Nuclear Power Plant NRC Special Inspection Report 05000440/2007010, dated
January 25, 2008, contains additional information on this event. The inspection report is
available on the NRCs public website in the Agencywide Documents Access and Management
System (ADAMS) under Accession No. ML080280499. This event is also the subject of
Licensee Event Report (LER) 07-004-001, dated February 15, 2008 (ADAMS Accession No.
ML080530390). NRC Review of Reactor Trip Data for 2007
The NRC Operating Experience Branch reviewed the reactor trip data for 2007 and noted that
although the total number of reactor trips fleet wide was typical, the proportion of reactor trips
caused by the FW system (or the condensate system) in 2007 was 37 percent, which is higher
than the typical 10 to 25 percent. The FW system problems often involved (1) insufficient
preventive and corrective maintenance, and (2) instrumentation and control malfunctions, particularly associated with the FW regulating valves. The NRC staff has also noted several
instances where station knowledge of digital systems was lacking, which resulted in a high
reliance on vendors for engineering, equipment recommendations, troubleshooting and
maintenance.
Actions that licensees have taken to improve overall FW system performance and reduce
operator challenges caused by FW system transients and the related reactor scrams include the
following:
Benchmark similar plants and evaluate actions to address single-point vulnerabilities that
have resulted in scrams caused by the FW system
Develop or improve long-term strategies to anticipate and prevent FW equipment problems
caused by aging and obsolescence
Review and take corrective actions resulting from FW-related operating experience
Ensure that FW system design improvements and major corrective actions are completed as
scheduled to improve overall main FW system reliability
Ensure that main FW system digital modifications are fully understood and properly
implemented, and that operators are trained on the modified system and abnormal operating
procedures regarding FW system responses to failures
Ensure that operators are trained in the monitoring of important parameters such as power
supply voltage to provide for early identification and correction of problems.
When the main FW system is lost, licensees rely on other systems to provide feedwater such as
the RCIC system at BWRs and the auxiliary feedwater (AFW) system at pressurized-water
reactors (PWRs). Since the NRC implemented the revised Reactor Oversight Process in 2000,
NRC inspection reports have documented more than 500 findings involving the main FW, AFW,
or RCIC systems. More than half of these findings involved maintenance errors and/or
corrective action issues. These findings also show that the AFW pumps were the primary
contributor in 14 of 17 greater than green FW-related inspection findings at PWR plants.
BACKGROUND
NRC IN 2000-01, Operational Issues Identified in Boiling Water Reactor Trip and Transient
(ADAMS Accession Number ML003682692), discussed an event at Hatch Unit 1 that involved
an automatic reactor trip on low reactor water level after one of two main FW lines was isolated
when a valve unexpectedly closed in the FW flow path to the reactor.
DISCUSSION
This IN describes FW system performance issues and actions that licensees have taken to
improve overall FW system performance and reduce operator challenges caused by FW system
transients and the related reactor trips. The reactor trip event at Perry began with the failure of
power supplies in the DFWCS, a non-safety related control system. Although there are no
specific NRC requirements related to DFWCS, its failure led to a loss of main FW and revealed
that the RCIC system was inoperable which necessitated the use of the HPCS system to
restore and maintain the reactor vessel level.
The RCIC system at BWRs and the AFW system at PWRs are systems important to safety that
are designed to provide feedwater upon a loss of the main FW system. The AFW systems are
safety-related and required to be operable as described in technical specifications and are
subject to the NRC requirements for Quality Assurance Criteria for Nuclear Power Plants and
Fuel Reprocessing Plants, covered in Title 10 of the Code of Federal Regulations (10 CFR)
Part 50, Appendix B, which also includes corrective action requirements. While the main FW
system is generally non-safety related, it is scoped under the Maintenance Rule (10 CFR 50.65)
and a loss of main FW may be subject to NRC review under the reactive inspection process, event follow-up, or the Reactor Oversight Process performance indicator (PI) for Scrams or the
PI for Unplanned Scrams with Complications.
Reducing initiating events caused by the main FW systems and ensuring the availability and
operability of the mitigating systems for response to loss of FW events will help enhance overall
reactor safety.
CONTACT
S
This IN requires no specific action or written response. Please direct any questions about this
matter to the technical contacts listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
/RA by MMaxin for/
Michael J. Case, Director
Division of Policy and Rulemaking
Office of Nuclear Reactor Regulation
Technical Contacts: Mark King, NRR/DIRS/IOEB
Geoffrey Wright, Region III, DRP
Operating Experience Branch
Perry Special Inspection Team Lead
301-415-1150
601-829-9602 E-mail: Mark.King@nrc.gov
E-mail: Geoffrey.Wright@nrc.gov
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.
DISCUSSION
This IN describes FW system performance issues and actions that licensees have taken to
improve overall FW system performance and reduce operator challenges caused by FW system
transients and the related reactor trips. The reactor trip event at Perry began with the failure of
power supplies in the DFWCS, a non-safety related control system. Although there are no
specific NRC requirements related to DFWCS, its failure led to a loss of main FW and revealed
that the RCIC system was inoperable which necessitated the use of the HPCS system to
restore and maintain the reactor vessel level.
The RCIC system at BWRs and the AFW system at PWRs are systems important to safety that
are designed to provide feedwater upon a loss of the main FW system. The AFW systems are
safety-related and required to be operable as described in technical specifications and are
subject to the NRC requirements for Quality Assurance Criteria for Nuclear Power Plants and
Fuel Reprocessing Plants, covered in Title 10 of the Code of Federal Regulations (10 CFR)
Part 50, Appendix B, which also includes corrective action requirements. While the main FW
system is generally non-safety related, it is scoped under the Maintenance Rule (10 CFR 50.65)
and a loss of main FW may be subject to NRC review under the reactive inspection process, event follow-up, or the Reactor Oversight Process performance indicator (PI) for Scrams or the
PI for Unplanned Scrams with Complications.
Reducing initiating events caused by the main FW systems and ensuring the availability and
operability of the mitigating systems for response to loss of FW events will help enhance overall
reactor safety.
CONTACT
S
This IN requires no specific action or written response. Please direct any questions about this
matter to the technical contacts listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) project manager.
/RA by MMaxin for/
Michael J. Case, Director
Division of Policy and Rulemaking
Office of Nuclear Reactor Regulation
Technical Contacts: Mark King, NRR/DIRS/IOEB
Geoffrey Wright, Region III, DRP
Operating Experience Branch
Perry Special Inspection Team Lead
301-415-1150
601-829-9602 E-mail: Mark.King@nrc.gov
E-mail: Geoffrey.Wright@nrc.gov
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.
DISTRIBUTION:
IN r/f
- Concurred via email
ADAMS Accession Number: ML080880115 OFFICE
DIRS/IOEB
RIII/BRP*
Tech Editor*
TL/DIRS/IOEB
ABC/DIRS/IOEB
NAME
MKing
GWright
HChang
LFields
BWhite
DATE
07/15/08
07/16/08
05/27/08
07/24/08
07/24/08 OFFICE
NRR/DIRS
DPR/PGCB
DPR/PGCB
BC/PGCB
D/NRR/DPR
NAME
FBrown
DBeaulieu
CHawes
MMurphy
MCase
DATE
07/28/08
07/28/08
07/29/08
07/30/08
07/30/08 OFFICIAL RECORD COPY