IR 05000454/2023012

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Biennial Problem Identification and Resolution Inspection Report 05000454/2023012 and 05000455/2023012
ML23292A356
Person / Time
Site: Byron  
Issue date: 10/19/2023
From: Hironori Peterson
NRC/RGN-III/DORS/ERPB
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2023012
Download: ML23292A356 (18)


Text

SUBJECT:

BYRON STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000454/2023012 AND 05000455/2023012

Dear David Rhoades:

On September 8, 2023, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Byron Station and discussed the results of this inspection with Harris Welt, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations problem identification and resolution program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for problem identification and resolution programs.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

October 19, 2023 If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Byron Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Byron Station.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Hironori Peterson, Chief Reactor Projects Branch 3 Division of Operating Reactor Safety Docket Nos. 05000454 and 05000455 License Nos. NPF-37 and NPF-66

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000454 and 05000455

License Numbers:

NPF-37 and NPF-66

Report Numbers:

05000454/2023012 and 05000455/2023012

Enterprise Identifier:

I-2023-012-0009

Licensee:

Constellation Energy Generation, LLC

Facility:

Byron Station

Location:

Byron, IL

Inspection Dates:

August 21, 2023 to September 08, 2023

Inspectors:

J. Bozga, Senior Reactor Inspector

R. Elliott, Senior Project Engineer

T. McGowan, Senior Resident Inspector

M. Siddiqui, Reactor Inspector

Approved By:

Hironori Peterson, Chief

Reactor Projects Branch 3

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Byron Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.

Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Perform ASME Relief Valve Scope Expansion Testing as Required by Procedure Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000454,05000455/2023012-01 Open/Closed

[H.4] -

Teamwork 71152B The inspectors identified a Green finding and associated non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (CFR) Part 50, Appendix B, Criterion V,

Instructions, Procedures and Drawings, for the licensees failure to follow Procedure BMP 3100-23, and test additional containment sump isolation relief valves within the time frame allowed by procedure. Specifically, when the 2SI121B failed to meet the as-found set-pressure testing acceptance criteria, the licensee was required to expand testing scope and test two additional valves within 3 months. Subsequently, 1SI121B was tested 9 months later, and 1SI121A was tested 13 months later, and both failed to meet the as-found testing acceptance criteria. Due to the additional relief valve failures, the licensee was required to further expand scope to the 2SI121A, which was tested 19 months later, and failed as-found testing.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 03.04)

(1) The inspectors performed a biennial assessment of the effectiveness of the licensees Problem Identification and Resolution program, use of operating experience, self-assessments and audits, and safety-conscious work environment.
  • Problem Identification and Resolution Effectiveness: The inspectors assessed the effectiveness of the licensees Problem Identification and Resolution program in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a 5-year review of the Auxiliary Feedwater System.
  • Operating Experience: The inspectors assessed the effectiveness of the licensees processes for use of operating experience.
  • Self-Assessments and Audits: The inspectors assessed the effectiveness of the licensees identification and correction of problems identified through audits and self-assessments.
  • Safety-Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Review of Safety-Conscious Work Environment Assessment of Safety-Conscious Work Environment The team reviewed the stations programs to establish and maintain a safety-conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, workers at the station expressed freedom to raise and enter safety concerns through any one of the various avenues available to them, and the team encountered no indications of chilling or retaliation.

Workers expressed favorable opinions of the Employee Concerns Program (ECP) during interviews, most workers were familiar with how to raise issues through the ECP, specifically, they knew who to contact on-site. There were several signs posted with the name and contact info of the ECP representative; this information was apparently well-known by the interviewees. The inspectors noted that issues were still being identified by the ECP and that most workers stated they felt no need to approach the ECP. The inspectors reviewed those issues documented in the ECP over the previous 2 years and identified no adverse trends.

Overall, inspectors found no evidence of challenges to the licensee's safety-conscious work environment, as licensee employees were willing to raise nuclear safety concerns through at least one of several means available.

No violations or findings were identified Assessment 71152B Assessment of the Corrective Action Program Assessment of the Corrective Action Program Based on the samples reviewed, the team determined that your staffs performance in each of the following areas adequately supported nuclear safety.

No violations or findings were identified.

Effectiveness of Problem Identification Overall, the station was effective at identifying issues at a low threshold and was properly entering them into the corrective action program (CAP) as required by station procedures.

During interviews, workers were familiar with how to enter issues into the CAP and stated that they were encouraged to use it to document issues. During plant walkdowns, the team observed numerous action tags, indicating that workers were identifying issues in the field.

The team determined that the station was generally effective at identifying negative trends that could potentially impact nuclear safety. For the areas reviewed, the team did not identify any issues in problem identification.

Effectiveness of Prioritization and Evaluation of Issues In-depth reviews of a risk-informed sampling of issue reports (IRs), work orders (WOs), and root and apparent cause and condition evaluations were completed. The team determined that the licensee had established a low threshold for entering deficiencies into the CAP, that the issues were generally being appropriately prioritized and evaluated for resolution, and that corrective actions (CAs) were implemented to mitigate the future risk of issues occurring that could affect overall system operability and/or reliability.

The inspectors noted that issues were properly screened with most either classified as Conditions Adverse to Quality (CAQ) or Non-Corrective Action Program (NCAP) items.

Through a selective review of CAP and NCAP items, the inspectors found no issues either with the assigned level of evaluation or the proposed corrective actions. Issues having potential operability concerns were properly addressed through the screening process and during control room observations and accompaniment of non-licensed operators during daily rounds; the inspectors did not identify any significant operator workarounds or similar deficiencies.

The inspectors also did a selective review of issues identified by the NRC either documented as observations, or for which findings or other enforcement was issued. These issues were properly documented and screened in the CAP.

Issue evaluations were generally sound and of good quality. Most issues were screened as low significance and were assigned a work group evaluation (the lowest level of review);more significant issues were assigned a Corrective Action Program Evaluation, or if highly significant, a root cause evaluation. The inspectors verified that the assigned evaluations were consistent with the significance of the issue as defined in the licensees process.

Effectiveness of Corrective Actions The team concluded that the licensee was generally effective in developing CAs that were appropriately focused to correct the identified problem, and to address the root and contributing causes for significant conditions adverse to quality to preclude repetition. The licensee generally completed CAs in a timely manner and in accordance with procedural requirements commensurate with the safety significance of the issue. For NRC-identified issues, the team determined that the licensee generally assigned CAs that were effective and timely. The inspectors also did a selective review of CAs that were still open at least 2 years after the issue was identified to verify that it was reasonable for these items to remain open and that the licensee was managing them correctly; no issues were identified.

The inspectors noted that while issue evaluations were generally sound, there were several examples where additional research was needed to verify that the appropriate corrective actions were taken, primarily due to a lack of clear documentation. This theme had previously been identified in earlier licensee self-assessments and CAP audits and several recent CAP items had been written to address this issue. These CAPs were still open; however, the inspector determined the proposed corrective actions were adequate.

Assessment 71152B Review of Operating Experience, Self-Assessment and Audits Assessment of Operating Experience and Self-Assessment and Audits Based on the samples reviewed, the team determined that licensee performance in the use of Operating Experience (OE) and Self-Assessments and Audits adequately supported nuclear safety.

No violations or findings were identified.

Use of Operating Experience The licensee routinely screened industry and NRC OE information for station applicability.

Based on these initial screenings, the licensee-initiated actions in the CAP to fully evaluate the impact, if any, to the station. When applicable, actions were developed and implemented in a timely manner to prevent similar issues from occurring. During interviews, licensee staff stated that operating experience lessons-learned were communicated during work briefings and department meetings and incorporated into plant operations.

Self-Assessments and Audits The inspectors reviewed several audits and self-assessments and deemed those sampled as thorough and intrusive with regards to following up with the issues that were identified through previous NRC inspections and in the self-assessments and fleet oversight audits.

Reviewed corrective actions for the identified issues were deemed reasonable and completed commensurate with their safety significance. The inspectors regarded licensee performance as adequately self-critical of their own performance and that performance-related issues were being identified through their self-assessment process.

Assessment 71152B Five Year Review of Units 1 and 2 Auxiliary Feedwater System The inspectors performed an expanded 5-year review of the Units 1 and 2 Auxiliary Feedwater System; specifically, by performing system walk-downs, evaluating condition reports and work orders. The inspectors also interviewed a craft personnel responsible for working on the system. Overall, the inspectors determined that the licensee was effectively managing issues associated with this system.

Recently, the licensee has observed challenges in the maintenance of the Auxiliary Feedwater System. Specifically, the licensee's root cause investigation of the failure of the 1B Auxiliary Feed system did not definitively determine the root cause that introduced foreign material in the system that caused the pump to fail to start on demand during a scheduled surveillance. This issue was documented in the CAP and the NRC resident inspectors have been reviewing it through the baseline inspection program. The inspectors identified no operability or other immediate safety concerns with this issue and concluded that the licensee had taken adequate actions to find and correct the cause of this issue.

No violations or findings were identified.

Failure to Perform ASME Relief Valve Scope Expansion Testing as Required by Procedure Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000454,05000455/2023012-01 Open/Closed

[H.4] -

Teamwork 71152B The inspectors identified a Green finding and associated non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (CFR) Part 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, for the licensees failure to follow Procedure BMP 3100-23 and test additional containment sump isolation relief valves within the time frame allowed by procedure. Specifically, when the 2SI121B failed to meet the as-found set-pressure testing acceptance criteria, the licensee was required to expand testing scope and test two additional valves within 3 months. Subsequently, 1SI121B was tested 9 months later and 1SI121A was tested 13 months later, and both failed to meet the as-found testing acceptance criteria. Due to the additional relief valve failures, the licensee was required to further expand scope to the 2SI121A, which was tested 19 months later, and failed as-found testing.

Description:

The containment sump isolation relief valves (SI121A/B) at Byron Station are normally closed valves and have a safety function to open to ensure the continued reliability of the containment recirculation sump isolation valves in the event of an overpressure condition resulting from pressure locking and thermal expansion. The failure of the SI121A/B valves reduces the redundancy of providing inventory from the containment sump to the reactor coolant system during recirculation.

The licensees American Society of Mechanical Engineers (ASME) Code of Record for Operation and Maintenance of Nuclear Power Plants (OM) is the 2004 Edition, with Addenda though 2006. In accordance with the OM code, the licensee categorized the containment sump isolation relief valves as Category C relief valves. The relief valves are accessible at full power and are replaced at least every 8 years during the in-service test.

Subsection ISTC-5240, Safety and Relief Valves, states, safety and relief valves shall meet the in-service test requirements of Mandatory Appendix I-1350.

Mandatory Appendix I-1350(c)(1) requires, for each valve tested for which the as-found set-pressure (first test actuation) exceeds the greater of either +/- tolerance limit of the Owner-established set-pressure acceptance criteria of I-1310(e) or +/- 3% of valve nameplate set-pressure, two additional valves shall be tested from the same valve group. Furthermore, I-1350 (c)(2) states if the as-found set-pressure of any additional valves tested in accordance with I-1350 (c)(1) exceeds the criteria noted therein, then all the remaining valves of that same valve group shall be tested.

On February 17, 2021, the Unit 2 containment sump isolation relief valve, 2SI121B, failed to meet the as-found set pressure testing acceptance criteria under Work Order (WO)04727979, Bench Test Previously Removed Relief Valve and Repair. The licensee replaced the valve with a pre-tested relief valve and entered the issue into their corrective action program as AR 04403027. As a result of the set-pressure failure, the licensee was required to expand testing scope and test two additional valves within the same valve group, as required by Mandatory Appendix I. On February 17, 2021, the licensee-initiated AR 04403055 and AR 04403056, to create WOs to expand testing scope to the 1SI121A and 1SI121B relief valves, respectively.

On November 10, 2021, the Unit 1 containment sump isolation relief valve, 1SI121B, failed to meet the as-found set-pressure testing acceptance criteria under WO 05043687, Replace Relief Valve 1SI121B. The licensee replaced the 1SI121B with a pre-tested relief valve, and initiated AR 04459919. As a result of the additional relief valve failure, the licensee was required to expand scope to all the remaining valves in the valve group, as required by I-1350(c)(2). On November 11, 2021, the licensee initiated AR 04460086 to create a WO to test the 2SI121A, the final valve in the valve group.

On March 07, 2022, the Unit 1 containment sump isolation relief valve, 1SI121A, failed the as-found set-pressure test under WO 04989712, Bench Test Previously Removed Relief Valve. The licensee replaced the valve with a pretested valve.

On September 09, 2022, the Unit 2 containment sump isolation relief valve, 2SI121A, failed the as-found set-pressure test under WO 05237431, Bench Test Previously Removed Relief Valve. The licensee replaced the valve with a pretested valve, and initiated AR 04521501 to perform repairs and additional testing on the valve.

The inspectors reviewed WOs 04727979, 05043687, and 05043687, and noted Section 4.4.3 of Procedure BMP 3100-23, which performed the as-found set-pressure bench testing, stated, in part, if an IST valve fails first as found set-pressure testassociated valves within same IST group may need to be tested. Specifically, Step 4.4.3.14 required, in part, this information shall be completed before this work order is closed out: determine if additional valves need testingensure additional relief valves are tested within 3 months of test date of valve failing as found testing. However, the inspectors noted Step 4.4.3.14 had not been performed as required in the associated work orders, and subsequently was not completed prior to WO closeout.

The inspectors determined the licensee failed to take the prompt and effective actions as a result of the relief valve failures. The licensee had several opportunities to schedule and perform additional relief valve testing, within the scheduling requirements of BMP 3100-23, but failed to perform the testing as required, causing a delay in the identification of additional relief valve testing failures.

Corrective Actions: The licensees corrective actions are to disassemble and inspect the valves to determine the cause of the relief valve testing failures.

Corrective Action References: AR 04700973, Procedure Enhancement for BMP 3100-23

Performance Assessment:

Performance Deficiency: The failure to ensure additional relief valves were tested within 3 months of a valve failing as-found testing, as a result of the as-found set pressure testing failure of the 2SI121B valve was contrary to 10 CFR 50 Appendix B, Criterion V, Instructions, Procedures, and Drawings, and was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee failed to take prompt and effective actions to perform relief valve scope expansion testing to other valves within the group, as a result of the 2SI121B relief valve failure. When a relief valve fails the set-pressure testing acceptance criteria, the procedure required the testing scope be expanded to additional valves from the same group, to identify any potential generic concerns that could apply to valves in the same valve group or other valve groups. The licensees failure to expand scope testing within the scheduling requirements of BMP 3100-23 caused a delay in the identification of additional set-pressure testing failures of the 1SI121A, 1SI121B, and 2SI121A valves.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors screened the finding in accordance with IMC 0609, Appendix A, Exhibit 2.

Specifically, the inspectors determined that this finding screened as Green or very low safety significance because the performance deficiency did not result in the loss of operability or probabilistic risk assessment functionality.

Cross-Cutting Aspect: H.4 - Teamwork: Individuals and work groups communicate and coordinate their activities within and across organizational boundaries to ensure nuclear safety is maintained. Specifically, work groups and supervision across several departments had multiple opportunities to communicate and coordinate activities to ensure additional relief valve testing was scheduled and performed as required, prior to work order closeout.

Enforcement:

Violation: Title 10, CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.

Licensee-established Procedure BMP 3100-23, IST Crosby Safety/Relief Valve Bench Testing, Rev 35, as the implanting procedure for IST relief valve testing. Section 4.4.3 of the procedure stated, in part, if an IST valve fails first as found set pressure testvalves within the same IST group may need to be tested. Step 4.4.3.14 required, in part this information shall be completed before this work order is closed out: determine if additional relief valves need testingensure additional relief valves are tested within 3 months of test date of valve failing as found testing.

Contrary to the above, from February 17, 2021, to September 09, 2022, the licensee failed to accomplish relief valve testing, an activity affecting quality, in accordance with written procedures. Specifically, the licensee failed to follow Step 4.4.3.14 of BMP 3100-23 and failed to ensure additional relief valves were tested within 3 months of the 2SI121B valve failing as-found set-pressure testing acceptance criteria.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Observation: Clear and concise documentation with respect to following American Society of Mechanical Engineers (ASME) Code of Record for Operation and Maintenance of Nuclear Power Plants (OM).

71152B Clear PI&R documentation is crucial for several reasons. Firstly, it serves as a historical record of issues that have arisen, providing valuable insights into recurring problems and their causes. Secondly, such documentation ensures clear communication among team members, allowing for the effective sharing of knowledge and solutions. This, in turn, promotes collaboration and minimizes the chances of the same problems reoccurring due to misunderstandings or lack of information. Additionally, clear and concise documentation supports accountability by tracking the responsible parties and their actions toward resolution.

The team noted the follow:

  • In the IR 04447391, Unit 1 Pressurizer safety valve (1RY8010B) failed as found test, the IR did not state how the licensee planned to satisfy the ASME OM code, nor did it specify in the two Licensee Event Report (LER) submitted how they are adhering to the ASME OM code. At a later date there was a CAP evaluation that stated the corresponding valves on Unit 2 will be tested, but did not clearly state how the specific ASME OM code would be met.
  • In the IR 04447342 on September 19, 2021, Safety Injection (SI) valve 1SI8856B failed its as found test and there were no plans documented for meeting ASME OM code. On November 30, 2021, IR 04463772 was generated during the 2021 PI&R, in response to the inspectors asking how the licensee planned to meet the ASME OM code for the failure of SI valve in IR 04447342.

These are examples of licensee's lack of clear and concise documentation of how they are satisfying the requirements of the ASME OM code. Upon further discussion with the licensee, they are considering being more explicit in their CAP process and documentation on how they are satisfying ASME OM code requirements.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On September 8, 2023, the inspectors presented the biennial problem identification and resolution inspection results to Harris Welt, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

00594046

Demin Resin Volume Inconsistent with UFSAR & Calcs

2/21/2007

04079285

Lack of Resin/Filter Control Impacts UFSAR Assumptions

11/30/2017

233520

Vendor Observation on MSSV MSA at Vendor Facility

03/27/2019

04331822

Generator Voltage Regulator Common Alarm

04/01/2020

04447342

1SI8856B Failed As-Found Testing

09/19/2021

04447391

1RY8010B Failed As-Found Testing at Vendor

09/19/2021

04450104

1RY8010A Failed As-Found Testing at Vendor

10/01/2021

04450108

1RY8010C Failed As-Found Testing at Vendor

10/01/2021

04463772

Spare Relief Valve Removed from Plant 1SI8856B

11/30/2021

04464358

NRC ID: PI&R Inspection - IR 04279156 - NCAP v. CAP

2/02/2021

04464412

NRC ID: PI&R Inspection - IR 04277073 - NCAP v. CAP

2/02/2021

04464431

NRC ID: Application of Buried Pipe and Sys Hlth on

0SX138A

2/02/2021

04464531

NRC IDed PI&R Concerns with Current NFPA 20

Noncompliance

2/03/2021

04467164

CO2 Storage Tank Trouble

2/16/2021

04470954

Byron NSRB Meetings Held on December 1 & 2, 2021

01/10/2022

04490983

Cyber Security Self-Assessment

04/07/2022

04497981

NRC ID - Lack of Design Basis Analysis for Tornado Impacts

05/05/2022

04499079

1Q22 NRC Integrated Insp Rpt: Green NCV for CO2

Actuation

05/11/2022

04499097

Security Equipment - Door 551 Nuisance Taper Alarms

05/11/2022

04506137

A Potential Trend in WO and Surveillance Paperwork

Closeouts

06/17/2022

04510682

Byron NSRB Meetings Held on June 21 & 22, 2022

07/13/2022

04518855

Unexpected Alarm

08/25/2022

04535496

22 M&T Training Objective 2 & 3 Self-Assessment

11/08/2022

04542707

NRC ID - Inadequate Past Operability Review for 1SX168

2/14/2022

04542707

NRC ID-Inadequate Past Operability Review for 1SX168

Failure

2/14/2022

71152B

Corrective Action

Documents

04546760

Byron NSRB Meetings Held on December 14-15, 2022

01/05/2023

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

04551946

Chemical Addition Issue

2/01/2023

04561699

NRC ID; Disconnect in Selective Leaching Procedure

03/13/2023

04690437

Missed Surveillance

07/13/2023

294984

NRC IN 19-09: Spent Fuel Cask Movement Issues

11/06/2019

4333276

Leak On AF Pumps Recirc Return to SX Piping

04/07/2020

4392079

Possible Through-Wall SX Leak - 1B AF Pp

2/25/2020

4403027

2SI121B Failed its As Found Lift Pressure Test

2/17/2021

4403055

Create WO to Test 1SI121A (Scope Expansion for 2SI121B)

2/17/2021

4403056

Create a WO to Test 1SI121B (Scope Expansion for

2SI121B)

2/17/2021

4418541

Through-wall SX Leak - 1B AF Pp Oil Cooler

04/23/2021

4447901

B1R24 FAC; Component SNM1MS116AA-E2 Low Wall

Thickness

09/22/2021

4448574

ASME Code Paperwork not Processed for 1VA08S and

2VA08S

09/25/2021

4448686

ASME Code Paperwork not Processed for 2VA08S Repairs

09/26/2021

4460086

Create a WO to Test 2SI121A (Scope Expansion for

1SI121B)

11/11/2021

4471596

Action to Review OPEX Industry Event Trend in Operator

Fundamentals

01/13/2022

4472994

Min Wall Piping Thickness Below 87.5% of Nominal

01/20/2022

4482044

1VA01SA Min Wall Piping Thickness Below 87.5% of

Nominal

03/02/2022

4482307

B1R25 FAC Piping Replacement WO Request for

1FW001/2C

03/03/2022

4494261

2VP01AD Min Wall Piping Thickness Below 87.5% of

Nominal

04/20/2022

4495057

2VP01AC Min Wall Piping Thickness Below 87.5% of

Nominal

04/23/2022

4499079

1Q22 NRC Integrated Insp Rpt: Green NCV for C02

Actuation

05/11/2022

21501

Relief Valve Failed As-Found Test

09/09/2022

4535936

B2R24 FAC Min-Wall Calc Evaluation Due Date Extension

Needed

11/09/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4536886

NRC RIS 2022-02 Op Leakage Inconsistent w/Op Eval Proc

11/12/2022

4540550

NRC ID: PZR PORV IST Test Requirements

2/02/2022

4560499

B1R25 FAC-1FW03CB-16" Evaluation Required

03/08/2023

4564310

B1R25 FAC/EPC Component Wall Thickness >120% Tnom

03/23/2023

4669118

Diver Required for VT-3 Exam of 0A SX M/U Pump Support

04/11/2023

4671174

Wall Loss Between 30&50% on 0SX32AB

04/19/2023

4671176

Wall Loss Between 30&50% on 0SX33AB

04/19/2023

4672502

NRC NCV 05000454/2023010-01, Selective Leaching

Examinations

04/24/2023

4675797

0D SXCT Structures Monitoring Inspection Observations

05/05/2023

4676538

Potential DIER OPEX Applicability to Byron Station

05/08/2023

4678277

0E SXCT Structures Monitoring - Concrete Degradation

05/15/2023

4679889

SXCT Structures Monitoring Inspection Observations

05/22/2023

4682694

NOS ID: Revise Exam Coversheets for NDE Testings

06/05/2023

4682694

NOS ID: Revise Exam Coversheets for NDE Testings

06/05/2023

4682700

NOS ID: Have NDE Level III Complete a MT Fluorescent

Demo

06/05/2023

4683251

NOS ID: Ensure License Extension Assignments are

Accepted

06/07/2023

4683573

NOS ID: Tendon Nonconformance Eval has Not Been

Approved

06/08/2023

4683576

NOS ID: Discrepancies Btwn Vendor Report and Exam

Datasheets

06/08/2023

4683580

NOS ID: Nonconformance Evals Not Archived W/ Vendor

Report

06/08/2023

4683658

NOS ID: Underground Ground Cable Water Contact

Documentation

06/09/2023

4683660

NOS ID: An Aging Management (AMP) Inspection Not

Retrievable

06/09/2023

4689036

FAC WO Request for Tee Replacement

(1FW03CB-16" 1FW03EB-6")

07/06/2023

AR 03995521

FLEX Readiness Fleet Review

04/07/2017

CA 4549945-08

Revise EQ Binder as a Result of NRC POV Inspection

08/02/2023

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

PI-AA-125-1001

(Root Cause

Investigation

Report)

1B AF Pump Failed to Start (RCI)

08/18/2023

4699955

Procedure Enhancement for Causal Evaluation

09/01/2023

Corrective Action

Documents

Resulting from

Inspection

4700973

Procedure Enhancement for BMP 3100-23

09/06/2023

Drawings

M-136

Diagram of Safety Injection

AZ

Engineering

Changes

0000338067

Replacement of AF Diesel Driven, Shutdown Safety Valve

(SSV)

09/06/2002

MRC Package

(8.22.23)

Management Review Committee (MRC) Package

08/22/2023

N56964-00-0049

2-17

Form NVR-1 Report of Repair/Replacement Activities for

Nuclear Pressure Relief Devices

01/17/2023

NES-EIC-30.00

EQ-BB-HE-10A

Environmental Qualification Engineering

NES-EIC-30.0

EG-BB-HE-10A

Environmental Qualification Engineering

6B

PI-AA-120

Issue Report Generation (Issue Identification and Screening

Process)

PI-AA-126-1001-

F-01

(2023) Byron Station Preparation for NRC Problem and

Resolution (PI&R) Inspection

Miscellaneous

Project BYR-

59609 (AT

4679424-02)

Failure Analysis of Valve, Solenoid, 1/4" NPT, 2-Way

Normally Open

06/08/2023

0BMSR 3.10.B.14

Diesel Fire Pump Engine 18-Month/1500 Hour Maintenance

BMP 3100-23

IST Crosby Safety/Relief Valve Bench Testing

CC-BY-118

Site Implementation of Diverse and Flexible Coping

Strategies (FLEX) and Spent Fuel Pool Instrumentation

Program

ER-AA-321-1007

Inservice Testing (IST) Program Corporate Technical

Positions

Procedures

HU-AA-104-101

Procedure Use and Adherence

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

MA-AA-716-010

Maintenance Planning

OP-AA-108-115

Operability Determinations

OP-BY-101-0001

Byron Operations Standard Philosophy Handbook

PI-AA-115-1003

Processing of Level 3 OPEX Evaluations

PI-AA-120

Issue Identification and Screening Process

PI-AA-125

Corrective Action Program (CAP) Procedure

NOS-BYR-22-01

(AR 4470287)

Maintenance Functional Area Audit Report

2/09/2022

NOSA-BYR-22-

(AR 4508002)

Operations Functional Area Audit

08/31/2022

Self-Assessments

NOSA-BYR-23-

(AR 4677340)

Engineering Programs Audit Report Byron Nuclear Station

06/14/2023

05157042

Replacement of the Fuel Shutoff Solenoid

03/17/2023

05187937

1SI8856A Relief Valve Test

09/19/2021

237710

Diesel Driven AF Pump Inspection per BMP 3203-1

03/23/2023

Work Orders

27979-03

EWP/MM Bench Test Previously Removed Relief Valve and

Repair

2/17/2021