IR 05000327/2019002
| ML19204A173 | |
| Person / Time | |
|---|---|
| Site: | Sequoyah |
| Issue date: | 07/23/2019 |
| From: | Lopez O NRC/RGN-II/DRP/RPB5 |
| To: | James Shea Tennessee Valley Authority |
| Omar Lopez-Santiago | |
| References | |
| IR 2019002 | |
| Download: ML19204A173 (17) | |
Text
July 23, 2019
SUBJECT:
SEQUOYAH NUCLEAR PLANT, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000327/2019002 AND 05000328/2019002
Dear Mr. Shea:
On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Sequoyah, Units 1 and 2. On July 17, 2019, the NRC inspectors discussed the results of this inspection with Mr. Matt Rasmussen and other members of your staff. The results of this inspection are documented in the enclosed report.
One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.
If you contest the violation or significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at Sequoyah.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC Resident Inspector at Sequoyah. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Omar R. Lopez-Santiago, Chief Reactor Projects Branch 5
Docket Nos.: 05000327 and 05000328 License Nos.: DPR-77 and DPR-79
Inspection Report 05000327/2019002 and 05000328/2019002
cc w/ encl: Distribution via LISTSERV
ML19204A173 OFFICE RII: DRP RII: DRP RII: DRS RII: DRS NAME N Childs D Hardage S Ninh O Lopez-Santiago DATE 7/19/2019 7/18/2019 7/19/2019 7/23/2019
Enclosure U.S. NUCLEAR REGULATORY COMMISSION
Inspection Report
Docket Numbers:
05000327 and 05000328
License Numbers:
Report Numbers:
05000327/2019002 and 05000328/2019002
Enterprise Identifier: I-2019-002-0023
Licensee:
Tennessee Valley Authority
Facility:
Sequoyah Nuclear Plant, Units 1 and 2
Location:
Soddy Daisy, TN 37379
Inspection Dates:
April 01, 2019 to June 30, 2019
Inspectors:
N. Childs, Resident Inspector
D. Hardage, Senior Resident Inspector
Approved By:
Omar R. Lopez-Santiago, Chief
Reactor Projects Branch 5
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a integrated inspection at Sequoyah, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Obstruction in Steam Generator Pressure Channel sense line results in engineered safeguard feature actuation system (ESFAS) channel inoperability Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000327/2019002-01 Open/Closed
[H.5] - Work Management 71111.15 The inspectors identified a green, non-cited violation of 10 CFR 50 Appendix B criterion XVI when the licensee failed to ensure the pressure instrumentation sense line for a steam generator pressure protection channel transmitter was not obstructed. Specifically, identified blockages in the sense line were not cleared and resulted in an inoperable ESFAS channel.
Additional Tracking Items
None.
PLANT STATUS
Unit 1 began the inspection period at rated thermal power (RTP). On April, 14, 2019, the reactor tripped on number 3 steam generator low level following a loss of the 'A' main feedwater pump. The unit was returned to RTP on April 17, 2019 and remained at or near RTP for the remainder of the inspection period.
Unit 2 began the inspection period at rated thermal power and remained at or near RTP for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Summer Readiness Sample (IP Section 03.01) (1 Sample)
The inspectors evaluated summer readiness of offsite and alternate current (AC) power systems on May 31, 2019.
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2 A component cooling system (CCS) header following the restoration of 2A2 CCS heat exchanger on April 5, 2019
- (2) Unit 1 offsite power while 1A start bus was out of service for inspection and planned maintenance on April 28, 2019
- (3) Common 1-IV and 0-IV vital inverters, III and 2-S vital chargers while 2-IV vital inverter was out of service for inspection and planned maintenance on April 30, 2019
71111.04S - Equipment Alignment
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
The inspectors evaluated system configurations during a complete walkdown of the High Pressure Fire Protection System on June 26, 2019.
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (5 Samples)
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Unit 1 and Unit 2 auxiliary building, elevation 759 on April 9, 2019
- (2) Emergency Raw Cooling Water Building on May 6, 2019
- (3) Diesel Generator Building, elevation 740.5 on May 22, 2019
- (4) Diesel Generator Building, elevation 722 on June 17, 2019
- (5) Unit 1 and Unit 2, Auxiliary Building - El. 734 (Vital Battery Board Rooms 1-4) on June 24, 2019
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
The inspectors observed and evaluated licensed operator performance in the main control room following a reactor trip on April 14, 2019.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
The inspectors observed and evaluated a simulator training scenario on May 29, 2019.
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Review of licensee activities in response to Part 21 2019-53993 regarding transformers installed in AMETEK vital inverters at SQN on April 15, 2019
- (2) Maintenance rule functional failure of the 1A1 main feed pump oil pump motor (CDE 3062) on May 3, 2019
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Unit 1 and Unit 2, week of April 14 - April 20, 2019, including protected equipment status reviews for scheduled maintenance on OB2 component cooling system heat exchanger and Unit 1 reactor startup
- (2) Unit 1 and Unit 2, week of April 21 - April 28, 2019, including protected equipment status reviews for scheduled maintenance on the 1A start bus and C control air compressor
- (3) Unit 1 and Unit 2, week of May 5 - May 11, including protected equipment status reviews for scheduled maintenance on 1-I vital invertor, 1A start bus and emergent maintenance on protection rack 1-R-3
- (4) Unit 2, week of May 26 - June 1, including protected equipment status reviews for scheduled maintenance on 2B containment spray pump and 2A1 480V shutdown board transformer replacement
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 02.02) (6 Samples)
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Unit 2 PORV 340A isolated due to excessive leakby (CR 1513968) on May 7, 2019 (2)1-PT-1-23 appears to lag other Loop 3 Steam Generator Pressure Instruments (CR
===1507948) on May 9, 2019
- (3) Unit 2 annunciator M-6B window A-1 LS-3-39D Steam Gen Loop 1 Low FW Flow/Low Water Level alarmed (CR 1518725) on May 22, 2019
- (4) Emergency Gas Treatment System (EGTS) Decay Cooldown Valve 0-FCV-0028A has a damaged seat (CR 1524125) on June 13, 2019
- (5) ERCW operability impacted by aligning cooling to station compressors during the summer (CR 1521279) on June 21,2019
- (6) Gas/water flow noted from 1-VLV-63-832 and 1-VLV-63-837 during cold leg injection piping vent (CR 1519228) on May 23, 2019
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)
The inspectors evaluated the following temporary or permanent modifications:
- (1) Temporary Modification SQN-1-2018-062-001, Install Tuned Vibration Damper on the 1A-A Charging Pump
- (2) Temporary Modification SQN-2-2019-063-001, Safety Injection System Continuous Pressure Relief Line
71111.19 - Post-Maintenance Testing
Post Maintenance Test Sample (IP Section 03.01)===
The inspectors evaluated the following post maintenance tests:
- (1) WO 119758872, 2A2 CCS heat exchanger cleaning and inspection, on April 8, 2019
- (2) WO 120454374, Replace LCP card and NVRAM in 1-R-3 on May 9, 2019
- (3) WO 118341145, 2-MOVP-067-0126A, Perform EQ inspection and maintenance on May 21, 2019
- (4) WO 120286121, 2B Containment Spray Pump, replace coupling due to high vibrations on May 29, 2019
- (5) WO 119584204, Main Control Room A/C Chiller oil cooler cleaning and internal inspection on June 16, 2019
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Inservice Testing (IP Section 03.01)
1-SI-SXP-070-201.A, Component Cooling Pump 1A-A Performance Test on April 12, 2019
Surveillance Tests (other) (IP Section 03.01) (3 Samples)
(1)1-SI-OPS-082-007.A, Electrical Power System Diesel Generator 1A-A on April 29, 2019 (2)2-PI-SFT-070-001.0, Performance Testing of Component Cooling Heat Exchangers 2A1, 2A2 on May 21, 2019 (3)0-SI-SFT-065-001.B, Emergency Gas Treatment System Filter Train B on June 13, 2019
71114.06 - Drill Evaluation
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)
Emergency preparedness drill conducted on May 15,
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===
- (1) Unit 1 unplanned scrams per 7000 critical power hours (April 2018 - March 2019)
- (2) Unit 2 unplanned scrams per 7000 critical power hours (April 2018 - March 2019)
IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2 Samples)
- (1) Unit 1 unplanned power changes per 7000 critical hours (April 2018 - March 2019)
- (2) Unit 2 unplanned power changes per 7000 critical hours (April 2018 - March 2019)
IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)
- (1) Unit 1 unplanned scrams with complications (April 2018 - March 2019)
- (2) Unit 2 unplanned scrams with complications (April 2018 - March 2019)
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (3 Samples)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Chemistry Department Safety Culture Concerns (CR 1484992).
- (2) Corrective actions to address Part 21 2019-02 from Weschler Instruments (CR
===1506204)
- (3) Operating experience review of cryofit coupling failure at Brunswick Nuclear Station (CR 1506831)
Semiannual Trend Review (IP Section 02.02)===
The inspectors reviewed the licensees corrective action program for potential adverse trends in non-functional radiation monitors that might be indicative of a more significant safety issue.
INSPECTION RESULTS
Obstruction in Steam Generator Pressure Channel sense line results in engineered safeguard feature actuation system (ESFAS) channel inoperability Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems
Green NCV 05000327/2019002-01 Open/Closed
[H.5] - Work Management 71111.15 The inspectors identified a green, non-cited violation of 10 CFR 50 Appendix B criterion XVI when the licensee failed to ensure the pressure instrumentation sense line for a steam generator pressure protection channel transmitter was not obstructed. Specifically, identified blockages in the sense line were not cleared and resulted in an inoperable ESFAS channel.
Description:
On April 14, 2019, Unit 1 reactor tripped on low steam generator level following the loss of a main feedwater pump. During the post trip review of this transient, the licensee noted that, following rapid pressure changes, one of the loop 3 steam generator pressure indicators, 1-PT-1-23, was lagging the indication of other steam generator pressure transmitters.
Specifically, the licensee noted pressure indication on the steam generators (except for 1-PT-1-23) increased from approximately 880 psig to 920 psig (40 psig) in less than a second and then remained steady for over a second while 1-PT-1-23 slowly increased by 16 psig over the same time period. Similarly, when steam generator pressures later increased approximately 60 psig in less than a second, 1-PT-1-23 slowly increased by 7 psig in the same time period.
The required response times for the steam pressure channel is 0.028 seconds. 1-PT-1-23 is used to monitor loop 3 steam line pressure and is one of three transmitters that are used with their instrument loops to provide the two-out-of-three (per steam line) logic required by Technical Specifications for Safety Injection and Steam Line Isolation. Due to this observed delayed response, operators declared 1-PT-1-23 inoperable.
It should be noted that, until the time of the trip on April 15, 2019, the licensee considered 1-PT-1-23 operable based on acceptable channel checks and calibrations. Prompted by questions raised by the inspectors, the licensee reviewed past operating experience which identified similar behavior of 1-PT-1-23 in 2015; this behavior was not recognized at that time and no corrective actions were taken. Plugging of steam generator pressure transmitter sense lines had been previously identified at Sequoyah. Condition Report (CR) 915880 was written in July 2014 documenting that steam generator instrument sense lines had been found plugged or partially plugged and erratic measurements had been attributed to partial sense line plugging. Actions were generated in the licensee's corrective action program to clear 1-PT-1-23 sense line to remove corrosion products during the upcoming refueling outage (1R20) and setup repetitive work orders for performance of this action. These actions were not performed.
Corrective Actions: 1-PT-1-23 was removed from service and the sense line was rodded out to remove accumulated material. 1-PT-1-23 was returned to operable status on April 16, 2019.
Corrective Action References: CR 1507948, CR 915880, WO 120407126, WO 116483457, PER 915889-003
Performance Assessment:
Performance Deficiency: The licensees failure to ensure identified blockages in the instrumentation sense line for a steam generator pressure protection channel transmitter were removed was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone. Specifically, identified blockages in 1-PT-1-23 sense line were not cleared and resulted in an inoperable engineered safeguard feature actuation system (ESFAS) channel.
Significance: The inspectors assessed the significance of the finding using Appendix A, Significance Determination of Reactor Inspection Findings for At - Power Situations. The finding screened to green because all four questions in Exhibit 2, "Mitigating Systems Screening Questions" were answered "no".
Cross-Cutting Aspect: H.5 - Work Management: The organization implements a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. The work process includes the identification and management of risk commensurate to the work and the need for coordination with different groups or job activities. The licensee created corrective action work orders several years prior to the event to clear the steam generator pressure transmitter sense lines. However, the work management process did not prioritize the execution of this work and these work orders were never performed.
Enforcement:
Violation: Title 10 CFR Part 50, Appendix B, Criteria XVI, Corrective Actions, requires, in part, that measures be established to assure conditions adverse to quality are promptly identified and corrected. Contrary to the above, from November 23, 2015 until April 14, 2019, the measures established by the licensee failed to correct an identified condition adverse to quality. Specifically, the licensee identified a condition adverse to quality, obstruction of a steam generator pressure transmitter sense line, but did not take action to correct the condition.
Enforcement Action: This violation is being treated as an non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On July 17, 2019, the inspectors presented the integrated inspection results to Mr. Matt Rasmussen and other members of the licensee staff.
THIRD PARTY REVIEWS
Inspectors reviewed Institute of Nuclear Power Operations report that was issued during the inspection period.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Procedures
Revision 39
Degraded Grid or Abnormal Voltage Conditions
Revision 15
NPG-SPP-07.16
On Line Work Control Power Systems Alerts/Offsite
Power
Revision 6
Miscellaneous
SQN U1 Protected Equipment List
04/30/2019
0-PE-2019
Protected equipment clearance for 2-IV vital inverter
and No. IV vital charger maintenance
04/29/2019
Procedures
0-SI-OPS-082-007.W
AC Electrical Power Source Operability Verification
Revision 45
2-SO-70-1
Component Cooling Water System "A" Train
Revision 49
Corrective Action
Documents
CR 1332919
Fire Protection System Pressure Decline
08/28/2017
CR 1445092
Poor Overall System Health on HPFP (026) Yard Ring
Header Valves
09/05/2018
Miscellaneous
SQN-DC-V-43.0
Sequoyah Nuclear Plant - High Pressure Fire
Protection Water Supply System
Revision 9
System Health Report
Scorecard
System 26 - Fire Protection
1st Quarter
2019
Work Orders
115815343; 119405060;
119405058; 1194045538
71111.05Q Fire Plans
AUX-0-669-00
Fire Protection Pre-Fire Plans Auxiliary Building - El.
669
Revision 4
AUX-0-734-00
Fire Protection Pre-Fire Plans Auxiliary Building - El.
734
Revision 4
AUX-0-734-01
Fire Protection Pre-Fire Plans Auxiliary Building - El.
734 Unit 1 Side
Revision 10
AUX-0-734-02
Fire Protection Pre-Fire Plans Auxiliary Building - El.
734 Unit 2 Side
Revision 9
AUX-0-759-01
Auxiliary Building Elevation 759 Unit 1 Side
Revision 6
AUX-0-759-02
Auxiliary Building Elevation 759 Unit 2 Side
Revision 6
DGB-0-722-00
Fire Protection Pre-Fire Plans Diesel Generator
Building El. - 722
Revision 7
DGB-0-740.5-00
Fire Protection Pre-Fire Plans Diesel Generator
Building - El. 740.5
Revision 5
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
ERCW-0-688-00
Fire Protection Pre-Fire Plans ERCW Building - El.
688
Revision 2
ERCW-0-704-00
Fire Protection Pre-Fire Plans ERCW Building - El.
704
Revision 2
ERCW-0-720-00
Fire Protection Pre-Fire Plans ERCW Building - El.
20
Revision 3
Procedures
NPG-SPP-18.4.7
Control of Transient Combustibles
Revision 13
71111.11Q Miscellaneous
SEG OPL273S1908
RCS Leak, LOCA, ES-1.2, Loss of Sump Recirc
01/10/2019
Procedures
0-GO-6
Power Reduction From 30% Reactor Power to Hot
Standby
Revision 64
0-SI-NUC-000-038.0
Revision
105
Corrective Action
Documents
CR 1508008
OE - Part 21 Ametek Solidstate Controls Inverters
04/15/2019
CR 1508784
SQN Supply Chain Request a Part 21 Evaluation
04/17/2019
CR 1508834
Loss of 1A1 Main Feed Pump Lube Oil Pump Results
in Trip of 1A Main Feed Pump Turbine
04/15/2019
CR 1513554
Maintenance Rule Functional Failure of 1A1 Main
Feed Pump Main Oil Pump Motor
05/03/2019
Miscellaneous
CDE 3062
1A Main Feedwater Pump Trip and Balance of Plant
Runback
04/14/2019
Procedures
NPG-SPP-03.4
Maintenance Rule Performance Indicator Monitoring,
Trending, and Reporting - 10CFR50.65
Revision 3
TI-4
Maintenance Rule Performance Indicator Monitoring,
Trending, and Reporting - 10CFR50.65
Revision 32
0-GO-16
System Operability Checklists
Revision 24
NPG-SPP-07.3.4
Protected Equipment
Revision 5
Corrective Action
Documents
CR 1310102
minute and 4 seconds of gas observed during
performance of 1A-A SI pump discharge piping vent
06/22/2017
CR 1514732
ACMP SO-19-14 U2 PORV Tailpipe Temperature
Change
05/07/2019
Drawings
2-47W610-3-1
Mechanical Control Diagram Main & Aux Feedwater
Sys
Revision 21
2-47W610-3-5
Mechanical Control Diagram Main & Aux Feedwater
Sys
Revision 5
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
2-47W611-99-6
Mechanical Logic Diagram Reactor Protection System
Revision 3
Operability
Evaluations
Past Operability Evaluation for CR
1310089/1310095/1310102
07/06/2017
Procedures
0-SO-68-3
Pressurizer Pressure Control
Revision 37
Calculations
47A43502008
Calculation for pipe support 47A435-2-8
Revision 1
MDQ0020632019000316 Flow Characteristics of SQN-2-2019-063-001, Safety
Injection Continuous Pressure Relief Line to
Centrifugal Charging Pump Suction
Revision 0
SCG-4M-00212
D
Qualification of CCP and Absorber per TMOD SQN-1-
2018-062-001
Revision 13
Engineering
Changes
SQN-1-2018-062-001
Install Tuned Vibration Damper on the 1A-A Charging
Pump
Revision 0
SQN-2-2019-063-001
Temporary Modification - Safety Injection System
Continuous Pressure Relief Line
Revision 1
Procedures
NPG-SPP-09.3
Plant Modifications and Engineering Change Control
Revision 30
NPG-SPP-09.3 IP-ENG-
001
Standard Design Process
Revision 0
NPG-SPP-09.5
Temporary Modifications - Temporary Configuration
Changes
Revision 15
Work Orders
119853291; 119890013;
20196052; 120222735;
20408521, 120408522,
20408523
Procedures
0-MI-EMV-317-146.0
Inspection and Preventive Maintenance of Limitorque
Motor Operators Maintenance Instruction
Revision 51
1-PI-ICC-001-03A.1
Calibration of Steam Generator Loop 1 Steam
Flow/Feed Flow Mismatch Channel I Rack 3 Loops 1-
F-1-3A (F-512) and 1-F-3-35A (F-510)
Revision 21
1-SI-ICC-001-02A.1
Channel Calibration of Steam Generator Loop 1
Steam Pressure Channel I Rack 3 Loop 1-P-1-2A (P-
514)
Revision 22
1-SI-ICC-001-09A.1
Channel Calibration of Steam Generator Loop 2
Steam Pressure Channel I Rack 3 Loop 1-P-1-9A (P-
24)
Revision 20
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
1-SI-ICC-030-045.1
Channel Calibration of Containment Pressure Channel
I Rack 3 Loop 1-P-30-45 (P-937)
Revision 20
2-SI-SXP-072-201.B
Containment Spray Pump 2B-B Performance Test
Revision 18
MMTP-144
Motor Operated Valve Diagnostic Testing
Revision 2
Work Orders
119970546
Machine rough head castings into finished condenser
heads
06/15/2019
Procedures
0-GO-16
System Operability Checklist
Revision 70
0-SO-82-1
Diesel Generator 1A-A
Revision 60
Installation and Removal of the DG Data Acquisition
System
Revision 11
1-SI-SXP-070-201.A
Component Cooling Pump 1A-A Performance Test
Revision 14
Work Orders
119534391
Emergency Gas Treatment System Filter Train B
06/13/2019
CCS Heat Exchanger Performance Test - 2A1 and
2A2
05/08/2019
Miscellaneous
Emergency Preparedness Drill
05/15/2019
Procedures
EPIP-1
Emergency Plan Classification Matrix
Revision 54
SAG-1
Main Control Room Severe Accident Guideline Initial
Response
Revision 8
SAG-2
Main Control Room Severe Accident Guideline TSC
Recommending Strategies
Revision 5
Corrective Action
Documents
CR 1397569
1,2-RM-90-400 Non-Functional Greater than 90 Days
03/13/2018
CR 1461088
0-RM-90-133/140 Out of Service Greater than Thirty
Days
10/29/2018
CR 1472608
Adverse Trend in Non-Functional Radiation Monitors
2/06/2018
CR 1484992
Anonymous condition report identified performance
gaps in chemistry department management
01/24/2019
CR 1485018
OE - Part 21 - EN 53833 - Potential Defect in
Weschler Instruments
01/24/2019
CR 1500304
Part 21 Issue for Engineering Review
03/19/2019
CR 1506204
Part 21 Material to be Returned to Westinghouse
04/09/2019
CR 1506831
Review Unusual Event at Brunswick which Required a
Shutdown on 03/28/2019
04/10/2019
Procedures
Main Feedwater Malfunctions
Revision 28
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
EPM-4
User's Guide
Revision 32