IR 05000498/1990004
| ML20006F592 | |
| Person / Time | |
|---|---|
| Site: | South Texas |
| Issue date: | 02/16/1990 |
| From: | Holler E NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML20006F590 | List: |
| References | |
| 50-498-90-04, 50-498-90-4, 50-499-90-04, 50-499-90-4, NUDOCS 9002280211 | |
| Download: ML20006F592 (12) | |
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APPENDIX-U.S. NUCLEAR REGULATORY COMMISSION l
REGION'IV NRC Inspection Report:
50-498/90-04 Operating License: NPF-76-50-499/90-04 NPF-80-i Dockets: 50-498 50-499 t
Licensee: Houston Lighting & Power Company (HL&P)
i P.O. Box 1700 a
Houston, Texas 77251
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Facility Name:- South Texas Project (STP), Units 1 and.2
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Inspection At: STP, Matagorda County, Texas -
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Inspection Conducted: January 1-31, 1990 Inspectors:
J. I. Tapia, Senior Resident-Inspector, Project"Section D Division of Reactor Projects R. J. Evans, Resident Inspector, Project Section'D
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Division of Reactor Projects l
Approved:
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J.' Holler, Chief, Project Section D cDate l
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Division of Reactor Projects
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Inspection Summary
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Inspection Conducted January 1-21, 1990 (Report 50-498/90-04; 50-499/90-04)-
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Areas Inspected:
Routine, unannounced inspection included ~ plant-status, operational safety verification, monthly maintenance and surveillance
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observations, complex surveillance observation, and initial licensee fitness-for-duty training.
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Results: Within the areas inspected, one noncited violation was' identified
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regard 1ng documentation of approved flammable liquid storage cabinets in vital areas of the plant (paragraph 4).
In general, an improvement in housekeeping from that seen in past inspections ~was observed throughout the a
plant (paragraphs 4 5, 6, and 7).
Inspection of a complex surveillance.
indicated compliance to approved procedures by technicians who< appeared-to be knowledgeable and competent (paragraph 7).
The licensee's continual behavior
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= observation program training for supervisors appeared to meet the. requirements of 10 CFR Part 26 (paragraph 8).
)p, 9002280211 900220 DR ADOCK 0500
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DETAILS
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1.
Persons Contacted
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- G. E. Vaughn, Vice President. Operations
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- W. H. Kinsey, Plant Manager
- W. L. Mutz, Manager, Operations Strategic Planning
' *M. R. Wisenburg, General Manager, Nuclear Safety Review Board
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- R. W. Chewning Vice President. Nuclear Assurance l
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- D. J. Denver, Manager, Nuclear Engineer.
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- A.- R. Mikus General Supervisor, Construction
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- A. W. Hamson, Supervisor, Licensing Engineer I
- C. A. Ayala, Supervisor, Licensing Engineer i
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' *W. A. Randlett, Security Manager i
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- J. A. Slabinski, Quality Engineer Supervisor / Nuclear Assurance
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- S. M. Dew, Manager, Nuclear Purchasing Material Management
- W. J. Jump, Maintenance Manager i
- A. C. McIntyre. Manager Support Engineering
- J. R. Lovell. Technical Services Manager i
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- J.
n. Loesch, Plant Operations Manager
- K. J. Christian.. Unit 1 Operations Manager e
- L. Giles Unit 2 Operations Manager
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- D. A. Leazar, Reactor Support Manager
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- A. K. Khosla, Senior Licensing Engineer licensee, architect engineer (AE)pectors also held discussion with various In addition to the above, the ins
, maintenance, and other contractar personnel during this inspection.
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- Denotes those individuals attending the exit interview conducted on-
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February 1,1990.
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2.
Plant Status
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Unit 1 began this inspection period at 100 percent reactor thennal power.
On January 3,1990, a Technical Specification (TS) required plant shutdown was initiated when a feedwater isolation valve failed its surveillance'
t requirements and was declared inoperable.. Reactor power was reduced to l
6 percent, the TS action statement exited, and the valve repaired.
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e level was increased to 100 percent reactor thermal power on January 8,
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1990. Unit I remained at 100 percent reactor, thennal power level through t
the end of the inspection period.
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Unit 2 began this inspection period in Mode 5 (cold shutdown) as a result i
of the inoperable No. 22 emergency diesel generator which failed on November 28, 1989. On January 6, 1990, No. 22 emergency diesel generator
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was declared operable and engineered safety features (ESF) loop tests were
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commenced. On January 8,1990, an inadvertent safety injection (SI);
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. occurred during the performance of a logic train functional test. On January 13,1990, Unit 2 entered Mode 3 and on January 15, 1990, the unit l
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'h was taken critical.
Unit 2 reached 100 percent reactor thermal power on-J January 22, 1990, and remained ct that power level through the close of
this inspection period.
3.
Onsite Followup of Events at Operating Power Reactors (93702)
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On January 3,1990, an operability (test was performed on the Unit 1FWIV)tosatisfy Train C feedwater isolation valve FWIVs are 18-inch, hydraulically opened, nitrogen assisted shut, gate
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valves.
Each valve has two associated solenoid valves in parallel which, upon receipt of an ESF A or B signal, dump hydraulic fluid to allow
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nitrogen to stroke the valve to the closed position. Each valve also has an associated pump module which consistr, of electric and air-driven pumps and a fluid reservoir.
This pump module maintains proper hydraulic system
pressure to open and close the valve as needed, t
The acceptance criteria for the feedwater system valve operability test
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includes the requirement that each of two safety-related FWIV solenoid valves associated with each ESF train change state when the solenoid i
valves receive actuation signals from redundant trains of the ESF actuation system. The FWIV stroked as required, but one of the two solenoid valves failed to actuate. Therefore, the acceptance criteria for the C train FWIV could not be met, the FWIV was declared inoperable, and TS 3.6.3 was entered. TS 3.6.3 requires the affected containment penetration to be
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isolated when one or more isolation valves are inoperable.
Because the FWIVs are the only containment isolation valves in the main feedwater line
and C train FWIV could not be shut because of forward feeding of the steam generators, the action statement of TS 3.6.3 could not be met and TS 3.0.3
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was entered. A notification of unusual event (NOVE) was declared at i
5:10 p.m. because of the TS-required shutdown and shutdown of Unit I was commenced. At 10:34 p.m., with the unit in Mode 2, C train FWIV was.
closed, the TS action statement exited, and the NOVE terminated. The plant remained in Mode 2 pending repair of the solenoid valve.- The
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solenoid valves for the C train FWIV were removed and the internals of all
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four solenoid valves were found to be covered with particulate contamination. This particulate contamination was subsequently determined to be dirt and corrosion products. Based on the findings with the C train FWIV solenoids, the licensee made the decision to rework all 16 FWIV solenoid valves. The hydraulic fluid for each FWIV was either filtered or changed to remove particulates in the system.
Additionally, a program to
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periodically sample and analyze the hydraulic fluid was initiated. The analysis results are to be used to initiate maintenance activities when
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the properties of the samples indicate hydraulic system degradation.
Functional testing of the FWIVs was completed on January 9,1990, and Unit I was returned to service.
On January 8,1990, with Unit 2 in Mode 5, an inadvertent SI occurred
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during the performance of the solid state protection system (SSPS) Logic-
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Train R function test.
An operator trainee was assisting in perfonning the functional test under the direct observation of a licensed operator.
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The test requires actuation of various Train R and Train S manual block l
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switches to the block position. The trainee placed the low steamline pressure handswitch for Train S to the block position and then released it. The spring return action of the handswitch caused the handswitch to i
pass through the neutral position back to the unblock position. This resulted in a low steam line pressure SI. All equipment that was not in
pull-to-lock operated as designed. No injection of water into the reactor coolant system occurred because all the SI pumps were in pull-to-lock as
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allowed for Mode S operation. The SI signal was reset and components were i
restored to normal.
Subsequent investigation determined that the operator trainee was unaware
that a quick release of the handswitch could result in the switch
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j traveling past the center position and cause a reverse actuation. The licensee issued a memorandum to all plant operations personnel discussing-i the event and emphasizing the use of positive control when manipulating
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spring return type switches. Additionally, the nuclear training
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department will modify its programs to include training in the proper operation of spring return switches prior to any on-the-job training and will include this incident in lessons-learned training for requalification.
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No violations or deviations were identified in this area of the
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inspection.
The licensee's actions appeared appropriate for the events
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encountered.
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4.
Operational Safety Verification (71707)
The purpose of this inspection was to ensure that the facility was being operated safely and in conformance with license and regulatory requirements. This inspection also included verifying that selected activities of the licensee's radiological protection program were being implemented in conformance with requirements and procedures, and that the licensee was in compliance with its approved physical security plan.
The inspectors visited the control rooms on a routine basis when onsite and verified that control room staffing, operator decorum, shift turnover,
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adherence to TS limiting conditions of operations (LCOs), and overall control room decorum were in accordance with requirements. The inspectors conducted tours in various locations of the plant to observe work and operations and to ensure that the facility was being operated safely and i
in conformance with license and regulatory requirements.
The essential chilled water systems (CH) were inspected to verify the operability and status of the systems.
Both the Unit 1. Train C, and i
Unit 2. Train B, subsystems were inspected. The inspection included
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comparison of as-found control switch, power supply breaker, and valve i
positions to positions required by the operating A-comparison of the operating) procedures to design documents (pro t
p1 ping and instrument
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diegrams (P& ids) was also performed. The procedures reviewed and walked _
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j down included:
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POP 02-CH-0001, " Essential Chilled Water System," Revision 7
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2 POP 02-CH-0001 " Essential Chilled Water System," Revision 3
Items noted during a technical review of the procedures included funless
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specifically noted, the items observed applied to both proceduresj:
i Step 2.3.3 listed Final Safety Analysis Report (FSAR), Section 9;4.5, i
as a procedure reference, but Section 9.4.5 (containment vent) had no-
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relationship to the procedures, j
Section 4.0, notes and precautions, did act include the essential
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chiller 30-minute start limitation.
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a The procedures used the same acronym "ECW" in different steps to
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refer to different systems, the essential chilled water, and essential cooling water systems.
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i Section 8.1 established the initial conditions needed to start an
essential chiller. The vendor manual wording indicated that a
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chiller status light check (such as control power available, system
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run, and oil pump status lights energized) was to be included as part
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of the chiller start instructions. The procedure did not perfonn
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these status light checks; however, the licensee previously detemined
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that status light checks were not necessary during chiller starts.
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Steps 8.1.9, 9.1.4, and 10.1.1.10 instructed operators to verify that
adequate flow existed to the chiller condensers. Step 8.1.9 referred i
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the operator to local-flow gauges. Step 9.1.4 referred the operator to local-flow status lights, and Step 10.1.1.10 referred the operator to both local lights and flow indicators. The procedure steps were
not consistent. The licensee stated the steps were to be revised.
Typographical errors were observed in Procedure IPOP02-CH-0001 which
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included:
(1) the word "chillerd was erroneously listed twice in i
Step 8.1.4;- (2) the essential chilled water checklist (-3) identified
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Valve 1-CH-0065 as a pressure switch and pressure indicator isolation
valve, but the valve was only a pressure irdicator isolation valve;
(3) the word " Train" was incorrectly spelled as." Trace" nine times in the checklist; (4) Valve 1-CH-0963 was listed twice in the' vent
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checklist; and (5) Vent Valves 1-CH-V1440 and 1-CH-V1511 were missing c
l from the vent checklist.
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Typographical errors were observed in Procedure 2 POP 02-CH-0001 which included:
(1) Valve 2-CH-948 was listed as an isolation valve in the.
valvechecklist(-2),butwasactually)adrainvalve;and(2)the required position LIP (Locked In Place was missi;.g from required position column for Valve 2-CH-0996.
Items observed during the walkdown of the system using the operating procedure and P& ids included:
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The wrong colored lens covers for two status ligbts were noted on
Essential Chiller 120. The low-water temperature light was found 'to be green colored but should have been red per the vendor manual drawings he motor space heater light was found red, but should have been The wrong colored lens covers for two status lights
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were also note.
Essential Chiller 22A. The excess purge light was found to be green but should have been red. The motor space heater light on Essential Chiller 22A was also red but should have been green.
- Differences between the system P& ids, Procedure IP0P02-CH-0001 wording, and installed Unit 1. Train C, chilled water components included:
(1) seven butterfly valves did not have designated positions (open, closed, locked) on the P& ids, (2) Valve 1-CH-1433 was a test connection valve that was listed as a drain on the P& ids, (3) Valve 1-CH-1529 was a sample valve that was listed as a drain on-the P&ID, (4) Valve 1-CH-1504 was a vent valve that had no designation (vent or drain) on the P&ID, and (5) the positions of six temperature instruments and vent valves were in slightly different locations in the plant than shown on the P& ids. There were no design change requests outstanding against any system P& ids.
- Differences between the system P& ids, Procedure 2 POP 02-CH-0001 wording, and installed Unit 2, Train B, chilled water components included:
(1) eight butterfly valves did not have designated positions (open, closed, locked) on the system P& ids; (2) Valves 1-CH-865 and 1-CH-866 were shown as normally closed vent valves on the P&ID and were identified as closed vent valves in the plant, but the valves were required to be open per the valve checklist (this revision of the procedure, Revision 3 had not been performed by operations personnel prior to the day of inspection);
(3) Vent Valve 2-CH-1500 was listed in the valve checklist but was not shown on the P&ID; (4) Vent Valves 2-CH-1690 and 2-CH-1691 and Drain Valve 2-CH-1693 were shcwn on the P&lD but were not listed in the valve checklist; and (5) the positions of four temperature indications and two vent valves were in slightly different locations in the plant than shown on the P& ids. There were no design change requests outstanding against any system P&ID.
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Other items observed during the walkdown included:
1) Temperature Instruments 1-CH-TI-9565 and 1-CH-TI-9565A (Train C)(were incorrectly taggedas1-CH-TI-9555and1-CH-TI-9555A(Train'A)intheplant; (2) the air line filter to 1-CH-TV-9496B had an air leak on a sealing surface (nomaintenanceworkrequesttagwasattached);(3)there were more vendor supplied instruments than were shown on the P& ids, including discharge temperature high, oil temperature high, and condenser water differential pressure; and (4)-the Unit 2 postaccident sampling system (PASS) coolcr air handling unit (AHU)
control switch was OFF. With the nonsafety-related PASS AHU off, the room temperature had increased about 10*F above desired temperature.
The switch to the PASS AHU should have been in AUTO per Procedure Checklist 2 POP 32-HF-0001-2, Revision 3.
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All valves, power supply breakers, and switch positions were noted to be in positions mquired to support plant operation.
Items noted by the inspector did not appear to directly impact safe operation of the plant.
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All observations were referred to the licensee for inclusion in the licensee's long-term program for procedure upgrade.
As part of the operational safety verification portion of the inspection, general housekeeping and potential fire hazards were inspected during q
nonroutine plant tours. This included the inspection of containers used
for storage of flamable liquids. Step 4.3.2 of Procedure OPGP03-ZF-0005,
i Revision 4. "Use of Fir.mmable Liquids and Gases " states that approved
storage areas shall be p(osted using a copy of the approved Storage of" Storage i
Liquids and Gases Form-1).
applicable liquids or gases in a location while not in actual use for-t
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8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or more.
The inspector found two flamable liquids storage cabinets in vital areas of the plant without the Storage of Liquids and Gases Form (-1) on or in j
the two cabinets. One cabinet was found inside the Unit 1, Room 067F i
(Essential Chiller Room C), and outside Unit 2. Room 067E (Essential
Chiller Room B). Both cabinets contained cans of pump or motor oil. The
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failure to follow approved plant procedures is a violation of TS 6.8.1.
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ThisviolationofTS(498/9004-01;499/9004-02) is not cited because it
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meets the criteria in Section V.A of the general statement of policy and procedure for NRC enforcement actions. The licensee was aware that the
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forms were missing, because representatives had removed the two forms.
The licensee intended to relocate the cabinets and had initiated paperwork l
to revise the two forms. However, the forms were not returned to the
cabinets in a timely manner. Long-term solutions considered by the i
licensee to prevent reccurrence included mvision of the fire hazards analysis report to allow a certain amount of combustibles and flammable
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liquids in the buildings. Procedures for weekly audits of combustibles'
and flammable liquids would then be performed to ensure the limits were
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maintained. This would then minimize administrative papemork needed to
keep individual cabinets in the vital areas of the plant.
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Oneviolation(noncited)andnodeviationswereidentifiedinthisareaof the inspection.
5.
Monthly Maintenance Observations (62703)
Selected maintenance activities were observed to verify whether the activities were being conducted in accordance with approved procedures.
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The Unit 2 activities observed include:
Preventive Maintenance (FH) EM-2-HF-87016764, Lubrication and
Inspection of Fuel Handling Building Exhaust Booster Fan 21B Motor Work Request (WR) NK-81572, Process Temperature Control
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Panel 9E282 ERR 0030 Calibration Check
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WR MS-88921, Replacement of Steam Generator 2C Pressure
Transmitter D2-MS-PT-0535
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The inspector verified that the activities were conducted in accordance with approved work instructions and procedures, test equipment was within
the current calibration cycles, and housekeeping was being maintained in
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an acceptable manner. All observations made were referred to the licensee for appropriate action.
PM EM-2-HF-87016764 was performed by electrical technicians to lubricate and inspect the 218 fan motor. The PM was missing Step 2.01 (Step 2.0 was followed by Step 2.02). Step 3.03 instructed the technician to measure the motor space heater current. This was performed at the circuit breaker distribution panel. However, there were two conductors (wires) on the circuit breaker, one wire going to the main exhaust fan heater and the second going to the exhaust booster fan heater. The technicians were not sure et first which wire went to which fan heater. Step 3.03 in the PM should have provided more specific instructions to avoid confusion.
WR NK-81572 was performed by instruirentation and control (I&C) technicians on process Temperature Control Panel 9E282 ERR 0030.
The WR provided instructions to record the circuit temperatures, calibrate temperature readout, if necessary, and obtain as-left data. The temperature readout was found to be low and was recalibrated. The as-left data was then recorded, and the data was within acceptance criteria limits.
WR MS-88921 was perforced by I&C technicians to replace Steam Generator 2C Pressure Transmitter D2-MS-PT-0535.
The postmaintenance test (Procedure 2 PSP 05-MS-0535)wasalsowitnessed. No specific concerns were identified with the transmitter replacement process. Conments regarding 2 PSP 05-MS-0535 are presented in paragraph 7 of this inspection report.
No violations or deviations were identified in this area of the inspection.
6.
Monthly Surveillance Observations (61726)
Selected surveillance activities were observed to ascertain whether the surveillance of safety-significant systems and components were being conducted in accordance with TS and other requirements. The following-surveillance tests were observed ano the documents reviewed:
IPSP03-CC-0003, " Component Cooling Water Pump 1C Inservice. Test,"
Revision 3 IPSP03-SI-0006, High Head Safety Injection Pump 1C Inservice Test,"
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Revision 4 2 PSP 03-CV-0012. " Chemical and Volume Control System Vaive Operability
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Test," Revision 1
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l 2 PSP 06-PK-0005, "4.16KV Class 1E Degraded Voltage Relay Channel
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Calibration /TADOT-Channel 1," Revision 2 t
2 PSP 02-HC-0935, " Containment Pressure Set 3 ACOT (P-0935) "
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Revision 0
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2 PSP 02-SI-0952, " Accumulator 2B Level Group 4 ACOT (L-0952) "
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Specific items inspected included verifying that as-left data was within acceptance criteria limits, the acceptance criteria as listed in the
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procedures agreed with values listed in the design documents or instrument i
setpoint indexes, and the test equipment used was within its current
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calibration cycles.
Following observation by the inspector of the
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surveillance activities, the procedures were reviewed for technical-accuracy and for confonnance to TS requirements.
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Selected inspector observations are discussed below:
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Procedures 1 PSP 03-CC-0003 and IPSP03-SI-0006 were perfonned by Unit 1 i
water (CCW) personnel to verify operability of the component cooling
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operations Pump IC and high head safety injection (HHSI) Pump 10.
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Observations noted during perfonnance of 1 PSP 03-CC-0003 included:
(1) Step 5.4 instructed the operator to verify that adequate pump oil level
existed, but failed to instruct the operator to verify that the motor had
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i sufficient oil; (2) Step 5.19.2 instructed the operator to record a flowrate using a nonsafety-related analog meter, but the information was
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also available in digital form on the safety-related qualified display processing system (QDPS); and (3) following completion of the test a measured flowrate of 400 gallons per minute (gpm) was noted through the
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residual heat removal (RHR) Heat Exchanger 1C although the outlet valve was shut. This suggested the outlet valve was leaking by; however, the 400 gpm measurement was within the instrument loop tolerance for the
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setpoint of 0 gpm. Observations noted during performance of IPSP03-SI-0006
included:
(1) Step 4.1 referenced a TS Section 3.5.4 which did not exist, and (2) procedure step numbering errors were noted in Step 5.27 and on i
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datasheet(-2)atStep5.7.1.
- Procedure 2 PSP 03-CV-0012 was perfonned by a Unit 2 reactor operations trainee under the supervision of a licensed operator to verify chemical
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and volume control system valve operability). Step 5.9.b.3 instructed Observations noted during
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performance of 2 PSP 03-CV-0012 included:
(1 operators to open local Valve CV-0239 (valve was manually shut in a preceeding step) without mentioning the fact that CV-0239 was required to
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be locked in place two and a half turns open; (2) Valve CV0239 was found full open, but should have been locked open (an investigation of this j
matter was initiated by the unit supervisor with appropriate followup by
i the licensee); (3) Valve FCV-0202 failed the stroke time test by 0.2 seconds and was declared inoperable (Valve FCV-0202 was reworked and later. passed the stroke time test); and (4) step numbering errors were noted in i
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Step 5.9.b.3 and on data sheet (-2) at Step 5.8.3.
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Procedure 2 PSP 06-PK-0005 was performed by electrical technicians to verify the accuracy of the 4.16KY Bus E2C degraded voltage relay. Observations r
made during procedure perfonnance included:
(1) the note prior to l
Step 7.6 actually applied to Steps 7.9.1 and 7.9.11, which were not on the same page as the note. The note should have been located just prior to
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the applicable steps to help remind the technicians which order to open and close certain relay knife switches; and (2) Step 7.9.10 instructed the
technician to remove test leads, but the leads were still energized. For safety reasons, the words "de-energize test equipment" should have been i
aded to the step prior to lifting the test leads.
Procedures 2 PSP 02-HC-0935 and 2 PSP 02-SI-0952 were perforned by I&C technicians to verify the accuracies of selected instrument loops for containnent pressure and SI accumulktor level. No concerns were identified
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with these two procedures.
i No violations or deviations were identified in this area of the inspection, s
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Complex Surveillance (61701)
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An inspection was perfonned to ascertain whether functional testing of the
more complex safety-related systems and subsystems was in confonnance with regulatory requirements and approved procedures.
The inspection included
witnessing the performance of Procedure 2 PSP 05-MS-0535, " Steam Pressure Loop 3 Set 2 Calibration (F-0535)," Revision 0.
A technical review of the procedure was also performed.
Surveillance 2 PSP 05-MS-0535 is routinely perfonned every 18 months, but was performed early because of replacement of the Pressure-Transmitter D2-MS-PT-0535.
The transmitter was replaced per WR MS-88921.
Procedure 2 PSP 05-MS-0535 was performed to satisfy the postmaintenance testing requirements. The procedure verified and reestablished the
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accuracies of the transmitter output, trip setpoints, computer point and
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visual alarm actuations, remote displays, and associated signal processing equipment.
Items inspected during performance of the surveillance procedure included:
(1) minimum crew requirements were met, (2) test prerequisites were completed, (3) required test equipment was within current calibration cycles, (4) the procedure used was approved and the most current revision
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available, and (5) as-left data was within acceptance criteria limits.
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Items inspected during the technical review of the procedure included:
(1) the acceptance criteria listed in the procedure agreed with design
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documents, (2) acceptance criteria tolerance was correct per design documents, and (3) the procedure instructions were thorough and complete.
Items observed during the inspection included:
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The Pressure Transmitter D2-MS-PT-0535 was found slightly
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out-of-tolerance and was re-adjusted. The as-left values were noted to be within acceptance criteria limit *
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- Step 7.4.7 of 2 PSP 05-MS-0535 instructed the technicians to ensure that several bistable status monitoring panel lights, annunciator windows, and computer alams were on. The succeeding steps after Step 7.4.7 did not list any computer alarms, although some were associated with the instrument loop.
- The Calibration Data Package 2 PSP 05-MS-0535-1. cover sheet referenced one TS section incorrectly while a second TS section was incorrectly punctuated. The wrong location for Instrument PB-535A was listed in the calibration data package. The correct location was P02-0624, but the data package listed the location as P02-0625.
- The calibration data package for'QDPS Computer Point MSPA0535 listed the wrong setpoint tolerance values.
Per the instrument scaling manual, Loop D2MS-P-0535, Revision 1, the required tolerance was plus or minus 4.9 psig.- The data package tolerance was plus or minus 4.0 psig,-which was a more conservative value. The as-found and as-left values recorded were within the more conservative tolerance limit (4.0psig).
The as-left values recorded were noted to be within acceptance criteria limits, the technicians appeared knowledgeable and competent, housekeeping was adecuate, and the surveillance test was performed in accordance with approvec procedure. All items observed were referred to the licensee for appropriate action.
No violations or deviations were identified in this area of the inspection.
8.
Observation of Initial Licensee Fitness-for-Duty Training (TI 2615/104)
The inspector attended the licensee's fitness-for-duty (FFD) training for.
supervisory and managerial personnel to determine acceptability of the training program implementation. On June 7, 1989, the NRC published the final rule and statement of policy on FFD programs for commercial nuclear power reactors (10 CFR Part 26) with an effective date for program implementation of January 3,1990. Appropriate FFD awareness training for employees and training for supervisors and escorts is required by the rule. The inspector attended the licensee's continual behavior observation program training for supervisory personnel during this -
inspection period. The training generally addressed the following areas:
The role and responsibilities of supervisory and managerial personnel in implementing the FF0 program;
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The roles and responsibilities of others, such as the personnel, medical, and employee assistance program staffst
Behavioral observation techniques for detecting degradation in performance, impaiment, or changes in employee behavior; and
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Procedures for initiating appropriate corrective action, including
referral to the Employee Assistance Program.
Training was conducted utilizing both lecture and video presentation and was found to properly address the FFD program requirements.
No violations or deviations were identified in this area of the inspection.
9.
Exit Interview (30703)
The inspectors met with licensee representatives (denoted in paragraph 1)
on February 1, 1990. The inspectors summarized the scope and findings of the inspection utilizing viewgraphs and an overhead projector to
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facilitate the presentation. The licensee noted that use of the viewgraphs facilitated understanding of the inspection findings. The licensee did not identify as proprietary any of the information provided to, or reviewed by, the inspectors.
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