IR 05000454/1980016
| ML19347B138 | |
| Person / Time | |
|---|---|
| Site: | Byron |
| Issue date: | 08/25/1980 |
| From: | Danielson D, Lee E K NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML19347B137 | List: |
| References | |
| 50-454-80-16, 50-455-80-15, NUDOCS 8010010649 | |
| Download: ML19347B138 (5) | |
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g U.S. NUCLEAR REGULATORY COMMISSION
OFFICE OF INSPECTION AND ENFORCEMENT
REGION III
Reports No. 50-454/80-16; 50-455/80-15 Docket Nos. 50-454; 50-455 Licenses No. CPPR-130; CPPR-131 Licensee:
Commonwealth Edison Company P. O. Box 767 Chicago, IL 60690 Facility Name:
Byron Station, Units 1 and 2 Inspe.-tion At:
Byron Site, Byron, IL Inspection Conducted: August 6-8, 1980 Inspector:
E. W. K. Lee $h I.
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%[ '!8k M 94[(L4(tk M d'/lJ 80 Approved By:
D. H. Danielson, Chief
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Engineering Support Section 2 Inspection Summary Inspection on Augus.t 6-8, 1980 (Reports No. 50-454/80-16; 50-455/80-15)
Areas Inspected: Reactor Coolant Pressure Boundary and Safety Related piping work activities, welding, procedures and records; previously identified items.
The inspection involved a total of 18 inspector-hours on site by one NRC inspector.
Results: No items of noncompliance or deviations were identified.
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DETAILS
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Persons Contacted Pri cipal Licensee Employees
- R. F. Choinard, QA Engineer
- J. T. McIntire, QA Supervisor
- J. T. Porter, Sr. QA Inspector
- J. Poulos, Field Engineer
- G. Sorensen, Project Superintendent Hunter Corporation
- M. L. Somsag, QA Supervisor The inspector also contacted and interviewed other licensee and contractor personnel, including area superintendents and craftsmen.
- Denotes those present at the exit interview.
Licensee Action on Previous Inspection Findings (Closed) Unresolved Item (454/80-07-01) - Shop weld of bellow:
It was determined that the shop weld of the bellow element to the weld end of the pipe spool should be flushed with the pipe spool.
It was established
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that the licensee has reinspected all such welds and repair was made to three welds thru a rework request. The inspector noted a nonconformance report was not initiated and emphasized that the QA manual requires that a NCR be written.
Functional or Program Areas Inspected 1.
Reactor Coolant Pressure Boundary and _ Safety Related Piping - Welding Material Control (Units land 2)
a.
Review of Documents The inspector reviewed the following documents:
(1) The inspector established that Hunter Corporation procedure for welding material control has not been revised since the last review (IE Inspection Reports No. 50-454/79-16 and 50-455/79-16, paragraph 4a)
(2) Receiving Inspection Report, Material Certification and Purchase Order for ER308 welding rod with heats Nos. 782850, 742234, 744424 and 464177.
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It was determined that the above documents met the PSAR,10 CFR
50, Appendix B and the applicable code requirements, b.
Control of Materials The inspector toured welding material issuing stations No. 3 and No. 5.
It was determined that (1) the welding materials are properly identified and segregated; (2) the temperature of the rod oven is maintained; (3) records are properly kept; and (4)
issuance and return of welding materials are controlled in accordance with approved procedures.
'io items of noncompliance or deviations were identified.
2.
Reactor Coolant Pressure Boundary Piping - Observation of Welding Activities (Units 1 and 2)
The inspector observed the following welding activities:
a.
Unit 2 Reactor Coolant System Welds No. 182 and No. 184 on drawing No. 2H-CBE-1 and weld No. 196 on drawing No. 2H-CBE12.
b.
Unit 1 Safety Injection System Weld No. FW166 on drawing No. SI-10.
c.
Unit 1 Reactor Coolant System Weld No. 595 on drawing No. S-RC-001-48 and weld No. 490 on drawing No. S-RC-001-54.
It was determined that (1) work was conducted in accordance with traveller; (2) proper welding materials were used; (3) welding pro-cedure requirements were met; (4) work areas as free of weld rod stubs; and (5) physical appearance was acceptable.
No items of noncompliance or deviations were identified.
3.
Reactor Coolant Pressure Boundary Piping - Observation of NDE Work Activities (Unit 2)
The inspector observed liquid penetrant examination of Reactor Coolant System weld No. 208 on drawing No. 2H-CBE-3.
It was determined that (1) surface condition was acceptable; (2) procedure requirements were met; and (3) personnel were properly qualified.
No item of noncompliance or deviations were identified.
4.
Reactor Coolant Pressure Boundary and Safety Related Piping - Weld Heat Treatment (Units 1 and 2)
a.
Review of Procedures The inspector reviewed the applicable welding procedures used-3-
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in welds stated in paragraphs 2 and 8 of this report and deter-
mined that preheating and monitoring methods are specified and acceptable.
b.
Observation of Preheating While observing welding activities for items stated in paragraphs 2 and 8 of this report, the inspector determined that preheat met the welding procedure requirements.
No items of noncompliance or deviations were identified.
5.
Reactor Coolant Pressure Boundary and Safety Related Piping Welder Qualification (Units 1 and 2)
The inspector established that Hunter Corporation procedure for a.
welder qualification has not been revised since the last review (IE Inspection Report Nos. 50-454/79-16 and 50-455/79-16).
b.
The inspector randomly selected the qualification accord of nineteen welders who performed welding on welds stated in para-graphs 2, 6, 8 and 10 of this report.
It was determined that the above documents met the requirements of ASME B&PV Code,Section IX.
No items of noncompliance or deviations were identified.
6.
Reactor Coolant Pressure Boundary Piping - Special Welding Application (Unit 2)
The inspector observed the --inding and weld repair of the Reactor Coolant System weld No. 184 on drawing No. 2H-CBE-1.
It was deter-mined that (1) work was conducted in accordance with instructions; (2) proper materials were used; and (3) procedure requirements were met.
No items of noncompliance or deviations were identified.
7.
Safety Related Piping - Review of Quality Records (Unit 1)
The inspector reviewed ASME data reports, manufacturing record sheets, certified material test reports, NDE reports and receiving inspection reports for the following components:
Safety Injection System spools No. SI-2-5 and No. SI-11-6 a.
b.
Auxiliary Feedwater System spool No. AF-8-3.
It was determined that the documents are legible and acceptable.
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P No items of noncompliance or deviations were identified.
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Safety Related Piping ;21.servation of Welding Activities -(Unit 1)
The inspector observed the following welding activities:
a.
Containment Spray System weld No. 14A on drawing No. CS-7 b.
Boron Recosery System weld No. 51 on drawing No. BR-6 c.
Chemical Volume and Control System weld No. 114 on dr9 wing No. CV-3 It was deter that (1) work was conducted in accordance with traveller; (2) proper welo.-g materials were used; (3) welding procedure requicements were met; (4) work area was free of weld rod stubs; and (5) physical appearance was acceptable.
No items of noncompliance or deviations were identified.
9.
Safety Related Piping - Observation of NDE Work Activities (Unit 1)
The inspector observed magnetic particle examination of Essential Service Water System Weld No. 93 on drawing No. SX-8.
It was determined that (1) surface condition was acceptable; (2) procedure requirements were met; (3) personnel were properly qualified and (4) equipment was currently calibrated.
No items of noncompliance or deviations were identified.
10.
Safety Related Piping - Special Welding Activities (Unit 1)
The inspector observed weld repair of the Residual Heat Removal System weld No. SR2 on drawing No. M538 Sheet 1.
It was determined that (1)
work was conducted in accordance with instructions; (2) proper materials were used and (3) procedure requirements were met.
No items of noncompliance or deviations were identified.
Exit Interview The inspector met with licensee representatives (denoted under Persons Contacted)
at the conclusion of the inspection on August 8, 1980. The inspector summarized the purpose and findings of the inspection. The licensee acknowleJ'-I the
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information.
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