IR 05000400/1991016

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Insp Rept 50-400/91-16 on 910615-0719.No Violations or Deviations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Security,Fire Protection,Surveillance & Maint Observation,Lers & Licensee Action on Prior Insp
ML18010A354
Person / Time
Site: Harris 
Issue date: 07/24/1991
From: Christensen H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010A347 List:
References
50-400-91-16, NUDOCS 9108120037
Download: ML18010A354 (8)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323 Report No.:

50-400/91-16 Licensee:

Carolina Power and Light Company P. 0.

Box 1551 Raleigh, NC 27602 Docket No.:

50-400 Facility Name:

Harris

Inspection Conducted:

June 15 - July 19, 1991 Inspectors:

J.

edrow, Senior Res>dent Inspector pgc License No.:

NPF-63 te igne

&II-M. Shannon, Resident Inspector Approved by:

H.

rsstensen, ection Division of Reactor Projects te igne ate cygne SUMMARY Scope:

This routine inspection was conducted by two resident inspectors in the areas of plant operations, radiological controls, security, fire protection, surveillance observation, maintenance observation, licensee event reports and licensee action on previous inspection items.

Numerous facility tours were conducted and facility operations observed.

Some of these tours and observations were conducted on backshifts.

Results:

No violations or deviations were identified.

9108120037 910725 PDR ADOCK 05000400

',

PDR

REPORT DETAILS 1.

Persons Contacted Licensee Employees P.

Beane, Manager, guality Control

  • J. Collins, Manager, Operations C. Gibson, Manager, Programs and Procedures C. Hinnant, General Manager, Harris Plant D. McCarthy, Manager, Site Engineering B. Meyer, Manager, Environmental and Radiation Monitoring T. Morton, Manager, Maintenance J. Nevill, Manager, Technical Support
  • C. Olexik, Manager, Regulatory Compliance R. Richey, Vice President, Harris Nuclear Project H. Smith, Manager, Radwaste Operation E. Willett, Manager, Outages and Modifications Other licensee employees contacted included office, operations, engineering, maintenance, chemistry/radiation and corporate personnel.

"Attended exit interview Acr onyms and initialisms used throughout this report are listed in the last paragraph.

2.

Review of Plant Operations (71707)

The plant continued in power operation (Mode 1) for the duration of this inspection period.

a.

Shift Logs and Facility Records The inspector reviewed records and discussed various entries with operations personnel to verify compliance with the Technical Specifications (TS) and the licensee's administrative procedures.

The following records were reviewed:

Shift Supervisor's Log; Control Operator's Log; Night Order Book; Equipment Inoperable Record; Active Clearance Log; Jumper and Wire Removal Log; Temporary Modification Log; Chemistry Daily Reports; Shift Turnover Checklist; and selected Radwaste Logs.

In addition, the inspector independently verified clearance order tagouts.

No violations or deviations were identified.

b.

Facility Tours and Observations Throughout the inspection period, facility tours were conducted to observe operations, surveillance, and maintenance activities in

progress.

Some of these observations were conducted during backshifts.

Also, during this inspection period, licensee meetings were attended by the inspectors to observe planning and management activities.

The facility tours and observations encompassed the following areas:

security perimeter fence; control room; emergency diesel generator building;. reactor auxiliary building; waste

'rocessing building; turbine building; fuel handling building; emergency service water building; battery rooms; electrical switchgear rooms; and the technical support center.

During these tours, the following observations were made:

(I)

Monitoring Instrumentation

- Equipment operating status, area atmospheric and liquid radiation monitors, electrical system lineup, reactor operating parameters, and auxiliary equipment operating parameters were observed to verify that indicated parameters were in accordance with the TS for the current operational mode.

(2)

Shift Staffing - The inspectors verified that operating shift staffing was in accordance with TS requirements and that control room operations were being conducted in an orderly and professional manner.

In addition, the inspector observed shift turnovers on various occasions to ver ify the continuity of plant status, operational problems, and other pertinent plant information during these turnovers.

(3)

Plant Housekeeping Conditions

-

Storage of material and components, and cleanliness conditions of various areas throughout the facility were observed to determine whether safety and/or fire hazards existed.

(4)

Radiological Protection Program - Radiation protection control

'ctivities were observed routinely to verify that

'Nese activities were in conformance with the facility policies and procedures, and in compliance with regulatory requirements.

The inspectors also reviewed selected radiation work permits to verify that controls were adequate.

(5)

Security Control - In the course of monthly activities, the inspector included a review of the licensee's physical security program.

The performance of various shifts of the security force was observed in the conduct of daily activities which included:

protected and vital area access controls; searching of personnel, packages, and vehicles; badge issuance and retrieval; escorting of visitors; patrols; and compensatory posts.

In addition, the inspector observed the operational status of Closed Circuit Television (CCTV) monitors, the Intrusion Detection system in the central and secondary alarm stations, protected area lighting, protected and vital area

barrier integrity, and the security organization interface with operations and maintenance.

(6)

Fire Protection

- Fire protection activities, staffing and equipment were observed to verify that fire brigade staffing was appropriate and that fire alarms, extinguishing equipment, actuating controls; fire fighting equipment, emergency equipment, and fire barriers were operable.

No violations or deviations were identified.

c.

Review of Nonconformance Reports Adverse Condition Reports (ACRs)

were reviewed to verify the following:

TS were complied with, corrective actions as identified in the reports were accomplished or being pursued for completion, generic items were identified and reported, and items were reported as required by the TS.

No violations or deviations were identified.

3.

Surveillance Observation (61726)

Surveillance tests were observed to verify that approved procedures were being used; qualified personnel were conducting the tests; tests were adequate to verify equipment operability; calibrated equipment was utilized; and TS requirements were followed.

The following tests were observed and/or data reviewed:

- NST-I0001

- NST-I0092

- MST-I0250

- MST-I0320

- LP-F-7050B Train A Solid State Protection System Actuation Logic II Master Relay Test Reactor Coolant Loop 2 Cold Leg Temperature Instrument (T-0420)

Reactor Coolant System Cold Over pressurization Instrument (P-0441) Operational Test Train B Solid State Protection System Actuation Logic 5 Master Relay Test Loop Calibration of Component Cooling Water Heat Exchanger B Service Water Flow

- LP-T-0469

- PIC-1058 Loop Calibration of Pressurizer Safety Valve High Temperature Channel Calibration Check and Stroking of a Milliampere Hydramotor Actuator

No violations or deviations were identified.

4.

Maintenance Observation (62703)

The inspector observ'ed/reviewed maintenance activities to verify that correct equipment clearances were in effect; work requests and fire prevention work permits, as required, were issued and being followed; quality control personnel were available for inspection activities as required; and, TS requirements were being followed.

Maintenance was observed and work packages were reviewed for the following maintenance activities:

Repair of the pressurizer backup heater control circuit.

Repair of a control rod drive control card failure.

Repair of an auxiliary feedwater pressure control valve.

Troubleshooting and repair of a reactor trip bypass breaker fuses holder.

Replacement of the upper bearing for the A emergency service water pump motor and retest in accordance with procedure OST-1214, Emergency Service Water System Operability Train A.

No violations or deviations were identified.

5.

Review of Licensee Event Reports (92700)

The following LERs were reviewed for potential generic impact, to detect trends, and to determine whether corrective actions appeared appropriate.

Events that were reported immediately were reviewed as they occurred to determine if the TS were satisfied.

LERs were reviewed in accordance with the current NRC Enforcement Policy.

a ~

(Open)

LER 91-09:

This LER reported an unplanned actuation of the auxiliary feedwater system due to personnel error while troubleshooting a

steam generator level instrument.

The licensee plans to review this event with maintenance personnel and developed additional procedure, guidance to enhance troubleshooting activities.

The LER will remain open pending completion of this action.

b.

(Closed)

LER 91-10:

This LER reported a reactor trip which occurred during surveillance testing on an RCS flow transmitter.

This event was discussed previously in NRC Inspection Reports 50-400/91-13 and 50-400/91-15 and was the subject of violations 400/91-15-01 and 400/91-15-02.

For record purposes, the LER will be closed and corrective action tracked by the violation c ~

d.

e.

(Open)

LER 91-11:

This LER reported that the concentration of boron in the refueling water storage tank was in excess of TS limits.

The licensee plans to review this event with chemistry and operations personnel and revise the surveillance test procedure to specify the acceptable range for boron concentration.

Other chemistry procedures will be reviewed to detect similar deficiencies.

The LER will remain open pending completion of these corrective actions.

(Closed)

LER 91-12:

This LER reported an unplanned actuation of the auxiliary feedwater system due to the failure of a main feedwater pump to start.

The licensee's investigation and testing performed on the main feedwater pump following the event could not determine a

reason for the pump not starting.

(Open)

LER 91-13:

This LER reported a reactor trip which occurred during plant cooldown.

The licensee plans to revise the surveillance test procedure to clarify restoration requirements and will re-emphasize communications and strict compliance with procedures to appropriate maintenance personnel.

Also an evaluation will be performed to determine possible alternatives to placing a nuclear instrument channel in the tripped condition during post-refueling startups.

(Open)

LER 91-15:

This LER reported an unplanned actuation of the auxiliary feedwater system due to an improperly adjusted feed flow transmitter dampening device.

The licensee has completed adjustment and testing of the feed flow transmitter and has returned it to service.

The LER will remain open until a review of the modification process is performed to identify improvements in acceptance testing.

6.

Licensee Action on Previously Identified Inspection Findings (92702

&

92701)

'a ~

(Closed)

IFI 400/90-10-01:

Review the licensee's activities to correct recurrent leakage problems associated with drain piping from containment cooling units.

The licensee has added supports to strengthen the affected piping under plant modification PCR-5327, Supports for Lines 2SWl-624SA-1 and 2SW1-625SA-1.

b.

(Closed)

Violation 400/90-20-02:

Failure to accurately document surveillance performance dates and times.

The inspector reviewed and verified implementation of the corrective actions listed in the licensee's response letter dated November 30, 1990.

These corrective actions included maintenance procedure clarifications and training of craft personnel when credit is taken for performance of another tas c.

(Closed)

Violation 400/90-20-03:

Failure to adhere to plant maintenance procedures.

The inspector reviewed and verified implementation of the corrective actions listed in the licensee's response letter dated November 30, 1990.

These corrective actions included reviewing work authorization requirements with appropriate craft personnel, inclusion of an independent verification log sheet into plant procedures, and appropriate training to craft personnel on the procedure changes.

d.

(Closed)

Violation 400/90-21-01:

Failure to properly implement a

radiochemistry procedure.

The inspector reviewed and verified implementation of the corrective actions listed in the licensee's response letter dated December 28, 1990.

The acid addition step was emphasized to chemistry technicians via the required reading program.

A study to determine the impact of omission of the acid was conducted and determined that acid addition was necessary for sample accuracy.

e.

(Closed)

Violation 400/90-21-05:

Failure to notify the NRC of employment termination of an SRO.

The inspector reviewed and verified implementation of the corrective actions listed in the licensee's response letter dated December 28, 1990.

Procedure guidance has been incorporated into the conduct of operations, medical, training program, and departure procedures to require notification of regulatory compliance upon change of the status of licensed personnel.

f.

(Closed)

Violation 400/91-06-02:

Failure to install a backflow preventer during the performance of local leak rate testing.

The inspector reviewed and verified completion of the corrective actions listed in the licensee's response letter, dated June 1, 1991.

This action included revising the applicable test procedures to include a signoff for verifying the installation of a backflow preventer, and also, training of test personnel on this requirement.

7.

Exit Interview (30703)

The inspectors met with licensee representatives (denoted in paragraph 1)

at the conclusion of the inspection on July 19, 1991.

During this meeting, the inspectors summarized the scope and findings of the inspection as they are detailed in this report.

The licensee representatives acknowledged the inspector's comments and did not identify as proprietary any of the materials provided to or reviewed by the inspectors during this inspectio.

Acronyms and Initialisms ACR CCTV CFR IFI LER LP MST NRC OST PCR PIC RCS/RC SRO TS Adverse Condition Report Closed Circuit Television Code of Federal Regulations Inspector Follow-up Item Licensee Event.Report Loop Calibration Procedure Maintenance Surveillance Test Nuclear Regulatory Commission Operations Surveillance Test Plant Change Request Process Instrument Calibration Reactor Coolant System Senior Reactor Operator Technical Specification