IR 05000321/1987016
| ML20235U158 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 07/10/1987 |
| From: | Belisle G, Mellen L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML20235U140 | List: |
| References | |
| 50-321-87-16, 50-366-87-16, NUDOCS 8707220376 | |
| Download: ML20235U158 (7) | |
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'o MUCLEAR REGULATORY COMMISSION .. " .[*' REGION li n '$ j 101 MARIETTA STREET, N.W.
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- I e ATLANT A, GEORGI A 30323
%,****/ a Report Nos.: 50-321/87-16 and 50-366/87-16 Licensee: Georgia Power Company P. O. Box 4545' Atlanta, GA 30302 Docket Nos.: 50-321 and 50-366 License Nos.: DPR-57 and NPF-5 Facility Name: Hatch 1 and 2
Inspection Conducted: June 15 - 17, 1987 7//d[[[ ! Inspector: ch "# I 0'a'te S'igned
L. S. Mellen / bu 8' _7 M[[7 . Approved by:_ G. A. Belisle, Ch%f, Quality Assurance Ddte signed Programs Section Division of Reactor Safety . l SUMMARY Scope: This routine, unannounced inspection was conducted in the areas of licensee actions on previously identified enforcement matters, and licensee actions on previously' identified inspection findings.
Results: No violations or deviations were identified.
! l l i ! 8707220376 870713 PDR ADOCK 05000321 G PDR
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. .. ( ' REPORT DET' AILS ' .i 1.
! Persons' Contacted' j Licensee Employees-
- M.:Blackwood,JSenior Nuclear' Engineer
.S. Brunson, Operating Experience Engineer
- G. Creighton, Procedure Specialist
' ~*C.:Dixon,' Quality Assurance (QA). Supervisor 1*P. Fornel, Maintenance Manager- .
- C Fuller,: Procedure Upgrade. Program (PUP)
- A. Miles, Clerk A R. Ott, Training Supervisor
- J. Ponder P13nt Engineer
- D. Read, Plant-Support Manager
J.- Robertson, PUP Group Leader . R 'S..Tipps,' Nuclear Safety and' Compliance Manager ! P.;Wahab, PUP Document Control. Clerk 'i Other : licensee ' employees. contacted included-engineers, -operators, - mechanics, security force members, and office personnel.
' .NRC Resident Inspectors
- J. Menning
- Attended exit interview 2.
Exit. Interview The inspection scope and findings were summarized on June 17, 1987, with - those persons. indicated in paragraph 1 above. No dissenting comments were received from the licensee.
The licensee did not identify as proprietary any of the materials provided Jto or reviewed by.the inspector during this inspection.
.. 3.
Licensee Action on Previous Enforcement Matters (92702) a.- (Closed) Violation 321,366/86-22-02: Failure to complete Maintenance Work Order (MWO) per procedure.
y' The licensee's response dated November 17, 1986, was considered l acceptable by Region II.
, I The inspector reviewed the corrective actions delineated in the
licensee's violation response. In the response to the violation, the
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licensee committed to revise Maintenance Program Procedure l 50AC-MNT-001-OS by January 10, 1987. The procedure was revised by a 1: ' - _ _ _ _ _ _ _ - _ - _ - - - _ _ _ _ _ _ _ _ _ _ _ _. _ _ _ _ _ _ _ _-_ _ _ _. _. _ _ _ _ _ _ _ _ - _ - _ .
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- temporary change notice and submi.tted. for typing. The procedure
- was removed. from typing.and revised. again. as.a.resultL of Lanother
' violation. The temporary change notice expired in: February-1987.
The. procedure. with-the minor modification: for this ' violation was.
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l-issued.on June.18, 1987; The. licensee is' reevaluating :its temporary procedure change program. - The. program that wil10 be implemented by, ' thel end of 1987 will increase the. length of time..a temporary procedure change; is in effect' and will - ensure ;that temporary i.
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- proc'edure. changes'. are reflected in y the copies available at all?
'- ' controlled document locations.
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(Closed) Violation. 321, ' 366/86-22-07. Failure :to: conduct periodic audits as required by NUREG-0737 paragraph I.C.S.7-and procedure 30AC-0PS-0030S.
' ' l ' -The licensee's 'responsei dated November.17, 1986, was considered acceptable by Region II.
The inspector reviewed Regulatory Compliance Procedure ' 43RC-REG-001-0N (Effectiveness Audit 'of the Operating Experience ' Program '- Revision 0) and selected audits performed in accordance-. .. with this procedure. These~ included: L .SOER 84-6 Reactor Trips Caused : by Turbine Control and l Protection System Failures L 'LER 2-86-13 Failure to; comply with TS 4.6.4.1 LSIL 442 Inspection of Atwood Morrill MSIV External i i
Springs ! ~ SIL 402 Wetwell/Drywell Inerting ! IEC 80-12 Valve shaft-to-key actuator may fall out when.
mounted below horizontal axis IEB 81-02 Failure of gate type valve to close against differential pressure In each case the effectiveness audit was' performed in accordance with procedure 43RC-REG-001-0N and was complete.
Additionally,- the inspector reviewed Administrative Control Procedure 30AC-0PS-003-0S (Plant Ope' rations - Revision 1), Section 8.11.3, which delineates the requirements for Operational Experience Assessment Reports (0 EAR).
Procedure 43RC-REG-001-0N. satisfactorily implements Section 8.11.3 of _ 30AC-0PS-003-0S.
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t(Closed) Violation 321, 366/86-22-06: Failure to document'and correct ' deficiencies identified during. maintenance.
- The.11censee's response dated November 17, 1986, was ? considered ' acceptable by' Region II.
The. inspector reviewed Administrative Control Proc'edure 10AC-MGR-004-05 (Deficiency Control System - Revision 1) < which.was : , revised to clarify conditions which required the initiation of' a - . deficiency report.
In addition, 'he -inspector r_eviewed the Deficiency Control System. training video tape which was shown to plant employees to explain.the. Deficiency Control System reporting requirements. The inspector reviewed the training documentation.for-this program. All aspects of the Deficiency Control System appear ~ adequate.
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(Closed) Violation 321, 366-84-46-02: Failure to notify Engineering of discrepancies found and to - obtain Engineering approval for.
substitution of parts.
The licensee's response dated January 25, 1985 was considered.
acceptable by Region II.
The inspector reviewed Deficiency Report 1-85-86 (Improperly Assembled Fire' Pump), Administrative Control Proceduro 20AC-ADM-003-0S (Vendor ~ Manual Control - Revision 1) Administrative
Control Procedure 10AC-ADM-004-0S (Deficiency Control System.- Revision 1) 'and' Engineering Service Procedure 42EN-ENG-007-0S (Vendor Manual Review - Revision 1). -The inspector reviewed the corrective.
action documentation for the specific violation noted and the procedures for control of the programmatic aspects of the violation, 20AC-ADM-003-0S and 42EN-ENG-007-OS. The inspector established there was adequate procedural control of the Vendor Manual Program and if fully implemented, reoccurrence of the violation should be precluded.
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(Closed) Severity Level IV Violation 321, 366-85-12-02: Failure to provide adequate calibration procedures in the maintenance tool shop.
., The lic.ensee's response dated June 28, 1985, was considered acceptable by Region II.
The violation referenced major procedure deficiencies found in procedure HNP-6943, which has been replaced with 52CP-CAL-005-0S (Calibration Check on Precision Measuring Equipment - Revision 2).
The inspector reviewed 52CP-CAL-005-0S and both procedures in the ,, reference section of the procedure, 50AC-MNT-001-OS (Maintenance Program - Revision 5) and 51GM-TOL-001-0S (Maintenance Shop Measuring and Test Equipment Control - Revision 1). The current revisions of these procedures appeared to adequately implement the corrective actions for the referenced violation.
Additionally the inspector l reviewed the following procedures:
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-l .. I 52CP-TOL-001-05, Torque Wrench Testing, Revision 1 ! 52CP-CAL-004-OS, Belt Tensioner Calibration, Revision 1 52CP-CAL-003-05, Crimping Tool Calibration, Revision 2 Although these procedures were not identified in the violation, the .j
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' licensee ' initiated or revised them during implementation of their corrective actions.
These procedures appeared adequate to perform their intended. functions.
The inspector reviewed evidence of training to the four procedures listed in this paragraph.
The licensee has satisfactorily addressed this item.
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(Closed) Unresolved Item 321, 366/86-22-01: Electrical backseating-and light to light stroke time testing of motor operated valves, this item is covered by Violation 321, 366/86-30-02 and the licensee's corrective actions will be reviewed with the licensee's response'to the violation. This item is administrative 1y closed.
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Unresolved Items l Unresolved items were not identified during this inspection.
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Licensee Action on Previously Identified Inspection Findings (92701) a.
(Closed) Inspector Follow-up Item 321,.366/86-22-04: ' Evaluation of additive torque wrench tolerance errors.
l ' The inspector reviewed General Maintenance Procedure 51GM-MNT-033-05 (Torquing Procedure - Revision 0) which. provides instructions for determining torque values, gasket stress, and stud stress.
This procedure adequately addresses the concerns of additive torque wrench tolerance errors, in that if a calibrated torque dial gauge cannot be added between the multiplier and the mechanical fastener, an engineering evaluation must be performed to ensure that no damage to equipment or fasteners will result from any errors introduced in the torque value by the torque multiplier.
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(Closed) Inspector Follow-up Item 321, 366/84-46-01: Establish an adequate program and controls to improve the present method of controlling vendor technical manuals.
The inspector reviewed Administrative Control Procedure 20AC-ADM-003-OS (Vendor Manual Control Revision 1), which - establishes the program to control the receipt, distribution, update and revision of plant vendor manuals.
The procedure established adequate control of the vendor manual program.
The inspector verified the implementation of the procedure by examining selected records and interviewing personnel in the document control area.
Additionally the inspector reviewed the documentation used by selected maintenance personnel. Although the program will not fully l l __
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be implemented until July 1987, the inspector did not identify specific failures or programmatic. weaknesses.
The method for recalling checked out vendor manuals could be improved, in that l manuals were often checked out by clerks and delivered to engineers j, who were not aware of the requirement to return manuals in within 10 days. At the time of the inspection there were ten delinquent vendor i I manuals.
The licensee agreed to consider changes to the check out procedure. The overall program is considered acceptable.
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(Closed) Inspector Follow-up Item 321, 366-85-12-04: Program revision to ensure that evaluations of out-of-tolerance M&TE
addresses the issue of multiple scales and a uniform policy on previous usage is established.
The inspector follow-up item references General Maintenance Procedure 51GM-CAL-001-0 which has been replaced by 51GM-TOL-002-0S (Control of 1&C Measuring and Test Equipment - Revision 0).
Section 7.4 of 51GM-T0L-002-0S addresses the specific concerns of multiple scales in ! Section 7.4.2.
The inspection reviewed Section 7.4 of General Maintenance Procedure 51GM-TOL-001-0S (Maintenance Shop Measuring and l Test Equipment Control - Revision 1) and compared the requirements to l' those of 51GM-TOL-002-05.
The requirements for corrective actions when M&TE equipment is out of calibration is essentially identical.
There are no further concerns at this time, d.
(Closed) Inspector Follow-up Item 321, 366/85-12-03: Timeliness of out-of-tolerance evaluations to be procedurally and effectively controlled.
l The inspector reviewed General Maintenance Procedure 51GM-TOL-001-05, ) l' Revision 1, Section 7.4.
This section addresses test equipment found defective or out of calibration and gives specific instructions on actions to be taken. The guidelines are clear and the procedure , i appropriately addresses the concern.
Attachment 5, Calibration ) Certification Review Form, appears to provide adequate assurance that i l M&TE used during period of suspect calibration will be appropriately J ' evaluated.
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(Closed) Inspector Follow-up Item 321, 366/85-19-02: Procedure to Describe Preventive Maintenance Program.
The inspector reviewed Administrative Control Procedure 50AC-MNT-001-0S (Maintenance Program - Revision 5), which establishes the requirements and responsibilities for the control of maintenance ] l activities and adequately describes the preventive maintenance ' program.
The procedure clearly defines the different types of maintenance activities and gives clear guidelines for procedure development.
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(Closed) Inspector Follow-up Item 321, 366/85-19-01: Update Procedure to Reflect Maintenance Work Order (MWO) requirements.
The inspector reviewed Administrative Contrul Procedure 50AC-MNT-001-05 (Maintenance Program - Revision 5) which contained the current requirements for the MWO program.
The program and the implementing procedures appeared to edequately address the inspector's concerns. There are no further concerns at this time.
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(Closed) Inspector Follow-up Item 321, 366/86-31-01: Provide fire fighting training for encillary personnel.
The licensee intends to have ten Health Physics (HP) personnel trained per the requirements of OSHA section 1910.56.
Two HP personnel have received the training at the Georgia Fire Academy, one health physicist is currently in training.
The remaining seven are tentatively scheduled for training by the end of 1987.
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(0 pen) Inspector Follow-up Item 322, 361/86-22-05: Provide engineering review of causes of main streamline break detection -- instrumentation.
The licensee had submitted a request for engineering review to evaluate if the Fenwal switches need replacing, need improvements in calibration, or if the turbine building environment has an adverse effect on Fenwal switch performance.
The evaluation will also include a determination of the Reactor Protection System input requirements the of the switches.
The licensee expects to have the results of the evaluation completed by the end of 1987.
This item will remain open pending the results of the engineering evaluation and subsequent implementation schedule.
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(Closed) Inspection and Enforcement Bulletin 86-01 (321, 366/BU-86-01): Minimum Flow Logic Problems that could disable Residual Heat Removal (RHR) pump.
The inspector reviewed the licensee response to BU-86-01 and the associated drawings.
The subject of the Bulletin is not applicable to Plant Hatch in that there is divisional separation of the minimum flow bypass valves. A failure of the flow sensing instrumentation in one RHR loop will not affect the minimum flow bypass valves in the redundant loop.
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